LER-1981-001, /01T-0:on 810106, Supports H-162,H-164 & H-166 Reported Not Modified Per IE Bulletin 79-14.Caused by Loss of Pertinent Drawings.Work on Supports Completed |
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EVENT DESCRIPTION AND PROBAGLE CONSEQUENCES h I o I 'l l On 1/6/81. the Duquesne f.icht Conn.inv Ennineering Department reported that 32" f
1 o,2 ; I Sill'-1. 2. 3-601 -02 support s H-162.11-164 and 11-166 had not been modified as orteln.illvl This is a violation of Technic.il 1 g o i. j i reported in the 8/14/80 IC Bullet in 79-14 letter.
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l o !1l l wall. resultine in failure of the other two steam lines due to falling debris.
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b Attachment To Ltit 81-001/01T Beaver Valley power Station Duquesne I.lght Company Docket No. 50-334 On January 6, 1981, the Duquesne Light Company Engineering Department reported that 32" SilP-1,2,3-601-Q2 supports11-162,11-164 and !!-166 had not been modified as reported to the NRC in the August 14, 1980 IE Bu11ctin 79-14 Ictter.
The design safety function of hangers !!-l'$2,11-164 and 11-166 is to protect other equipment if one pipe should break and result in a large pipe whip. TheThe shim deficiency was in the number of shim stacks that limit pipe movement.
stacks help distribute the pipe break loads uniformly over the honeycomb collapse collar. This collapse collar dissipates energy due to pipe breaks, thus minimizing the loads imposed upon the valve house wall. This wall acts as the last safety-rcisted support for all three main steam lines.
It was determined in the IE Bulletin 79-14 of fort that the shim stack installed was not according to the design drawings and would not adequately distribute the load properly. Because of this, there was an increased possibility that the design loads of the valve house wall would be exceeded if one of the main steam lines ruptured. This wall failure would cascade into the two remaining steam lines which are supported of f this wall.
The problem with this nonconformance being missed appears to be in the transmittal of records between the concerned departments. A drawing package transmitted to the contractor was illegible and so it was sent back to the construction department. New drawings were made, excluding the ones of the supports in question, and were then re-transmitted. When the new drawings were compared to the transmittal list, they matched and were accepted.
All design change packages for modifications of Beaver Valley power Station are reviewed during turnover activitics to assure that as-built conditions are in This accordance with required engineering as part of the turnover program.
check is made concurrently by the Construction Department, Start-up Group, and the Station Engineering Group. In addition, a review is made to assure that all applicable Technical Specifications can be met utilizing the as-modified station equipment. A final safety review is performed to assure that the "as built" configuration does not constitute an unreviewed safety question as defined by 10 CFR 50.59.
As allowed by the turnover program, the Station Engineering Group conducted a 25., review on three design change packages (those associated with pipe supports, as-built corrections, and seismic reanalyses) because of their peculiar nature and magnitude. The above described discrepancy was discovered by the Construction Department during a final follow-up check.
Upon receiving the discrepancy report from the Mechanical Engineering Department, the Station Superintendent ordered the plant startup to discontinue until the discrepancy was corrected and the Quality Assurance Manager assured him that no other discrepancies had occurred..
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Attachment To LER 81-001/0lT bd g
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f Ileaver Valley Power St.ition 3
Duquesne 1,lght Company Docket No. 50-334 The Quality Assurance !!anager requested a final review of the three design change packages of concern and conducted an investigation of the problem to determine if the program contained weaknesses allowing this to occur. During this review, one other discrepancy was discovered on hanger ll-4A on the river water system which was determined not to be a significant safety concern; however, the discrepancy was corrected immediately.
On January 9,1981, the Quality Assurance !!anager assured the Superintendent that all reviews were complete and that there was a high degree of assurance that no other discrepancies existed. On that basis, the Superintendent released the station to continue startup activitics. The Quality Assurance !!anager has subsequently issued a report of his investigation with recommended action to prevent this type of oversight from recurring. Corrections are being made in an expeditious manner.
