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 Start dateReporting criterionTitleEvent descriptionSystemLER
ENS 401345 September 2003 13:33:0010 CFR 50.72(b)(3)(v)(A), Loss of Safety Function - Shutdown the Reactor
10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
High Pressure Coolant Injection (Hpci) Declared Inoperable.

At 09:30 EDT, Unit 1 was performing the HPCI Quarterly Flow verification surveillance. Shortly after the initiation of the system an abnormally loud bang was heard. System flow of approximately 5200 gpm and discharge pressure of approximately 1300 psi was achieved at approximately 09:33. Approximately 4 seconds after reaching rated system flow HPCI discharge pressure increased to approximately 1675 psi and system flow dropped to approximately 2700 gpm. HPCI had been declared inoperable at 08:35 EDT to perform the surveillance and will remain inoperable until the cause of the loss of system flow is corrected. Because HPCI is a single train ECCS (Emergency Core Cooling System) safety system, this event results in the loss of an entire safety function which requires an 8 hour ENS notification in accordance with 10CFR50.72(b)(3)(v) and the guidance provided under NUREG-1022, rev. 2. There are no other ECCS systems presently out of service. Reactor Core Isolation Cooling (RCIC) is fully operable and HPCI entered Tech Spec 3.5.1 (14 day Limiting Condition of Operation). All other ECCS systems are fully operable. The NRC Resident Inspector was notified of this event by the licensee.

  • * * RETRACTION FROM WALSH TO CROUCH ON 10/02/03 @ 1548 EDT* * *

On 09/05/2003, PPL Susquehanna LLC made an ENS notification per 10CFR50.72(b)(3)(v) in response to an apparent loss of the HPCI (High Pressure Coolant Injection) safety function. In the event, results of HPCI Quarterly Flow Surveillance testing did not meet acceptance criteria established for the system. Investigation into the cause of the failed HPCI surveillance revealed a 360-degree weld crack on the HPCI Test Line to Condensate Storage Tank (CST) Valve, HV155F008. HV155F008 is not in the reactor vessel injection flowpath. The impact of this crack, which was located between the valve seat cage assembly and the valve body, was that the HPCI Test Line to CST valve was not capable of throttling over the full range of HPCI system flows. Valve performance became erratic at higher flows because the valve seat cage was lifted out of the valve body into the flow path, increasing system resistance, and preventing attainment of design flow in the HPCI test loop. While the ability to effectively test the HPCI system using the test return path to the CST was compromised, the HPCI injection flowpath to the reactor vessel was not adversely affected by the damaged valve. Accordingly, the HPCI system maintained full capability for providing sufficient coolant to the reactor vessel in the event of a small break loss-of-coolant accident. Because the HPCI safety function was not compromised by the identified test path obstruction, this ENS notification is being retracted. The Licensee has notified the NRC Resident Inspector. Notified R1DO (Cobey).

High Pressure Coolant Injection
Reactor Core Isolation Cooling
ENS 4014711 September 2003 04:40:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News ReleaseOffsite Notification Made to Pennsylvania Emergency Management Agency (Pema)At 2314 EDT on 9/10/03 a fire was reported at the Unit 1B Reactor Feed Pump. The Fire Brigade was activated and the fire was extinguished at 2322 (8 minutes after identification). To support removal of the feed pump from service reactor power was reduced to 63%. Due to notifying the Pennsylvania Emergency Management Agency (PEMA) and other outside agencies, this event is being reported under 10CFR50.72(b)(2)(xi)." The NRC Resident Inspector was notified by the Licensee.
ENS 4017329 August 2003 14:25:0010 CFR 50.73(a)(1), Submit an LERInvalid Actuation of Containment Isolation ValvesOn August 29th, 2003 at approximately 1025 EDT, an electrical perturbation affecting both Unit 1 & 2 at PPL Susquehanna LLC resulted in a partial isolation of Primary Containment Isolation valves on Division 1, specifically A & B Containment Radiation Monitors and the Containment Instrument Gas Purge supply valve. This event is being reported as an invalid system actuation and is reportable under 10CFR 50.73(a)(2)(iv)(A). The condition meets the criteria of 10CFR 50.73(a)(2)(iv)(B)(2) due to a general containment isolation signal that affected containment isolation valves in more than one system. This notification is being provided via 60 day optional phone call as permitted under 10CFR 50.73(a)(1) in lieu of a written LER. The event was initiated when Operators were returning a Unit 1 13.8 KV Non-ESS breaker back in service following routine maintenance. When the breaker was restored to its closed position, a fault downstream of the breaker caused it to immediately re-open. The 13.8 Kv system supplies power to both unit's Division 14kV ESS busses. The perturbation was sufficient to cause several 'fail closed' containment isolation valves to actuate and close. The transient caused other non-safety related plant equipment to trip/auto-start, no other safety-related equipment or functions were lost. There also were no challenges to the reactor systems or containments. All plant equipment and/or systems were capable of being restored to their original alignment. The fault that caused the electrical perturbation originated at a non-ESS transformer and is currently being replaced. The licensee will inform the NRC Resident Inspector.Primary containment
ENS 4018219 September 2003 20:00:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessLoss of Emergency Sirens Due to Storm

