IR 05000263/2010007

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November 10, 2010

Mr. Timothy Site Vice President Monticello Nuclear Generating Plant Northern States Power Company, Minnesota 2807 West County Road 75 Monticello, MN 55362-9637

SUBJECT: MONTICELLO NUCLEAR GENERATING PLANT PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION REPORT 05000263/2010007

Dear Mr. O'Connor:

On October 1, 2010, the U.S. Nuclear Regulatory Commission (NRC) completed a Problem Identification and Resolution (PI&R) inspection at your Monticello Nuclear Generating Plant. The enclosed report documents the inspection results, which were discussed on October 1, 2010, with you and other members of your staff. The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel. The inspection concluded that your staff was effective at identifying problems and incorporating them into the corrective action program (CAP). In general, issues were appropriately prioritized, evaluated, and corrected; audits and self-assessments were thorough and probing, and operating experience was appropriately screened and disseminated. Your staff was aware of the importance of having a strong safety-conscious work environment and expressed a willingness to raise safety issues. The inspectors also observed that actions taken to address a declining trend in Human Performance appeared to be effective. However, your staff was not fully effective in addressing an adverse trend in contractor oversight and in work control and planning, which had begun earlier this year. Although both issues were captured in the CAP program, the underlying causes were not fully understood. This resulted in corrective actions being more reactive, instead of proactive, when responding to related issues. The inspectors were concerned that this adverse trend, if not resolved, would negatively impact the significant number of work activities planned for next year. No violations or findings were identified during this inspection. In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records System (PARS) component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,/RA/

Kenneth Riemer, Chief Branch 2 Division of Reactor Projects

Docket No. 50-263 License No. DPR-22

Enclosure:

Inspection Report 05000263/2010007

w/Attachment:

Supplemental Information cc w/encl: Distribution via ListServe

U. S. NUCLEAR REGULATORY COMMISSION REGION III Docket No. 50-263 License No. DPR-22 Report No: 05000263/2010007 Licensee: Northern States Power Company, Minnesota Facility: Monticello Nuclear Generating Station Location: Monticello, MN Dates: September 13 - October 1, 2010 Inspectors: N. Shah, Project Engineer - Team Lead D. Sand, Acting Resident Inspector - Monticello C. Scott, Reactor Engineer G. O'Dwyer, Reactor Engineer M. Phalen, Plant Support Specialist Approved by: Kenneth Riemer, Chief Branch 2 Division of Reactor Projects Enclosure

SUMMARY OF FINDINGS

........................................................................................................... 1

REPORT DETAILS

OTHER ACTIVITIES

...................................................................................................... 3

4OA2 Problem Identification and Resolution

.................................................. 3 4OA6 Management Meetings ........................................................................................ 8

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

..................................................................................................... 1

LIST OF ITEMS

OPENED, CLOSED AND DISCUSSED ......................................................... 1

LIST OF DOCUMENTS REVIEWED

......................................................................................... 2

LIST OF ACRONYMS

US [[]]

ED .................................................................................................. 15

Enclosure

SUMMAR Y
OF [[]]
FINDIN [[]]
GS [[]]
IR [[05000263/2010007; 09/13/2010 - 10/01/2010; Monticello Nuclear Generating Station; Biennial Baseline Inspection of the Identification and Resolution of Problems. This team inspection was performed by four regional inspectors and the resident inspector. No violations or findings were identified. Identification and Resolution of Problems Overall, the Corrective Action Program (]]

CAP) was good. Issues were effectively identified, evaluated and corrected. Nuclear Oversight (NOS) audits and department self-assessments

were generally critical and identified issues that were captured in the (CAP). Operating Experience (OE) was well communicated and appropriately evaluated. A strong safety culture was evident, based on interviews with licensee staff and a review of the types of issues captured in the

CAP and Employee Concerns Program (
ECP ). The inspectors observed that the evaluation of
OE in Apparent Cause Evaluations (
ACE s) had improved since the
2008 PI&R inspection. Specifically,
ACE s now discussed whether the failure to properly evaluate previously identified
OE was a potential precursor of the event. The licensee took proactive efforts to address a declining trend in the Security Department Safety-Conscious Work Environment (

SCWE). The inspectors received positive feedback

during interviews with Security officers, and noted an increasing trend in the number of issues identified by the Security force. The licensee's actions to address the previous cross-cutting issues in Human Performance and a potential cross-cutting issue in Issue Evaluation appeared good. The corrective actions

appeared appropriate and the inspectors noted improving performance over the last six months in these areas. However, the inspectors noted that the licensee had recurring problems with managing the

CAP backlog and with ensuring that items identified during management observations were captured in the
CAP. The inspectors also identified some examples where licensee staff had changed due dates for subtasks without referencing the source
CAP report. The inspectors identified that

CAP implementing procedures did not provide good guidance regarding how to evaluate "critical" and "non-critical" component failures. Specifically, some component failures, which could reasonably be considered "critical," (i.e., had significant consequences) could be classified as "non-critical" using the current guidance. The inspectors observed that there were continuing issues related to work planning and execution and with contractor control. Although both problems were captured in the CAP,

the underlying causes were not yet fully understood, resulting in most of the corrective actions

being reactive rather than proactive. For example, it was unclear whether the underlying

causes that affected site human performance were the same issues that were affecting the contractor performance. In addition, as previously stated, some issues identified through management observations associated with these topics may not be captured in the CAP.

Although the station continued to evaluate the issue, it remained an area of concern given the significant outage work planned for the next year.

Enclosure

A. [[]]

NRC-Identified and Self-Revealed Findings No findings were identified. B. Licensee-Identified Violations No violations of significance were identified.

Enclosure

REPORT [[]]
DETAIL S 4.
OTHER [[]]
ACTIVI TIES
4OA 2 Problem Identification and Resolution (
PI&R ) (71152B) The activities documented in sections .1 through .4 constituted one biennial sample of
PI&R as defined in Inspection Procedure (
IP ) 71152. .1 Assessment of the Corrective Action Program (CAP) Effectiveness a. Inspection Scope The inspectors reviewed the licensee's
CAP implementing procedures and attended
CAP program meetings to assess the implementation of the
CAP by site personnel. The inspectors reviewed risk and safety significant issues in the licensee's
CAP since the last
NRC [[]]

PI&R inspection in November 2008. The issues selected were appropriately varied across the NRC cornerstones, and were identified through

routine daily plant activities, licensee audits and self-assessments, industry operating

experience reports, and

NRC inspection activities. The inspectors also reviewed a selection of apparent, common and root cause evaluations for more significant
CAP items. The inspectors performed a more extensive review of the licensee's efforts to address ongoing issues with human performance and issue evaluation. This review consisted primarily of a five year search of related issues identified in the
CAP and discussions with appropriate licensee staff to assess the licensee's corrective actions. During the reviews, the inspectors evaluated whether the licensee staff's actions were in compliance with the facility's

CAP and 10 CFR Part 50, Appendix B requirements.

