05000339/LER-1982-058-03, /03L-0:on 820830,inner Personnel Hatch Door Determined to Have Unacceptable Leak Rate.Caused by Seal Being Dirty from Containment Entries.Seal Cleaned & Lubricated

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/03L-0:on 820830,inner Personnel Hatch Door Determined to Have Unacceptable Leak Rate.Caused by Seal Being Dirty from Containment Entries.Seal Cleaned & Lubricated
ML20027B946
Person / Time
Site: North Anna 
Issue date: 09/16/1982
From: Cartwright W
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20027B942 List:
References
LER-82-058-03L-01, LER-82-58-3L-1, NUDOCS 8209300354
Download: ML20027B946 (1)


LER-1982-058, /03L-0:on 820830,inner Personnel Hatch Door Determined to Have Unacceptable Leak Rate.Caused by Seal Being Dirty from Containment Entries.Seal Cleaned & Lubricated
Event date:
Report date:
3391982058R03 - NRC Website

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U.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT CONTROL BLOCK / / / / / / / (1)

(PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)

/0/1/

/v/A/N/A/S/2/ (2)

/0/0/-/0/0/0/0/0/-/0/0/ (3)

/4/1/1/1/1/ (4)

/ / / (5)

LICENSEE CODE LICENSE NUMBER LICENSE TYPE CAT

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R O

/L/ (6)

/0/5/0/0/0/3/3/9/

(7)

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(8)

/0/9/1/6/8/2/ (9)

R DOCKET NUMBER EVENT DATE REPORT DATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES (10)

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/ On August 30, 1982, with Unit No. 2 in Mode 2, the inner personnel hatch door was/

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/ determined to have an unacceptable leak rate.

The exterior containment personnel /

/0/4/

/ hatch door was properly sealed; therefore, the health and safety of the general /

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/ public were not affected. This occurrence is within the action statement of

/

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/ T.S. 3.6.1.3 and reportable pursuant to T.S. 6.9.1.9.b.

There are no generic

/

/0/7/

/ implications associated with this event.

/

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/

/

SYSTEM

CAUSE

CAUSE COMP.

VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE

/0/9/

/S/A/ (11)

/E/ (12)

/B/ (13) /P/E/N/E/T/R/ (14) /A/ (15)

/Z/ (16)

SEQUENTIAL OCCURRENCE REPORT REVISION LER/R0 EVENT YEAR REPORT NO.

CODE TYPE NO.

(17) REPORT NUMBER

/8/2/

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/L/

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ACTION FUTURE EFFECT SHUTDOWN ATTACHMENT NPRD-4 PRIME COMP. COMPONENT TAKEN ACTION ON PLANT METHOD HOURS SUBMITTED FORM SUB. SUPPLIER MANUFACTURER

/E/ (18)

/Z/ (19)

/Z/ (20) /Z/ (21) /0/0/0/0/ (22) /N/ (23) /N/ (24) /A/ (25) /C/3/1/0/ (26)

CAUSE DESCRIPTION AND CORRECTIVE ACTIONS (27)

/1/0/

/ The seal was dirty from containment entries. The seal was c1 caned, lubricated

/

/1/1/

/ and tested satisfactorily.

/

/1/2/

/

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/1/3/

/

/

/1/4/

/

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FACILITY METHOD OF STATUS

% POWER OTHER STATUS (30) DISCOVERY DISCOVERY DFSCRIPTION (32)

/1/5/

/C/ (28)

/0/0/2/ (29)

/

NA

/

/B/ (31)

/ Periodic Surveillance /

ACTIVITY CONTENT RELEASED OF RELEASE AMOUNT OF ACTIVITY (35)

LOCATION OF RELEASE (36)

/1/6/

/Z/ (33)

/Z/ (34)

/

NA

/

/

NA

/

PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION (39)

/1/7/ /0/0/0/ (37) /Z/ (38)

/

NA

/

PERSONNEL INJURIES NUMBER DESCRIPTION (41)

/1/8/ /0/0/0/ (40) /

NA

/

LOSS OF OR DAMAGS TO FACILITY TYPE

DESCRIPTION

/1/9/

/Z/ (42)

/

NA

/

PUBLICITY ISSUED DESCRIPTION (45)

NRC USE ONLY

/2/0/

/N/ (44)

/

NA

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NAME OF PREPARER W. R. CARTWRIGHT PHONE (703) 894-5151 0209300354 820916 PDR ADOCK 05000339 S

PDR