LER-1978-033, Update LER 78-033/03L-1:on 781205,while Operating Diesel 12U for Surveillance,Low Cooling Water Alarm Received & Confirmed.Caused by Flow Restriction Due to Mussel Debris in Heat Exchanger.Svc Water to Diesel Modified |
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| 3361978033R00 - NRC Website |
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@ l While operating the 120 diesel for surveillance, the low cooling water flow alarm was l,
g I received. The cooling water low flow was confirmed by high differential pressure across l In accordance with Tech. Spec. Section 3.8.1-1, action statement l
oI41 I the heat exchangers.
o TTl I a, the diesel was declared inoperable and the operability of the remaining AC sources wasl i + 161 I verified.
The diesel is a Fairbanks Morse, 38 TD 8-1/8, rated at 2,750 KW.
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43 44 47 CAUSE DEsCR;PTION AND CORRECTIVE ACTIONS h t lal l Investigation revealed mussel sheels in the heat exchanger.
The HX was cleaned and D/G I
1111 I operability confirmed. Weekly inspections 17 weeks before and 3 weeks after this event 1
Tyyj l have shown only trace mussel debris.
All previous LER corrective actions'have been I
i 131 I compieted or are continuing at the specified frequency.
A duplex strainer has been I
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LER 78-33/3L-1 Millstone Unit 2 Docket No. 50-336 Cause Description and Corrective Action Mussel debris has caused a flow restriction in the diesel heat exchangers on five previous occasions.
Only this incident has occurred after the chlorine system diffuser modific.ation was completed.
No mussel incidents have occurred after the 12/5/78 incident.
The service water to the diesel has been modified to include a duplex basket strainer at the heat exchanger inlet of each diesel engine. The weekly cleaning and inspection of the diesel heat exchangers has been discontinued.
The duplex basket strainer will be inspected weekly.
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| 05000336/LER-1978-014, Forwards LER 78-014/03L-0 | Forwards LER 78-014/03L-0 | | | 05000336/LER-1978-014-03, /03L-0 on 780617:while Performing Monthly Control Element Assembly Surveillance Testing,Assembly 2 Dropped to Zero Steps from 178 Steps.No Component Failures Causing Control Element Assembly to Drop | /03L-0 on 780617:while Performing Monthly Control Element Assembly Surveillance Testing,Assembly 2 Dropped to Zero Steps from 178 Steps.No Component Failures Causing Control Element Assembly to Drop | | | 05000245/LER-1978-018-03, /03L-0 on 780905:during Surveillance on Vessel Level Instru,It Was Found That 1 of the 4 Reactor low-low Water Level Switches Was Nonfunctional,Due to Mech Hangup Caused by Dry Lubrication | /03L-0 on 780905:during Surveillance on Vessel Level Instru,It Was Found That 1 of the 4 Reactor low-low Water Level Switches Was Nonfunctional,Due to Mech Hangup Caused by Dry Lubrication | | | 05000245/LER-1978-018, Forwards LER 78-018/03L-0 | Forwards LER 78-018/03L-0 | | | 05000336/LER-1978-019-03, /03X-2 on 780803:while Operating 13U Diesel for Surveillance,Leaking Injector Pump Observed.Caused by Elemental Lead Inclusions,Resulting in Stress Risers at Surface of Valve Cages | /03X-2 on 780803:while Operating 13U Diesel for Surveillance,Leaking Injector Pump Observed.Caused by Elemental Lead Inclusions,Resulting in Stress Risers at Surface of Valve Cages | | | 05000336/LER-1978-019, Forwards LER 78-019/03X-2 | Forwards LER 78-019/03X-2 | | | 05000245/LER-1978-021-03, /03L-0:on 780914,gas Turbine Tripped While Output Voltage Being Adjusted.Caused by Faulty Gas Generator Speed Switch 3A in Electronic Controls | /03L-0:on 780914,gas Turbine Tripped While Output Voltage Being Adjusted.Caused by Faulty Gas Generator Speed Switch 3A in Electronic Controls | | | 05000336/LER-1978-021-03, /03L-0:on 780827,during Steady State Operation, Plant Computer Experienced Malfunction W/Spare Annunciator Point & Was Taken Out of Svc.Caused by Improper Installation of Spare