05000327/LER-1980-035-01, /01T-0:on 800421,during Pipe Hanger Insp, Discovered That Pipe Hanger from Previous Design Revision Had Not Been Removed from Auxiliary Feedwater Sys Pipe. Caused by Personnel Error.Pipe Hanger Removed

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/01T-0:on 800421,during Pipe Hanger Insp, Discovered That Pipe Hanger from Previous Design Revision Had Not Been Removed from Auxiliary Feedwater Sys Pipe. Caused by Personnel Error.Pipe Hanger Removed
ML19309H661
Person / Time
Site: Sequoyah 
Issue date: 05/02/1980
From: Ken Wilson
TENNESSEE VALLEY AUTHORITY
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19309H655 List:
References
LER-80-035-01T, LER-80-35-1T, NUDOCS 8005130628
Download: ML19309H661 (2)


LER-1980-035, /01T-0:on 800421,during Pipe Hanger Insp, Discovered That Pipe Hanger from Previous Design Revision Had Not Been Removed from Auxiliary Feedwater Sys Pipe. Caused by Personnel Error.Pipe Hanger Removed
Event date:
Report date:
3271980035R01 - NRC Website

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  • ennessee Valley Authority Sequoyah Nuclear Plant LER SUPPLEMENTAL IhTORMATICN SQRO-50-327/8035 Technical Specification Involved:

6.9.1.12.1 Reported Under Technical Specification 6.9.1.12.1 Date of Occurrence:

4/21/80 Time of Occurrence: 0900 CST Unit 1 i,

i Identification and Description of Occurrence During a recent pipe hanger inspection, it was discovered that a pipe hanger from a previous design revisien had not been removed from an auxiliary feedwater system pipe. This constituted a hanger configuration which had not been seismically analyzed.

Conditions Prior to Occurrence Mode 5 and filling and venting RCS.

Action Specified in the Technical Specification Surveillance Requirements Met Due to Inoperable Eauipment N/A Apparent Cause of Occurrence Personnel error. Pipe hanger should have been removed.

Analysis of Occurrence N/A

Corrective Action

The pipe hanger installed from the previous design revision was removed; therefore, the system should operate with no adverse effects as designed.

Failure Date

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N/A

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