Information Notice 2005-21, Plant Trip and Loss of Preferred AC Power from Inadequate Switchyard Maintenance

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Plant Trip and Loss of Preferred AC Power from Inadequate Switchyard Maintenance
ML051740051
Person / Time
Issue date: 07/21/2005
From: Hiland P
NRC/NRR/DIPM/IROB
To:
Koshy T, NRR/DE/EEIB, 415-1176
References
IN-05-021
Download: ML051740051 (4)


UNITED STATES

NUCLEAR REGULATORY COMMISSION

OFFICE OF NUCLEAR REACTOR REGULATION

WASHINGTON, D.C. 20555-0001 July 21, 2005 NRC INFORMATION NOTICE 2005-21: PLANT TRIP AND LOSS OF PREFERRED AC

POWER FROM INADEQUATE SWITCHYARD

MAINTENANCE

ADDRESSEES

All holders of operating licensees for nuclear power reactors, except those who have

permanently ceased operations and have certified that fuel has been permanently removed

from the reactor vessel.

PURPOSE

The U.S. Nuclear Regulatory Commission (NRC) is issuing this information notice to inform

addressees about loss of power events as a result of inadequate preventive and corrective

maintenance practices on switchyard breakers and current transformers. It is expected that

recipients will review the information for applicability to their facilities and consider actions, as

appropriate, to avoid similar problems. However, suggestions contained in this information

notice are not NRC requirements; therefore, no specific action or written response is required.

DESCRIPTION OF CIRCUMSTANCES

On May 5, 2004, Dresden Unit 3 was at full power and Dresden Unit 2 was shutdown when an

automatic reactor scram and a subsequent loss of offsite power event occurred during activities

to reconfigure breakers in the 345 kV switchyard. Operations personnel manually opened

switchyard breaker 8-15 in accordance with the switching order. However, when the A and B

phases opened, the C phase of switchyard breaker 8-15 failed to fully open within the required

time. This failure produced current imbalances in Unit 2 and Unit 3 switchyard ring busses (tied

together through a breaker), which led to the opening of several other switchyard breakers.

Unit 3 scrammed due to turbine load reject, and offsite power was lost to the Unit 3 safety- related emergency core cooling system (ECCS) busses. The failed breaker was an I-T-E

Imperial Corporation (current vendor ABB) sulfur hexafluoride (SF6) gas circuit breaker (type

362GA). This breaker used independent pole operators for each of the three phases. The

breaker was built and installed in the Dresden 345 kV switchyard in the late 1970's.

On May 6, 2004, the licensee and personnel of the transmission and distribution company, Exelon Energy Delivery (EED), discovered that ABB, the current breaker vendor, had issued a

product advisory in July 2003 for I-T-E Imperial Corporation GA and GB breakers to warn that

the operating mechanisms may experience delayed trip or in some cases failures to trip due to

age and application related problems. In addition, the advisory noted that the breakers at

highest risk were those operated less than twice per year. The product advisory recommended

that the operating mechanism in high-risk applications be rebuilt using new trip latch

mechanism kits at the earliest convenience.

While disassembling the trip latch mechanism of Breaker 8-15, EED and licensee personnel

discovered that the sealed bearing for the trip latch mechanism did not roll freely. The failure of

the sealed bearing to roll freely, directly contributed to the failure of the C phase of

Breaker 8-15 to open within the required time. The NRC special inspection team reviewed the

maintenance history of Breaker 8-15. The last preventive maintenance on Breaker 8-15 was

done on March 27, 2002, and included routine inspection, lubrication and maintenance, a

contact resistance test, and a travel timing test. The inspection team noted that the breaker

failed the timing test on the C Phase. The breaker was last cycled in October 2002 and then

remained in the closed position until May 5, 2004.

The NRC inspection team noted that the EED procedure stated that the breaker should be

lubricated after a failed timing test. However, the vendor manual stated that, the operating

mechanism should be disassembled and cleaned and lubricated when the operating

mechanism showed signs of difficult or sluggish operation. In addition, the manual stated that

under ordinary circumstances, the life of the grease in sealed bearings should be at least

10 years and that if oxidation of the lubricant made the bearing sluggish, the bearing must be

replaced. The EED preventive maintenance program and procedures for breakers did not

include routine replacement of worn out breaker parts. In addition, the EED maintenance

procedures did not instruct maintenance personnel to disassemble sluggish operating

mechanisms to check for degraded bearings, nor did the procedures specify the appropriate

lubricants for the various parts of the breaker.