Photodarlington Optical Isolator ILCA2-55 | /03L-0:on 780827,during Steady State Operation, Plant Computer Experienced Malfunction W/Spare Annunciator Point & Was Taken Out of Svc.Caused by Improper Installation of Spare Photodarlington Optical Isolator ILCA2-55 | | | 05000245/LER-1978-021, Forwards LER 78-021/03L-0 | Forwards LER 78-021/03L-0 | | | 05000336/LER-1978-022-03, /03L-0 on 780906:Loss of Methyl Iodide Removal Efficiency for a Ebfs Train. Cause Unknown | /03L-0 on 780906:Loss of Methyl Iodide Removal Efficiency for a Ebfs Train. Cause Unknown | | | 05000336/LER-1978-022, Forwards LER 78-022/03l-0 | Forwards LER 78-022/03l-0 | | | 05000336/LER-1978-023-03, /03L-0 on 780912:during Routine steady-state Operation,Spent Fuel Storage Ventilation Gaseous Radiation Monitor Failed Low.Caused by Shorted Local Alarm Horn Which Blew Power Supply Fuse.Horn Disconnected & Fuse Replaced | /03L-0 on 780912:during Routine steady-state Operation,Spent Fuel Storage Ventilation Gaseous Radiation Monitor Failed Low.Caused by Shorted Local Alarm Horn Which Blew Power Supply Fuse.Horn Disconnected & Fuse Replaced | | | 05000336/LER-1978-023, Forwards LER 78-023/03L-0 | Forwards LER 78-023/03L-0 | | | 05000245/LER-1978-023, Forwards LER 78-023/03L-0 | Forwards LER 78-023/03L-0 | | | 05000336/LER-1978-024-03, /03L-0 on 781004:during Surveillance Testing, Setpoint for Reactor Protec Sys Reactor Coolant Low Flow Trip on Channel B Was Out of Spec.Setpoint Was Readjusted. Rev Will Req Low Flow Trip Unit Setpoint Be Reset | /03L-0 on 781004:during Surveillance Testing, Setpoint for Reactor Protec Sys Reactor Coolant Low Flow Trip on Channel B Was Out of Spec.Setpoint Was Readjusted. Rev Will Req Low Flow Trip Unit Setpoint Be Reset | | | 05000336/LER-1978-024, Forwards LER 78-024/03L-0 | Forwards LER 78-024/03L-0 | | | 05000336/LER-1978-025-03, /03L-0 on 781007:daily Tech Spec 4.3.1.1.1.,Table 4.3-1,items 2.a & 2.b,Nuc Pwr Surveillance & Delta-T Pwr Channel Calibr Not Performed Due to Personnel Error. Supervisors Told to Perform Req Surveillance | /03L-0 on 781007:daily Tech Spec 4.3.1.1.1.,Table 4.3-1,items 2.a & 2.b,Nuc Pwr Surveillance & Delta-T Pwr Channel Calibr Not Performed Due to Personnel Error. Supervisors Told to Perform Req Surveillance | | | 05000336/LER-1978-025, Forwards LER 78-025/03L-0 | Forwards LER 78-025/03L-0 | | | 05000336/LER-1978-026, Forwards LER 78-026/03L-0 | Forwards LER 78-026/03L-0 | | | 05000336/LER-1978-026-03, /03L-0 on 781025:Analysis of Instru Installations Revealed That Two Transmitters Assoc W/Channel a Steam Generator Low Water Lever Were non-seismically Mounted. Channel a SG Was Bypassed.Seismic Brackets Will Be Used | /03L-0 on 781025:Analysis of Instru Installations Revealed That Two Transmitters Assoc W/Channel a Steam Generator Low Water Lever Were non-seismically Mounted. Channel a SG Was Bypassed.Seismic Brackets Will Be Used | | | 05000336/LER-1978-027-03, /03L-0 on 781024:plant Computer Malfunction Caused CEA Pulse Counting Position to Be in Oper.Cause of Computer Failure Could Not Be Traced | /03L-0 on 781024:plant Computer Malfunction Caused CEA Pulse Counting Position to Be in Oper.Cause of Computer Failure Could Not Be Traced | | | 05000336/LER-1978-027, Forwards LER 78-27/03L-0 | Forwards LER 78-27/03L-0 | | | 05000336/LER-1978-028-03, /03L-0 on 781115:spent Fuel Pool(Sfp)Ventilation Particulate & Gaseous Setpoints Exceeded Tech Specs Setpoints of Table 3.3-6,items 2.c & 2.d.Caused by Monitor Recalibr W/O Taking Into Account Tech Spec Limit | /03L-0 on 781115:spent Fuel Pool(Sfp)Ventilation Particulate & Gaseous Setpoints Exceeded Tech Specs Setpoints of Table 3.3-6,items 2.c & 2.d.Caused by Monitor Recalibr W/O Taking Into Account Tech Spec Limit | | | 05000336/LER-1978-028, Forwards LER 78-028/03L-0 | Forwards LER 78-028/03L-0 | | | 05000336/LER-1978-029-03, /03L-0 on 781025:during Oper,Surveillance Test on Channel a Reactor Protec Sys Core Protec Calculator Reveated Sys Ground Traced to Signal for Pressurizer Pressure W/In Containment Boundary.Source Not Known at This Time | /03L-0 on 781025:during Oper,Surveillance Test on Channel a Reactor Protec Sys Core Protec Calculator Reveated Sys Ground Traced to Signal for Pressurizer Pressure W/In Containment Boundary.Source Not Known at This Time | | | 05000336/LER-1978-029, Forwards LER 78-029/03L-0 | Forwards LER 78-029/03L-0 | | | 05000336/LER-1978-030, Forwards LER 78-030/03L-0 | Forwards LER 78-030/03L-0 | | | 05000245/LER-1978-030-03, /03L-0 on 781215:suppression Chamber Oxygen Concentration Was Too High Due to a Slow Nitrogen Purge Rate.Personnel Were Reminded to Monitor Parameters | /03L-0 on 781215:suppression Chamber Oxygen Concentration Was Too High Due to a Slow Nitrogen Purge Rate.Personnel Were Reminded to Monitor Parameters | | | 05000245/LER-1978-030, Forwards LER 78-030/03L-0 | Forwards LER 78-030/03L-0 | | | 05000336/LER-1978-030-03, /03L-0:on 781106 CEA 63 in Regulating Group 3 Reed Switch Position Indicator Channel Inoperable.Caused by Intermittent Open in the Reed Switch Assembly Power Supply Lead Which Produced Erratic Indication | /03L-0:on 781106 CEA 63 in Regulating Group 3 Reed Switch Position Indicator Channel Inoperable.Caused by Intermittent Open in the Reed Switch Assembly Power Supply Lead Which Produced Erratic Indication | | | 05000245/LER-1978-031-03, /03L-0 on 781218:during Nuclear Review Board Audit a Surveillance Requirement (Reduced High Flux Prior to Startup) Was Found Unaccomplished Since Its Introduction. Caused by Procedural Error | /03L-0 on 781218:during Nuclear Review Board Audit a Surveillance Requirement (Reduced High Flux Prior to Startup) Was Found Unaccomplished Since Its Introduction. Caused by Procedural Error | | | 05000245/LER-1978-031, Forwards LER 78-031/03L-0 | Forwards LER 78-031/03L-0 | | | 05000336/LER-1978-031, Forwards LER 78-031/03L-0 | Forwards LER 78-031/03L-0 | | | 05000336/LER-1978-031-03, /03L-0:on 781107 C Reactor Bldg Closed Cooling Water Temp Was Found Low Due to Failed Svc Water Temp Control Valve Shear Pin Connecting Actuator to Valve. Caused by Sheared Tension Pin | /03L-0:on 781107 C Reactor Bldg Closed Cooling Water Temp Was Found Low Due to Failed Svc Water Temp Control Valve Shear Pin Connecting Actuator to Valve. Caused by Sheared Tension Pin | | | 05000245/LER-1978-032-03, /03L-0 on 781227:diesel Fire Pump Fuel Oil Sample Surveillance Inadvertently Overlooked During Routine Survey of Completed Surveillances.Not on Surveillance Schedule. Subsequently Added to Schedule | /03L-0 on 781227:diesel Fire Pump Fuel Oil Sample Surveillance Inadvertently Overlooked During Routine Survey of Completed Surveillances.Not on Surveillance Schedule. Subsequently Added to Schedule | | | 05000245/LER-1978-032, Forwards LER 78-032/03L-0 | Forwards LER 78-032/03L-0 | | | 05000336/LER-1978-032, Forwards LER 78-032/03L-0 | Forwards LER 78-032/03L-0 | | | 05000336/LER-1978-032-03, /03L-0 on 781130:Channel B Reactor Protect Sys Core Protection Calculator Positive 18 Volt Logic Power Supply Failed.Caused by Normal Aging of a Capacitor in the Auxiliary Rectifier Circuit | /03L-0 on 781130:Channel B Reactor Protect Sys Core Protection Calculator Positive 18 Volt Logic Power Supply Failed.Caused by Normal Aging of a Capacitor in the Auxiliary Rectifier Circuit | | | 05000336/LER-1978-033-03, /03L-0 on 781205:while Operating 12U Diesel for Surveillance,Low Cooling Water Flow Alarm Received.Caused by Shells in the Heat Exhanger | /03L-0 on 781205:while Operating 12U Diesel for Surveillance,Low Cooling Water Flow Alarm Received.Caused by Shells in the Heat Exhanger | | | 05000336/LER-1978-033, Forwards LER 78-033/03L-0 | Forwards LER 78-033/03L-0 | | | 05000336/LER-1978-034, Forwards LER 78-034/03L-0 | Forwards LER 78-034/03L-0 | | | 05000336/LER-1978-034-03, /03L-0 on 781227:during Surveillance,Svc Water Isolation Valve 2-SW-3.2A Failed to Close.Caused by Actuating Air Flow Being Blocked | /03L-0 on 781227:during Surveillance,Svc Water Isolation Valve 2-SW-3.2A Failed to Close.Caused by Actuating Air Flow Being Blocked | |
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