05000219/LER-1978-035-01, /01T-0 on 781227:torus Water Temp in Excess of Tech Specs.Caused by Failure of Operations Personnel to Recognize Torus Water Temp Nearing Tech Spec Limit

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/01T-0 on 781227:torus Water Temp in Excess of Tech Specs.Caused by Failure of Operations Personnel to Recognize Torus Water Temp Nearing Tech Spec Limit
ML19289C404
Person / Time
Site: Oyster Creek
Issue date: 01/05/1979
From: Ross D
JERSEY CENTRAL POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19289C402 List:
References
LER-78-035-01T, LER-78-35-1T, NUDOCS 7901120139
Download: ML19289C404 (3)


LER-1978-035, /01T-0 on 781227:torus Water Temp in Excess of Tech Specs.Caused by Failure of Operations Personnel to Recognize Torus Water Temp Nearing Tech Spec Limit
Event date:
Report date:
2191978035R01 - NRC Website

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2 l During normal operation, the torus water temperature was found to be in l

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The average value for the four suppres-l sion pool thermocouolas at the time of the incident was 95.35'F.

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40 41 42 43 44 47 cAUSE OEsORIPTION AND CORRECTIVE ACTIONS i it l The cause of the occurrence is attributed to the failure 'f operations l

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Reportable Occurrence No. 50-219/78-35/IT-0 Page 2 January 5, 1979 Analysis of Occurrence The suppression pool water temperature limits were established to reduce the affects of the steam quenching vibration phenomenon which may occur at elevated suppression pool water temperature during a loss-of-coolant accident.

The requirement for reactor scram for suppression pool water temperature in excess of 110*F. was developed to prevent exceeding 160*F.

during relief valve operation.

The 95'F. limit for power operation is intended to provide a 10*F. allowance for testing which adds heat to the suppression pool and still provide a 5'F. margin below the scram requirement.

Since the suppression pool water temperature did not exceed the IIO*F.

limit during this incident, there appears to be minimal safety significance.

Additionally, the time the suppression pool temperature exceeded the 95'F.

limit was minimal.

Corrective Action

The torus water temperature was reduced to less than 95'F. by operation of the containment spray system.

The appropriate procedure changes will be made to insure that the containment spray system is operated as required to maintain torus water temperature to less than 90*F.

The PORC recognizes that there is an increasing frequency of administrative related problems and will formally address these problems in the near future.

Failure Data None.