05000336/LER-1980-015-03, /03L-0:on 800321,following Reactor Trip,Condensate Storage Tank Level Was Below Tech Spec Requirements.Caused by Gland Seal Header Relief Valve Being Stuck Open, Necessitating Use of Auxiliary Feedwater Sys

From kanterella
Revision as of 04:00, 2 January 2025 by StriderTol (talk | contribs) (StriderTol Bot insert)
(diff) ← Older revision | Latest revision (diff) | Newer revision → (diff)
Jump to navigation Jump to search
/03L-0:on 800321,following Reactor Trip,Condensate Storage Tank Level Was Below Tech Spec Requirements.Caused by Gland Seal Header Relief Valve Being Stuck Open, Necessitating Use of Auxiliary Feedwater Sys
ML19309E590
Person / Time
Site: Millstone 
Issue date: 04/18/1980
From: Stratman R
NORTHEAST NUCLEAR ENERGY CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19309E581 List:
References
LER-80-015-03L, LER-80-15-3L, NUDOCS 8004220679
Download: ML19309E590 (1)


LER-1980-015, /03L-0:on 800321,following Reactor Trip,Condensate Storage Tank Level Was Below Tech Spec Requirements.Caused by Gland Seal Header Relief Valve Being Stuck Open, Necessitating Use of Auxiliary Feedwater Sys
Event date:
Report date:
3361980015R03 - NRC Website

text

_ - _ _... _

CONTROL BLOCK:

l l

\\

l l

l (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 6 l Cl Tl MI NI Sl 21@l o lo l-10 lo lo lo l-10 lo lo l@l411 11 11 l11@l I

l@

o i 7

8 9 LICENSEE CODE le 15 LICENSE NUM6ER 25 26 LICENSE TYPg Jo 67 car 68 i

CON T l L l@] Ol 5 l010 l0 l3 l 3 l6 l@l 0131211181 Ol@l 01411181810 l@

[

o i sOU C 7

8 60 El DOCKET NUMBER 68 69 EVENT OATE 74 75 REPORT DATE 80 8

EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h IFo11owing a reactor trip, the Condensate Storage Tank Level was below the level rcquir-l O 2 led by Specification 3.7.1.3 for a period of less than 4.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />.

Following the reactor I 0 2 Ltrip the Gland Seal Header relief valve stuck openwhich required that main condenser i

O 4

{

im isi Ivacuum be broken and the Auxiliary Feedwater System utilized. This caused the low levell ;

l Condition in the Condensate Storage Tank. There are no probable consequences because thel

O 6 l unit was operated in accordance with Technical Specification 3.7.1.3.

Similar events - I O 7 f5Tii1 ILER 77-26 dated 3/28/77, LER 79-40 dated 12/4/79 and LER 80-07 dated ~3/27/80.

I f CODE S BC E COMPONENT CODE S

dE S

ODE I N l F l@ [Ll@ [Z_j@ l Z I Z l Z l Z l Z I Z l@ [Jj@ l_Z_j @

Z O 9 7

8 9

10 11 12 13 sa 39 20 SEQUENTIAL OCCURRENCE REPORT REVISION f

LE R EVENT YEAR REPORT 10; CODE TYPE NO.

@,agg/RO I 81 01 L-J l 0111 51 Lc_1 10 13 I W

L---I lo_I 21 22 23 24 26 27 28 29 30 31 32 K

AC N

P NT ME O HOURS SB IT FORM 8.

50 L1 MAN F CTURER LLl@LZ_J@

l_z]@

LZ_J@

loIoIoIoI LN_j@

[N_j@

[Z_l@

lZl9I9l9l@

33 34 35 36 31 40 41 43 43 44 4y CAUSE DESCRIPTION ANDCoRRECTIVE ACTIONS h l The Gland Seal Header relief valve stuck open following a reactor trip which required i i O E l that Main Condenser Vacuum be broken. This necessitated the use of the Auxiliary Feed-l h I water System which caused the Condensate Storage Tank level to decrease below th'e limiti l allosed by the Technical Specifications. At this time the operability of the backup i

i 3 gi fire water system was verified and the tank level restored.

Il ST US

% POWER OTHER STATUS is O R DISCOVERY DESCRIPTION

% (_G_j@ 101010 l@l NA l

[Z_j@l Operator Observation ll 12 n

45 46 en l A8nviTY CO0 TENT MtLEASED OF RELE ASE AMOUNT OF ACTIVITY IOCATION OF RELEASE i

l NA l

l NA I'

u.ls.1 LZ_1 @ LZ_l@#Es i

' nRsONNR Ex,0s OEsCHiPuON@

[

NuM.Ea TvPE

' Li.Lt! 1010 I ol@LZ_l@l NA

' nRsONNEL iN2U%Es oEsCRiPnON@

Nuu ER l' !a.i lo 10 lo l@l NA l

fO,s 0, On O"cETO,AC,LiTvg 8004820 6 79l rij @ li"l @ l NA

' 30 i

l/

2: 9 10 l... d !.Njt @ DESCRIPTION l

NA l

llll1llllllll I:IsU

.~

SS 69 30

- fr 0 10 NW-W Robert A. Stratman enous:

rwarumrm m en