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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO
MONTHYEARML20029C6191994-04-14014 April 1994 Special Rept:On 940328,meteorological Tower Instrumentation Not Returned to Svc within Allowed Out of Svc Time.Caused by Difficulty in Calibr of Input Card.Meteorological Monitoring Instrumentation Declared Operable on 940408 ML20046A0321993-07-19019 July 1993 Special Rept:On 930704,TS Time Limit Expired for SGTS Exhaust Stack High Range Radioactivity Monitor Declared Inoperable on 930701 Due to Low Sample Flow Reading. Suspected Degraded Pump Replaced.Followup Will Be Provided ML20029B1901991-02-27027 February 1991 Rev to RO Dtd 910205 Re Valid Failure of Div II Diesel Generator During Surveillance Testing on 910106.Caused by Failure of A-3 Relay Tachometer Due to Broken Wire.Caution Added to Vendor Manual Re Bench Testing Relay ML20043D1631990-05-30030 May 1990 Supplemental Special Rept on Test Failures of Div I Diesel Generator at Plant on 891220 & 900111.Problem Caused by Misapplication of Woodward EGB13P Model 9903-266 Governor. Mods Not Warranted.Diesel Generator Being Tested Weekly ML20043B3021990-05-21021 May 1990 Special Rept:On 900502,during Performance of Semiannual Channel Calibr,Personnel Identified That 60-meter Wind Direction Instrumentation Not in Calibr.Instrumentation Declared Operable on 900510 After Procedure Completed ML20043A9821990-05-15015 May 1990 Ro:On 900508,discovered That Replacement Bellows Had Tie Rods Installed to Limit Bellows Expansion.Div I & II Diesel Generators Declared Inoperable & Controlled Plant Shutdown Initiated.Unusual Event Terminated on 900509 ML20012F0591990-03-29029 March 1990 Special Rept:On 891120-1230,valid Test Failures of Div I Diesel Generator.Current Valid Failure Count for Diesel Generator Is Three.Diesel Generator Continues to Be Tested on Weekly Basis Per Tech Spec Table 4.8.1.1.2.1 ML20006F6351990-02-20020 February 1990 Ro:On 900212,Tech Specs 3.6.1.8 & 3.6.1.1 Entered Due to Failed Local Leak Rate Test on Primary Containment Penetration MC-102.Plant Shutdown Commenced & Notification of Unsual Event Declared.Plant Placed in Shutdown Condition ML20006D1541990-01-29029 January 1990 Special Rept:On 891230,during Test to Restore Diesel Generator 1A to Operable Status Following Failure on 891227, Generator Cranked But Did Not Start.Caused by Failure of Contacts on K19 Control set-up Relay.Relay Replaced ML20005G3371990-01-11011 January 1990 Special Rept:On 891211,failure of Diesel Generator DG1A to Start Noted.Caused by Failure of K19 Starting Relay.Diesel Generator Governor & Defective Speed Sensing Relay Replaced ML20005F8111990-01-0404 January 1990 Special Rept:On 891219,differential Air Temp Instrumentation Inoperable for More than 7 Days.Caused by Problem in Temp Probe on Meteorological Tower.Tower Differential Temp Instrumentation Declared Operable on 891229 ML20005E0811989-12-20020 December 1989 Special Rept:On 891120,Div 1 Diesel Generator 1A Failed During Surveillance Testing.Caused by Erratic Start Times. Diesel Generator Governors Readjusted ML19332E6121989-11-29029 November 1989 Special Rept:On 891030,test Failure of Div II Diesel Generator Occurred.Caused by Cam/Spring Holding Fallen Screw in Console Section of Panel.Holding Screw Reinstalled in Switch.Control Switch Will Be Inspected in Upcoming Outage 1994-04-14
[Table view] Category:LER)