Specifically, whether licensee personnel were identifying plant issues at the proper

threshold, entering the plant issues into the station's CAP in a timely manner, and

assigning the appropriate prioritization for resolution of the issues. The inspectors also evaluated the timeliness and effectiveness of corrective actions for selected issue reports, completed investigations, and

NRC findings. All documents reviewed during this inspection were listed in the Attachment to this report. b. Assessment (1) Effectiveness of Problem Identification The licensee's implementation of the
CAP was generally good. Workers were encouraged to identify issues and were familiar with the various avenues available (NRC,
CAP , etc). This was evident by the large number of

CAP items generated

annually, which were reasonably distributed across the various departments. A shared

computerized database was used for creating individual reports and for subsequent

management of the processes of issue evaluation and response. This included

determining the issue's significance, addressing such matters as regulatory compliance

and reporting, and assigning any actions deemed necessary or appropriate.

Enclosure In reviewing licensee management observations conducted between June and October

2010, the inspectors found several examples of items that were apparently not captured in the

CAP. Most of the examples were concerned with industrial safety or work planning issues that should have been captured in the

CAP. In one example, a worker

observing an industrial safety concern stated that because the worker had not met a

management expectation, vice a procedural requirement, the issue wasn't going to be

documented in the

CAP. The licensee documented the inspectors' concern as

CAP item 1251890. The licensee was also good at identifying and resolving trends. The inspectors noted a large number of trends identified through the "binning" of issues or via the quarterly department roll-up meeting (DRUM) reports. During the November 2008, PI&R review, the inspectors identified that the licensee's trending program was somewhat limited in that it did not always identify trends with

issues affecting the same functional area, but having dissimilar aspects. Subsequently,

the licensee initiated an effort to assign cross-cutting criteria (analogous to NRC criteria)

to apparent and root cause evaluations, which were then trended. Although the

inspectors considered this a positive effort, it was too early to determine its overall effectiveness. Findings No findings were identified. (2) Effectiveness of Prioritization and Evaluation of Issues Overall, CAP issues were being properly screened. The majorities of issues were of low level and were either closed to trend or at a level appropriate for a condition evaluation.

Licensee staff appropriately challenged

CAP items during screening meetings and were cognizant of potential trends. Most issues were closed to a work request or to another

CAP item. The inspectors noted that both the parent and daughter documents had the

necessary verbiage to document the interrelationship. Although fewer in number, the

inspectors did not have any concerns with those issues assigned an apparent cause

evaluation (ACE) or root cause evaluation. There were no items in the operations, engineering, or maintenance backlogs that were risk significant, individually or collectively. There were no classifications or immediate operability determinations with which the inspectors disagreed. Root and apparent cause evaluations were generally of good quality and were well documented. During the

2006 PI&R inspection, the inspectors noted that

ACEs did not

consider whether the failure to consider industry OE was a precursor to events.

Additionally, licensee management did not always address issues with ACE quality that

were identified during the evaluation grading process. The inspectors noted that subsequent

ACE s now addressed whether
OE was properly used prior to the event and that
ACE quality issues were communicated to the originating departments. Station Procedure

FP-E-SE-02, "Component Classification," was used by licensee staff to distinguish between a "critical" and "non-critical" component failure. The procedure

was written specifically to address equipment reliability, but was referenced in the CAP

for use during cause evaluations. Although the stated guidance was adequate for

Enclosure equipment reliability considerations, it was not appropriate for

CAP evaluations. For example, this procedure specifically defines any component failure that results in a significant radiological release as a "non-critical" component failure. From a

CAP perspective, any component failure resulting in significant radiological consequences would be "critical." The inspectors were concerned that this procedure may result in

some component failures being treated as less significant under the

CAP , then appropriate. The licensee initiated

CAP item 1250116 to review this issue. Since 2006, the licensee has experienced numerous issues in human performance. Initially, these issues were primarily of low significance (i.e., did not result in an NRC finding). However, the issues continued through 2008, with the significance of the

findings increasing, until an adverse trend in human performance had become evident. The licensee's early efforts to address this trend were largely ineffective, as the licensee originally believed that the human performance issues were limited to specific behaviors or work groups, instead of a more widespread concern involving fundamental human

behaviors. Subsequently, the licensee identified that the issues were principally due to a

lack of resources and an inappropriate tolerance for risk among workers. Several

corrective actions were initiated, including additional training to site workers on

configuration control and risk management. The inspectors noted that performance had

improved among site workers in the past six months. However, the licensee was still dealing with an adverse trend in contractor human performance, primarily related to oversight and work planning and execution. Although this issue was captured in the CAP (items 1249158 and 1247197), the

underlying causes are not yet fully understood, and many of the corrective actions, to date, have been more reactive than proactive. For example, it is unclear whether the

underlying causes that affected site human performance were also affecting the contractor performance. To date, the majority of the issues have been of low significance (i.e., not resulting in an

NRC finding); however, the overall trend was similar to the previous issue with site human performance. Findings Introduction: The inspectors identified an Unresolved Item (
URI ) regarding the High Energy Line Break (HELB) Analyses. Description: As part of the review of the
ACE for an adverse trend in double disc gate valve (

DDGV) local leak rate testing (LLRT) performance documented in CAP 1202466,

the inspectors noted that the ACE had determined that the valves' performance

degradation did not prevent the valves from performing their safety function. The

ACE only addressed the valves' safety function of providing containment isolation. The inspectors questioned if the safety function of the high pressure coolant injection (

HPCI), reactor core isolation cooling (RCIC) and reactor water cleanup (RWCU) steam supply

valves to close after detection of a

HE [[]]

LB should have been considered. The licensee

responded that the ACE did not need to consider the effect of the valves' increased

leakage on the

HELB analyses because any leakage would not impact the alternate shutdown path. The inspectors reviewed the assumptions and acceptance criteria of the
HELB calculations for
HPCI ,
RCIC and
RW [[]]

CU line breaks and identified potential

inconsistencies between the calculations' assumptions with Technical Specifications'

and

UFS [[]]

AR allowed values for valve closure times, incorporation of delay actuations,

and isolation initiation signals. The licensee entered the NRC concerns with these

Enclosure potential inconsistencies into the

CAP by initiating

CAP 01252363 on October 1, 2010. The licensee stated that the calculations were appropriate and provided the inspectors

with some original licensing documents for the

HELB analyses; however, additional questions remained. This issue will be tracked as
URI 05000263/201007-01 pending further
NRC review of the licensee responses and the
HELB [[analyses and determination of the original and current licensing bases. (3) Effectiveness of Corrective Actions The inspectors concluded that corrective actions for identified deficiencies were generally timely and adequately implemented, commensurate with their safety significance. Those corrective actions addressing selected]]
NRC [[documented violations were also generally effective and timely. The inspectors verified that work orders were in place (and scheduled) for selected, open actions that were two years old or greater. During interviews, the inspectors noted that some individuals did not refer back to the parent]]

CAP when changing due dates for associated subtasks (such as work requests).