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| 05000334/LER-1981-001-01, /01P-0:on 810106,IE Bulletin 79-14 Evaluation & Reanalysis of Piping & Supports Revealed H-162,H-164 & H-166 to Be Less Conservative than Original Design.Caused by QA Breakdown | /01P-0:on 810106,IE Bulletin 79-14 Evaluation & Reanalysis of Piping & Supports Revealed H-162,H-164 & H-166 to Be Less Conservative than Original Design.Caused by QA Breakdown | | | 05000334/LER-1981-001, Forwards LER 81-001/01T-0 | Forwards LER 81-001/01T-0 | | | 05000334/LER-1981-002, Forwards LER 81-002/01T-0 | Forwards LER 81-002/01T-0 | | | 05000334/LER-1981-002-01, /01T-0:on 810107,during Shutdown,Seal Flow Dropped Below Min on 1C Reactor Coolant Pump.Caused by Sensitive Valving.Pump Restarted within 20 Minutes | /01T-0:on 810107,during Shutdown,Seal Flow Dropped Below Min on 1C Reactor Coolant Pump.Caused by Sensitive Valving.Pump Restarted within 20 Minutes | | | 05000334/LER-1981-003-03, /03L-0:on 810102,containment Outer Airlock Door Failed Seal Leakage Surveillance Test.Cause Not Stated. Seals Cleaned,Greased & Realigned.Airlock Returned to Svc | /03L-0:on 810102,containment Outer Airlock Door Failed Seal Leakage Surveillance Test.Cause Not Stated. Seals Cleaned,Greased & Realigned.Airlock Returned to Svc | | | 05000334/LER-1981-003, Forwards LER 81-003/03L-0 | Forwards LER 81-003/03L-0 | | | 05000334/LER-1981-004-03, /03L-0:on 810106,air Flow Calculations on Control Room Emergency Supply Fans Indicated Flow Rates in Excess of Tech Specs.Cause Not Stated.Adjustment Made to Supply Fans Inlet Damper | /03L-0:on 810106,air Flow Calculations on Control Room Emergency Supply Fans Indicated Flow Rates in Excess of Tech Specs.Cause Not Stated.Adjustment Made to Supply Fans Inlet Damper | | | 05000334/LER-1981-004, Forwards LER 81-004/03L-0 | Forwards LER 81-004/03L-0 | | | 05000334/LER-1981-005-03, /03L-0:on 810107,101A & 101B Detectors Electrolyte Discovered Not Dripping.Cause Not Stated.Wicks Replaced & Orifices Cleaned.Engineering Requested to Evaluate Sys | /03L-0:on 810107,101A & 101B Detectors Electrolyte Discovered Not Dripping.Cause Not Stated.Wicks Replaced & Orifices Cleaned.Engineering Requested to Evaluate Sys | | | 05000334/LER-1981-006, Forwards Updated LER 81-006/03X-1.Detailed Event Analysis Encl | Forwards Updated LER 81-006/03X-1.Detailed Event Analysis Encl | | | 05000334/LER-1981-006-03, During Surveillance Tests on Low Head Safety Injection Pumps,Water in Recirculation Line on Refueling Water Storage Tank Found Frozen.Caused by Heat Trace Circuit Thermostat Line in Off Position | During Surveillance Tests on Low Head Safety Injection Pumps,Water in Recirculation Line on Refueling Water Storage Tank Found Frozen.Caused by Heat Trace Circuit Thermostat Line in Off Position | | | 05000334/LER-1981-007-03, /03L-0:on 810114,101A & 101B Detectors Electrolyte Discovered Not Dripping.Cause Not Stated.Wicks Replaced & Orifices Cleaned.Engineering Requested to Evaluate Sys | /03L-0:on 810114,101A & 101B Detectors Electrolyte Discovered Not Dripping.Cause Not Stated.Wicks Replaced & Orifices Cleaned.Engineering Requested to Evaluate Sys | | | 05000334/LER-1981-008-03, /03L-0:on 810112,low Pressure Alarm Received on Safety Injection Accumulator SI-TK-1C.Caused by Leaking Drain Valve.Pressure Restored Above Tech Spec Limit & Valves Will Be Repaired or Replaced During Next Outage | /03L-0:on 810112,low Pressure Alarm Received on Safety Injection Accumulator SI-TK-1C.Caused by Leaking Drain Valve.Pressure Restored Above Tech Spec Limit & Valves Will Be Repaired or Replaced During Next Outage | | | 05000334/LER-1981-008, Forwards LER 81-008/03L-0 | Forwards LER 81-008/03L-0 | | | 05000334/LER-1981-009-03, /03L-0:on 810117,MOV-SI-864B Containment Isolation Valve Stroked Shut