LER-1979-106, /01T-1:on 791112,while Performing Calculations for IE Bulletin 79-02,11 Seismic Hangers Found Not as Conservative as Required by Design Criteria.Caused by Design Errors by Itt Grinnell in Initial Calculations |
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U.S. NUCLE AR REGULATCRY COMMISSION 60 FORM 36G m
LICENSEE EVENT REPORT c,
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8 60 68 DOCKET NUVSER 68 tn EVENT OATE 74 75 REPORT DATE 80 EVENT OESCRIPTION AND PROBABLE CONSEQUENCES h
@ l While perfohiing calculations for I. E.Bulletin 79-02. ITT Grinnell personnel dis-I l
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( g l covered the design of 11 seismic hangers was not as conservative as was required On July 25 further I
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@ l analysis of base plate ficxibility found that the anchor bolts for pipe supports
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@ l support structure for anchors A-55, A-61 A-79_, A-80, and A-83 had a factor of I@ l safety of less than 2. This finding is reportable under T.S. 6.9.1.8.i.
(NP-32-79-13 1
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lg;7; l prior to the unit returning to operation. The items reported July, 1980, were the re-l 1
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TOLEDO EDISON COMPANY DAVIS-BESSE NUCLEAR POWER STATION UNIT ONE SUPPLEMENTAL INFORMATION FOR LER NP-32-79-13 DATE OF EVENT: November 12, 1979 FACILITY: Davis-Besse Unit 1 IDENTIFICATION OF OCCURRENCE:
Design of eleven seismic supports was not as conserva-tive as required.
l Conditions Prior to Occurrence:
The unit was in Mode 5, with Power (MWT) = 0, and Load (Gross MWE) = 0.
Description of Occurrence: While performing calculations for IE Bulletin 79-02, ITT Grinnell personnel discovered the design of eleven seismic hangers was not as conder-i vative as was required by the design criteria used by ITT Grinnell.
Four of the hangers did not meet the NRC. criteria for pipe support operability. On five other supports, the slenderness ratio exceeded the design criteria of 200 used by ITT Grinnell. The remaining two supports were analyzed to have a maximum deflection of approximately.5 inches which could result in stresses on the piping in excess of the design criteria of ITT Grinnell. These analyses were performed assuming the worst case design base earthquake loading.
On July 25, 1980, while performing the base plate flexibility analysis, pipe supports 1
41-HBC-36-H3 on service water, 33A-GCB-8-H1 on decay heat, and H-17, SR-31, SR-32, and SR-39 on main feedwater were analyzed. The results showed that the anchor bolts had a factor of safety less than two.
Also the common support structure (i.e., one support for five anchors) for anchors A-55 high pressure injection, A-61 low pressure injection, A-79, A-80, and A-83 i I containment spray was analyzed for base plate flexibility. The results showed that the anchor bolts had a factor of safety less than two.
Further information on the affected hangers is contained on Attachment 1.
Since more than one part of a redundant system was affected, this incident is being reported in cecordance with Technical Specification 6.9.1.8.1.
These design deficiencies were discovered while the unit was in cold shutdown during a unit outage.
i Designation of Apparent Cause of Occurrence:
The cause of this occurrence was design errors by ITT Grinnell in the initial calculations of the stresses and deflections in these hangers. These design errors were discovered while calculating base plate forces cad moments for the analysis required by IE Bulletin 79-02.
The errors in the original design were random and not due to a general deficiency in the original design method.
Items reported July 25, 1980,- were the result of a change in the design criteria as to what constitutes a rigid base plate. The base plates for these supports were 1
originally analyzed as rigid base plates and under the new criteria are now considered flexible.
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TOLEDO EDISON COMPANY DAVIS-BESSE NUCLEAR POWER STATION UNIT ONE PAGE 2 SUPPLEMENTAL INFORMATION FOR LER NP-32-79-13 Analysis of Occurrence:
There was no danger to the health and safety of the public cr to station personnel. These supports are not required for normal system performance but are required only to protect the systems from a worst case condition of maximum carthquake loading.
The affected systems have been re-analyzed taking into account the non-conservative cupport designs.
These analyses show that all affected safety systems would have performed their safety function if a design basis accident had occurred.
Corrective Action
All affected hanger modifications were completed by 1200 hours0.0139 days <br />0.333 hours <br />0.00198 weeks <br />4.566e-4 months <br /> en November 15, 1979, prior to the unit returning to operation.
Details on the work performed, the applicable facility change request (identical to work order number), and the location of hanger is contained in Attachment 1.
l t
The design of all Q-listed supports attached to concrete on 2 " and larger piping l;
(over 1000 supports) have been reviewed during work performed while responding to j
IE Bulletin 79-02.