The inspectors identified several examples where the revised due dates for subtasks were inconsistent with the parent CAP. Although none of the identified examples were highly significant, the inspectors were concerned that the practice may result in other

changes having a greater operational impact. The licensee initiated CAP item 1250089 to evaluate this issue. The station has a recurring problem with managing the backlog. A recent licensee initiative to redefine the items tracked in the backlog has reduced the numbers, but didn't

necessarily address the issue. The licensee currently tracks only Corrective Actions, Corrective Actions to Prevent Recurrence, and operability issues. Other items, that used to be part of the backlog, were instead tracked as CAP action items. However, the

inspectors noted that there was no formal effort to determine whether the CAP action

items were being addressed in a timely fashion (i.e., no performance indicator similar to

the formal backlog indicator). Since these action items were corrective actions (albeit of lower significance), the inspectors were concerned that some may not get implemented. Complicating the issue was an apparent mixed message from station management,

who expressed the view that the backlog numbers weren't important so long as items were being properly managed. Since this issue was already captured in the

CAP , the inspectors' observations were included as part of the ongoing licensee evaluation. Findings No findings were identified. .2 Assessment of the Use of Operating Experience (
OE ) a. Inspection Scope The inspectors reviewed the licensee's implementation of the facility's
OE program. Specifically, the inspectors reviewed implementing
OE program procedures, attended
CAP meetings to observe the use of

OE information, completed evaluations of OE

issues and events, and selected assessments of the OE composite performance

indicators. The inspectors' review was to determine whether the licensee was effectively

Enclosure integrating OE experience into the performance of daily activities, whether evaluations of issues were proper and conducted by qualified personnel, whether the licensee's

program was sufficient to prevent future occurrences of previous industry events, and whether the licensee effectively used the information in developing departmental assessments and facility audits. The inspectors also assessed if corrective actions, as a result of

OE experience, were identified and effectively and timely implemented. Documents reviewed during this inspection are listed in the Attachment to this report. b. Assessment In general,
OE was effectively used at the station. The inspectors observed that
OE was discussed as part of the daily station planning meetings, at shift turnover meetings, and at maintenance pre-briefings. Also, the inspectors determined that

OE was

appropriately reviewed during causal evaluations. During interviews, several licensee personnel commented favorably on the use of

OE in their daily activities. The inspectors noted that the

OE evaluation for a relay failure that resulted in the inoperability of a safety-related train at Harris (Action Request (AR) 1233871) was

somewhat limited in scope. The evaluation identified that similar relays were used at Monticello, but in non-safety related equipment; therefore, no actions were required. However, there was no documented evaluation whether a failure of these relays in the

affected equipment could have had any significant operational impact. The licensee documented this issue as

CAP item 1252873. Findings No findings were identified. .3 Assessment of Self-Assessments and Audits a. Inspection Scope The inspectors assessed the licensee staff's ability to identify and enter issues into the

CAP program, prioritize and evaluate issues, and implement effective corrective actions, through efforts from departmental assessments and audits. b. Assessment The inspectors concluded that self-assessments and audits were typically accurate, thorough, and effective at identifying issues and enhancement opportunities at an

appropriate threshold level. The audits and self-assessments were completed by

personnel knowledgeable in the subject area, and the quality of the NOS audits was

thorough and critical. The self-assessments were acceptable but were not at the same

level of quality as the

NOS audits. The inspectors observed that

CAP items had been

initiated for issues identified through the

NOS audits and self-assessments. The inspectors observed selected meetings of the Performance Assessment Review Board and reviewed board meeting minutes over the past six months. The Board provided oversight for the

CAP including the self-assessment program. The inspectors identified no issues with the Board's performance during the inspection.

Enclosure Findings No findings were identified. .4 Assessment of Safety-Conscious Work Environment (SCWE) a. Inspection Scope The inspectors assessed the licensee's

SCWE through the reviews of the facility's
ECP implementing procedures, discussions with
ECP [[coordinators, interviews with personnel from various departments, and reviews of issue reports. The inspectors also reviewed the results of licensee safety culture surveys. b. Assessment The inspectors determined that the plant staff were aware of the importance of having a strong]]

SCWE and expressed a willingness to raise safety issues. No one interviewed had experienced retaliation for safety issues raised, or knew of anyone who had failed to

raise issues. All persons interviewed had an adequate knowledge of the

CAP and
ECP process. These results were similar to the findings of the licensee's safety culture surveys. Based on these interviews, the inspectors concluded that there was no evidence of an unacceptable
SCWE. The inspectors noted that the licensee had taken proactive efforts to address a declining

SCWE trend within the Security force. This trend had been identified through

self-assessments and audits conducted in 2009. The number of issues self-identified by

the security staff had increased since the corrective actions were implemented.

Additionally, during interviews with the inspectors, Security staff commented favorably

on the licensee initiatives to improve the

SCWE. The inspectors determined that the
ECP process was being effectively implemented. The review of the selected
ECP issues indicated that site personnel were appropriately using the

CAP and ECP to identify concerns. However, many staff were unaware of the

other avenues the licensee had to raise concerns (collectively known as the

PEA [[]]

CH process). For example, most staff were unaware of the Differing Professional Opinions

(DPO) program for addressing engineering issues. Additionally, some newer staff confused safety culture with industrial safety. Similar issues were identified during the

2008 PI&R inspection. The licensee captured these issues as

CAP item 1252870. Findings No findings were identified. 4OA6 Management Meetings .1 Exit Meeting Summary On October 1, 2010, the inspectors presented the inspection results to Mr. O'Connor and other members of the licensee staff. The licensee acknowledged the issues

presented. The inspectors confirmed that none of the potential report input discussed was considered proprietary.

ATTACH [[]]
MENT [[:]]
SUPPLE [[]]
MENTAL [[]]
INFORM [[]]
ATION Attachment
SUPPLE [[]]
MENTAL [[]]
INFORM [[]]
ATION [[]]
KEY [[]]
POINTS [[]]
OF [[]]

CONTACT Licensee H. Butterworth, Fleet Operations Standards Director P. Byers, Security Manager

J. Early, Emergency Preparedness Manager

N. Haskell, Engineering Director

M. Holmes, Radiation Protection/Chemistry Manager

K. Jepson, Business Support Manager J. Mestad, Employ Concerns Program Manager D. Neve, Regulatory Affairs Manager

J. Ohotto, Design Engineering Manager

T. O'Connor, Site Vice-President

S. Porter, System Engineering Manager S. Radebaugh, Acting Plant Manager S. Sharpe, Operations Manager

G. Sherwood, Program Engineering Manger
T. Toglery, Nuclear Oversight Manager J. Windchill, Fleet Performance Assessment Manager Nuclear Regulatory Commission K. Riemer, Chief, Branch 2, Division of Reactor Projects
LIST [[]]
OF [[]]
ITEMS [[]]
OPENED ,
CLOSED [[]]
AND [[]]
DISCUS SED Opened:
URI 05000263/201007-01