At approximately 1535 (ET) on 9/19/03 the Susquehanna Control Room was notified that the 7.2 Kv supply line to the Tank Mountain repeater for activation of all emergency sirens was unavailable (approximately 121 sirens in Lucerne and Columbia Counties). The backup batteries for the repeater were reported to be supplying power for repeater activation. Following further discussion with Emergency Planning personnel, Susquehanna LLC could not determine how long the battery supply would be available. At 1600 the ability to activate the emergency sirens was declared inoperable due to the inability to determine the status of the power source. Loss of ability to activate the emergency sirens is reportable under 10CFR50.72(b)(3)(xiii), Loss of Emergency Preparedness Capabilities, as an eight hour notification. The Susquehanna LLC Emergency Plan incorporates alternate means, i.e. Route Alert Teams, to notify the public during an emergency situation. The licensee notified the NRC Resident Inspector and will be notifying State and local agencies.

  • * * * UPDATE FROM R. FRY TO M. RIPLEY 2105 ET 09/19/03 * * * *

As of 2010 hours (ET) on 9/19/2003, power was restored to the repeater that is used for emergency siren activation and the emergency sirens are considered operable. The NRC resident inspector has been updated. The licensee will be notifying State and local agencies. Informed R1DO (H. Gray)

ENS 4019624 September 2003 04:53:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge
Automatic Scram at Susquehanna on Low Water LevelAt 0053 hours on September 24, 2003 with Susquehanna Unit 1 operating at 100% power an automatic reactor scram occurred due to low water level. At the time of the scram, reactor feed pump testing was in progress and the 'C' reactor feed pump tripped. The reactor recirc pumps runback initiated as expected when water level reached 30" with the feed pump tripped. Level continued to drop and reached the Level 3 auto scram setpoint. Level continued to drop and reached a low level of approximately -48" wide range. Reactor Core Isolation Cooling and High Pressure Coolant Injection auto started at their initiation setpoints and injected to the vessel to recover level. All level 2 and 3 containment isolations occurred as expected. The reactor recirc pumps tripped as expected when level 2 was reached. Reactor Pressure was controlled with bypass valves, there were no Safety Relief Valve lifts. There are no challenges to containment. Unit 1 is currently stable in Mode 3 with both reactor recirc pumps restarted. A human performance error was the cause of the reactor feed pump trip. Investigation is continuing into the plant response to the reactor feed pump trip. The NRC Resident Inspector was notified of this event.High Pressure Coolant Injection
Reactor Core Isolation Cooling
Safety Relief Valve
ENS 4027223 October 2003 20:40:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentNonemergency Notification Due to Failure to Maintain Control Structure Habitability Envelope

During routine monitoring, Control Room personnel noted control structure pressure differential was below the 1/8" (inches of water pressure) required to maintain the Control Structure Habitability Envelope. A walkdown of the Control Structure and initial investigation has revealed no obvious problems that would cause the low positive pressure condition. Due to the inability of the Control Structure HVAC to maintain a positive pressure, both trains of Control Room Emergency Outside Air Supply system were declared inoperable. This is considered a Loss of Safety Function in accordance with 10 CFR 50.72(b)(3)(v)(D). The licensee has notified the NRC Resident Inspector.