MONTHYEARML20029C6191994-04-14014 April 1994 Special Rept:On 940328,meteorological Tower Instrumentation Not Returned to Svc within Allowed Out of Svc Time.Caused by Difficulty in Calibr of Input Card.Meteorological Monitoring Instrumentation Declared Operable on 940408 ML20046A0321993-07-19019 July 1993 Special Rept:On 930704,TS Time Limit Expired for SGTS Exhaust Stack High Range Radioactivity Monitor Declared Inoperable on 930701 Due to Low Sample Flow Reading. Suspected Degraded Pump Replaced.Followup Will Be Provided ML20029B1901991-02-27027 February 1991 Rev to RO Dtd 910205 Re Valid Failure of Div II Diesel Generator During Surveillance Testing on 910106.Caused by Failure of A-3 Relay Tachometer Due to Broken Wire.Caution Added to Vendor Manual Re Bench Testing Relay ML20043D1631990-05-30030 May 1990 Supplemental Special Rept on Test Failures of Div I Diesel Generator at Plant on 891220 & 900111.Problem Caused by Misapplication of Woodward EGB13P Model 9903-266 Governor. Mods Not Warranted.Diesel Generator Being Tested Weekly ML20043B3021990-05-21021 May 1990 Special Rept:On 900502,during Performance of Semiannual Channel Calibr,Personnel Identified That 60-meter Wind Direction Instrumentation Not in Calibr.Instrumentation Declared Operable on 900510 After Procedure Completed ML20043A9821990-05-15015 May 1990 Ro:On 900508,discovered That Replacement Bellows Had Tie Rods Installed to Limit Bellows Expansion.Div I & II Diesel Generators Declared Inoperable & Controlled Plant Shutdown Initiated.Unusual Event Terminated on 900509 ML20012F0591990-03-29029 March 1990 Special Rept:On 891120-1230,valid Test Failures of Div I Diesel Generator.Current Valid Failure Count for Diesel Generator Is Three.Diesel Generator Continues to Be Tested on Weekly Basis Per Tech Spec Table 4.8.1.1.2.1 ML20006F6351990-02-20020 February 1990 Ro:On 900212,Tech Specs 3.6.1.8 & 3.6.1.1 Entered Due to Failed Local Leak Rate Test on Primary Containment Penetration MC-102.Plant Shutdown Commenced & Notification of Unsual Event Declared.Plant Placed in Shutdown Condition ML20006D1541990-01-29029 January 1990 Special Rept:On 891230,during Test to Restore Diesel Generator 1A to Operable Status Following Failure on 891227, Generator Cranked But Did Not Start.Caused by Failure of Contacts on K19 Control set-up Relay.Relay Replaced ML20005G3371990-01-11011 January 1990 Special Rept:On 891211,failure of Diesel Generator DG1A to Start Noted.Caused by Failure of K19 Starting Relay.Diesel Generator Governor & Defective Speed Sensing Relay Replaced ML20005F8111990-01-0404 January 1990 Special Rept:On 891219,differential Air Temp Instrumentation Inoperable for More than 7 Days.Caused by Problem in Temp Probe on Meteorological Tower.Tower Differential Temp Instrumentation Declared Operable on 891229 ML20005E0811989-12-20020 December 1989 Special Rept:On 891120,Div 1 Diesel Generator 1A Failed During Surveillance Testing.Caused by Erratic Start Times. Diesel Generator Governors Readjusted ML19332E6121989-11-29029 November 1989 Special Rept:On 891030,test Failure of Div II Diesel Generator Occurred.Caused by Cam/Spring Holding Fallen Screw in Console Section of Panel.Holding Screw Reinstalled in Switch.Control Switch Will Be Inspected in Upcoming Outage 1994-04-14