HELB Analysis Potentially Non-Conservative

Attachment

LIST [[]]
OF [[]]
DOCUME [[]]
NTS [[]]
REVIEW [[]]
ED The following is a list of documents reviewed during the inspection. Inclusion on this list does not imply that the
NRC inspectors reviewed the documents in their entirety, but rather, that selected sections of portions of the documents were evaluated as part of the overall inspection effort. Inclusion of a document on this list does not imply
NRC acceptance of the document or any part of it, unless this is stated in the body of the inspection report.
PLANT [[]]
PROCED URES Number Description or Title Date or Revision
FP -
PA -ARP-01
CAP Action Request Process Revision 27
FG -PA-CAE-01 Corrective Action Effectiveness Review Manual Revision
6 FG -
PA -ACE-01 Apparent Cause Evaluation Manual Revision 17
FG -
PA -RCE-01 Root Cause Evaluation Manual Revision
17 FG -
PA -CTC-01
CAP Trend Code Manual Revision 12
FP -PA-OE-01 Operating Experience Program Revision 14
FG -
PA -KPI-01 Performance Indicator Data Reporting Revision
0 FP -E-
SE -02 Component Classification Revision 4 EWI-05.02.01 Maintenance Rule Program Document Revision 16
B. 5.12 System Basis Document: Area Radiation Monitor Revision 3 B.7.1 System Basis Document: Liquid Radwaste Revision 2
CORREC TIVE
ACTION [[]]
PROGRA M
DOCUME [[]]
NTS Number Description or Title Date or Revision
AR 114145-13 Incorrect Grounding Trucks Installed in 4
KV Cubicles 9/8/2008
AR 1150968 Continuing Issues With
FME Control on Turbine Floor 8/20/2009
AR 1168344-01
TS Action for
CREF Exited Prior to all
PMT s Being Completed 3/8/2009
AR 1166773-01 Adverse Trend in Rigor of Implementing
SOER Recommendations 2/26/2009
AR 1170876 Lack of Safety Related Material Control/Traceability 9/14/2009
AR 1167946-01 Level A and B
CA s Closed to Actions Outside the
CAP 3/21/2009
AR 1205719-02
ARM [[]]
S&C Refurb Not Performed
IAW Tech Manual 12/4/2009
AR 1211312
NOS Finding: Configuration Control Performance Issues 3/3/2010
AR 1226594 Work Tasks Authorized Without Proper C/O C/L Hung 6/18/2010
AR [[]]
1228190 NOS Finding-Weak Barriers in Work Management 5/25/2010
AR 1237891 Failed Bellows Spring in Positioned Removed from
CV -1242 6/28/2010

AR 1158526 Adverse Trend In Work Package Quality 12/10/2008

Attachment

CORREC [[]]
TIVE [[]]
ACTION [[]]
PROGRA M
DOCUME [[]]

NTS Number Description or Title Date or Revision AR 01167235

AR 01167240

AR 01173666
AR 01155107

AR 01184941

AR 01167237

AR 01139421
AR 01160675

AR 01143116 AR 01232720

AR 01158536

AR 01157274
AR 01150364

AR 01151413

AR 01213390
AR 01211101

AR 01190071 AR 01189968

AR 01188955

AR 01187271
AR 01177444

AR 00826605

AR 01083164

AR 01151933

AR 01154270
AR 01153455

AR 01116586

AR 01136919

AR 0123272

AR 01182625

AR 01196988
AR 01194357 Potential Trend
WM [[]]
ID 'd in Ops 4th Qtr 2008
DRUM Potential Trend
JP&P [[]]
ID 'd in Ops 4th Qtr
2008 DR [[]]

UM

Adverse Trend in FME issues

Ops

CSE [[]]

ID's AFI in Objective 3 Adverse Trend: work plan changes made w/o review & approval

Potential trend

DP [[]]
ID 'd in Ops 4th Qtr
2008 DR [[]]
UM Adverse Trend in Program Management Issues
AFI Independent
FSA Monti Human Performance Adverse Trend in
OS [[]]

HA reportable injuries Recirc riser relay did not respond to de-energize

position during IST

LOR Annual Operating Exam Issues

Proposed NRC Violation - Reactor Level Control

- 9/11 Scram

HP [[]]

CI failed to trip when Rx level rose to 48" Rx Low Low Water Level signal received during

CRD pump start

Voltage of cell 116 in #17 battery is at 2.07 Volts

Not all Tech Specs were entered 2009 Ops

CSE -
AFI Objective
5 AFI 5.1 A

SBGT Flow Not Within Band

Assessment

AFI [[]]

ID'd for licensed operator

medicals

B

SB [[]]

GT failed to operate as expected

Adverse Trend - Procedure performed without

OPS Auth.

GE Part 21 (SC05-03) Potential to exceed low

pressure limit

Main Steam Line plugs interfere with separator

removal

SP [[]]

DS Disp 710 showing incorrect configuration of circuit breaker

NRC Commitments in procedures not meeting

requirements

Station challenged by projects interface/alignment issues Unplanned rise in Offgas Radiation and Stack

WG [[]]

RM's

Loss of motor cooling to Div

II [[]]
RHRSW Pumps
LP [[]]

CI Select Interlock Channel Functional

Test Failure Adverse Trend; Inadequate maintenance of QA reports

Adverse Trend; Badge control by site personnel

Door-18, Condenser room flood door found closed1/29/2009

1/29/2009

3/18/2009

10/13/2008 6/09/2009

1/29/2009

9/07/2010

11/26/2008 8/5/2008 5/13/2010

11/7/2008

3/26/2009

9/21/2008 9/21/2008

1/12/2010

2/17/2009 7/20/2009 7/20/2009

7/10/2009

6/28/2009

4/9/2009 3/30/2005

3/20/2007

9/24/2008

10/8/2008

10/2/2008 10/31/2007

5/6/2008

6/25/2010

5/19/2009

9/9/2009

8/20/2009

Attachment

CORREC [[]]
TIVE [[]]
ACTION [[]]
PROGRA M
DOCUME [[]]
NTS Number Description or Title Date or Revision
AR 01178894

AR 01159084

AR 01150362
AR 01151075
AR 01216130
FME - Drier Measurement Platform Wheel Inadequate shutdown margin during

EOC-23 core

alterations

Reactor Scram Number 121 occurred on Sept

11th, 2008 Ops Trng

CSE identifies

AFI's in Objective 1-4 Performance gaps to industry standards not recognized 4/20/2009 11/13/2008

