LER-1980-035, /03L-0:on 800410,while Attempting to Switch from Decay Heat Removal Train 1 to Train 2,cooler 2 Outlet Valve Would Not Open.Caused by Malfunctioning of Valve Operator Radial Arm.Radial Arm Was Readjusted |
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| 3461980035R03 - NRC Website |
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LICENSEE EVENT REPORT 8005120%
CONTROL DLOCK: l l
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CC'4*T lojil 3{C"y l L l@l 0 l 5 l 0 l-l0 l 3 l 74 75 REPORT DATE 63 R
g C3 bJ EVENT OATE 60 61 COCKET NUYdEH EVENT DESCRIPTION AND PROBABLE CONSEGJENCES h1129 hours while attempt 7
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19 l 2 l l(NP-33-80-43) on 4/10/80 at let Valve DH14A would not open l j o j 3 l lcoval (DUR) Train #1 to DHR Train #2, DHR Cooler #2 Out Train #1 was returned to service and Train #2 was declared inoperable.
j Jo14llbeyond 20%.
the time.
Therefore, the station did not enter the actior]
j o l s ; lThe station was in Mode 5 at lo lc l l statement of Technical Specification 3.5.2 which requires both DHR trains to be o There was no danger to the health and safety of the public l ling in Modes 1, 2, and 3.
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DHR Train #1 was operating properly.
1 o la i lor station personnel.
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40 di 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h 1: lo l lThe cause of the occurrence can be traced to the radial arm of the valve operat The arm works in a very narrow area and it moved slightly sideways where it made I l,;,jl age.
in its meunting bracket. This restricted its movement to only 20%. l l contact with a bolt
, 7 The valve was declared operable at l
g,,.,j lUnder W O 328-80, the radius arm was readjusted.
Toledo Edison is investigating need for further corrections.
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8 9 11 12 LOSS OF OR DAVAGE To FACILITY l
TYPE C E SC RIP TIO N El Z l@l NA 80 7
8 9 10 NRC USE ONLY PUR L ICI TY ISSUED
DESCRIPTION
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PHONE:
NAME OF PREPARER R
TOLEDO EDISON COMPANY DAVIS-BESSE NUCLEAR POWER STATION UNIT ONE SUPPLEMENTAL INFORMATION FOR LER NP-33-80-43
'l DATE OF EVENT: April 10, 1980 FACILITY: Davis-Besse Unit 1 Decay Heat Removal Cooler #2 outlet flow control valve IDENTIFICATION OF OCCURRENCE:
DH14A would not open beyond 20%
The unit was in Mode 5, with Power (MRT) = 0, and Conditions Prior to Occurrence:
Load (Gross MWE) = 0.
i On April 10, 1980 at 1129 hours0.0131 days <br />0.314 hours <br />0.00187 weeks <br />4.295845e-4 months <br /> while attempting to Description of Occurrence:
switch to #2 Decay Heat Removal Train for maintenance on #1, DH14A would not open Technical Specification 3.5.2.c requires two independent emergency beyond 20%.
Being core cooling systems (ECCS) subsystem to be operabic in Modes 1, 2, and 3.
This event is being reported in Mode 5, the unit did not enter the action statement.
l l
to document a component failure.
i The improper operation of valve DH14A l
Designation of Apparent Cause of Occurrence:
failure.
The proximity of the radius ara can be attributed to a nochanical component to the bracket mounting bolts allows only marginal clearance. Any movement of the of the radius arm towards the mounting bracket causes binding and limits movement radius arm.
3 There was no danger to the health and safety of the public I
. Analysis of Occurrence:
or to station personnel.
The #1 Decay Heat Removal train was operable during this time.
Under Maintenance Work Order IC-328-80, the radius arm on the d
Corrective Action
valve shaf t was moved away from the mounting bracket, thus providing clearance and allowing the valve to stroke fully. After meeting stroke time acceptance criteria required by Surveillance Test ST 5051.01, the valve was declared operable and returned I
to service on April 11, 1980 at 0750 hours0.00868 days <br />0.208 hours <br />0.00124 weeks <br />2.85375e-4 months <br />.