Supports on piping smaller than 2b" were not designed by ITT
~
Crinnell.
The following items reported July 25, 1980, will be modified by the following FCRs:
41-HBC-3 6-1123 by FCR 80-093 supplement 14 33A-GCB-8-111 by FCR 80-088 supplement 12 1
SR-32 & SR39 by FCR 80-125 supplement 2 H-17 & SR31 by FCR 80-125 supplement 3 A-55, A-61, A-79, by FCR 80-089 supplement 9 A-80, A-83 These discrepancies will be corrected prior to startup from the current refueling outage. Attachment I will be updated when that work is complete.
Failure Data:
There has been one previously reported similar occurrence, see Licensee Event Report NP-32-79-08.
LER #79-106 m m
ATTACHMENT 1 LICENSEE EVENT REPORT NP-32-79-13 FCR/W.O.
HANGER NO.
LOCATION CONTROLLING ITEM WORK PERFORMED 79-379 41-HBC44-HS Service Water Supply to Emer-SF < 2 1/4" x 5" cover bar welded to gency Core Cooling Room. Cooler channel 1-3 79-380 33A-HCB2-H44 Borated Water Storage Tank SF < 2 3" x 3" x 3/8" angle iron added Supply to E=crgency Core Cooling System 1 79-331 34-CCBS-H17 Containment Spray Pump 1-1 Deflection ~.5" Mded 2-1/2" pipe and 3/4" x.
discharge x 7" Cusset plates79-381 34-HCC38-H19 Containment Spray Pump 1-1 Deflection ~.5" Added 2-1/2" pipe and 3/4" x 5" Recirculation Test Line x 7" Gusset plates79-387 34-EBD19-H79 Main Steam (upstream of Slenderness ratio > 200 1/2" x 4-1/2" stiffener bar MS-107A) added to I-beam, replaced kickers with W4 x 13 I-beam 79-388 6C-EBD14-H43 Auxiliary Feed Pump 1-2 Slenderness ratio > 200 Replaced kicker with 4" x 4" x Discharge 3/8" structural tubing 79-389 31-CCB21-H22 Letdown Delay Coil SF < 2 1/2" x 5" cover bar added 79-390 33A-GCB4-H5 High Pressure Injection Slenderness ratio > 200 3/8" x 3-1/2" bar added to 1-2 Suction flanges79-391 34-6CB S-il2 Containment Spray Pump 1-2 Slenderness ratio > 200 3/8" x 4-1/2" stiffener plate Discharge added to kicker 3/8" x 4-1/2" stiffener plate 79-392 36-HBC39-H8 Component Cooling Water Slenderness ratio y 200 Supply to Letdown Coolers added to kicker 79-393 41-HBC36-H26 Service Water Outlet of SF < 2 1/4" x 2-3/4" stiffener plate Component Cooling Water added, W6 x 15 beam added Heat Exchanger 1-3 LER #79-106
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| 05000346/LER-1979-001-03, /03L-0 on 790102:monthly Functional Test Not Performed on Reactor Protection Sys Channel 2 within Allowable Time.Caused by Breakdown in Communications Between Testing Personnel & Test Coordinator | /03L-0 on 790102:monthly Functional Test Not Performed on Reactor Protection Sys Channel 2 within Allowable Time.Caused by Breakdown in Communications Between Testing Personnel & Test Coordinator | | | 05000346/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000346/LER-1979-002-03, /03L-1 on 790102:main Steam Valves 106 & 106A Failed to Open,Resulting in Auxiliary Feed Pump Afp 1-1 Being Taken Out of Operation.Caused by Dirt Buildup on Valve Stems as Result of New Const | /03L-1 on 790102:main Steam Valves 106 & 106A Failed to Open,Resulting in Auxiliary Feed Pump Afp 1-1 Being Taken Out of Operation.Caused by Dirt Buildup on Valve Stems as Result of New Const | | | 05000346/LER-1979-002, Forwards LER 79-002/03L-1 | Forwards LER 79-002/03L-1 | | | 05000346/LER-1979-003-03, /03L-0 on 790104:control Room Emergency Ventilation Sys Damper HV5311E Inoperable.Caused by Leaking Pneumatic Operator.New Operator Installed.Damper Operated & Tested for Response Time & Declared Operable | /03L-0 on 790104:control Room Emergency Ventilation Sys Damper HV5311E Inoperable.Caused by Leaking Pneumatic Operator.New Operator Installed.Damper Operated & Tested for Response Time & Declared Operable | | | 05000346/LER-1979-003, Forwards LER 79-003/03L-0 | Forwards LER 79-003/03L-0 | | | 