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Category:SAFETY EVALUATION REPORT--LICENSING & RELATED ISSUES
MONTHYEARML20210Q0521999-08-0404 August 1999 Safety Evaluation Approving Relief Request 10 to License DPR-22 Per 10CFR50.55a(g)(6)(i).Inservice Exam for Relief Request 10,Parts A,B,C,D & E Impractical & Reasonable Assurance of Structural Integrity Provided ML20205N0861999-04-12012 April 1999 Safety Evaluation Re Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves ML20204H4951999-03-18018 March 1999 SER Concluding That Licensee Established Acceptable Program to Verify Periodically design-basis Capability of safety-related MOVs at Monticello.Therefore Staff Concludes Licensee Adequately Addressed Action Required in GL 96-05 ML20199E4871999-01-0606 January 1999 SER Accepting Licensee 951116,960214 & 0524 Responses to NRC Bulletin 95-002, Unexpected Clogging of Residual Heat Removal Pump Strainer While Operating in Suppression Pool Cooling Mode ML20198P0691998-12-28028 December 1998 Safety Evaluation Concluding That NSP Proposed Alternative to Paragraph III-3411 of App III to 1986 Edition of Section XI of ASME Code Provides Acceptable Level of Quality & Safety.Alternative Authorized ML20198D0751998-12-10010 December 1998 Safety Evaluation Supporting NSP Proposed Change to EOPs to Use 2/3 Core Height as Potential Entry Condition Into Containment Flooding ML20195E3691998-11-12012 November 1998 Safety Evaluation Concluding That Licensee USI A-46 Implementation Has Met Purpose & Intent of Criteria in GIP-2 & Staff Sser 2 for Resolution of USI A-46 ML20199G7051997-11-19019 November 1997 Safety Evaluation Authorizing Relief Request 8 of Third 10 Yr Inservice Insp Interval ML20059C4051993-10-25025 October 1993 Safety Evaluation Re Inservice Testing Program Relief Requests GR-7 & RCIC-6 for Plant.Proposed Alternative to OM-1 Safety & Valve Relief Valve Requirements Authorized Based on Alternative Providing Acceptable Level of Quality ML20128Q6511985-07-0303 July 1985 Safety Evaluation Re Item 1.1 of Generic Ltr 83-28, Post-Trip Review. Review Program & Procedures Acceptable ML20148N4711978-11-0606 November 1978 Safety Eval Supporting Amend 37 to Provisional Oper Lic DPR-22.Concludes Issuance of Amend Will Not Be Inimical to Nation or People ML20126C1921977-03-0808 March 1977 SER Accepting Proposed Pumpback Sys for Plant ML20128E0801976-08-26026 August 1976 Safety Evaluation Supporting Amend to License DPR-22,re Proposed Interim Program for Offsite Shipment of Spent Fuel ML20127P4091976-07-25025 July 1976 Safety Evaluation Re Amend to License DPR-22,proposing Shipment of Sf from Monticello Nuclear Generating Plant Using GE IF-300 Shipping Cask ML20128D9621976-05-27027 May 1976 Safety Evaluation Supporting Amend 19 to License DPR-22. Amend Changes Involved Reduction in MSL Low Pressure Isolation Setpoint & Reduction in MCPR for 8x8 & 7x7 Fuel ML20126C1771976-04-0202 April 1976 SER Accepting Util Request for Change in Main Steam Isolation Pressure Setpoint Value & Operating Min Critical Power Ratio Limits ML20125A4521975-09-30030 September 1975 Safety Evaluation of Plant Conformance to Requirements of App K to 10CFR50 & Acceptability of Proposed GETAB-based TS ML20127K4141975-09-15015 September 1975 Safety Evaluation Accepting Amend 12/change 20 to DPR-22 Changing Hydraulic Snubber TS ML20127H2311975-07-15015 July 1975 Safety Evaluation Accepting TS Changes Proposed in Re Suppression Pool ML20127K2411975-07-0808 July 1975 Safety Evaluation Accepting Increased Limitations of U-235 ML20127K3281975-04-10010 April 1975 SER Accepting Amend 9/change 18 to DPR-22 Correcting Typos ML20127J5131975-02-0303 February 1975 Safety Evaluation Accepting Amend 7 (TS Change 16) to DPR-22 Re Reactor Vessel Matl Surveillance Program ML20128E0551974-10-16016 October 1974 Suppl Safety Evaluation Supporting License DPR-22 Re Full Term Operating License Application ML20127J6381974-08-20020 August 1974 Safety Evaluation Accepting Amend 6 to DPR-22 Re Use of 250 Mci Kr-85 ML20127M8571974-05-14014 May 1974 Safety Evaluation Accepting Use of 8x8 Fuel ML20127G6501974-03-30030 March 1974 Safety Evaluation Accepting Loading of 8x8 Fuel Assemblies in Core ML20127G6211974-03-14014 March 1974 Safety Evaluation Accepting 