  • * * * RETRACTION FROM A. FITCH TO M. RIPLEY 1343 ET 12/12/03 * * * *

At the time of the original 8-hour ENS notification was made, both trains of the Control Room Emergency Outside Air Supply (CREOAS) system were declared inoperable due to the failure of the Control Structure HVAC system to maintain the control structure habitability envelope at a pressure greater than + 1/8" w.g. (water gauge) with respect to outside atmosphere. Subsequent to this event, an evaluation was performed which determined that the requirement to maintain the control structure habitability envelope at a pressure greater than + 1/8" w.g. is only applicable during emergency operating conditions. Under emergency conditions, the CREOAS system, in conjunction with the Control Structure HVAC system, is required to maintain control structure pressure greater than + 1/8" w.g. in accordance with Technical Specification 3.7.3. However, during normal plant operation, the design function of the Control Structure HVAC system is to maintain the habitability envelope at a positive pressure above atmospheric. No specific value is required. Differential pressure readings for the control structure indicated that pressure was maintained above atmospheric at the time of this event. On October 24, 2003, surveillance testing successfully demonstrated that the Control Structure HVAC and CREOAS systems were capable of maintaining the control structure habitability envelope at a pressure greater than + 1/8" w.g. As such, there was no loss of safety function. The licensee has notified the NRC Resident Inspector. Notified R1DO (A. Della Greca)