9/12/2008

9/18/2008 1/30/2010

AR 01144214-02 Trend-
RCE Grades Low in 2 Areas 7/2008
AR 01173245 Actions to Address Equipment Problems are Shortsighted 4/15/2009
AR 01186832 Core Spray Pump Quarterly Test Terminated Due to No Flow 6/25/2009
AR 1191812 Adverse Trend in Failure Rates to
ACE s Assigned to Projects 7/31/2009
AR 01216127
PI. 2-2
ACE s Do Not Always Address Org or Prgrm Contributors 1/30/2010
AR [[]]
01174411 PRNMS Ineffective Condition Evaluation
CE 01162340-02 3/23/2009
AR 01187909 Accountability in Meeting
CAP Action Due Dates Tracking 7/2/2009
AR 01238254
PI&R [[]]
FSA [[]]
AFI Rigor in Resolving
NRC Violations Not Consistent 6/22/2010
AR [[]]
1222439 MNGP [[]]
EPU Mod 3 Surveillance 3/12/2010
AR 01208801 Three
NRC X-Cutting Findings in One Aspect 12/1/2009
AR 01216516 Station hs Three Potential Findings in One
NRC Xcut Aspect 2/2/2010
AR 01215513 Potential Adverse Trend Recent Events/Near Misses 1/27/2010
AR 01170720 Inconsistent
CAP Problem Statements
CA Quality
ACE Quality 2/25/2009
AR 01232886 Adverse Trend-Corrective Action Backlog Exceeding Goal 5/14/2010
AR 01150601 Ops Tng
CSE Identifies Ineffective Closure of
CA 9/15/2008
AR 01157287 Red
KPI -
NRC Cross Cutting Aspects (H.4.c.) Oversight 10/29/2008
AR 1226438 Site Received Fourth P.1.c Cross Cutting Aspect from
NRC 4/8/2010
AR 01147103 Adv Trnd in Organization Perf. Leads to Near Miss Events 8/9/2008
AR 01137245 Station
KPI for
NRC Cross-Cutting Issue-Potential Red 5/9/2008
AR 01184816 Evaluation of Project Dept Clock Resets During 2009 Outage 6/8/2009
AR 01163396 Adverse Trend in
HU Identified in 3 Quarter 2008 Site

DRUM 12/22/2008

Attachment

CORREC [[]]
TIVE [[]]
ACTION [[]]
PROGRA M
DOCUME [[]]
NTS Number Description or Title Date or Revision
AR 01135426
CAPR s From
RCE s Non Institutionalized 4/23/2008
AR 01138493 Adverse Trend in Human Performance 5/22/2008
AR 01158802 Potential Adverse Trend-Station Cross Cutting Issues
PI&R 11/11/2008
AR 1161531 Reoccurring Qualification Issues at Monticello 12/05/2008
AR 1199160 Unexpected
AR -10 Discharges on the Range 12/01/2010
AR 1140153 Adverse Trend in Refueling Floor Activities 12/17/2009
AR 1169027 High Radiation Controls Violation 06/01/2010
AR 1170636 Security Human Performance Adverse Trend 03/24/2009
AR 1161679 Potential Adverse Trend - Security Weapons / Ammo Handling 01/16/2009
AR 1210338 Adverse Trend -
BRE Issues 12/30/2010
AR 1150642 Incomplete Information Sent to
NRC on an Operator's License Renewal Application 09/15/2008
AR 1136955 Adverse Trend in Service Water Radiation Monitor Flow 05/07/2008
AR 1177731 Adverse Trend in
LLRT Radiation Exposure 04/10/2009
AR 1164409 Increased Trend in Badge Control Issues 03/02/2009
AR 1135335 Adverse Trend in Emergency Planning Drill / Exercise Report Timeliness 08/21/2008
AR 1215924
EP Department Performance Has Declined 03/12/2010
AR 1174197 Lengthy Out Of Service Time for
EP Equipment 07/31/2009
AR 1216118
EP 1-1
ERO personnel Make Knowledge Based Errors 09/03/2010
AR 1215924 Site
EP Precursors to Further Declining Performance 10/29/2010
AR 1188771 Follow-up
PAR Development Inaccurate / Untimely 11/17/2009
AR 1135335 Adverse Trend in Emergency Planning Drill / Exercise Report Timeliness 08/21/2008
AR 1215924
EP Department Performance Has Declined 03/12/2010
AR 1217199 Security Officer Failed to Perform a Security Patrol 08/31/2010
AR 1168195 Rx Water Soluble Co-60 No Longer Trending Down 02/05/2009
AR 1207385
SGI Package Not Properly Marked 03/31/2010
AR 1204338 New Security Door to Intake Tunnel Found Closed04/23/2010
AR 1156598 Security Force on Force Exercises 08/21/2009
AR 1238171 Unexpected Dose rates Encountered During
RWCU [[]]
BW 06/21/2010
AR 1164240 Movement of Radioactive material Not in Accordance with
AWI 01/02/2009
AR 1196952 Low level of Tritium in Monitoring Well (MW-9) 09/09/2009 AR 1207960
AR 01214941 Unexpected Change in

DW CAM Particulate Activity

Inadequate Documentation of Design Inputs 12/10/2009 02/22/2010

Attachment

CORREC [[]]
TIVE [[]]
ACTION [[]]
PROGRA M
DOCUME [[]]

NTS Number Description or Title Date or Revision AR 01222023

AR 01214814

AR 01197923

AR 01228141

AR 01176068
AR 01179388

AR 01194527

AR 01195119

AR 01197202
AR 01171823

AR 01174949

AR 01227229
AR 01166312

AR 01170967

AR 01088210

AR 01139415
AR 01137297

AR 01209649-01

AR 01065983

AR 1088210-01

AR 01181868

AR 01192130
AR 01190129

AR 01120865

AR 01166314
AR 01107707

AR 01166308

AR 01155275

P-109C,

13 RHR [[]]

SW Pump D/P in Alert Range

Adverse Trend in Bearing Failures on

11 CRD Pump
CBDI [[]]

FOF Mod Did Not Assess Impact to T-44

Tank SRV Lift Test Surveillance Interval Potentially Missed

Thin Pipe Identified During

MIC Exam On 18 A
RHR [[]]

SW

Appendix J Programmatic Deficiencies Post-Modification Testing Issues

Adverse Trend in Engineering Department

HP Clock Resets
CD [[]]

BI- Calculation Quality- Adverse Trend

EPU -Wiring Discrepancy Discovered in Field Adverse Trend in Feedwater Heater Level Transmitter Replacement
1AR [[]]

XFMR Lockout Caused By 1N^ Ground

Fault

Declining Trend-Engineering Work Process-Work Control Mgmt Adverse Trend Control of Engineering MTE

Part of Head Vent Line Not Insulated

D10 125VDC Div 1 Battery Charger Unavailability

Exceeds MR Goal

D10 Exhibits Erratic Voltage Output During Surveillance Clearance and Tagging Issues

Degraded

HELB Flow Path Over The

SLAE Room

Missing Instillation On The Head Vent Valve

Manifold Equalizing Valve Failure Causes 'B' Main Steam Line Flow Isolation Instrument to Become Inoperable

Work Performed Without Adequate Tag-Out

Protection

Failure to Promptly Identify Failed

SBGT Surveillance Failures of V-

AC-4 (B4305) and V-AC-5 (B3305)

