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LER-1981-022, /03L-0:on 810514,amp Reading for Heat Tracing Panel 9,circuit 20C,found Below Acceptance Criteria.Caused by Excessive Heat.Tracing Replaced & Tested.Design Change Initiated |
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NRC FORM 366
.LICENSEE EVENT REPORT U.S. NUCLEAR REGULA. TORY COMMISSION li-7')
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BO EVENT DESCRIPTION AND PR06ASLE CONSEQUENCES@
I With Unit No. 2 at 100% power, PT-27C revealed* that amn readino for heat tracing
.III!]. J Panel 9, circuit 20C, was below the acceptance criteria stipulated in the PT.
This
([II] I event is contrary to T.S. 3.2.B.5 and is reportable per T.s: 6.6.2.b(2).. ~he [TI)) _I redundant. heat tracing circuit was operable, therefore, the health* and safety of the J..
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20 1:=l 31 BO REVISION NO. w 32 COMPONENT ACTION l'UTURE EF;:ECT
~ ATTACHMENT NPRc-4 PRIMECOMP.
TAKEN ACTION ON PLANT METHOD HOURS ~ SUBMITTED FORMliUB.
SUPPI.IER MANUl'ACTURER
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D:I]J j The loss of heat tracing was aue to excessive heat. The defective heat trac;n2 was o:::IIJ replaced and tested.
A design change has been initiated tq change tbe manner by
!III!
which these borated lines are heat traced.
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ATTACHMENT 1 SURRY POWER STATION, UNIT No. 2 DOCKET NO:
50-281 REPORT NO:
81-022/03L-0 EVENT DATE:
05-14-81 TITLE OF EVENT:
HEAT TRACING FAILURE
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- 1.
DESCRIPTION OF EVENT
With Unit No. 2 at 100% power, PT-27C revealed that the amp reading for heat tracing Panel 9, circuit 20C (".C" BAST recirc. line), was below the acceptance criteria stipulated in the PT.
This event is contrary to Technical Specification 3.2.B.5, and is reportable per Technical Specification 6.6.2.b(2).
- 2.
PROBABLE CONSEQUENCES and STATUS of REDUNDANT EQUIPMENT:
The heat tracing circuits are intended to maintain a fluid temperature above that needed for flow.
The redundant heat tracing.circuit was operable, therefore, the health and safety of the public were not affected.
- 3.
CAUSE
The loss o:1; heat tracing was due to excessive heat.
- 4.
U1MEDIATK CORRECTIVE ACTION:
The irrnnediate corrective action was to verify that the redundant circuit was operable.
- 5.
SUBSEQUENT CORRECTIVE ACTION:
The defective heat tracing tape-was** replaced and tested within the time span specified by Technical Specifications.
- 6.
ACTION TAKEN TO PREVENT RECURRENCE:
No additional actions were deemed necessary.
- 7.
GENERIC IMPLICATIONS:
A task force has reviewed the total spectrum of the Heat Tracing system and a Design Change is being prepared as a result of the Task Force's study.
Long lead items are being procured.
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Action taken c..
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Future action I-
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Effect on plant ~
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Shutdown method c:::-
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Hours 0
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Attachments
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~ '{I Prime component supplier -;G, ~-
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Component manufacturers -'--tR(2. v'LM ~
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Method of discovery
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Facility status
- 33. Activity -:released
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Contents of.release
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Amount of activity
Personnel exposure type
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Type damage/loss L
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| 05000280/LER-1981-001, Forwards LER 81-001/01T-0 | Forwards LER 81-001/01T-0 | | | 05000280/LER-1981-001-01, /01T-0:on 810225,w/unit Defueled for Steam Generator Replacement,Routine Testing Exam of Loop a Main Steam Piping Revealed Linear Indications.Caused by Corrosion Pitting.Subj Areas Will Be Repaired | /01T-0:on 810225,w/unit Defueled for Steam Generator Replacement,Routine Testing Exam of Loop a Main Steam Piping Revealed Linear Indications.Caused by Corrosion Pitting.Subj Areas Will Be Repaired | | | 05000281/LER-1981-001-03, /03L-0:on 810102,one Boric Acid Flow Path to Core Inoperable.Caused by Personnel Inadvertently Closing Valve 2-CH-226.Flow Path Restored & Personnel Reinstructed | /03L-0:on 810102,one Boric Acid Flow Path to Core Inoperable.Caused by Personnel Inadvertently Closing Valve 2-CH-226.Flow Path Restored & Personnel Reinstructed | | | 05000280/LER-1981-002-03, /03L-0:on 810122,radiation Alarm Setpoint for Component Cooling Sys Found Greater than Twice Background. 