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARU-603277, Monthly Operating Rept for Sept 1999 for Clinton Power Station,Unit 1.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Clinton Power Station,Unit 1.With ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers U-603267, Monthly Operating Rept for Aug 1999 for Clinton Power Station,Unit 1.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Clinton Power Station,Unit 1.With U-603245, Monthly Operating Rept for Jul 1999 for CPS Unit 1.With1999-07-31031 July 1999 Monthly Operating Rept for Jul 1999 for CPS Unit 1.With ML20211C9621999-07-26026 July 1999 ISI Summary Rept U-603232, Special Rept:On 990531 Lpms Was Declared Inoperable Due to Receipt of High Vibration & Loose Parts Alarm Which Did Not Clear.Lpms Was Restored to Operable Status on 990707 After Alignment & Tension on Recorder Tape Drive Was Adjusted1999-07-0909 July 1999 Special Rept:On 990531 Lpms Was Declared Inoperable Due to Receipt of High Vibration & Loose Parts Alarm Which Did Not Clear.Lpms Was Restored to Operable Status on 990707 After Alignment & Tension on Recorder Tape Drive Was Adjusted U-603233, Monthly Operating Rept for June 1999 for Clinton Power Station,Unit 1.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Clinton Power Station,Unit 1.With U-603222, Monthly Operating Rept for May 1999 for Clinton Power Station.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Clinton Power Station.With ML20210K8391999-05-11011 May 1999 British Energy Annual Rept & Accounts 1998-99 ML20206H1231999-05-0505 May 1999 Illinois Power Co CPS Main CR Simulator Certification Rept U-603210, Monthly Operating Rept for Apr 1999 for Cps,Unit 1.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Cps,Unit 1.With U-603204, Final Part 21 Rept 21-99-003 Re Deficiency in Commercial Grade Dedication Process Used by Circuit Breaker Refurbishment Supplier Trentec for Westinghouse Breaker 1AP05EH.Issue Determined Not Reportable Per 10CFR211999-04-30030 April 1999 Final Part 21 Rept 21-99-003 Re Deficiency in Commercial Grade Dedication Process Used by Circuit Breaker Refurbishment Supplier Trentec for Westinghouse Breaker 1AP05EH.Issue Determined Not Reportable Per 10CFR21 U-603192, Monthly Operating Rept for Mar 1999 for Clinton Power Station,Unit 1.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Clinton Power Station,Unit 1.With U-603182, Part 21 Rept Re Deficiency in Commercial Grade Dedication Process Used by Circuit Breaker Refurbishment Supplier, Trentec.Condition Rept 1-99-01-136 Was Initiated to Track Investigation & Resolution of Issue1999-03-12012 March 1999 Part 21 Rept Re Deficiency in Commercial Grade Dedication Process Used by Circuit Breaker Refurbishment Supplier, Trentec.Condition Rept 1-99-01-136 Was Initiated to Track Investigation & Resolution of Issue U-603176, Monthly Operating Rept for Feb 1999 for Clinton Power Station,Unit 1.With1999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Clinton Power Station,Unit 1.With ML20207F2031999-02-10010 February 1999 Rev 1 to CPS COLR for Reload 6 Cycle 7 ML20202J0181999-02-0303 February 1999 SER Accepting Changes in Quality Assurance Program,Which Continues to Meet Requirements of App B to 10CFR50 U-603144, Monthly Operating Rept for Dec 1998 for Clinton Power Station,Unit 1.With1998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Clinton Power Station,Unit 1.With U-603223, Illinova Corp 1998 Annual Rept. with1998-12-31031 December 1998 Illinova Corp 1998 Annual Rept. with U-603115, Part 21 Interim Rept 21-98-021 Re Deficiencies in Matl Dedication Process Used by Goulds Pumps in Supplying SR Parts to Npps.Issue Is Not Reportable Under 10CFR21. Dedication Process Did Not Affect Ability of Components1998-12-0404 December 1998 Part 21 Interim Rept 21-98-021 Re Deficiencies in Matl Dedication Process Used by Goulds Pumps in Supplying SR Parts to Npps.Issue Is Not Reportable Under 10CFR21. Dedication Process Did Not Affect Ability of Components U-603124, Monthly Operating Rept for Nov 1998 for Clinton Power Station,Unit 