Adverse Trend for Engineering Non-Mod

EC Backlog

Failures of V-AC-4 Declining Trend for Engineering- Process Failure Mode-RR1

Increasing Trend for System Health Assessment

KPI 04/06/2010 03/31/2010 11/02/2009

05/14/2010

03/31/2009 04/23/2009

11/13/2009 09/25/2009

11/11/2009 03/04/2009 10/25/2009 04/14/2010

2/19/2009

05/29/2009 09/21/2010 09/29/2010

05/09/2008 02/04/2010

01/05/2007 04/20/2007 05/12/2009

08/03/2009

08/21/2009 05/22/2009 01/22/2009

09/19/2007 01/01/2009

10/14/2008

Attachment

ROOT ,
APPARE NT
AND [[]]
COMMON [[]]
CAUSE [[]]
EVALUA TIONS Number Description or Title Date or Revision
AR 1140145 Incorrect Grounding Trucks Installed in 4
KV Cubicles 6/6/2008
EFR 1140145-24 Effectiveness Review of
CAP 1140145-05 Truck Installation Procedure 11/6/2009
EFR 114145-25 Effectiveness Review of Grounding Truck Installation 11/6/2009
AR [[]]
1150968 JLG Lift Basket Contacts 115
KV 9/17/2008
EFR 1150968-10 Effectiveness Review for
AR [[]]
CAP 1150968 Lift Contacts 115
KV 9/30/2009
PCR 1152979 Revise
FP -SC-GEN-08 Revision 2 9/30/2008
AR 1158526 Adverse Trend in Work Package Quality 11/7/2008
AR 1166773 Adverse Trend in Rigor of Implementing
SOER Recommendations 1/26/2009
AR 1167946 Mid Cycle
FSA [[]]
AFI 11-CAsClosed to Actions Outside the
CAP 2/3/2009
AR [[]]
1168344 TS Action for
CREF Exited Prior to all
PMT s Being Completed 2/5/2009
AR 1170876 Lack of Safety Related Material Control/Traceability 2/25/2009
AR 1183728 Continuing Issues with
FME Control on Turbine Floor 5/29/2009
AR 1183728 Continuing Issues with
FME Control on Turbine Floor 5/29/2009
AR 1166773-01 Adverse Trend in Rigor of Implementing
SOER Recommendations 1/26/2009
AR 1167946-01 Level A and B
CA s Closed to Actions Outside the
CAP 2/3/2009
AR [[]]
1168344 TS Action for
CREF Exited Prior to All
PMT s Being Completed 2/5/2009
AR 1202466 Adverse Trend in Double Disc Gate Valve
LLRT Performance 10/14/2009
AR [[]]
1205719 ARM S&C Refurb not Performed
IAW Tech Manual 11/4/2009
AR 1211312
NOS Finding: Configuration Control Performance Issues 12/18/2009
AR 1226594 Work Tasks Authorized Without Proper C/O C/L Hung 4/9/2010
AR [[]]
1228190 NOS Finding-Weak Barriers in Work Management 4/20/2010
AR 1237891 Failed Bellows Spring In Positioned Removed from
CV -1242 6/18/2010
AR [[]]
1095181 PRA Compliance With Regulatory Guide 1.200 6/5/2007
AR [[]]
1121269 SOER 07-02 on Intake Cooling Water Blockage 12/14/2007
AR [[]]
01237478 PI&R [[]]
FSA ; All req's for
CAP 01189206 not performed 6/16/2010
AR [[]]
01237558 PI&R [[]]

FSA; Trend in security trng team used for shift needs 6/16/2010

Attachment

CORREC [[]]
TIVE [[]]
ACTION [[]]
PROGRA M
DOCUME [[]]
NTS Number Description or Title Date or Revision
AR 01237585
PI&R [[]]
FSA ;
CAP closed out to action in
GAR 6/16/2010
AR [[]]
01237702 PI&R [[]]
FSA ; Documenting Completion of actions unclear in
2 FBM s 6/17/2010
AR [[]]
01237779 PI&R [[]]
FSA ; No
CAP tracking completion of Top Ten Eqp. Items 6/17/2010
AR [[]]
01237802 PI&R [[]]
FSA ; No action to track completion of work under B
CAP 6/17/2010
AR [[]]
01237820 CAP extension documentation missing, found during
PI&R [[]]
FSA 6/18/2010
AR [[]]
01237838 PI&R [[]]
FSA -
CAPR process not followed for form revision 6/18/2010
AR [[]]
01237839 PI&R [[]]
FSA Typos and dated info in Ops Burden Report 6/18/2010
AR 01237876
PI&R [[]]
OE evaluation uploaded in sharepoin is not correct 6/18/2010
AR [[]]
01237905 PI&R [[]]
FSA - overdue operating experience actions 6/18/2010
AR 01237917 2010
PI&R [[]]
FSA Lack of documentation for level of effort 6/18/2010
AR 01237928
2010 PI&R [[]]
FSA [[:]]
CAP not written for identified issue 6/18/2010
AR [[]]
01238082 PI&R [[]]
FSA [[]]
CAP s -
INPO [[]]
AFI s don't considtently meet standards 6/21/2010
AR [[]]
01238284 PI&R [[]]
FSA [[]]
AFI Root Cause Statements -
CA Line of Sight 6/22/2010
AR 01238292
PI&R [[]]
FSA [[]]
AFI Independent workers applying own standards on
CAP initially 6/22/2010
AR [[]]
01243250 PI&R [[]]
FSA - Ops Status Notes Not Sustainalbe for Fire Pump 7/28/2010
AR 01243411
PI&R [[]]
FSA Review
ACE to
CE for 01174955 7/29/2010
AR [[]]
01243430 PI&R [[]]
FSA corrective action for
AR 1199936 7/29/2010
AR [[]]
01243485 PI&R [[]]
FSA -
CAP Improperly closed to no action 7/29/2010
AR [[]]
01243644 PI&R [[]]
FSA -
CAP 01141018 Screening N Notes are incorrect 7/30/2010
AR [[]]
01243728 PI&R [[]]
FSA -
EFR assignment
CAP 01165741 had no goal stated 7/30/2010
AR 01244435
PI&R Inspection self assessment identified 4kv rooms issue 8/5/2010
AR 01139415 D10 125
VDC Battery Charger Unavailability exceeds
MR goal 5/30/2008
AR 01155593 Inability to attract personnel due to Industry Competition 10/15/2008
AR 01158868
RF [[]]
24 MS 38 for preoutage work in jeopardy 11/11/2008
AR [[]]
01159308 IR 24