Toledo Edison is investigating further 4
corrective action that may be required on this or other similar valves.
There have been no previously reported failures of this type valve Failure Data:
l operator.
6 1
LER #80-035 i
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| 05000346/LER-1980-001, Forwards LER 80-001/01T-0 | Forwards LER 80-001/01T-0 | | | 05000346/LER-1980-001-01, /01T-0:on 800103,during Plant Heatup,Safety Features Actuation Sys Channels 1 & 3 Tripped at 1,600 Psig, Causing Level 2 Actuation.Operators Correctly Tripped Reactor Coolant Pumps.Caused by Procedural Deficiency | /01T-0:on 800103,during Plant Heatup,Safety Features Actuation Sys Channels 1 & 3 Tripped at 1,600 Psig, Causing Level 2 Actuation.Operators Correctly Tripped Reactor Coolant Pumps.Caused by Procedural Deficiency | | | 05000346/LER-1980-002, Forwards LER 80-002/03L-0 | Forwards LER 80-002/03L-0 | | | 05000346/LER-1980-002-03, /03L-0:on 800103,after Actuating of Safety Features Actuation Sys Level 2,demin Water Valve DW68318 Did Not Indicate Closed & Monitor Light Did Not Indicate Properly.Caused by Maladjusted Position Indicator Switch | /03L-0:on 800103,after Actuating of Safety Features Actuation Sys Level 2,demin Water Valve DW68318 Did Not Indicate Closed & Monitor Light Did Not Indicate Properly.Caused by Maladjusted Position Indicator Switch | | | 05000346/LER-1980-003-03, /03L-0:on 800103,during Auxiliary Feedwater Pump Test,Pump l-1 Was Declared Inoperable.Caused by Improperly Adjusted Slip Clutch Between Governor Manual Speed Adjustment Shaft & Remotely Controlled Speed Changer Motion | /03L-0:on 800103,during Auxiliary Feedwater Pump Test,Pump l-1 Was Declared Inoperable.Caused by Improperly Adjusted Slip Clutch Between Governor Manual Speed Adjustment Shaft & Remotely Controlled Speed Changer Motion | | | 05000346/LER-1980-003, Forwards LER 80-003/03L-0 | Forwards LER 80-003/03L-0 | | | 05000346/LER-1980-004-03, /03L-0:on 800107,control Rod 5-11 Absolute Position Indication Declared Inoperable Due to Fluctuating Signals.Possibly Caused by Isolation of Position Indication Cabling & Electrical Penetration | /03L-0:on 800107,control Rod 5-11 Absolute Position Indication Declared Inoperable Due to Fluctuating Signals.Possibly Caused by Isolation of Position Indication Cabling & Electrical Penetration | | | 05000346/LER-1980-004, Forwards LER 80-004/03L-0 | Forwards LER 80-004/03L-0 | | | 05000346/LER-1980-005, Forwards LER 80-005/03L-0 | Forwards LER 80-005/03L-0 | | | 05000346/LER-1980-005-03, /03L-0:on 800110,Tech Spec Late Date Passed W/O Performance of Boric Acid Flowpath Heat Tracing Weekly Test. Caused by Known Deficiency in Design of Sys Resulting in Inability to Maintain Min Temp Necessary During Startup | /03L-0:on 800110,Tech Spec Late Date Passed W/O Performance of Boric Acid Flowpath Heat Tracing Weekly Test. Caused by Known Deficiency in Design of Sys Resulting in Inability to Maintain Min Temp Necessary During Startup | | | 05000346/LER-1980-006-03, /03L-0:on 800112,found Fiberglass Insulation Stuffed Into Open Wall Ventilator Between Water Treatment Bldg & Svc Water Valve Room,Causing Fire Damper to Be Inoperable.Figerglass Removed | /03L-0:on 800112,found Fiberglass Insulation Stuffed Into Open Wall Ventilator Between Water Treatment Bldg & Svc Water Valve Room,Causing Fire Damper to Be Inoperable.Figerglass Removed | | | 