1.With1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Clinton Power Station,Unit 1.With U-603114, Part 21 Rept 21-98-049 Re W Dhp Circuit Breaker Refurbished by Nuclear Logistics,Inc Which Failed to Operate.Caused by Trip Latch out-of-adjustment & Incorrectly Sized Ratchet Lever Assembly Bushing.Breakers Were Returned to Vendor1998-11-25025 November 1998 Part 21 Rept 21-98-049 Re W Dhp Circuit Breaker Refurbished by Nuclear Logistics,Inc Which Failed to Operate.Caused by Trip Latch out-of-adjustment & Incorrectly Sized Ratchet Lever Assembly Bushing.Breakers Were Returned to Vendor U-603103, Monthly Operating Rept for Oct 1998 for Clinton Power Station,Unit 1.With1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Clinton Power Station,Unit 1.With U-603101, Special Rept:On 980918,discovered That Triaxial Seismic Accelerometers Had Not Been Properly Calibrated.Caused by Inadequate Calibration Procedure.Calibration to Be Performed off-site1998-10-28028 October 1998 Special Rept:On 980918,discovered That Triaxial Seismic Accelerometers Had Not Been Properly Calibrated.Caused by Inadequate Calibration Procedure.Calibration to Be Performed off-site ML20154F8701998-10-0606 October 1998 Safety Evaluation Authorizing Proposed Alternative to Requirements of OMa-1988,Part 10,Section 4.2.2.3 for 21 Category a Reactor Coolant Sys Pressure Isolation Valves U-603091, Monthly Operating Rept for Sept 1998 for Clinton Power Station,Unit 1.With1998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Clinton Power Station,Unit 1.With ML20153F9871998-09-17017 September 1998 Safety Evaluation Accepting 980225 Proposed Rev 26 to Illinois Power Nuclear Program Qam ML20151U1391998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Clinton Power Station,Unit 1 ML20237E3991998-08-27027 August 1998 SER Accepting Licensee Response to NRC Bulletin 95-002, Unexpected Clogging of Residual Heat Removal Pump Strainer While Operating in Suppression Pool Cooling Mode, for Clinton Power Station ML20237A1521998-08-0707 August 1998 SER Re Mgt Services Agreement at Clinton Power Station. Approval Under 10CFR50.80 Not Required ML20151Y6591998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Clinton Power Station,Unit 1 U-603033, Part 21 Rept 21-98-039 Re Shrinkage of Medium & High Density Silicone Seals Designed & Installed by Bisco Using Dow Corning Sylgard 170 Matl.Caused by Coefficient of Thermal Expansion.Will Inspect & Rework/Repair Suspected Seals1998-07-20020 July 1998 Part 21 Rept 21-98-039 Re Shrinkage of Medium & High Density Silicone Seals Designed & Installed by Bisco Using Dow Corning Sylgard 170 Matl.Caused by Coefficient of Thermal Expansion.Will Inspect & Rework/Repair Suspected Seals U-603041, Monthly Operating Rept for June 1998 for Clinton Power Station,Unit 11998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Clinton Power Station,Unit 1 ML20151U1501998-06-30030 June 1998 Revised Monthly Operating Rept for June 1998 for Clinton Power Station,Unit 1 U-603023, Monthly Operating Rept for May 1998 for Clinton Power Station,Unit 11998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Clinton Power Station,Unit 1 U-603014, Special Rept:On 980512,lightning Struck Primary Meteorological Monitoring Instrumentation Tower Damaging 60- Meter Wind Speed & Associated Transmuter Circuit Card. Surveillance Testing Performed1998-05-28028 May 1998 Special Rept:On 980512,lightning Struck Primary Meteorological Monitoring Instrumentation Tower Damaging 60- Meter Wind Speed & Associated Transmuter Circuit Card. Surveillance Testing Performed ML20236E7991998-05-26026 