LER-1980-027, /03L-0:on 80823,during Monthly surveillance,42-11 Test Control Rod Could Not Be Withdrawn After Partial Insertion.Caused by Closed Drive Withdraw Riser Isolation Valve CRD-102.Valve Opened & Rod Was Operable |
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| 2631980027R03 - NRC Website |
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NRC FORM 366 U.S. NUCLEAR RnGULATORY COMMISSION l
(7 77)
LICENSEE EVENT REPORT CONTROL BLOCK: l l
l l
l l lh (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1 6
f0Til l M i N l M l N l Pl 1l@l 0l 0l -l 0l 0l q q q-l0l0l@l4l 1l 1l 1l 1l@l 'l lg 7
8 9 LICENSEE CODE 14 lb LICENSE NuusER 26 26 L6 CENSE TYPE JO b7 C AT b8 CON'T IOIiI
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7 8
60 61 DOCKET NUMBER 68 EVENT DATE 74 75 REPORT DATE 60 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h FOT21 l During a monthly surveillance test control rod 42-11 was unable to be withdrawn I
iO i3i I after partially inserting it.
The corresnanding Hydraulic Control Unit was checkedi I o l41 l and tne Drive Withdraw Riser Isolation Valve. CRD-102. was found closed. With l
I Ioisl I this valve closed control rod would not scram properiv.
All other control rods 1
10 is I l onerational. Event renneted ner T A 6. 7. R 9. r-Frent hnd no effect on nublic l
l 0 l 7 l 1 health and safety. No pTevious similar occurrences.
I 101811 I
CODE SUSCODE COMPONENT CODE SUB ODE SU E
CODE lO191 lR lB l@ [A_j@ lB l@ lV l A l L lV l E l Xl@ gg lD l @
7 8
9 to 11 12 13 18 19 20 SEOUENTIAL OCCURRENCE REPORT REVISION ggp EVENTYEAR R EPORT NO.
CODE TYPE N O.
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. l-l l 012l71 l/l l0131 lLI l_]
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_ 21 22 23 24 26 27 28 M
30 31 32 HOURS IT D FOR B.
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lGl0]8l0lg 33 34 3b 36 31 40 43 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h g l Operator left CRD-102 closed when HCU 42-11 was isolated for recharcine the Scram l m i Accumulator with Nitrocen Aucust 9, 1980. Valve was opened and rod denonstrated I
i 2 I operable.
Procedure will be revised to provide additional assurance of nrener i
Li_LU l valve nositionine.
I mI STA $
% POWER OTHER STATUS Dis O R COVERY DJSCRIPTION Ii is I [Ejg l0 l 7 l Oj@l NA l
lB[gl Operator 0$servation j
80 ACTivtTY CO TENT Li1LI W @D OF RELEASElZJ@l_. NA l
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RELE ASE AMOUNT OF ACTIVITY LOCATION OF RELEASE 7
8 9 10 11 44 45 go PERSONNEL EXPOSURES NUYBE R TYPE DESCRIPTION -
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PERsONNE L iNeuWits OEsCRiPnON@
7.uvaER li t a l l 0 ! O l 01@l NA l
F 8 9 11 12 60 Loss OF OR DAMAGE TO FACILITY R [Z_j @ l l
7 8 9 10 go NRC USE oNLY [TTTI ITE@lDESCR'PTION I
NA l
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S 9 10 68 69 80 E NAME OF PREPARER PHONE:
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| 05000263/LER-1980-006-03, /03L-0:on 800226,during Refueling Outage,Seven of Main Steam Line Area Temp Switches Found to Trip Above Required Level.Caused by Setpoint Drift.Switches Recalibr | /03L-0:on 800226,during Refueling Outage,Seven of Main Steam Line Area Temp Switches Found to Trip Above Required Level.Caused by Setpoint Drift.Switches Recalibr | | | 05000263/LER-1980-006, Forwards LER 80-006/03L-0 | Forwards LER 80-006/03L-0 | | | 05000263/LER-1980-007-01, /01T-0:on 800303,during Refuel Shutdown,Cable Routing for HPCI & Automatic Depressurization Sys Cables Identified Lack of Physical Separation Between Automatic Depressurization Sys Cables & Ones for Div of HPCI Sensors | /01T-0:on 800303,during Refuel Shutdown,Cable Routing for HPCI & Automatic Depressurization Sys Cables Identified Lack of Physical Separation Between Automatic Depressurization Sys Cables & Ones for Div of HPCI Sensors | | | 05000263/LER-1980-007, Forwards LER 80-007/01T-0 | Forwards LER 80-007/01T-0 | | | 05000263/LER-1980-011-01, /01T-0:on 800306,during Refueling Outage,Repairs to Outboard MSIV Stop Valve Revealed Flow Path Between Secondary Containment & Turbine Bldg When MSIV Poppet Was Pulled.Caused by Lack of Preventive Procedure Controls | /01T-0:on 800306,during Refueling Outage,Repairs to Outboard MSIV Stop Valve Revealed Flow Path Between Secondary Containment & Turbine Bldg When MSIV Poppet Was Pulled.Caused by Lack of Preventive Procedure Controls | | | 05000263/LER-1980-011, Forwards LER 80-011/01T-0 | Forwards LER 80-011/01T-0 | | | 05000263/LER-1980-013-01, /01T-0:on 800309,during Refueling Operations,Rod Withdrawn Block Not Received When Refueling Bridge Traversed Core.Caused by Actuating Arm Out of Adjustment.Components Readjusted & Interlocks Tested Prior to Refueling | /01T-0:on 800309,during Refueling Operations,Rod Withdrawn Block Not Received When Refueling Bridge Traversed Core.Caused by Actuating Arm Out of Adjustment.Components Readjusted & Interlocks Tested Prior to Refueling | | | 05000263/LER-1980-013, Forwards LER 80-013/01T-0 | Forwards LER 80-013/01T-0 | | | 05000263/LER-1980-015-01, /01T-0:on 800317,during Refueling Outage & Insp Required by IE Bulletin 79-01B,unqualified Splices Found in Power Cables for Inboard MSIV Solenoid Valves.Cause Not Stated.Splices Replaced W/Qualified Matls | /01T-0:on 800317,during Refueling Outage & Insp Required by IE Bulletin 79-01B,unqualified Splices Found in Power Cables for Inboard MSIV Solenoid Valves.Cause Not Stated.Splices Replaced W/Qualified Matls | | | 05000263/LER-1980-015, Forwards LER 80-015/01T-0 | Forwards LER 80-015/01T-0 | | | 05000263/LER-1980-016, Forwards LER 80-016/01T-0 | Forwards LER 80-016/01T-0 | | | 05000263/LER-1980-016-01, /01T-0:on 800327,during Refueling,Supports for SRV Pneumatic Supply Sys Would Not Meet Seismic Class I Requirements.Caused by Inadequate Design & Installation of Sys.Sys Was Upgraded to Satisfy Requirements | /01T-0:on 800327,during Refueling,Supports for SRV Pneumatic Supply Sys Would Not Meet Seismic Class I Requirements.Caused by Inadequate Design & Installation of Sys.Sys Was Upgraded to Satisfy Requirements | | | 05000263/LER-1980-017, Forwards LER 80-017/01T-0 | Forwards LER 80-017/01T-0 | | | 05000263/LER-1980-017-01, /01T-0:on 800328,Bechtel Power Corp Notified Util That Control Rod Driveline Hydraulic Piping Frame Supports Would Not Meet OBE Stress Limits.Caused by Eds Computer Code Error.Supports Modified | /01T-0:on 800328,Bechtel Power Corp Notified Util That Control Rod Driveline Hydraulic Piping Frame Supports Would Not Meet OBE Stress Limits.Caused by Eds Computer Code Error.Supports Modified | | | 05000263/LER-1980-018, Forwards LER 80-018/03L-0 | Forwards LER 80-018/03L-0 | | | 05000263/LER-1980-018-03, /03L-0:on 800411,during Routine Operator Insp, Attachment