05000346/LER-1980-006, Forwards LER 80-006/03L-0 | Forwards LER 80-006/03L-0 | | | 05000346/LER-1980-007, Forwards LER 80-007/03L-0 | Forwards LER 80-007/03L-0 | | | 05000346/LER-1980-007-03, /03L-0:on 800116,ref Position Verification for Group 5,rod 11,was Made 1-h & 40 Minutes Late.Caused by Operator Oversight Due to Lack of Adequate Reminder Sys. Multiple Timer Sys Will Prevent Recurrence | /03L-0:on 800116,ref Position Verification for Group 5,rod 11,was Made 1-h & 40 Minutes Late.Caused by Operator Oversight Due to Lack of Adequate Reminder Sys. Multiple Timer Sys Will Prevent Recurrence | | | 05000346/LER-1980-008-03, Gap Discovered in Wall Where Five two-inch Conduits Go from Electrical Penetration Room 2 to Cable room.Six-inch Gap Around Ventilation Duct Also Found.Caused by Improper Initial Installation | Gap Discovered in Wall Where Five two-inch Conduits Go from Electrical Penetration Room 2 to Cable room.Six-inch Gap Around Ventilation Duct Also Found.Caused by Improper Initial Installation | | | 05000346/LER-1980-008, Forwards Revised LER 80-008/03L-1 | Forwards Revised LER 80-008/03L-1 | | | 05000346/LER-1980-009, Forwards LER 80-009/03L-0 | Forwards LER 80-009/03L-0 | | | 05000346/LER-1980-009-03, /03L-0:on 800122,discovered That NI-7 Indication on Computer Group 38 Was Reading Less than Heat Balance Power,Putting NI-7 Below Instrumentation Operability Limit Line.Caused by Extremely Tight Calibr Band at 100% Power | /03L-0:on 800122,discovered That NI-7 Indication on Computer Group 38 Was Reading Less than Heat Balance Power,Putting NI-7 Below Instrumentation Operability Limit Line.Caused by Extremely Tight Calibr Band at 100% Power | | | 05000346/LER-1980-010-01, /01T-0:on 800214,reanalysis of RCS Pipe Restraints Per IE Insp Rept 50-346/79-23 Revealed Design Deficiency on Two Reactor Coolant Hot Leg Pipe Whip Restraints at Top of Each RCS Hot Leg.Caused by Design Error | /01T-0:on 800214,reanalysis of RCS Pipe Restraints Per IE Insp Rept 50-346/79-23 Revealed Design Deficiency on Two Reactor Coolant Hot Leg Pipe Whip Restraints at Top of Each RCS Hot Leg.Caused by Design Error | | | 05000346/LER-1980-010, Forwards LER 80-010/01T-0 | Forwards LER 80-010/01T-0 | | | 05000346/LER-1980-011, Forwards LER 80-011/03L-0 | Forwards LER 80-011/03L-0 | | | 05000346/LER-1980-011-03, /03L-0:on 800131,during Normal Operation, Operations Personnel Received Half Trip on Steam & Feedwater Rupture Control Sys Channels 1/3.Caused by Spurious Trip from +25 Volt Dc Power Supply PS03 in Sglic Channel 1 | /03L-0:on 800131,during Normal Operation, Operations Personnel Received Half Trip on Steam & Feedwater Rupture Control Sys Channels 1/3.Caused by Spurious Trip from +25 Volt Dc Power Supply PS03 in Sglic Channel 1 | | | 05000346/LER-1980-012-03, /03L-0:on 800201,operator Noticed Loss of Control Room Position Indication for Letdown Cooler Isolation Valve MU2A.Caused by Design Deficiency.Apparently,Someone Brushed Up Against Disconnect Breaker Switch.Switch Reposition | /03L-0:on 800201,operator Noticed Loss of Control Room Position Indication for Letdown Cooler Isolation Valve MU2A.Caused by Design Deficiency.Apparently,Someone Brushed Up Against Disconnect Breaker Switch.Switch Repositioned | | | 05000346/LER-1980-012, Forwards LER 80-012/03L-0 | Forwards LER 80-012/03L-0 | | | 05000346/LER-1980-013, Forwards LER 80-013/03L-0 | Forwards LER 80-013/03L-0 | | | 05000346/LER-1980-013-03, /03L-0:on 800208,w/reactor Startup in Progress, Personnel Noted Control Rod 5-11 Absolute Position Indication Was Not Responding.Caused by Blown Fuse F14 in Position Ref Panel | /03L-0:on 800208,w/reactor Startup in Progress, Personnel Noted Control Rod 5-11 Absolute Position Indication Was Not Responding.Caused by Blown Fuse F14 in Position Ref Panel | | | 05000346/LER-1980-014, Forwards LER 80-014/03L-0 | Forwards LER 80-014/03L-0 | | | 05000346/LER-1980-014-03, /03L-0:on 800208,pressurizer Sample Sys Containment Isolation Valve RC240B Failed to Close Twice. Caused by Improper Torque Switch Setting & Stripped Screw on Closing Contactor.Settings Readjusted & Switch Replaced | /03L-0:on 800208,pressurizer Sample Sys Containment Isolation Valve RC240B Failed to Close Twice. Caused by Improper Torque Switch Setting & Stripped Screw on Closing Contactor.Settings Readjusted & Switch Replaced | | | 05000346/LER-1980-015, Forwards LER 80-015/03L-0 | Forwards LER 80-015/03L-0 | | | 05000346/LER-1980-015-03, /03L-0:on 800210,during Normal Startup,Control Rod 5-11 Absolute Position Indication Declared Inoperable.Caused by Numerous Asymmetric Rod Alarms.Data from Current Failure Evaluated | /03L-0:on 800210,during Normal Startup,Control Rod 5-11 Absolute Position Indication Declared Inoperable.Caused by Numerous Asymmetric Rod Alarms.Data from Current Failure Evaluated | | | 05000346/LER-1980-016, Forwards LER 80-016/03L-0 | Forwards LER 80-016/03L-0 | | | 05000346/LER-1980-016-03, /03L-0:on 800213,while Reviewing Station Log,Shift Foreman Discovered That Containment Airlock Seal Leakage Test Had Not Been Performed After Last Entry Into Containment During Startup.Caused by Procedural Inadequacy | /03L-0:on 800213,while Reviewing Station Log,Shift Foreman Discovered That Containment Airlock Seal Leakage Test Had Not Been Performed After Last Entry Into Containment During Startup.Caused by Procedural Inadequacy | | | 05000346/LER-1980-017-03, /03L-0:on 800217,operations Personnel Noted That Safety Features Actuation Sys Channel 3 Borated Water Storage Tank Level Indication Was Six Feet Higher than Other Meters.Caused by Freezing of Transmitter Sensing Line | /03L-0:on 800217,operations Personnel Noted That Safety Features Actuation Sys Channel 3 Borated Water Storage Tank Level Indication Was Six Feet Higher than Other Meters.Caused by Freezing of Transmitter Sensing Line | | | 05000346/LER-1980-017, Forwards LER 80-017/03L-0 | Forwards LER 80-017/03L-0 | | | 05000346/LER-1980-018-03, /03L-0:on 800226,safety Features Actuation Sys Channel 3 Borated Water Storatge Tank Level Indication Was Discovered Reading Four Feet Higher than Other Three Channels.Caused by Inadequate Design of Freeze Protection | /03L-0:on 800226,safety Features Actuation Sys Channel 3 Borated Water Storatge Tank Level Indication Was Discovered Reading Four Feet Higher than Other Three Channels.Caused by Inadequate Design of Freeze Protection | | | 05000346/LER-1980-018, Forwards LER 80-018/03L-0 | Forwards LER 80-018/03L-0 | | | 05000346/LER-1980-019, Forwards LER 80-019/01T-0 | Forwards LER 80-019/01T-0 | | | 05000346/LER-1980-019-01, /01T-0:on 800325 Reactor Flux/Flow Trip Setpoints Were Not Verified to Be Properly Reset within 4-h of Manual Shutdown of Rcp.Caused by Attention Given to Feedwater Swings.Trip Setpoints Verified Later | /01T-0:on 