05000327/LER-1980-070-03, /03L-0:on 800517,during Cooldown from Mode 3, Refueling Water Storage Tank Water Level Fell Below Required Limit.Caused by Failure to Initiate Early Makeup.Makeup Immediately Initiated

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/03L-0:on 800517,during Cooldown from Mode 3, Refueling Water Storage Tank Water Level Fell Below Required Limit.Caused by Failure to Initiate Early Makeup.Makeup Immediately Initiated
ML19318A957
Person / Time
Site: Sequoyah 
Issue date: 06/16/1980
From: Record D
TENNESSEE VALLEY AUTHORITY
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19318A951 List:
References
LER-80-070-03L, LER-80-70-3L, NUDOCS 8006240433
Download: ML19318A957 (2)


LER-1980-070, /03L-0:on 800517,during Cooldown from Mode 3, Refueling Water Storage Tank Water Level Fell Below Required Limit.Caused by Failure to Initiate Early Makeup.Makeup Immediately Initiated
Event date:
Report date:
3271980070R03 - NRC Website

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NRC FOR%t 068 U. S. PdVCLE AR REGULATORY COYYlSSIOf4 (7 77)

LICEi45EE EVENT REPORT EXHIBIT A

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e UPTION AND pao 9aSLT CONSEcvENCES h' EVENT DESO:

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water level fel"l below reou' ired level while in Mode 4 T.S.

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ini.it requires at least 370,000 gallons in the RWST.

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lilal! During plant cooldown. makeup to the refueling water storaRe tank 1

t i t i i 1 was no t initiated early enough to prevent the RWST level from dropping i

rT1I below T.S. limits. Upon discovery, makeup to RWST immediately initiated.t

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T;nnass3 Velisy Authority Sequoyah Nuclear Plant LER SUPPLEMENTAL INFORMATION SQRO-50-327/ 8070 Technical Specification Involved 3.1.2.6 Reported Under Technical Saecification 6.9.1.13.b Late of Occurrence: -5/17/80 0450 CDST Identification and Description of Occurrence:

During unit 1 cooldown from Mode 3, RWST level fell below required water level while still in Mode 4.

Conditions Prior to Occurrence:

Unit 1 in Mode 3 Apparent Cause of Occurrence:

The de=and on RWST water due to RCS shrink and pressurizer level was underestimated during unit 1 cooldown and makeup not started in time to maintain RWST level.

Analysis of Occurrence:

There was no danger to public health and safety.

Corrective Action

Cooldown was continued to Mode 5 (where required level is only 35,443 gallons) while. continuously making up to the RWST.

Failure Data:

N/A l

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