05000366/LER-1981-084-03, /03L-0:on 810903,during Power Increase,High Pressure Coolant Injection Delta P Switch Actuated at Level Outside Tech Specs.Caused by Setpoint Drift.Switch Recalibr. Analog Trip Sys Will Be Installed

From kanterella
Revision as of 05:03, 21 December 2024 by StriderTol (talk | contribs) (StriderTol Bot insert)
(diff) ← Older revision | Latest revision (diff) | Newer revision → (diff)
Jump to navigation Jump to search
/03L-0:on 810903,during Power Increase,High Pressure Coolant Injection Delta P Switch Actuated at Level Outside Tech Specs.Caused by Setpoint Drift.Switch Recalibr. Analog Trip Sys Will Be Installed
ML20011A477
Person / Time
Site: Hatch 
Issue date: 10/01/1981
From: Nix R
GEORGIA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20011A472 List:
References
LER-81-084-03L-01, LER-81-84-3L-1, NUDOCS 8110130465
Download: ML20011A477 (2)


LER-1981-084, /03L-0:on 810903,during Power Increase,High Pressure Coolant Injection Delta P Switch Actuated at Level Outside Tech Specs.Caused by Setpoint Drift.Switch Recalibr. Analog Trip Sys Will Be Installed
Event date:
Report date:
3661981084R03 - NRC Website

text

' MHC (OHM,uu w.w...-

k w wa.as w o. w.......

.w.

LICENSEE EVENT REPORT P

control BLOCK: l l

l l

l l lh (PLEASE PRINT CR TYPE ALL REXUIRED INFORMATI!N) i e

@ l Gl Al El Il Hj 2 l@l 0 l 0 l -l 0 l 0 l 0 l 0 l 0 l - l 0 l 0 l@[4 l 1 l 1 l 1 l 11@l l

l@

7 8 9 LIC'NSEE COOE le 15 LICENbt NUMBER 2S 26 LICENSE TYPE JG 57 CAT b8 CON'T m

s

, ~.,

A Z,% l Ll@l 0l 5 l 0 l 0 l 0 l 3 l 6 I 6 l@l 0 l 9 l 0 l 3 l 8 l 1 l@l 1 l 0 l 0l ll 8 l 1 l@

7 8

60 61 DOCK ET NUVBER 68 69 EVENT OATE 74 75 REPORT DATE 80 EVENT oESCRIPTioN AND PROBABLE CONSEQUENCES h [TITI l With the plant increasino power from 238 MWt, 2E41-N005, HPCI Steam Line l

ITTTII Delta P Switch, was found to actuate at +204.5" H2O Delta P.

Tech Specs i

1014 l [

Tabl( 3.3.2-2 requires actuation at </= +196" Hp0 Del ta P.

Redundant I

[TITl I rwitch 2E41-N004 was operable and in tolerance.

Plant operation or the l

I O l s'l I public's health and safety were not affected.

This is a repetitive event l

1017] I as last reported on Reportable Occurrence Report No. 50-366/1980-141.

1 I O la l l l

^

'$oE C

CODE

$ 8C DE COMPONENT CODE SUBCOdE SU E

g l Sl Fl@ [_X_j@ l Z l@ l I l N l S l T I R l U l@ J@ J @

7 8

9 10 II 12 13 19 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION L E RIRO EVENT YE AR REPORT NO.

CODE TYPE N O.

@,agg 18 l11 l-l 10l814I l/l I 01 31 l Ll l-l

0 l 21 22 23 24 28 27 28 29 30 31 32 AK A

Of ON PL NT M

HOURS 22 SC I FOR B.

SUP IE MANUFACTUfER l E l@W@

l Z l@

lZl@

l0l0l0l0l W@

lNl@

lNl@

lB l0 l8 l0 lg 33 J4 35 36 31 40 43 42 4

4 47 CAUSE oESCnlPTION AND CORRECTIVE ACTloNs h gl The cause of.this evert has been attributed to setpoint drift.

The instru-l i i I

ment was recalibrated per HNP-2-5202, Barton Model 288A Calibration, and I

iii2i l returned to service.

This instrument will be replaced as part of a design I

i 3 l change installing an analog trip system.

A follow-up report will be sub-I i

4 I

mitted upon completion of the corrective action.

I 7

8 9 80 5

5

% POWE R OTHER STATUS DIS O Y

DISCOVERY CESCRIPTION

[,C_j@ ! 0 l 1 l 0 l@l NA l

d_j@[ Surveillance testing.

l i s ACTIVITY CO TENT ftELEASED OF RELE ASE AMCUNT OF ACTIVITY LOCATION OF RELEASE

[" T el [_ Z_] @ [ Z j @ l NA l

l NA l

7 8 9 10 11 44 45 80 PERSONNEL EXPOSURES NUMBER TYPE

DESCRIPTION

l 01 01 0l@l Z l@l n3 l

i 7 PERSONNEL tNJUR ES oESCRiPTiON@

NuueEn l 0l 010l@l NA l

1 R 7

8 9

t 12 80 LOSS OF OR OAMAGE TO FACILITY TYPE
- DESCRtPTION

[_Zj@l NA l

5 9 7

8 9 10 80 DESCRsPTION ISSUEDI NA I

PDR ADOCK 05000366

,,,L, i l l f i l l l i l l l ?

PI N

8110130465 811001 0

so

  • S pop g R. T. Nix, Supt. of Maint.

m-W-M

{

pgggg

b

.s

/,

.s 2,$,,

~ e.

LER No.:' 50-366/1981-084, Licensee: Geo *gia Power Company Fac'il i ty:

Edwin I. Hatch Docket No. : 50-J66 l

Narrative

Report for LER 50-366/1981-084.

i On September 3,1981, with Unit II increasing power from 238 MWt, 2E41-N005, High Pressure Coolant Injection Steam Line Differential Pressure ' Switch, was found to actuate at +204.5" water Delta P.

Tech Specs Table 3.3.2-2 requires actuation at </= +196" of water Delta P.

Redundant switch 2E41-N004 was operable and in tolerance.

Plant operation or the public's health and safety were not affected.

This is a repetitive event as last reported on Reportable Occurrence Report No. 50-366/1980-141.

~

The cause of this event has been attributed to setpoint drif t.

The instru-ment was immediately recalibrated per HNP-2-5202, Barton Model 288A Cali-bration, and returned to service. A design change has been submitted to replace this instrument with an analog trip system.

A follow-up report will be submitted upon completion of this corrective action.

Unit I uses this same type of instrument for this application.

A generic review revealed that in this application this type instrument has inherent probl ems.

(

- W 6

.e

'}

g #9 e'

1

  • e

+

e.

L

)

\\

.g, m.