740123 Proposed Changes During Refueling Outage ML20127G6661973-11-27027 November 1973 Safety Evaluation Accepting Proposed Changes Re Reactivity ML20128D8411973-11-27027 November 1973 SER Accepting Util 720922 Request for Change to TS Re Rod Drop Accident ML20127J5461973-11-15015 November 1973 Safety Evaluation Accepting 731026 & 31 Proposed Changes to TS Re off-gas Holdup Sys ML20127G6941973-10-18018 October 1973 Safety Evaluation Accepting Removal of Stated Control Rod Inventory Restriction ML20127G7121973-10-0202 October 1973 Safety Evaluation Accepting Increase in Safety Valve Set Points,Per 730913 Request to Change TS ML20127N7601973-08-24024 August 1973 Safety Evaluation of Fuel Densification Effects on Plant ML20127M7511972-01-14014 January 1972 Safety Evaluation Accepting Proposed Change 2 to DPR-22 TS Re Gaseous Radwaste Sys Design ML20127N6411970-03-30030 March 1970 Suppl 1 to SE in Matter of NSP Monticello Nuclear Generating Plant Unit 1 1999-08-04
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217D1261999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Monticello Nuclear Generating Plant.With ML20216E7031999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Monticello Nuclear Generating Plant.With ML20210Q0521999-08-0404 August 1999 Safety Evaluation Approving Relief Request 10 to License DPR-22 Per 10CFR50.55a(g)(6)(i).Inservice Exam for Relief Request 10,Parts A,B,C,D & E Impractical & Reasonable Assurance of Structural Integrity Provided ML20210Q6611999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Monticello Nuclear Generating Plant.With ML20209F7901999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Monticello Nuclear Generating Plant.With ML20195H0351999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Monticello Nuclear Generatintg Plant.With ML20206N1721999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Monticello Nuclear Generating Plant.With ML20205N0861999-04-12012 April 1999 Safety Evaluation Re Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves ML20205P5701999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Monticello Nuclear Generating Plant.With ML20204H4951999-03-18018 March 1999 SER Concluding That Licensee Established Acceptable Program to Verify Periodically design-basis Capability of safety-related MOVs at Monticello.Therefore Staff Concludes Licensee Adequately Addressed Action Required in GL 96-05 ML20205G7391999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Monticello Nuclear Generating Plant.With ML20202F7901999-01-25025 January 1999 1999 Four Year Simulator Certification Rept for MNGP Simulation Facility ML20199E4871999-01-0606 January 1999 SER Accepting Licensee 951116,960214 & 0524 Responses to NRC Bulletin 95-002, Unexpected Clogging of Residual Heat Removal Pump Strainer While Operating in Suppression Pool Cooling Mode ML20199F6211998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Mngp.With ML20205H0561998-12-31031 December 1998 Northern States Power Co 1998 Annual Rept. with ML20198P0691998-12-28028 December 1998 Safety Evaluation Concluding That NSP Proposed Alternative to Paragraph III-3411 of App III to 1986 Edition of Section XI of ASME Code Provides Acceptable Level of Quality & Safety.Alternative Authorized ML20198D0751998-12-10010 December 1998 Safety Evaluation Supporting NSP Proposed Change to EOPs to Use 2/3 Core Height as Potential Entry Condition Into Containment Flooding ML20198B2531998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Monticello Nuclear Generating Plant.With ML20195E3691998-11-12012 November 1998 Safety Evaluation Concluding That Licensee USI A-46 Implementation Has Met Purpose & Intent of Criteria in GIP-2 & Staff Sser 2 for Resolution of USI A-46 ML20195D2381998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Monticello Nuclear Generating Plant.With ML20198J4451998-10-22022 October 1998 Rev 2 to SIR-97-003, Review of Test Results of Two Surveillance Capsules & Recommendations for Matls Properties & Pressure-Temp Curves to Be Used for Monticello Rpv ML20154L3471998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Monticello Nuclear Generating Plant.With ML20153F0511998-09-21021 September 1998 Rev 2 to MNGP Colr,Cycle 19 ML20153E9361998-09-0808 September 1998 Rev 