But Failed to Reopen During Surveillance Test.Caused by Valve Open Torque Cutout Switch Being Out of Adjustment.Switch Adjusted & Returned to Svc | /03L-0:on 810117,MOV-SI-864B Containment Isolation Valve Stroked Shut But Failed to Reopen During Surveillance Test.Caused by Valve Open Torque Cutout Switch Being Out of Adjustment.Switch Adjusted & Returned to Svc | | | 05000334/LER-1981-009, Forwards LER 81-009/03L-0 | Forwards LER 81-009/03L-0 | | | 05000334/LER-1981-010-03, /03L-0:on 810121,RCS Loop 1 Low Flow Channel 414 Annunciator Began Intermittently Flashing in Alarm.Caused by Low Voltage Input to Transmitter.Annunciator Adjusted & Channel Returned to Svc 810123 | /03L-0:on 810121,RCS Loop 1 Low Flow Channel 414 Annunciator Began Intermittently Flashing in Alarm.Caused by Low Voltage Input to Transmitter.Annunciator Adjusted & Channel Returned to Svc 810123 | | | 05000334/LER-1981-011-03, /03L-0:on 810121,electrolyte Detectors 101A & B Found Not Dripping & 101C Detector Had Slow Drip Rate.Cause Under Investigation.Detectors Adjusted,Repaired & Declared Operable on 810129 | /03L-0:on 810121,electrolyte Detectors 101A & B Found Not Dripping & 101C Detector Had Slow Drip Rate.Cause Under Investigation.Detectors Adjusted,Repaired & Declared Operable on 810129 | | | 05000334/LER-1981-012-03, /03L-0:on 810203,all Three Chlorine Detectors Failed Drip Rate Criteria.Cause Under Investigation. Detectors Repaired & Declared Operable 810204 | /03L-0:on 810203,all Three Chlorine Detectors Failed Drip Rate Criteria.Cause Under Investigation. Detectors Repaired & Declared Operable 810204 | | | 05000334/LER-1981-013-03, /03L-0:on 810121,routine Lab Analysis Showed That Methyl Iodide Removal Efficiency for Bed Had Fallen Below Acceptable Level Resulting in Inoperability of Main Filter Bank 1A.Caused by Worn Out Charcoal Bed.Bank Repacked | /03L-0:on 810121,routine Lab Analysis Showed That Methyl Iodide Removal Efficiency for Bed Had Fallen Below Acceptable Level Resulting in Inoperability of Main Filter Bank 1A.Caused by Worn Out Charcoal Bed.Bank Repacked | | | 05000334/LER-1981-014-01, /01T-0:on 810221,while Preparing for Plant Startup,Weld Leak Occurred in Rcs.Cause of Weld Failure Is Unknown.New Procedure Was Implemented & Instrument Line Relocated.Followup Rept Will Be Provided | /01T-0:on 810221,while Preparing for Plant Startup,Weld Leak Occurred in Rcs.Cause of Weld Failure Is Unknown.New Procedure Was Implemented & Instrument Line Relocated.Followup Rept Will Be Provided | | | 05000334/LER-1981-014, Forwards LER 81-014/01T-0 | Forwards LER 81-014/01T-0 | | | 05000334/LER-1981-015-03, /03L-0:on 810204,RCS Loop 1 Low Flow Annunciator Alarmed Intermittently.Flow Channel 414 Declared Inoperable & Bistable Tripped.Caused by Leaking Diaphragm.Diaphragm Replaced | /03L-0:on 810204,RCS Loop 1 Low Flow Annunciator Alarmed Intermittently.Flow Channel 414 Declared Inoperable & Bistable Tripped.Caused by Leaking Diaphragm.Diaphragm Replaced | | | 05000334/LER-1981-015, Forwards LER 81-015/03L-0 | Forwards LER 81-015/03L-0 | | | 05000334/LER-1981-016-03, /03L-0:on 810207,packing Leak Found in Steam Trap Isolation Valve.Caused by Valve Stem Packing Failure.Packing Rings Added | /03L-0:on 810207,packing Leak Found in Steam Trap Isolation Valve.Caused by Valve Stem Packing Failure.Packing Rings Added | | | 05000334/LER-1981-016, Forwards LER 81-016/03L-0 | Forwards LER 81-016/03L-0 | | | 05000334/LER-1981-017-03, /03L-0:on 810207,analog Rod Position Indicator Channels H2 & B8 & Associated Rods Were Declared Inoperable When Indications Exceeded Tech Spec.Caused by non-linearity in Indicator Calibr Curves.Tech Spec Mod Proposed | /03L-0:on 810207,analog Rod Position Indicator Channels H2 & B8 & Associated Rods Were Declared Inoperable When Indications Exceeded