Weld of Ripple to Level Switch Float Chamber Assembly on Moisture Separator Level Switch LS-1188 Found Cracked.Caused by Improper Weld Procedure | /03L-0:on 800411,during Routine Operator Insp, Attachment Weld of Ripple to Level Switch Float Chamber Assembly on Moisture Separator Level Switch LS-1188 Found Cracked.Caused by Improper Weld Procedure | | | 05000263/LER-1980-020-03, /03L-0:on 800427,during post-maint Startup of Reactor Recirculation Sys,Inaccessible Recirculation Valve Motor Failed.Cause Not Stated.Motor Is Limitorque Type SMB-2 W/Magnetic Brake | /03L-0:on 800427,during post-maint Startup of Reactor Recirculation Sys,Inaccessible Recirculation Valve Motor Failed.Cause Not Stated.Motor Is Limitorque Type SMB-2 W/Magnetic Brake | | | 05000263/LER-1980-020, Forwards LER 80-020/03L-0 | Forwards LER 80-020/03L-0 | | | 05000263/LER-1980-021, Forwards LER 80-021/03L-0 | Forwards LER 80-021/03L-0 | | | 05000263/LER-1980-021-03, /03L-0:on 800515,during Normal Startup,Reactor Core Isolation Cooling Control Power Fuse Opened.Caused by Shorted Relay Coil in Circuit Due to Ac Relay Inadvertently Installed by Maint Personnel.Relay Replaced | /03L-0:on 800515,during Normal Startup,Reactor Core Isolation Cooling Control Power Fuse Opened.Caused by Shorted Relay Coil in Circuit Due to Ac Relay Inadvertently Installed by Maint Personnel.Relay Replaced | | | 05000263/LER-1980-022, Forwards LER 80-022/03L-0 | Forwards LER 80-022/03L-0 | | | 05000263/LER-1980-022-03, /03L-0:on 800529,primary Containment Oxygen Concentration Exceeded 5% by Weight Tech Spec Limit.Caused by Open Svc Air Isolation Valve to Drywell.Procedures Have Been Revised to Assure Proper Valve Positioning | /03L-0:on 800529,primary Containment Oxygen Concentration Exceeded 5% by Weight Tech Spec Limit.Caused by Open Svc Air Isolation Valve to Drywell.Procedures Have Been Revised to Assure Proper Valve Positioning | | | 05000263/LER-1980-023, Forwards LER 80-023/03L-0 | Forwards LER 80-023/03L-0 | | | 05000263/LER-1980-023-03, /03L-0:on 800601,air Ejector Offgas Radiation Monitors Dropped to About 20% Normal for About 40 Minutes. 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Caused by Mechanical Vacuum Pump Offgas Sample Valve Being Incorrectly Opened.Valve Now Wired Shut | | | 05000263/LER-1980-025, Forwards Updated LER 80-025/03L-1 | Forwards Updated LER 80-025/03L-1 | | | 05000263/LER-1980-025-03, Outboard HPCI Steam Supply Valve Operator Failed & Inboard Valve Closed.Caused by Breakdown of Motor Winding Insulation in Peerless Dc Motor on SMB-O Operator.Motor Replaced W/Class H Motor | Outboard HPCI Steam Supply Valve Operator Failed & Inboard Valve Closed.Caused by Breakdown of Motor Winding Insulation in Peerless Dc Motor on SMB-O Operator.Motor Replaced W/Class H Motor | | | 05000263/LER-1980-027-03, /03L-0:on 80823,during Monthly surveillance,42-11 Test Control Rod Could Not Be Withdrawn After Partial Insertion.Caused by Closed Drive Withdraw Riser Isolation Valve CRD-102.Valve Opened & Rod Was Operable | /03L-0:on 80823,during Monthly surveillance,42-11 Test Control Rod Could Not Be Withdrawn After Partial Insertion.Caused by Closed Drive Withdraw Riser Isolation Valve CRD-102.Valve Opened & Rod Was Operable | | | 05000263/LER-1980-027, Forwards LER 80-027/03L-0 | Forwards LER 80-027/03L-0 | |
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