1 to MNGP Colr,Cycle 19 ML20153B0861998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Monticello Nuclear Generating Plant.With ML20237B8461998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Monticello Nuclear Generating Plant ML20236W5041998-07-21021 July 1998 ISI Exam Summary Rept - Refueling Outage 19 ML20236R1941998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Monticello Nuclear Generating Plant ML20249A5861998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Monticello Nuclear Generating Plant ML20247K3971998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Monticello Nuclear Generating Plant ML20217D8731998-04-13013 April 1998 Rev 0 to MNGP Colr,Cycle 19 ML20217F6431998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Monticello Nuclear Generating Plant ML20216D1041998-03-0505 March 1998 Rev 21 to Operational QA Plan ML20216H6481998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Monticello Nuclear Generating Plant ML20203G1431998-02-10010 February 1998 Rev 2 to Inservice Insp Exam Plan,Third Interval,920601- 020531 ML20203B2821998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Monticello Nuclear Generating Station ML20202F9161998-01-29029 January 1998 Special Rept:On 980128,two of Three Fire Protection Pumps Were Removed from Svc as Result of Sys Configuration Necessary to Support Planned Maintenance.Fire Pumps Were Returned to Svc on 980128 ML20216D2071997-12-31031 December 1997 1997 Annual Rept for Northern States Power Co ML20197J8131997-12-31031 December 1997 Revised Evacuation Time Estimates for Plume Exposure Pathway Emergency Planning Zone at Monticello Nuclear Power Plant. W/One Oversize Drawing ML20198P2201997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Monticello Nuclear Generating Plant ML20203J7131997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Monticello Nuclear Generating Plant ML20199G7051997-11-19019 November 1997 Safety Evaluation Authorizing Relief Request 8 of Third 10 Yr Inservice Insp Interval ML20199H8181997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Monticello Nuclear Generating Plant ML20217K2081997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Monticello Nuclear Generating Plant ML20216H7771997-08-31031 August 1997 Monthly Operating Rept for Aug 1997 for Monticello Nuclear Generating Plant ML20217K2741997-07-31031 July 1997 Monthly Operating Rept for Jul 1997 for Monticello Nuclear Generating Plant ML20196H1081997-07-0808 July 1997 Rev 20 to Operational QA Plan ML20141B9271997-06-30030 June 1997 LOCA Containment Analyses for Use in Evaluation of NPSH for RHR & Core Spray Pumps ML20149E2921997-06-30030 June 1997 Monthly Operating Rept for June 1997 for MNGP ML20148S6341997-06-23023 June 1997 NPSH - Rept of Sulzer Bingham Pump 1999-09-30
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r -UNITED STATES NUCLEAR REGULATORY COMMISSION
- W AS HIN GT O N, D. C. 2 0 5 5 5 SAFETY EVALUATION BY THE OFFICE OF NUCLEAR REACTOR REGULATION SUPPORTING AMENDMENT NO. 12 TO LICENSE NO. DPR-22 (CIRNGE NO. 20 TO THE TECHNICAL SPECIFICATIONS)
NORTi!ERN STATES POWER COMPANY MONTICELLO NUCLEAR GENERATING PLANT DOCKET NO. 50-263 INTRODUCTION During the summer of 1973, inspections at two reactor facilities revealed a high incidence of inoperable hydraulic shock suppressors (snubbers) manufactured by Bergen Paterson Pipe Support Corporation. As a result of those findings, the Office of Inspection and Enforcement required each operating reactor licensee to immediately inspect all Bergen Paterson snubbers utilized on safety systems and .to reinspect then 45 to 90 days
. after the initial inspection. Snubbers supplied by other manufacturers were to be inspected on a lower priority basis.
Since a long term solution to climinate recurring failures was not immediately availabic, the Division of Reactor Licensing sent a letter dated October 2,1973, to operating facilities (including Monticello) utilizing Bergen Paterson snubbers specifying continuing surveillance requirements and requesting a submittal within one year of proposed Technical Specifications for a snubber surveillance program. On August 15,1975, .':orthern States Power Company proposed Technical Specifications for hydraulic snubbers at the Monticello reactor.