MS 13 for work order planning above control band 11/15/2008

Attachment

CORREC [[]]
TIVE [[]]
ACTION [[]]
PROGRA M
DOCUME [[]]
NTS Number Description or Title Date or Revision
AR 01167860 Mid cycle
FSA [[]]
AFI 3 - Insufficient operations staffing plan 2/3/2009
AR 01179605 Greater than 1 yr will be needed to qualify a
SM candidate 4/25/2009
AR 01180220 Quality issues found on Isophase Bus Cooling System 4/30/2009
AR 01200192 Emergent Contractor Trng request diverts Maint Training resource 9/29/2009
AR [[]]
01217990 EP Drill - Not enough controllers in the Plant during drill 2/12/2010
AR [[]]
01227941 RWCU restoration time discrepancy 4/19/2010
AR [[]]
01230850 EM&P Resource Availability impacts scheduled work 5/3/2010
AR 01233699 Operations unable to support system walkdown 5/20/2010
AR 01237487 Personnel removed from Training to cover Shift staffing need 6/15/2010
AR 01240903 Supervisor pulled from training to meet staffing needs 7/9/2010
AR 01227056 One Live Ammo Round at
STF Mixed with Training Rounds 4/13/2010
AR 01225619 Unable to Obtain Definitive Reading of
TS Required Parameter 4/2/2010
AR 01181388 "B" Safety Relief Valve Leaking 5/8/2009
AR 01243585 Program Deficiencies From
PHC Not Incorporated into
CAP 7/30/2010
AR 01181249
HPCI Governor Valve Failed to Open During Overspeed Test 5/7/2009
AR 01083169 Crack Like Indication on Steam Dryer Found in 2007
RFO 3/20/2007
AR 01070668 Rx Bldg
RR Doors Switched in
HELB Gothic Model 1/8/2007
AR 01206949 Incorrect Severity Assigned to
CAP 01184369-02 11/16/2009
AR [[]]
01243568 PI&R [[]]
FSA Potential
AR 1150849 Screening 7/30/2010
AR 01225682
1AR Transformer Pad Has Sunk about 1 inch since Install 4/4/2010
AR 01225762 #12
RHRSW Pump has Excessive Packing Leakage 4/5/2010
AR 01225888
11 SW Pump Inducing Vibrations on 13
ESW Pump 4/6/2010
AR 01225997
CAP Closure Review-"B" Action Closure Quality Issues 4/6/2010
AR 01226060 12
RFP [[]]
L.O. Cooler Piping Rusting Through Upstream of
TI -1555 4/6/2010
AR 01135291 Internal Threads on
WDW 7 Look Bad 4/22/2008
AR 01135409 Questionable Off-Gas Sample 4/23/2008

AR 01136879 Oil Flush on 11 Service Water Motor Ineffective 5/6/2008

Attachment

CORREC [[]]
TIVE [[]]
ACTION [[]]
PROGRA M
DOCUME [[]]

NTS Number Description or Title Date or Revision AR 01137901 The Site Lacks a Single Tracking Mechanism for

Failed

PMT s 5/15/2008
AR [[]]
01138283 CAP 1102406 Trending Closed to "B'
ACE With No Reference 5/20/2008
AR 01138824 Battery Chargers Maintenance Rule Status Declining 5/27/2008
AR 01178034 Employee Exceeded Work Hours 4/13/2009
AR 01179554
SBLC Tank Level is Lower After Draining and Refilling 4/25/2009
AR 01179701 Lack of Alternative Access Increases Operator Response Time 4/27/2009
AR 01216080 Snowmelt Causes Possible
EOP Entry Alarm 1/29/2010
AR [[]]
01217767 RR -4902 Has Incorrect Chart paper During Test 0289-A 2/11/2010
AR 01219159 Alt N2 Train Pressures at Low End of Allowed Operating Band 2/19/2010
AR 01212202
RCIC is Conservatively Declared Inoperable 12/31/2009
AR 01212209 Both
LPCI Subsystems Declared Inoperable During Venting 12/31/2009
AR 0119936 Voltage Drop Evaluation for
RHR and
RHRSW [[]]
ASCO Sol. Valves 9/28/2009
AR 01197431
CDBI -Undocumented Assumption in Calculation 06-104 9/12/2009
AR 01200723
CDBI P-111B Calculated Starter Voltage Lower Than Expected 10/2/2009
AR 01210817
NRC Feedback on Reportability of
SBGTS Event 12/15/2009
AR 01150773 Some Station Log Entries Were Not Made During
SCRAM 121 9/16/2008
AR 01151413 Rx Low Low Water Level Signal Received During
CRD Pump Start 9/21/2008
AR [[]]
01200304 AO -2945 Failed to Open During 0253-01 "A"
SBGT [[]]
QTRLY Test 9/29/2009
AR [[]]
01220488 NRC Violation for Failure to Make 10
CFR 50.72 Notification 3/1/2010
AR 01175537
NDE Examiner Procedure Non-Compliance 3/29/2009
AR 01216894 Loss of Offsite Power 10
CFR 50.72 Reporting Reqts. 2/4/2010
AR 01082564 Reactor Core Water Level Recorder Found Failed Upscale 3/16/2007
AR [[]]
01131103 ITS 125V
DC Charger
SR 3.8.4.2-Option 2 Unachievable 3/14/2008
AR 01106816 Charcoal Filter Iodine Loading Calcs Non-Conservative 8/14/2007
AR 01143954 11/12

CT Pump Operation Safety Enhancement Opportunity 07/13/2008

Attachment

CORREC [[]]
TIVE [[]]
ACTION [[]]
PROGRA M
DOCUME [[]]
NTS Number Description or Title Date or Revision
AR 01243644
PI&R [[]]
FSA -
CAP 01141018 Screening N Notes are Incorrect 07/30/2010
AR 01237813 Buried Pipe Health Report Issues/ Exemplary Rating Questioned 06/18/2010
AR 01158314 11 Air Compressor
PM Deleted But Has
NRC Commitement 11/05/2008
AR 01184683 Adverse Trend-
DW Floor and Equipment Drain Sump Issues 06/05/2009
AR 01184683-03
EFR - Effectiveness of Potentiometers
DWEDS ,
DWFDS 07/31/2010
AR 01197773 Revise
ISP -RHR-0558-01 as Interim Action for
RCE 1181868 11/09/2009
AR 01197769 Revise 0056 as Interim Corrective Action For
RCE 1181868 12/11/2009
AR 01181868 Leaking Manifold Valve for
DPIS -2-117A B Stm Line Flow 05/13/2009
AR 01093089 Non-Conservative Input to
AST Post- Local pH 06/15/2009
AR 01064602 Shortcomings in Cross Referencing
CAPS and
WR s 06/10/2008
AR 01087740 Pipe Downstream of
PCV -1242 is Significantly Thinned 06/05/2009
AR 01070668
RX Bldg
RR Doors Switched in
HELB Gothic Model 01/16/2009
AR 01127660 Surveillance 1467 Extended Twice 03/29/2008
AR 01119232 Abandoned Limit Swithces in Second Floor
EFT Building 03/27/2008
AR 01107610 3 Inch Movement on Moisture Sep. to 14B Htr Pipe 07/15/2009
AR 01105975 Guidance for Use of Third
RBCCW Heat Exchanger Inadequate 09/30/2008
AR 01130761
CV -1729 Not Controlling at 7000gpm, Results in Unplanned
LCO 03/12/2008
AR 01149748 Loss of Level Indication C
MSDT Dump Controller
LC -1003 09/05/2008
AR 01243477 Question Regarding the Control of Radiograpers 07/29/2010
AR 01129677 Area for Improvement 03/03/2008
AR 01243430
PI&R [[]]
FSA Corrective Action for
AR 1199936 07/29/2009 01150085 Possible Inconsistency Between
MPR Setpoint and Calc Input 09/10/2008 01149441 Results of
MET [[]]
CSP Assessment Concluded Further Migration 09/03/2008 01079705

LAR Required for Use of Tormis Code Methodology 02/28/2007 01197771

011977701

Revise

ISP -

RHR-0552-01 as interim action for RCE1181868

Revise 0060 As Interim Corrective Action for

RCE1181868 09/15/2009 09/15/2009

09/15/2009 09/15/2009

Attachment

CORREC [[]]
TIVE [[]]
ACTION [[]]
PROGRA M
DOCUME [[]]