May 1998 Final Part 21 Rept Re W Dhp Circuit Breaker Auxillary Switch Operating Assembly Anomalies.Caused by Loss of Breaker Safety Function.Dhp Circuit Will Be Inspected ML20248F3531998-05-21021 May 1998 Part 21 Rept Re Electronic Equipment Repaired or Reworked by Integrated Resources,Inc from Approx 930101-980501.Caused by 1 Capacitor in Each Unit Being Installed W/Reverse Polarity. Policy of Second Checking All Capacitors Is Being Adopted U-603004, Part 21 Rept Re 980107 Determination That Itt Barton Model 580A Series Differential Pressure Indicating Switches Operating Forces Too Low.Manufacturing Sys Allowed Switches to Be Mixed.Evaluation Concludes Issue Not Reportable1998-05-15015 May 1998 Part 21 Rept Re 980107 Determination That Itt Barton Model 580A Series Differential Pressure Indicating Switches Operating Forces Too Low.Manufacturing Sys Allowed Switches to Be Mixed.Evaluation Concludes Issue Not Reportable ML20216A9601998-05-0808 May 1998 Part 21 Rept Re Failure of 12 Volt DC Inverter Power Supply. Caused by Inadequately Sized Output Transistor Pair Combined W/Degraded Capacitors.Licensee Plans to Replace All Output Transistors & Degraded Capacitors U-602995, Part 21 Interim Rept 21-98-021 Re Deficiencies in Matl Dedication Process Used by Goulds Pumps During Use of Portable Metal Analyzer.Util Identified Discrepancies Which Are Acceptable W/Some Exception of Some Replacement Parts1998-05-0505 May 1998 Part 21 Interim Rept 21-98-021 Re Deficiencies in Matl Dedication Process Used by Goulds Pumps During Use of Portable Metal Analyzer.Util Identified Discrepancies Which Are Acceptable W/Some Exception of Some Replacement Parts U-603006, Monthly Operating Rept for Apr 1998 for Clinton Power Station,Unit 11998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Clinton Power Station,Unit 1 U-602994, Part 21 Rept Re Final Rept 21-98-008,on 980113,reliance Electric Motors Supplied by Rockwell International for Hydrogen Recombiner Cooling Fans Do Not Have nameplate- Specified High Temperature Bearings.Fan Motors Acceptable1998-04-29029 April 1998 Part 21 Rept Re Final Rept 21-98-008,on 980113,reliance Electric Motors Supplied by Rockwell International for Hydrogen Recombiner Cooling Fans Do Not Have nameplate- Specified High Temperature Bearings.Fan Motors Acceptable ML20216B1351998-04-21021 April 1998 Rev 0 to Illinois Power Co Clinton Power Station SVC Design Rept U-602979, Final Part 21 Rept 21-97-059 Re Discrepancies Found During Receipt Insp of Three Refurbished safety-related W Dhp Circuit Breakers.Util Completed Evaluation,Per 10CFR21 & Concludes That Condition Is Not Reportable1998-04-0707 April 1998 Final Part 21 Rept 21-97-059 Re Discrepancies Found During Receipt Insp of Three Refurbished safety-related W Dhp Circuit Breakers.Util Completed Evaluation,Per 10CFR21 & Concludes That Condition Is Not Reportable U-602976, Monthly Operating Rept for Mar 1998 for Clinton Power Station1998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Clinton Power Station ML20217H5771998-03-27027 March 1998 Safety Evaluation Concluding That No Significant Safety Hazards Introduced at CPS for Net 32% Ampacity Derating Factor for 1 H & 3 H Conduit Fire Barrier Sys & 1 H Cable Tray Fire Barrier Sys.Requests Response Addressing Issue U-602968, Interim Part 21 Rept 21-97-055 Re Westinghouse Dhp Circuit Breaker Auxiliary Switch Operating Assembly Anomalies. Initially Reported on 980116.Util Currently Evaluating Suppliers Response to Questions Re Issue1998-03-24024 March 1998 Interim Part 21 Rept 21-97-055 Re Westinghouse Dhp