On June 12, 2002, with DC Cook Unit 1 at approximately 68% power and Unit 2 at 100%

power, an emergency alert condition was entered after a catastrophic failure and resultant fire

of a current transformer for the 345 kV switchyard L breaker. The catastrophic failure of the

current transformer and the subsequent switchyard switching actions resulted in the loss of the

preferred offsite power source to Units 1 and 2. On June 19, 2002, the NRC special inspection

team reviewed the licensees preventive maintenance program for 345 kV switchyard current

transformers. The vendors preventive maintenance recommendations included annual

inspections and transformer oil analysis every 2 years. The inspection team reviewed historical

maintenance activities on the L breaker current transformers and determined that preventive

maintenance activities were last done in October 1998. The periodicity of preventive

maintenance activities was consistent with American Electric Power (AEP) system guidelines, but not with the vendors recommendations. Additionally, the licensee did not periodically

perform several vendor-recommended tests, including tests of oil dielectric strength and oil acid

factor, and a measurement of the resistance of the current transformer primary (to compare

with the results in the test report). During followup discussions, licensee personnel stated that

the types of testing performed and the testing frequencies were based on AEP system

operating experience rather than vendor recommendations. Licensee personnel were unable to

readily provide specific operating experience data that justified the 4-year preventive

maintenance testing frequency. Licensee personnel subsequently determined that there were

approximately one hundred twenty six 345 kV current transformers in the AEP system similar in

design to the transformers located in the DC Cook 345 kV switchyard. Since 1990, there have

been two catastrophic failures (both associated with the D. C. Cook 345 kV switchyard L

breaker). No current transformers of this type had been removed from service based on

preventive maintenance testing. Following the June 12, 2002, current transformer failure, AEP collected oil samples from the

D.C. Cook 345 kV switchyard breaker current transformers for analysis. The oil analyses were

completed 3 months before the normal schedule as part of the licensees extent-of-condition

evaluation. During the oil sampling, AEP personnel discovered that two current transformers

for N1 switchyard breaker were last sampled in September 1998, with gas analyses results

significantly above the acceptable level. Based on this result, licensee replaced the N1 breaker

current transformers and returned the breaker to service on June 29, 2002. The AEP system

operating experience data did not justify a less frequent analysis than recommended by the

vendor.

DISCUSSION

The discrepancies, between the licensees maintenance practices for switchyard breaker and

current transformers and the vendor recommendations, contributed to the inadvertent

switchyard breaker trips that resulted in a plant trip and loss of offsite power (LOOP) to safety

busses. Unnecessary plant trips and LOOP events could be reduced by following vendor

recommendations with feedback from operating experience to determine the appropriate

schedule and extent of maintenance.

CONTACT

This information notice requires no specific action or written response. Please direct any

questions about this matter to the technical contact listed below or the appropriate Office of

Nuclear Reactor Regulation (NRR) project manager.

/RA/

Patrick L. Hiland, Chief

Reactor Operations Branch

Division of Inspection Program Management

Office of Nuclear Reactor Regulation

Technical Contact:

Thomas Koshy, NRR Allan Barker, RIII

301-415-1176 630-829-9679 E-mail: txk@nrc.gov E-mail: arb3@nrc.gov

NRR Project Manager: Richard Laura, NRR

301-415-1837 E-mail: ral1@nrc.gov

Note: NRC generic communications may be found on the NRC public Website, http://www.nrc.gov, under Electronic Reading Room/Document Collections.

ML051740051 OFFICE EEIB:DE Tech Editor OES:IROB:DIPM BC:EEIB:DE

NAME TKoshy (RLaura for PKleene) RALaura JACalvo

DATE / /2005 07/05/2005 07/05/2005 07/18/2005 OFFICE TL:C:IROB:DIPM C:IROB:DIPM

NAME EJBenner (MJRoss-Lee PLHiland

for)

DATE 07/19/2005 07/21/2005