HVAC
ENS 403672 December 2003 19:15:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News ReleaseOffsite Notification Due to Onsite FatalityAt 1230 hrs, with both units at 100% power the Control Room was notified of a Medical Emergency at the Access Processing Facility on the Owner Controlled Area outside of the Protected Area. The affected individual was a contract employee working for Site Access Services. An ambulance and paramedics arrived on site at 1242 hrs. First Aid and CPR were initiated at the scene. The individual was transported offsite at 1257 hrs to the local Hospital. At 1415 hrs the control room was notified that the individual had passed away. This constitutes an event of public significance and therefore reportable under 10CFR50.72(b)(2)(XI) as a 4 hour ENS notification. The licensee notified the NRC Resident Inspector and Pennsylvania Emergency Management Agency.
ENS 4044113 January 2004 12:30:0010 CFR 26.73, ApplicabilityContract Employee Fitness for DutyA contract employee tested positive for illegal drugs during Pre-Access testing for unescorted access. The employee's access to the plant was denied. Contact the HOO for additional details. The licensee notified the NRC Resident Inspector.
ENS 4044915 January 2004 00:50:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News ReleaseOffsite Notification of Accident Involving 2 Trucks Carrying Empty New Fuel Shipping ContainersThe following information was provided by the licensee via facsimile: On 1/14/2004 at 19:56 hours, the Shift Manager was notified by the Clinton County, PA Emergency Management Agency of vehicle accident involving trucks that were carrying a shipment from Susquehanna. The trucks were carrying empty shipping boxes from a shipment of new fuel that had previously been delivered to Susquehanna. These empty boxes were being shipped in accordance with U.S. Department of Transportation regulations (49CFR173.428 Empty Class 7 (Rad Mat)). On 1/15/2004 at 10:20 hours, additional information was provided to the control room indicating that this accident could cause increased public interest due to the severity of the accident. The two tractor trailers involved in the shipment were amongst the vehicles in the accident. One of the truck drivers was seriously injured. The trucks were severely damaged. Clinton County, PA, Emergency Management Agency was called to the scene by initial responders as well as the Pennsylvania Department of Environmental Protection. Both surveyed the boxes and found no indication of radiation/contamination. The shipping boxes and vehicles are being held by the towing company until the shipping company can provide replacement vehicles. The licensee has notified the NRC Resident Inspector.
ENS 4048629 January 2004 01:33:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News ReleaseOffsite Notification to Local Law Enforcement Due to Fire Brigade ActivationAt 2018 hrs, the Control Room was notified of smoke coming from the Unit 2 Vital UPS room. The Field Unit Supervisor (FUS) was dispatched to the room to investigate. At 2026 hrs, the Fire Brigade was activated. When the FUS arrived at the Vital UPS Panel he reported that there was smoke coming from the panel. He opened the panel and observed smoke coming from the transformer in the panel. He did not observe any flames at any time while dealing with the event. At 2029 hrs, Security was notified and subsequently notified the State Police at 2033 hrs. At 2033 hrs, the transformer was deenergized and the smoke began to dissipate. Entry into the Emergency Plan was evaluated and it was determined that no entry conditions exists at this time. Due to the notification of the Local Law Enforcement Agency, this event constitutes an Offsite Notification and therefore reportable under 10CFR50.72(b)(2)(xi) requiring a 4 hr ENS notification. When the transformer was deenergized, all loads were automatically transferred to the alternate power supply. The loss of this transformer did not affect any safety related equipment and does not require entry into any TS LCO Action Statements. The licensee notified state/local agencies and the NRC Resident Inspector. No press release is planned.
ENS 404982 February 2004 14:01:0010 CFR 26.73, ApplicabilityFitness for DutyA contractor foreman/supervisor was determined to be under the influence of alcohol during a pre-access FFD test as part of processing for unescorted access. The supervisor was denied unescorted access to the protected area. Contact the HOO for additional details The licensee notified the NRC Resident Inspector.
ENS 4050910 February 2004 00:00:00Other Unspec ReqmntVoluntary Report of a Press ReleaseOn 2/9/04 PPL issued a Press Release concerning the NRC decision to send an Inspection team to investigate the cause of the loose bolts found on one of the Emergency Diesel Generator and two other events involving Emergency Diesel Generators at the Susquehanna site. The NRC Resident Inspector was notified.Emergency Diesel Generator
ENS 4053118 February 2004 05:00:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News ReleaseOffsite Notification to Pema of Mislabeled ContainerAt 1500 on 2/16/2004, a tractor trailer with two intermodals (sea land containers) arrived at SSES (Susquehanna Steam Electric Station) from Race, LLC placarded radioactive 'empty'. Upon inspection it was determined that one of the intermodals had equipment in it contrary to the bill of lading and DOT regulations. This equipment was surveyed and found to be non-contaminated and non-radioactive. There was no radioactive exposure to any individuals as a result. Operations personnel were made aware of this event at 1630 on 2/18/2004. It was determined that this event may be of public significance and is reportable under 10CFR 50.72 (b)(2)(xi). The Pennsylvania Emergency Management Agency (PEMA) is being notified of this incident. The licensee notified NRC Resident Inspector.
ENS 4053521 February 2004 15:05:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News ReleaseOffsite Notification of Medical Event at SusquehannaAt 10:05 AM PST, the Susquehanna LLC Shift Manager was notified that a member of the general public required medical assistance. The individual was at a company owned public recreation area adjacent to the Susquehanna LLC River Intake access road. The recreation area is outside the protected area. An ambulance was called to the scene, arriving at 10:28 and leaving at 10:52. The individual was transported to a local hospital. The LLEA and PEMA were notified of the incident. The NRC Resident Inspector was notified.
ENS 4055428 February 2004 05:54:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News ReleaseOffsite Notification to State Based on Medical Transport of Injured WorkerAt 00:54 AM EST, the Main Control Room was notified than an individual had fallen approx. 12 feet from scaffolding. An ambulance was requested to the site, and arrived on site at 01:20. The individual is not contaminated and was transported to a local hospital at 01:40. PEMA (Pennsylvania Emergency Management Agency) was notified of the incident. The licensee informed the NRC Resident Inspector.
ENS 405643 March 2004 17:45:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News ReleaseOffsite Notification of Injured IndividualAt 12:45 PM EST, the Main Control Room was notified that an individual needed medical assistance at the South Building. The individual was light headed and nauseous. An ambulance was requested to the site, and arrived on site at 01:04 PM. The individual was not contaminated and was transported to a local hospital at 01:12 PM. Pennsylvania Emergency Management Agency (PEMA) was notified of the incident. This requires a voluntary report due to the offsite notification on an emergency vehicle responding to the site. The licensee notified the NRC Resident Inspector.
ENS 405664 March 2004 10:20:0010 CFR 50.72(b)(3)(ii)(A), Seriously DegradedRcic Steam Supply Failed Llrt

Appendix J Local Leak Rate Testing (LLRT) of the RCIC Steam Supply failed the Combined Main Steam Isolation Valves leakage limit of 300 scfh. The Combined MSIV leakage limit includes MSIV'S, MSL Drains, HPCI Steam Supply and RCIC Steam Supply. The volume between RCIC Steam Supply valves could not be pressurized therefore, the Minimum Pathway leakage limit is considered to be exceeded. This is also considered a failure of the Primary Containment Air Leakage Minimum Pathway leakage limit of 1.0 La. The identified degraded condition is reportable as a condition of the nuclear power plant, including its principle safety barriers being seriously degraded per 10CFR50.72(b)(3)(ii) requiring an 8-hr ENS notification. The RCIC Steam Supply line was tested successfully approximately two years ago during the last refueling outage. The licensee will inform the NRC Resident Inspector.