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Panels 8 & 9 Circuits Were Below Acceptance Criteria.Caused by Excessive Temps Breaking Down Insulation.Defective Heat Tracing Replaced | /03L-0:on 810114,at 100% power,PT-27 (Heat Tracing) Revealed Amp Readings for Panels 8 & 9 Circuits Were Below Acceptance Criteria.Caused by Excessive Temps Breaking Down Insulation.Defective Heat Tracing Replaced | | | 05000281/LER-1981-008-03, /03L-0:on 810206,output Amperage for RM-CC-106 Reduced in Nonconservative Direction.Caused by Failed Remote Indicator Module in Auxiliary Bldg.Module Isolated & RM-CC-106 Recalibr.Monitor Will Be Repaired | /03L-0:on 810206,output Amperage for RM-CC-106 Reduced in Nonconservative Direction.Caused by Failed Remote Indicator Module in Auxiliary Bldg.Module Isolated & RM-CC-106 Recalibr.Monitor Will Be Repaired | | | 05000280/LER-1981-008-03, /03L-0:on 810410,process Vent Radiation Monitor Found Inoperable.Caused by Broken Pump Drive Belt Due to Misalignment.Drive Belt Replaced & Radiation Monitor Operability 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Filter Banks Were Found to Be Less Efficient than Required by Tech Spec.Caused by Formation of Void Areas Due to Settling of Charcoal in Filters.Charcoal Added | | | 05000280/LER-1981-015, Forwards LER 81-015/03L-0,updated LER 81-035/03X-1 & Corrected LER 81-036/03L-0 | Forwards LER 81-015/03L-0,updated LER 81-035/03X-1 & Corrected LER 81-036/03L-0 | | | 05000280/LER-1981-015-03, /03L-0:on 810603,spent Fuel Pit Overflowed Into New Fuel Handling Area & Outside to Storm Drain.Caused by Leaking Diaphragm Valve & Defeated High Level Alarm Annunciator.Valve Repaired | /03L-0:on 810603,spent Fuel Pit Overflowed Into New Fuel Handling Area & Outside to Storm Drain.Caused by Leaking Diaphragm Valve & Defeated High Level Alarm Annunciator.Valve Repaired | | | 05000281/LER-1981-015-03, /03L-0:on 810315,PT-26.1 Revealed That Process Vent Radiation Monitor Pump Failed to Rotate.Caused by Failure of Pump Bearings.Pump Replaced | /03L-0:on 810315,PT-26.1 Revealed That Process Vent Radiation Monitor 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Fire Watch Posted & Seal Installed | /03L-0:on 810702,discovered That No Fire Watch Had Been Posted for Two Unsealed Fire Barrier Penetrations in Cable Spreading Room Area.Caused by Const Personnel Error. Fire Watch Posted & Seal Installed | | | 05000280/LER-1981-018-03, Ler 81-018/03L-0:on 810702,power Operated Relief Valves Lifted to Mitigate Overpressurization Transient.Caused by Unisolated Charging Flow Control Valve.Valve Isolated. RCS Pressure Reduced Below Setpoint | Ler 81-018/03L-0:on 810702,power Operated Relief Valves Lifted to Mitigate Overpressurization Transient.Caused by Unisolated Charging Flow Control Valve.Valve Isolated. RCS Pressure Reduced Below Setpoint | | | 05000281/LER-1981-018-03, /03L-0:on 810318,amp Readings for Heat Tracing Panel 10,circuit 4A,were Below Acceptance Criteria Per PT-27.Caused by Excessive Heat.Defective Heat Tracing Replaced & Tested | /03L-0:on 810318,amp Readings for Heat Tracing Panel 10,circuit 4A,were Below Acceptance Criteria Per PT-27.Caused by Excessive Heat.Defective Heat Tracing Replaced & Tested | | | 05000280/LER-1981-019-01, /01T-0:on 810707,urgent Failure Alarm for Control Rods Occurred,Indicating Rods Were Inoperrable.Caused by Blown Fuse in Power Cabinet.Fuse Replaced | /01T-0:on 810707,urgent Failure Alarm for Control Rods Occurred,Indicating Rods Were Inoperrable.Caused by Blown Fuse in Power Cabinet.Fuse Replaced | | | 05000281/LER-1981-019-03, /03L-0:on 810218,amp Readings for Heat Tracing Panel 9,circuit 6A Were Low.Caused by Excessive Heat.Heat Tracing Replaced | /03L-0:on 810218,amp Readings for Heat Tracing Panel 9,circuit 6A Were Low.Caused by Excessive Heat.Heat Tracing Replaced | | | 05000281/LER-1981-020-03, /03L-0:on 810223,during Full power,RM-CC-106 Alert & High Alarm Lights Energized W/O Initiating Required Automatic Action.Caused by Failed Card in Alarm Circuit.Card Replaced & Tested | /03L-0:on 810223,during Full power,RM-CC-106 Alert & High Alarm Lights Energized W/O Initiating Required Automatic Action.Caused by Failed Card in Alarm Circuit.Card Replaced & Tested | | | 05000280/LER-1981-020-03, Ae Notified Util of Seven Masonry Block Wall Sections in Fuel Bldg Not Meeting IE Bulletin 80-11 Design Requirements.Cause Not Stated.Block Walls Will Be Replaced | Ae Notified Util of Seven Masonry Block Wall Sections in Fuel Bldg Not Meeting IE Bulletin 80-11 Design Requirements.Cause Not Stated.Block Walls Will Be Replaced | | | 05000281/LER-1981-020, Forwards LER 81-020/03L-0 | Forwards LER 81-020/03L-0 | | | 05000280/LER-1981-021-03, /03L-0:on 810704,chemical Addition Tank Found to Contain 86% of Vol Required,Following Level Transmitter Recalibr.Caused by Use of Pure Water Instead of Sodium Hydroxide Solution in Original Calibr Procedure | /03L-0:on 810704,chemical Addition Tank Found to Contain 86% of Vol Required,Following Level Transmitter Recalibr.Caused by Use of Pure Water Instead of Sodium Hydroxide Solution in Original Calibr Procedure | | | 05000280/LER-1981-021, Forwards LER 81-021/03L-0.W/o Encl LERs 81-022/03L-0 & 81-028/03L-0 | Forwards LER 81-021/03L-0.W/o Encl LERs 81-022/03L-0 & 81-028/03L-0 | |
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