Circuit Breaker Auxiliary Switch Operating Assembly Anomalies. Initially Reported on 980116.Util Currently Evaluating Suppliers Response to Questions Re Issue U-602960, Part 21 & Deficiency Rept Re Commerical Grade Dedication Program of Sentry Equipment Corp.Initially Reported on 980217.IP Performed an Addl Assessment at Sentry Facility on 980226.Next Rept Will Be Submitted by 9804111998-03-12012 March 1998 Part 21 & Deficiency Rept Re Commerical Grade Dedication Program of Sentry Equipment Corp.Initially Reported on 980217.IP Performed an Addl Assessment at Sentry Facility on 980226.Next Rept Will Be Submitted by 980411 U-602954, Interim Part 21 rept,21-98-008 Re Identification That Bearings Installed in Hydrogen Recombiner B Cooling Fan Motor 0HG04CB Were Not Same as Bearings Specified on Motor Nameplate.Will Complete Evaluation of Issue by 9805131998-03-0909 March 1998 Interim Part 21 rept,21-98-008 Re Identification That Bearings Installed in Hydrogen Recombiner B Cooling Fan Motor 0HG04CB Were Not Same as Bearings Specified on Motor Nameplate.Will Complete Evaluation of Issue by 980513 1999-09-30
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U.601632 1A7 90(03 29).LP 8E.110e til/NotR POWER COMPANY y cteos Pata 57AtsoN. P.o. to 98. et mos ittisois ont March 29, 1990 f
L Docket No, 50 461 U.S. Nuclear Regulatory Commission
! Document Control Desk Washington, D.C. 20555 i
Subject:
Special Report: Supplemental Report on Test Failures of the Division I Dianel Cenerator at Clinton Power Station (CPS)
Dwar Str:
L Sy SPECIAL REPORTS dated December 20, 1989 and January 11, 1990, Illinois Power (IP) reported valid test failures of the Division I diesel generator (Dw'1.A) as a result of slow starts on November 20, 1989, December 11, 1989 and December 27, 1989. Additionally,.by SPECIAL REPORT dated January 29, 1990, IP reported a valid test failure of DG1A as a result of a failure to start on December 30, 1989. The January 11, 1990 and January 29, 1990 SPECIAL REPORTS identified that an Action Plan i
had been developed to identify the root cause and resolve those factors which may have contributed to the slow starts of DG1A. Additionally, the January 29, 1990 SPECIAL REPORT identified that a failure analysis would be performed on the K19 control relay failure which had caused the-DCIA failure to start on December 30, 1989. This supplemental SPECIAL REPORT provides the available results of this Action Plan and K19 control relay failure analvsis.
DCIA Action Plan Detailed assessments of DG1A commenced following the slow start on November 20, 1989. The initial investigation relied upon instruisentation which could be installed with DCIA in service. This initial investigation was previously discussed in the January 29, 1990 SPECIAL REPORT. As described in that SPECIAL REPORT, corrective action for the December 27, 1989 slow start led to the replacement of the Woodward Covernor actuator on the 12. cylinder engine (DG1A utilites
- B tanden 12. cylinder and 16. cylinder diesel engines). The decision to replace the 12. cylinder engine governor was based upon the observed characteristics of the response of DG1A during starting sequences.
Instrumentation installed on the DGIA control system circuitry per the Action Plan had not revealed any specific cause far the slow starts outside of the governor itself. Since plant operating conditions
. precluded installing full instrumentation per the Action Plan prior to the governor replacement, the functional characteristics of the removed (
governor could not be fully assessed prior to its removal.