Tech Spec.Caused by non-linearity in Indicator Calibr Curves.Tech Spec Mod Proposed | | | 05000334/LER-1981-018-03, /03L-0:on 810208,analog Rod Position Indicator Channels H2,P8,F10 & K10 Exceeded Tech Specs.Caused by Loss of Indicator Accuracy in Calibr Curves Region.Tech Spec Mod Proposed | /03L-0:on 810208,analog Rod Position Indicator Channels H2,P8,F10 & K10 Exceeded Tech Specs.Caused by Loss of Indicator Accuracy in Calibr Curves Region.Tech Spec Mod Proposed | | | 05000334/LER-1981-019-01, /01T-0:on 810305,RHR Low Flow Alarm Actuated, Accompanied by Low Current on Operating Pump.Caused by Loss of Suction Pump During Reduction of RCS Level | /01T-0:on 810305,RHR Low Flow Alarm Actuated, Accompanied by Low Current on Operating Pump.Caused by Loss of Suction Pump During Reduction of RCS Level | | | 05000334/LER-1981-019, Forwards LER 81-019/01T-0 | Forwards LER 81-019/01T-0 | | | 05000334/LER-1981-020-03, /03L-0:on 810209,remote Control Room Multipoint Recorder Temp Channels Declared Inoperable.Caused by Accidental Repositioing of Local Test Switch Midway Through Gaseous Waste Discharge.Switch Returned to Normal Position | /03L-0:on 810209,remote Control Room Multipoint Recorder Temp Channels Declared Inoperable.Caused by Accidental Repositioing of Local Test Switch Midway Through Gaseous Waste Discharge.Switch Returned to Normal Position | | | 05000334/LER-1981-020, Forwards LER 81-020/03L-0 | Forwards LER 81-020/03L-0 | | | 05000334/LER-1981-021-03, /03L-0:on 810210,safety Injection Accumulator 1B, (SI-TK-1B) Low Level Alarm Sounded.Caused by Chemist Leaving Valve Open Following Sampling & Tank Draining Down. Valve Shut | /03L-0:on 810210,safety Injection Accumulator 1B, (SI-TK-1B) Low Level Alarm Sounded.Caused by Chemist Leaving Valve Open Following Sampling & Tank Draining Down. Valve Shut | | | 05000334/LER-1981-022-03, /03L-0:on 810211,control Room Chlorine Detector 101B Was Tripped Upon Discovering That Electrolyte Was Not Dripping.Cause Not Stated.Flow Orifice Cleaned & Wick Replaced.Investigation Underway | /03L-0:on 810211,control Room Chlorine Detector 101B Was Tripped Upon Discovering That Electrolyte Was Not Dripping.Cause Not Stated.Flow Orifice Cleaned & Wick Replaced.Investigation Underway | | | 05000334/LER-1981-023-03, /03L-0:on 810212,w/plant Increasing Power from 75% to 80%,delta Flux Out of Target Band Alarm Received. Xenon Transient Associated W/Power Change Caused Axial Flux Difference to Temporarily Exceed Target Band | /03L-0:on 810212,w/plant Increasing Power from 75% to 80%,delta Flux Out of Target Band Alarm Received. Xenon Transient Associated W/Power Change Caused Axial Flux Difference to Temporarily Exceed Target Band | | | 05000334/LER-1981-024-03, /03L-0:on 810215,during Increase in Power,Delta Flux Out of Target Band Alarm Received.Caused by Xenon Transient Associated W/Power Change Resulting in Increase Axial Flux Differential.Power Increase Stopped | /03L-0:on 810215,during Increase in Power,Delta Flux Out of Target Band Alarm Received.Caused by Xenon Transient Associated W/Power Change Resulting in Increase Axial Flux Differential.Power Increase Stopped | | | 05000334/LER-1981-025-03, /03L-0:on 810216,increased Leakage from Reactor Coolant (Rc) Loop 1A RTD Manifold Hot Leg Valve RC-20 Reported.Caused by Attempted Maint to Repair Valve.Temp Channels Returned to Svc | /03L-0:on 810216,increased Leakage from Reactor Coolant (Rc) Loop 1A RTD Manifold Hot Leg Valve RC-20 Reported.Caused by Attempted Maint to Repair Valve.Temp Channels Returned to Svc | | | 05000334/LER-1981-026-03, /03L-0:on 810218,RCS Loop Flow Channel Indication Failed to Meet Min Flow Surveillance Check Requirement. Caused by Transmitter Delta Pressure Transducer Diaphragm Leakage.Transmitter Replaced | /03L-0:on 810218,RCS Loop Flow