NTS Number Description or Title Date or Revision 01197768

01197774

252368

250089

2149351

01159968 Revise 0060 As Interim Corrective Action for RCE1181868

Revise

ISP -

RHR-0558-02 As Interim Action for

RCE 1181868
NRC -

PI&R-Question on Classification of

DW Sumps
NRC [[]]
PI&R -
CA 's Not Created for Interim

RCE Actions

Several

NRC Findings had Improper
AR Assignments per

ARP-01

IPB Mod Design Issues with Service Water Valves 10/10/2010

09/16/2010 10/04/2010 11/20/2008

OPERAT [[]]
ING [[]]
EXPERI [[]]
ENCE Number Description or Title Date or Revision
OE 31215 Jet Pump Wedge Wear 5/25/2010 01175420

NRC IN 2009-03: Solid State Protection System Card Failure Results in Spurious Safety Injection

Actuation and Reactor Trip 6/11/2009 01137557 Station

OE Evaluation of Industry Documents 5/13/2008 01143701 Station
OE Evaluation of
OE 26794 7/10/2008

OE 31105 Water Detected in a Cable Pit Beneath a MCC which Contained Safety-Related Cables

(Cook Plant) 5/7/2010 01245020 Station

OE Evaluation of
OE 31283 8/10/2010 01149696 Fisher Information Notice 1997-01, Supplement 1 9/5/2008
01193202 MNGP [[]]
OE Evaluation of
PINGP [[]]
AR 01192430 8/11/2009 01126257 Part 21:
GE Fuel Rod Thermal-Mechanical Methodology 02/05/2008 Weekly
OE Screening Minutes 06/10/2010 01180269 Fleet
OE Evaluation of
INPO [[]]
OE 28618 01142237
OE 26962 Flux Map Gaps Ginna 12/02/2009 01145374 Station
OE Screen Team Review of
OE for Week 07/18/2008 09/23/2008 01142952 Westinghouse Detached P-Grid Dimples 01/09/2009 01149492 Station
OE Screen Team Review of
OE For Week of 08/29/2008 10/31/2008 01157701 Station
OE Evaluation of

EO for Week of 10/31/2008 09/30/2009

Attachment

AUDITS ,
ASSESS MENTS
AND [[]]
SELF -ASSESSMENTS Number Description or Title Date or Revision 01121234
FASA of
XCEL s Energy's
MNGP [[]]
EPU Outage Project Readiness 12/17/2008
1205004 EPU Outage Readiness Assessment 6/10/2010 2010-02-014 Corrective Action Program 5/14/2010 2010-01-029 Corrective Action Program 3/12/2010
SAR [[]]
01205025 PI&R Readiness 9/9/2010
SAR 01249160 Site Roll-up Meeting Results 1st and 2nd Quarter
2010 SAR 01116710 Component Design Bases Inspection Focused Self-Assessments 11/17/2008
NOS 1st Quarter 2010 Assessment Report 05/14/2010
NOS 4th Quarter 2009 Assessment Report 03/01/2010
QF -0426 Focused Self-Assessment
MNGP Dry Cask Loading Readiness Revision 2
QF -0402 Fleet Focused Self Assessment Report: Reportability
SAR 01117506 Revision 3 1133118 Exposure Monitoring and Dose Control 11/06/2008
CONDIT ION
REPORT S
GENERA TED
DURING [[]]
INSPEC TION Number Description or Title Date or Revision
AR 1250188
NRC [[]]
PI&R Process Control for
WO from
CA Process
AR [[]]
1250127 NRC [[]]
PI&R Closure Documentation for 1150601-06 Inadequate 9/17/2010
AR 1250089
NRC [[]]
PI&R [[:]]
CA s Not Created for Interim
RCE Actions 9/16/2010
AR [[]]
1249923 NRC [[]]
PI&R [[:]]
NRC is Questioning Status of 125V
DC 9/15/2010
AR 1251890
PI&R Inconsistencies in Observation Program 9/29/2010
AR 1249158 Contactor Oversight Insufficient to Prevent Performance Issues 10/11/2010
AR 1243583 Incorrect
CAP Severity Determination 9/24/2010
AR [[]]
1252870 NRC [[]]
PI&R [[:]]
PEACH Process Not Well Understood 10/5/2010

AR 1252873 OE Not Well Evaluated Beyond the Event 10/5/2010

Attachment

MISCEL [[]]
LANEOU S Number Description or Title Date or Revision 3784 A(1) Action/Performance Improvement Plant Revision 0
NSPM [[]]
CAP Screening Package 9/16/2010 Performance Assessment Review Board Package 9/14/2010 Alignment Teamwork and Oversight Meeting 9/15/2010
WO 384150
IC -RHR,
ISP -
RHR -0552-01
RX Recirc Loop
DP -LPCI
INTR [[]]
FUNCT T 01/27/2010
WO 00388188
IC -RCI,
0060 RC [[]]

IC High Steam Flow Sensor Test 2/18/2010

Attachment

LIST [[]]
OF [[]]
ACRONY [[]]
MS [[]]
USED [[]]
ACE Apparent Cause Evaluation
ADAMS Agencywide Document Access Management System

AR Action Request CAP Corrective Action Program

CFR Code of Federal Regulations

CAQ Condition Adverse to Quality

DPO Differing Professional Opinion
DRP Division of Reactor Projects

DRUM Department roll-up meeting ECP Employee Concerns Program

GAR General Action Request
HE [[]]
LB High Energy Line Break
HPCI High Pressure Coolant Injection

IMC Inspection Manual Chapter IN Information Notices

IP Inspection Procedure

IST In-service test
LER Licensee Event Report
MNGP Monticello Nuclear Generating Plant
MP [[]]

FF Maintenance Preventable Functional Failure

NCV Non-Cited Violation

NOS Nuclear Oversight

NRC U.S. Nuclear Regulatory Commission
OE Operating Experience

PARS Publicly Available Records System PM Preventive Maintenance

PI&R Problem Identification & Resolution
RC [[]]
IC Reactor Core Isolation Cooling
RHR Residual Heat Removal

RHRSW Residual Heat Removal Service Water RPS Radiation Protection Specialist

RPS Reactor Protection System
SC [[]]
AQ Significant Condition Adverse to Quality
SC [[]]
WE Safety-Conscious Work Environment
SDP Significance Determination Process
SFP Spent Fuel Pool
US [[]]

AR Updated Safety Analysis Report

WO Work Order

T. O'Connor -2-

No violations or findings were identified during this inspection. In accordance with

10 CFR 2.390 of the
NRC 's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the
NRC Public Document Room or from the Publicly Available Records System (
PARS ) component of
NRC 's document system (
ADAMS ).
ADAMS is accessible from the

NRC Website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room). Sincerely,

/RA/

Kenneth Riemer, Chief Branch 2 Division of Reactor Projects

Docket No. 50-263

License No. DPR-22 Enclosure: Inspection Report 05000263/2010007 w/Attachment: Supplemental Information

cc w/encl: Distribution via ListServe