05000368/LER-1950-368, /03L-0 on 790514:during Mode 3,supply Valves to Steam Generator Would Not Respond to Control Room Demand Signal.Caused by Blown Fuse & Stuck Relay.Similar to LER 50-368/79-026.Repairs Made & Valves Proven Operable

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/03L-0 on 790514:during Mode 3,supply Valves to Steam Generator Would Not Respond to Control Room Demand Signal.Caused by Blown Fuse & Stuck Relay.Similar to LER 50-368/79-026.Repairs Made & Valves Proven Operable
ML19273B960
Person / Time
Site:  Entergy icon.png
Issue date: 06/12/1979
From: Shively C
ARKANSAS POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19273B940 List:
References
LER-79-037-03L, LER-79-37-3L, NUDOCS 7906180587
Download: ML19273B960 (1)


LER-1950-368, /03L-0 on 790514:during Mode 3,supply Valves to Steam Generator Would Not Respond to Control Room Demand Signal.Caused by Blown Fuse & Stuck Relay.Similar to LER 50-368/79-026.Repairs Made & Valves Proven Operable
Event date:
Report date:
3681950368R00 - NRC Website

text

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.N RC FORM 366 O 771 U. S. NUCLE AR REGULATORY COMMISSION LICENSEE EVENT REPORT EXHIBIT A CONTROL etOcic [

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61 oOCgET sVMBE R 68 Ca EVENT DATE 74 75 HF,OHI C AT E 80 EVENT DESCAIPTION AND PROBA0LE CONSEQUENCES h [During Mode 3 operation, while utilizing the steam driven o

2 g,i,j; Emergency Feedwater Pump, 2P7B, for normal auxiliary l feed, supply valves, 2CV-1039-2 and 2CV-1076-2, to a

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Steam Generator, 2E24B, would not respond to a Control c

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Room demand signal.

The 2P7A feedwater loop to 2E24B

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Iwas declared inoperable. This occurrence is similar to i

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- 368/79-026.

Reportable per T.S.6.9.1.9 (b).

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J' 40 45 41 43 de 41 CALSE OESCA#TICN AND CORREC flVE ACTIO'.S h i; (Unit was niaced in Mode 5 operation, due to an unrelated i

i j iproblem, meeting the requirements of Action Statement gT.S.3.7.1.2. Investigation revealed a blown fuse in the j

l 2CV-1039-2 circuitry and a stuck relay overriding the

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,,, i 2CV-1076-2 operation. Repairs were made 6 valves proven operable.

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