Channel Indication Failed to Meet Min Flow Surveillance Check Requirement. Caused by Transmitter Delta Pressure Transducer Diaphragm Leakage.Transmitter Replaced | | | 05000334/LER-1981-027-03, /03L-0:on 810218,at 98% Power,All Three Chlorine Detectors Failed to Meet Min Electrolyte Drip Rate Criteria Specified in Surveillance Test.Caused by Dirty Wicks Which Prevented Flow of Electrolyte.Wicks Cleaned | /03L-0:on 810218,at 98% Power,All Three Chlorine Detectors Failed to Meet Min Electrolyte Drip Rate Criteria Specified in Surveillance Test.Caused by Dirty Wicks Which Prevented Flow of Electrolyte.Wicks Cleaned | | | 05000334/LER-1981-028-03, /03L-0:on 810219,during Power Operation,Results of Surveillance Test Revealed Reactor Coolant Leakage of 2.09 Gpm.Caused by Failure of Gland Flange on Valve.Split Gland Flange Used as Mod to Repair Valve.Work Completed 81022 | /03L-0:on 810219,during Power Operation,Results of Surveillance Test Revealed Reactor Coolant Leakage of 2.09 Gpm.Caused by Failure of Gland Flange on Valve.Split Gland Flange Used as Mod to Repair Valve.Work Completed 810221 | | | 05000334/LER-1981-029-01, /01T-0:on 810325,discrepancy Noted Between Plant Mod Manual & Tech Spec 4.0.5 During Review of Inservice Insp Requirements.Caused by Misinterpretation of NRC Endorsement of ASME XI Code as Authorization to Invoke Tech Spec | /01T-0:on 810325,discrepancy Noted Between Plant Mod Manual & Tech Spec 4.0.5 During Review of Inservice Insp Requirements.Caused by Misinterpretation of NRC Endorsement of ASME XI Code as Authorization to Invoke Tech Spec | | | 05000334/LER-1981-029, Forwards LER 81-029/01T-0 | Forwards LER 81-029/01T-0 | | | 05000334/LER-1981-029-03, Containment Isolation Check Valve Found to Have Too Low Opening Pressure & Leakage in Excess of Measuring Device Used for Type C Testing.Cause Unknown.Maint Performed | Containment Isolation Check Valve Found to Have Too Low Opening Pressure & Leakage in Excess of Measuring Device Used for Type C Testing.Cause Unknown.Maint Performed | | | 05000334/LER-1981-030, Forwards LER 81-030/03L-0 | Forwards LER 81-030/03L-0 | | | 05000334/LER-1981-030-03, /03L-0:on 810309,diesel Generator 2 Would Not Restart After Being Brought to Speed & Tripping,Apparently Due to Overspeed.Caused by Failed Taper Pin & Bent Level in Governor of Diesel.Turbocharger,Taper Pin & Level Replaced | /03L-0:on 810309,diesel Generator 2 Would Not Restart After Being Brought to Speed & Tripping,Apparently Due to Overspeed.Caused by Failed Taper Pin & Bent Level in Governor of Diesel.Turbocharger,Taper Pin & Level Replaced | | | 05000334/LER-1981-031-01, /01T-0:on 810427,free Chlorine Measured at Outfall Structure & Duration of Condenser Tube Chlorination Exceeded Tech Spec Limits.Caused by Communication Problem Re Inservice Portions of Sys.Overchlorination Stopped | /01T-0:on 810427,free Chlorine Measured at Outfall Structure & Duration of Condenser Tube Chlorination Exceeded Tech Spec Limits.Caused by Communication Problem Re Inservice Portions of Sys.Overchlorination Stopped | | | 05000334/LER-1981-031, Forwards LER 81-031/01T-0 | Forwards LER 81-031/01T-0 | | | 05000334/LER-1981-032, Forwards LER 81-032/01T-0 | Forwards LER 81-032/01T-0 | | | 05000334/LER-1981-032-01, /01T-0:on 810502,vibrations in Feed Line a & High Feed Flow W/Rising Level in Steam Generator a Found During Moisture Carryover Test.Caused by Malfunction of Feed Regulating Valve a Due to Disconnected Actuator | /01T-0:on 810502,vibrations in Feed Line a & High Feed Flow W/Rising Level in Steam Generator a Found During Moisture Carryover Test.Caused by Malfunction of Feed Regulating Valve a Due to Disconnected Actuator | | | 05000334/LER-1981-033, Has Been Canceled | Has Been Canceled | |
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