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As identified in the January 11, 1990 SPECIAL REPOkT, prior to i replacement of the 12. cylinder engine governor on December 27, 1990, the governors of DGIA were different models. Both sodels were approved for use on the installed diesels and the governor manufacturer had stated ,
that the tvo models were interchangeable. Replacement of the governor '
on the 12. cylinder engine (EGB.13P model 9903 266) resulted in restoring t
- consistency in the models for the two engines. The currently installed i governors are both EGB.13P model 9903 265. ;
1 Purther specific testing of DGIA under the Action Plau was i accomplished on February 23, 1990. Test instrumentation was installed (
to allow monitoring of 24 additional points (10 on the air start system, ;
4 on the agine governor, 6 on the fuel system, and 4 on the !
start / con;tol circuitry). In addition to using this test !
instrumentation, existing pressure gauges, the installed General l Electric Transient Analysis Recorder (GETARs), and observations by l support personnel were utilized, During the four start attempts on i February 23, 1990, all external characteristier. of the DG1A response j were observed to be normal. The governor actuators responded to the ;
start signals properly, as did the air start actors and fuel pumps. !
DGIA start times ranged between 9.4 and 8.9 seconds, with the first ;
start being the slowest. Start times of the successive three starts !
vere all within the 9.1 to B.9 second range that has been characteristic i of DG)A starts subsequent to the 12.cylindor engine governor i replacement. ;
The measured pressure and flow characteristics of the air start system indicate that the existing air start system design is adequate. !
As discussed in the January 29, 1990 SPECIAL REPORT, modifications to i the air start piping to improve air start motor performance had '
previously been recommended for evaluation. A recom w.dation to proceed I with this improvement is being reassessed based upon the data obtained ;
under the Action Plan. :
Similarly, fuel system characteristics were also assessed as being !
adequate. Two modifications, one to provide continuous operation of the i fuel priming pumps during diesel generator operation (Field Alteration :
DGP023), and one to raise the setpoint of the fuel oil day tank level ;
switches to reduce the likelihood of air entrainment during transfer 1 pump testing (Field Alteration D0F002) are being pursued as reliability l enhancements. No immediate corrective actions were determined to be i required for maintaining fuel system operability. ,
i A central feature of the investigation under the Action Plan has i been assessment of governor operation, rollowing the 12.c)1inder !
governor replacement on December 27, 1989, the relative responses of the r 12 cylinder and 16. cylinder engine governors of DG1A were assessed. !
Using stop watches, the duration of the
- full fuel" output stroke of each governor was simultaneously measured. The times for both governors l were between 7 and 8 seconds for the duration of the maximum fuel demand >
signal. The times for DG1A to reach rated speed during these tests were between 8.9 and 9.1 seconds.
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i During the add!tional testing conducted on Dbrtary 23, 1990, a >
more detailed asm.essment. of the response of the g6vernors was conducted. :
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These tests showed that the magnitude and duration of the input.and output pressure signals of each governor booster servomotor were very ;
similar, and that the governor internal actuating, fluid pressure built !
up properly and was maintained throughout the diesel generator '
acceleration to rated speed. Conettrrently, observers stationed at the ,
governors evaluated fuel rack motion. All observation results were favorable, i
As previously noted, the governor on the 12 cylinder engine .
(Woodward ECB.13P, model 9903 266 S/N 2113014) was replaced before an i An. situ assessment of the starting response of this device could be ,
conducted. Since it is essential to understand what impact operation of this governor had on the DG1A start time, the governor was returned to j Woodward for functional testing. The following discussion details the ,
results of this functional testing. ,
Testing at Woodward (wirnessed by an IP engineer) was planned to recreate the conditions surrounding an engine start from standby conditions following a dormant period. However. limitations in the t testing facilities did :not allow the questionable governor (model 9903 266) to ho tested in tandem with an ECB.13P model 9903 265 governor.
Therefore, the response characteristics of operating the model 9903 266 governor alone were evaluated. This was done using a test stand with an acceleration rate s/9t to match that of the CPS DCIA. :
Ten test starts were conducted. The first test start was expected to be the most representative of the CPS conditions since the slow i starts had only occurred following some dormant tito. During this first test start, the governor did display a lack of response. However, this i test was interrupted by a Woodward Covernor engineer who felt that the governor was not responding because of internal air pockets. The ,
subsequent nine test results were very consistent. During these tests, L the governor setpoints were annessed as being correct. In all tests, '
the initial response (zero RPr( to 200 300 RPM) of the model 9903 266 ,
governor was observably slower than that known to occur during starts j using a 9903 265 model governor. The impact of the slower response of r the 9903 266 model actuator is not yet fully understood. However, i further testing of the removed governor at Woodward is planned.