800325 Reactor Flux/Flow Trip Setpoints Were Not Verified to Be Properly Reset within 4-h of Manual Shutdown of Rcp.Caused by Attention Given to Feedwater Swings.Trip Setpoints Verified Later | | | 05000346/LER-1980-020, Forwards LER 80-020/03L-0 | Forwards LER 80-020/03L-0 | | | 05000346/LER-1980-020-03, /03L-0:on 800306,control Operator Noted No Control Room Indication for Containment Vacuum Relief Isolation Valve CV5072.Caused by Breaker BE1139 Being Closed,Probably Resulting from Someone Bumping Into Breaker | /03L-0:on 800306,control Operator Noted No Control Room Indication for Containment Vacuum Relief Isolation Valve CV5072.Caused by Breaker BE1139 Being Closed,Probably Resulting from Someone Bumping Into Breaker | | | 05000346/LER-1980-021, Forwards LER 80-021/03L-0 | Forwards LER 80-021/03L-0 | | | 05000346/LER-1980-021-03, /03L-0:on 800313,during Diesel Fire Protection Pump Weekly Test,Pump Could Not Be Stopped W/Control Button. Once Stopped,Pump Could Not Be Started.Cause Not Determined by Scheme Check.Retrial of Pump Proved Successful | /03L-0:on 800313,during Diesel Fire Protection Pump Weekly Test,Pump Could Not Be Stopped W/Control Button. Once Stopped,Pump Could Not Be Started.Cause Not Determined by Scheme Check.Retrial of Pump Proved Successful | | | 05000346/LER-1980-022-03, /03L-0:on 800317,operations Personnel Noticed Loss of Control Room Indication for Containment Dihydrogen Analyzer 2 Discharge Line Valve CV5010E.Caused by Const Personnel Accidentally Opening Breaker | /03L-0:on 800317,operations Personnel Noticed Loss of Control Room Indication for Containment Dihydrogen Analyzer 2 Discharge Line Valve CV5010E.Caused by Const Personnel Accidentally Opening Breaker | | | 05000346/LER-1980-022, Forwards LER 80-022/03L-0 | Forwards LER 80-022/03L-0 | | | 05000346/LER-1980-023, Forwards LER 80-023/03L-0 | Forwards LER 80-023/03L-0 | | | 05000346/LER-1980-023-03, /03L-0:on 800327,discovered That Control Rod Groups 3 & 4 Were Moving in on Their Own.Group 3 Was 0% Withdrawn.Group 4 Was 90% Withdrawn.Caused by Component Failure.Component Replaced | /03L-0:on 800327,discovered That Control Rod Groups 3 & 4 Were Moving in on Their Own.Group 3 Was 0% Withdrawn.Group 4 Was 90% Withdrawn.Caused by Component Failure.Component Replaced | | | 05000346/LER-1980-024-03, /03L-0:on 800327,following Normally Initiated Reactor Trip,Auxiliary Feed Pump Turbine 1-2 Main Steam Isolation Valve MS-107 Closed.Cause Unknown.Further Investigation of Valve & Operator Will Be Pursued | /03L-0:on 800327,following Normally Initiated Reactor Trip,Auxiliary Feed Pump Turbine 1-2 Main Steam Isolation Valve MS-107 Closed.Cause Unknown.Further Investigation of Valve & Operator Will Be Pursued | | | 05000346/LER-1980-024, Forwards LER 80-024/03L-0 | Forwards LER 80-024/03L-0 | | | 05000346/LER-1980-025-03, /03X-1:on 800330,control Rod Group 5,rod 11 Absolute Position Indication Declared Inoperable.Caused by Fluctuating Signals Resulting in Numerous Asymmetric Rod Alarms Due to Defective Reed Switch Assemblies | /03X-1:on 800330,control Rod Group 5,rod 11 Absolute Position Indication Declared Inoperable.Caused by Fluctuating Signals Resulting in Numerous Asymmetric Rod Alarms Due to Defective Reed Switch Assemblies | | | 05000346/LER-1980-025, Forwards LER 80-025/03X-1 | Forwards LER 80-025/03X-1 | |
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