During our review of the proposed change, we found that certain modifications were necessary. These modifications were discussed with Northern States and have been incorporated into the proposed Technical Specifications.
EVALUATION ,
Snubbers are designed to prevent unrestrained pipe motion under dynamic loads as might occur during an earthquake.or severe transient while allowing normal thermal movement during startup and shutdown.
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The consequence of an inoperable snubber is an increase in the probability l of structural damage to piping resulting from a seismic or other pcstulated i event which initiates dynamic loads. It is, therefore, necessary that snubbers installed to protect safety system piping be operable during reactor operation and be inspected at appropriate intervals to assure j their operability.
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- Examination of defective snubbers at reactor facilities has shown that the high incidence of failures observed in the surmer of 1973 was caused by severo degradation of seal materials and subsequent leakage of the
- hydraulic fluid. The basic seal materials used in Bergen Paterson 4 snubbers were two types of polyurethane; a millabic gum polyester type i containing plastici
- ers and an unadulterated molded type. Shterial tests performed at several laboratories (Reference 1) established that the millabic gum polyurethane deteriorated rapidly under the temperature and moisture conditions present in many snubber locations. Although the molded polyurethane exhibited greater resistance to these conditions, it also may be unsuitabic for application in the higher temperature
! environments. Data are not currently availabic to precisely define an upper temperature limit for the molded polyurethane. The investigation indicated that seal materials are available, primarily ethylene propylene compounds, which should give satisfactory performance under the most severe conditions expected in reactor in:ta11ations.
! An extensive seal replacement program has been carried out at many reactor i facilities. Experience with ethylene propylene seals has been very
- good with no serious degradation reported thus far. Although the seal replacement program has significantly reduced the incidence of snubber failures, some failures continue to occur. These failures have generally i been attributed to faulty snubber assembly and installation, loose 3 fittings and connections and excessive pipe vibrations. The failures have been observed in both PNRs and BWRs and have not been limited to units manufactured by Bergen Paterson. Because of the continued incidence of snubber failures, we have concluded that snubber opera-j bility and surveillance requirements should be incorporated into the Technical' Specifications. We have further concluded that these require-ments should be applied to all safety related hydraulic snubbers, regardless of manufacturer, in all light water cooled reactor facilities.
4 We have developed the attached Technical Specifications and Bases to provide additional assurance _of satisfactory snubbers performance and 4 reliability. The specifications require that snubbers be operable during T
(1) Report H. R. Erickson, Bergen Paterson.to K. R. Goller, NRC, October 7, 1974,
Subject:
Hydraulic Shock Sway Arrestors 2
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4 reactor operation and prior to startup. Because snubber protection is required only during relatively low probability events, a period of 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> is allowed for repair or replacement of defective units before the reactor must be shut down.
An inspection program is specified to provide additional assurance that the snubbers remain operable. The inspection frequency is based upon maintaining a constant level of snubber protection. Thus the required inspection interval varies inversely with the observed snubber failures.
The longest inspection interval allowed in the Technical Specifications after a record of no snubber failures has been established is nominally-18 months. Experience at operating facilities has shown that the required i surveillance program should provide an acceptable level of snubber performance-provided that the seal materials are compatible with the operating environment. Snubbers containing seal caterial'which has not
- been demonstrated to be compatibic with the operating environment are required to be inspected every 31 days until compatibility is established or an appropriate seal change is completed.
To further increase the level of snubber reliability, the Technical Specifications require functional tests and internal inspections of snubbers at least once each refueling cycle. The tests will verify proper piston movement, lock up and bleed, and the internal inspections will monitor for wear, breakdown and deterioration that cannot be observed by the external inspections.
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CONCLUS:0NS We have concluded that the proposed additions to the Technical Specifi-cations, as modified, increase the probability of successful snubber
. performance, increase reactor safety and we therefore find them acceptabic.
We u.ve concluded, based on the considerations discussed above, that:
(1) because the change does not involve a significant increase in the probability or consequences of accidents previously considered and does not involve a significant decrease in a safety margin, the change does not involve a significant ha ards consi.deration, (2) there is reasonable assurance that the health and safety of the public will not be. endangered by operation in- the proposed manner, and (3) such activities will be conducted in compliance with the Commission's regulations and the issuance of this amendment will not be inimical to the common defense and security or to the health and safety of the public.
Date:
SEP 151975 4
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