05000416/LER-1983-052-03, /03L-0:on 830411,while Reviewing Vessel Head Installation Work Package,Discovered Head Flange/Vessel Flange Thermocouples Not Physically Reinstalled During Insulation Installation.Cause Under Evaluation

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/03L-0:on 830411,while Reviewing Vessel Head Installation Work Package,Discovered Head Flange/Vessel Flange Thermocouples Not Physically Reinstalled During Insulation Installation.Cause Under Evaluation
ML20023D477
Person / Time
Site: Grand Gulf Entergy icon.png
Issue date: 05/11/1983
From: Rohrer M
MISSISSIPPI POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20023D466 List:
References
LER-83-052-03L, LER-83-52-3L, NUDOCS 8305200532
Download: ML20023D477 (1)


LER-1983-052, /03L-0:on 830411,while Reviewing Vessel Head Installation Work Package,Discovered Head Flange/Vessel Flange Thermocouples Not Physically Reinstalled During Insulation Installation.Cause Under Evaluation
Event date:
Report date:
4161983052R03 - NRC Website

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