05000346/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000346/LER-1979-004-03, /03L-0 on 790105:failure to Post Guards at Entrance to Containment During Periods of Free Access. Caused by Personnel Error.Special Order 84 Revised to Require Posting of Guards | /03L-0 on 790105:failure to Post Guards at Entrance to Containment During Periods of Free Access. Caused by Personnel Error.Special Order 84 Revised to Require Posting of Guards | | | 05000346/LER-1979-005, Forwards LER 79-005/03L-0 | Forwards LER 79-005/03L-0 | | | 05000346/LER-1979-005-03, /03L-0 on 790106:during Surveillance Testing, Borated Water Storage Tank Level Bistable Was Tripped;Valves DH9A Opened & DH7A Closed.Caused by Component Failure of Output Relay K51A & Instrument Drift | /03L-0 on 790106:during Surveillance Testing, Borated Water Storage Tank Level Bistable Was Tripped;Valves DH9A Opened & DH7A Closed.Caused by Component Failure of Output Relay K51A & Instrument Drift | | | 05000346/LER-1979-006-03, /03L-0:on 790105,reviewer Noted 781228 Record of Continuous Alarm at Contact Data Record Point F018.Panel C4705 Not Reset.Caused by Failure of Indicator Lights on Panel C4705.Panel Reset,Clearing F018.Surveillance Modified | /03L-0:on 790105,reviewer Noted 781228 Record of Continuous Alarm at Contact Data Record Point F018.Panel C4705 Not Reset.Caused by Failure of Indicator Lights on Panel C4705.Panel Reset,Clearing F018.Surveillance Modified | | | 05000346/LER-1979-006, Forwards LER 79-006/03L-0 | Forwards LER 79-006/03L-0 | | | 05000346/LER-1979-007-03, /03L-0 on 790110:during Performance of Surveillance Test,Channel 2 of Containment Hydrogen Analyzer Was Found Inoperable.Caused by Defective Zener Diode in Millivolt Converter | /03L-0 on 790110:during Performance of Surveillance Test,Channel 2 of Containment Hydrogen Analyzer Was Found Inoperable.Caused by Defective Zener Diode in Millivolt Converter | | | 05000346/LER-1979-007, Forwards LER 79-007/03L-0 | Forwards LER 79-007/03L-0 | | | 05000346/LER-1979-008, Forwards LER 79-008/03L-0 | Forwards LER 79-008/03L-0 | | | 05000346/LER-1979-008-03, /03L-0 on 790109:during Surveillance Testing, Containment Recirculation Fan 1-1 Failed to Run.Cause Attributed to Buildup of non-conductive Film on Auxiliary Controller Contacts | /03L-0 on 790109:during Surveillance Testing, Containment Recirculation Fan 1-1 Failed to Run.Cause Attributed to Buildup of non-conductive Film on Auxiliary Controller Contacts | | | 05000346/LER-1979-009, Forwards LER 79-009/03L-0 | Forwards LER 79-009/03L-0 | | | 05000346/LER-1979-009-03, /03L-0:on 790112,power to Vital Bus Y2 Lost. False Integrated Control Sys Signal Resulted in Reactor & Full Steam & Feedwater Rupture Control Sys Trip.Caused by Blown 125 Volt DC Fuse to Inverter | /03L-0:on 790112,power to Vital Bus Y2 Lost. False Integrated Control Sys Signal Resulted in Reactor & Full Steam & Feedwater Rupture Control Sys Trip.Caused by Blown 125 Volt DC Fuse to Inverter | | | 05000346/LER-1979-010-03, /03L-0:on 790112,Sys 7 Data Logger Experienced Core Dump,Voiding Computer Memory Bank Which Rendered Remote Monitoring of Fire Detection Sys Inoperable & Placed Unit in Action Statement of Tech Spec 3.3.3.8.Cause Unknown | /03L-0:on 790112,Sys 7 Data Logger Experienced Core Dump,Voiding Computer Memory Bank Which Rendered Remote Monitoring of Fire Detection Sys Inoperable & Placed Unit in Action Statement of Tech Spec 3.3.3.8.Cause Unknown | | | 05000346/LER-1979-010, Forwards LER 79-010/03L-0 | Forwards LER 79-010/03L-0 | | | 05000346/LER-1979-011-03, /03L-0:on 790115,reactor Coolant Pump 1-2-2 Started W/Incorrect Breaker Alignment,Causing Low Voltage Relays to Trip Which de-energized Both 4.16 Kv Essential Buses C1 & D1.Caused by Personnel Error | /03L-0:on 