05000313/FIN-2013003-01
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Finding | |
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Title | Failure to Evaluate and Correct Excessive Containment Isolation Valve Leakage |
Description | The inspectors identified a non-cited violation of Unit 2 Technical Specification 6.5.16, Containment Leakage Rate Testing Program, for the failure to evaluate and take appropriate corrective actions to achieve acceptable performance for containment isolation valves that exceed the local leak rate administrative limit. The licensee entered this issue into the corrective action program as Condition Report CR-ANO-2-2013-01370. The failure to perform a cause determination and take appropriate corrective actions for containment isolation valves that exceed the local leak rate administrative limit was a performance deficiency. The performance deficiency was more than minor because it was associated with the procedure quality attribute of the Barrier Integrity Cornerstone and adversely affected the cornerstone objective to provide reasonable assurance that physical design barriers protect the public from radionuclide releases caused by accidents or events, and is therefore a finding. Specifically, the failure to perform a cause determination and take appropriate corrective actions adversely affected the licensee\'s ability to ensure containment isolation valves function properly. Using Manual Chapter 0609, Attachment 4, Initial Characterization of Findings, and Appendix A, The Significance Determination Process (SDP) for Findings at Power, the finding is determined to have very low safety significance because it did not represent an actual open pathway in the physical integrity of reactor containment, containment isolation system, or heat removal components, and the finding did not involve an actual reduction in function of hydrogen igniters in the reactor containment. Since the cause of the performance deficiency occurred more than three years ago, the inspectors concluded that the finding was not representative of current licensee performance and no cross-cutting aspect was assigned. |
Site: | Arkansas Nuclear |
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Report | IR 05000313/2013003 Section 1R22 |
Date counted | Jun 30, 2013 (2013Q2) |
Type: | NCV: Green |
cornerstone | Barrier Integrity |
Identified by: | NRC identified |
Inspection Procedure: | IP 71111.22 |
Inspectors (proximate) | A Fairbanks A Sanchez B Tindell D Allen D Bradley I Anchando J Melfi R Azua W Schaup |
Violation of: | Technical Specification - Procedures Technical Specification |
INPO aspect | |
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Finding - Arkansas Nuclear - IR 05000313/2013003 | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Arkansas Nuclear) @ 2013Q2
Self-Identified List (Arkansas Nuclear)
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