M19 fontrol Relav Failure Analysis The January 29, 1990 SPECIAL REPORT identified that the relay [
manufacturer would perform a failure analysis of the K19 control relay.
The results of this analysis are presented below. ;
As identified in the January 29, 1990 SPECIAL REPORT, the DCIA '
failure to start was caused by a failure of the 2D 2E contact pair of the K19 relay. Failure analysis of the K19 relay (Potter and Brumfield Company type MDR, model number 5095) revealed high contact resistance ,
across the 2D 2E contacts. The small load that this relay contact pair -
carries (22 mA) has been evaluated as being insufficient to ensure ,
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F electrical cleaning of the contactor surfaces following extended usage.
This led to circuit interruption, resulting in the DGIA failure to F start.
! This relay failure is not considered to be related to the observed slow st.ert, problem. No further corrective actions are being considered for immediate septementation, however, relay operation is being monitored during routine diesel generator tests. The service history of the K19 relay at CPS provides assurance that the recently installed relay will provide several years of reliable service under normal operating conditions. An appropriate frequency for periodic replacement of this relay is currently being evaluated.
G2nclM19na rollowing replacement of the governor on the 12. cylinder engine on December 27, 1989, no subsequent start attempts have resulted in start times in excess of the 12 second limit of the Technical Specifications, except for the one start attempt that failed due to the K19 control relay malfunction. (As identified above, the December 30, 1989 failure is considered to be independent of the slow start problem.) The objective data strongly suggests that replacement of the 12. cylinder engine governor with a model 9903 265 under the Action Plan has resolved the DG1A slow start problem. Although, as discussed above, the root cause has not been conclusively identified, implementation of the Action Plan has confirmed the effectiveness of corrective actions and effected a thorough investigation.
Further testing of the removed governor at Woodward during April, 1990 is planned. Scheduling of specific dates for this additional testing is dependant upon development of a test method which will more fully assess the performance of this governor under simulated operational conditions. Until this additional testing can be completed, the remaining spare model 9903 266 governor at CPS has been placed on hold to prevent it from being used as a replacement. The results of this additional testing vill be provided in an additional supplemental report by May 31, 1990.
Additionally, the Action plan testing and analysis results have been reviewed for applicability to the Division 2 (DG1B) and 3 (DG10) diesel generator units. The DGIA slow start problem has not occurred on either of these two units, DG1B has always had the same model governors (EGB.13P model 9903 265) on both engines and has never displayed a tendency to start slowly. DG1C is a single. engine unit and utilizes a L
completely different type of governor (Woodward model UG.8). DGIC has never experienced a slow start. The reliability enhancements being l considered for the DGIA air start system and fuel system are likewise l being considered for DG18.
The K19 relay problem does not impact DG10, since DG1C does not utilize this type of relay in any application. DG1B does use a Potter 6 l Brumfield MDR 5095 relay in an application identical to that used in IXil A. This DG1B relay is scheduled to be replaced under MVR D08247 l during the current plant outage (PO 3).
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Additional Information As of March 26, 1990, a total of 13 successful, successive, valid tests of DG1A have been completed since the last valid failure on December 30, 1989. The current valid failure count for DG1A is 3 in the last 20 valid tests performed and 8 in the last 100 valid testa performed (only 81 valid tests 1. ave been performed for DG1A since receipt of the operating license). Therefore, DG1A continues to be tested on a weekly basis in accordance with Technical Specification Table 4.8.1.1.2 1.
Sincerely yours, 9 %qb T.A.Spabgenbbrg,III Manager Licensing an Safety DAS/can ec: NRC Clinton Licensing project Manager NRC Resident Office Illinois Department of Nuclear Safety i
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