790115,reactor Coolant Pump 1-2-2 Started W/Incorrect Breaker Alignment,Causing Low Voltage Relays to Trip Which de-energized Both 4.16 Kv Essential Buses C1 & D1.Caused by Personnel Error | | | 05000346/LER-1979-011, Forwards LER 79-011/03L-0 | Forwards LER 79-011/03L-0 | | | 05000346/LER-1979-012-03, /03L-0:on 790116,during Surveillance Testing,Heat Traced Line Temp Measurement Points Below 105 F Limit.Caused by Injection of Makeup (Flush) Water After Boron Injection at Temp Lower than 105 F.Tests Rerun Satisfactorily | /03L-0:on 790116,during Surveillance Testing,Heat Traced Line Temp Measurement Points Below 105 F Limit.Caused by Injection of Makeup (Flush) Water After Boron Injection at Temp Lower than 105 F.Tests Rerun Satisfactorily | | | 05000346/LER-1979-012, Forwards LER 79-012/03L-0 | Forwards LER 79-012/03L-0 | | | 05000346/LER-1979-013, Forwards LER 79-013/03L-0 | Forwards LER 79-013/03L-0 | | | 05000346/LER-1979-013-03, /03L-0:on 790116,when Makeup Pump 1 Started for Surveillance testing,1/2 Inch Nipple at Discharge of Attached Gear Driven Lube Oil Pump Failed,Resulting in Oil Spray Which Required Pump Shutdown | /03L-0:on 790116,when Makeup Pump 1 Started for Surveillance testing,1/2 Inch Nipple at Discharge of Attached Gear Driven Lube Oil Pump Failed,Resulting in Oil Spray Which Required Pump Shutdown | | | 05000346/LER-1979-014-03, /03L-0:on 790116,during Shutdown,Boric Acid Addition Tanks (Baat) Total Vol 3-1/3% Below Tech Spec 3.1.2.9 Requirements.Caused by Reduced Baat Vol After Completion of Required Testing Followed by RCS Boration | /03L-0:on 790116,during Shutdown,Boric Acid Addition Tanks (Baat) Total Vol 3-1/3% Below Tech Spec 3.1.2.9 Requirements.Caused by Reduced Baat Vol After Completion of Required Testing Followed by RCS Boration | | | 05000346/LER-1979-014, Forwards LER 79-014/03L-0 | Forwards LER 79-014/03L-0 | | | 05000346/LER-1979-015-03, /03L-0:on 790117,core Flood Tank 1-2 Isolation Valve CF1A Would Not Close by Remote Operation.Caused by Loose Set Screw.Cracked Pinion Gear & Associated Key Replaced Per Maint Work Order 78-2928 | /03L-0:on 790117,core Flood Tank 1-2 Isolation Valve CF1A Would Not Close by Remote Operation.Caused by Loose Set Screw.Cracked Pinion Gear & Associated Key Replaced Per Maint Work Order 78-2928 | | | 05000346/LER-1979-015, Forwards LER 79-015/03L-0 | Forwards LER 79-015/03L-0 | | | 05000346/LER-1979-016-03, /03L-0:on 790124,emergency Lock Failed Leak Rate Test While Unit in Mode 5.Caused by Loosening of Shaft Seal (Teflon Packing) Due to Routine Use of Escape Lock.Packing Will Be Replaced During Next Convenient Outage | /03L-0:on 790124,emergency Lock Failed Leak Rate Test While Unit in Mode 5.Caused by Loosening of Shaft Seal (Teflon Packing) Due to Routine Use of Escape Lock.Packing Will Be Replaced During Next Convenient Outage | | | 05000346/LER-1979-016, Forwards LER 79-016/03L-0 | Forwards LER 79-016/03L-0 | | | 05000346/LER-1979-017-03, /03L-0:on 790130,photoelectric Smoke Detector Ds 8605-E in Emergency Diesel Generator 1-1 Area Not Functional.Caused by Failure of Detector.New Detector Ordered & Fire Watch Patrol Established in Area | /03L-0:on 790130,photoelectric Smoke Detector Ds 8605-E in Emergency Diesel Generator 1-1 Area Not Functional.Caused by Failure of Detector.New Detector Ordered & Fire Watch Patrol Established in Area | | | 05000346/LER-1979-017, Forwards LER 79-017/03L-0 | Forwards LER 79-017/03L-0 | | | 05000346/LER-1979-018, Forwards LER 79-018/03L-0 | Forwards LER 79-018/03L-0 | | | 05000346/LER-1979-018-03, /03L-0:on 790130,valves SP17A2 & SP17B2 Lifted Below Setpoint Range & Declared Inoperable.Caused by Loose Spindle on Main Steam Line Code Safety Valve SP17A2.Valve SP17A2 Gagged & SP17B2 Tested Satisfactorily | /03L-0:on 790130,valves SP17A2 & SP17B2 Lifted Below Setpoint Range & Declared Inoperable.Caused by Loose Spindle on Main Steam Line Code Safety Valve SP17A2.Valve SP17A2 Gagged & SP17B2 Tested Satisfactorily | | | 05000346/LER-1979-019-03, /03L-0 on 790129:suction & Discharge Valves on Containment Spray Pump Were Closed.Caused by Personnel Error | /03L-0 on 790129:suction & Discharge Valves on Containment Spray Pump Were Closed.Caused by Personnel Error | | | 05000346/LER-1979-019, Forwards LER 79-019/03L-0 | Forwards LER 79-019/03L-0 | | | 05000346/LER-1979-020-03, /03L-0 on 790205:10 of 18 Main Steam Safety Valves Found Outside Setpoint Range.Believed Caused by Changing Ambient Conditions at Valve Locations.Valves Adjusted & Retested Satisfactorily | /03L-0 on 790205:10 of 18 Main Steam Safety Valves Found Outside Setpoint Range.Believed Caused by Changing Ambient Conditions at Valve Locations.Valves Adjusted & Retested Satisfactorily | | | 05000346/LER-1979-020, Forwards LER 79-020/03L-0 | Forwards LER 79-020/03L-0 | | | 05000346/LER-1979-021-03, /03L-0 on 790205:containment High Pressure Alarms Were Received & Safety Features Actuation Sys Channel 2 Erroneously Tripped.Cause Unknown.No Deficiencies Found from Surveillance Tests.Channel Returned to Operation | /03L-0 on 790205:containment High Pressure Alarms Were Received & Safety Features Actuation Sys Channel 2 Erroneously Tripped.Cause Unknown.No Deficiencies Found from Surveillance Tests.Channel Returned to Operation | | | 05000346/LER-1979-021, Forwards LER 79-021/03L-0 | Forwards LER 79-021/03L-0 | | | 05000346/LER-1979-022, Forwards LER 79-022/03L-0 | Forwards LER 79-022/03L-0 | | | 05000346/LER-1979-022-03, /03L-0 on 790208:diesel Fire Pump Battery Electrolyte Level in Four Cells Was Below Top of Cell Plates.Caused by Procedural Error.Levels Restored,Pump Declared Operable & Unit Removed from Action Statement | /03L-0 on 790208:diesel Fire Pump Battery Electrolyte Level in Four Cells Was Below Top of Cell Plates.Caused by Procedural Error.Levels Restored,Pump Declared Operable & Unit Removed from Action Statement | | | 05000346/LER-1979-023, Forwards LER 79-023/01T-0 | Forwards LER 79-023/01T-0 | | | 05000346/LER-1979-023-01, /01T-0 on 790228:Startup Transformer 01 Taken Out of Svc;Surveillance Tests Not Performed within One Hour, Contrary to Tech Spec Requirements.Caused by Personnel Error.Testing Completed as Soon as Error Realized | /01T-0 on 790228:Startup Transformer 01 Taken Out of Svc;Surveillance Tests Not Performed within One Hour, Contrary to Tech Spec Requirements.Caused by Personnel Error.Testing Completed as Soon as Error Realized | | | 05000346/LER-1979-024, Forwards LER 79-024/03L-0 | Forwards LER 79-024/03L-0 | | | 05000346/LER-1979-024-03, /03L-0 on 790214:fire Alarm Panel C4706 Signaled, Indicating Laundry Room Detector DS8630 as Source.Detector Declared Inoperable as No Cause for Signal Found.Cause of Event Undetermined.Possibly Due to Gases or Dust | /03L-0 on 790214:fire Alarm Panel C4706 Signaled, Indicating Laundry Room Detector DS8630 as Source.Detector Declared Inoperable as No Cause for Signal Found.Cause of Event Undetermined.Possibly Due to Gases or Dust | | | 05000346/LER-1979-025-03, /03L-0 on 790213:Ohio Edison Relay Testing Actuated Transfer Trip Receiving Relay & Tripped Switchyard Breakers.Caused by Failure of Util to Notify Toledo Edison Before Performing Relay Testing | /03L-0 on 790213:Ohio Edison Relay Testing Actuated Transfer Trip Receiving Relay & Tripped Switchyard Breakers.Caused by Failure of Util to Notify Toledo Edison Before Performing Relay Testing | | | 05000346/LER-1979-025, Forwards LER 79-025/03L-0 | Forwards LER 79-025/03L-0 | |
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