            • RETRACTED ON 4/14/2004 AT 1610 EST FROM FRY TO HEISSERER*****

At the time the original 8-hour ENS notification was made, it was declared that the Appendix J Local Leak Rate Test of the RCIC Steam Supply had failed the combined Main Steam Isolation Valves Minimum Pathway leakage limit of 300 scfh. The combined MSIV leakage limit includes MSIVs, MSL Drains, HPCI Steam Supply and the RCIC Steam Supply. The volume between the inboard and outboard RCIC Steam Supply valves could not be pressurized, therefore the Minimum Pathway leakage limit was considered to be exceeded. Subsequent to this event, during performance of an additional Local Leak Rate Test of the RCIC Steam Supply Penetration, it was demonstrated that the as-found Appendix J and combined MSIV Minimum Pathway leakage and the Primary Containment Air Leakage Minimum Pathway of 1.0 La were not exceeded as previously reported. The original Local Leak Rate Test was performed between the combination of two parallel inboard valves and the outboard valve. The subsequent test determined that the outboard isolation valve did not exceed Minimum Pathway criteria. The majority of the leakage was from the smaller inboard RCIC warm-up line isolation valve of the three RCIC Steam Supply valves. The post-maintenance test of the penetration measured leakage that was within acceptable limits. As such, the condition of the nuclear power plant, including its principle barriers, was not significantly degraded. The NRC Resident Inspector has been notified. Notified R1DO (B. McDermott).

Main Steam Isolation Valve
Primary containment
ENS 405716 March 2004 10:28:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News ReleaseOffsite Notification at Susquehanna Involving a Traffic AccidentOn 3/06/04 at 0528 Plant Security was notified of an accident at the entrance to the site involving an employee leaving work and a south bound vehicle on PA Route 11. There were no reported injuries. Local law enforcement was contacted and investigated the incident. Because of the involvement of a LLEA and potential media or general public interest in the event, the Pennsylvania Emergency Management Agency (PEMA) was notified of the incident at 0812 hours. Based on the notification to a government agency and possible public interest, this event was determined to be reportable under 10CFR50.72(b)(2)(xi). The NRC Resident Inspector was notified.
ENS 405737 March 2004 03:10:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessSpds Will Be De-Energized for More than 8 Hours Due to Refueling Outage Activities

At 22:10 on March 6, 2004 the Unit 1 Safety Parameter Display System (SPDS) was deenergized during planned refuel outage activities. It has been determined that it will not be restored within the required eight hours. Currently, restoration is scheduled for March 7, 2004 at 17:00. All required instrumentation is available in the control room. Since the Unit 1 SPDS computer system will be unavailable for greater than 8 hours, this is considered a Loss of Emergency Assessment Capability and therefore reportable under 10CFR50,72(b)(3)(xiii). Unit 1 is currently in Mode 5 for the planned 13th Refuel and Inspection Outage. The licensee notified the NRC Resident Inspector

        • Update at 2219 EST on 03/07/04 by Gordon Robinson taken by MacKinnon ****

SPDS is still out of service and it will be restored to service by 0600 EST on 03/08/04. R1DO (M. Shanbaky) notified. NRC Resident has be notified of the update by the licensee.

  • * * UPDATE ON 03/09/04 @ 1122 BY GRANT FERNSLER TO C. GOULD* * *

As of 1117 the SPDS was energized and restored to service. The NRC Resident Inspector was notified. Reg 1 RDO(Cobey) was notified.

Safety Parameter Display System
ENS 405747 March 2004 07:01:0010 CFR 50.72(b)(3)(iv)(A), System ActuationStart of the "a" Emergency Diesel Generator During Emergency Service Supply Bus OutageAt 0201 on 03/07/2004, with Susquehanna Unit 1 in its 13th Refueling and Inspection Outage, the 'A' Emergency Diesel Generator auto started during preparations for a scheduled 1A ESS(Emergency Service Supply) Bus outage. While performing the procedure for removal of the ESS Bus from service, two incorrect fuses were removed. This caused the normal supply breaker to open on sensed undervoltage deenergizing the 1'A' ESS Bus. The alternate breaker also attempted to close as designed, but tripped open immediately due to the sensed undervoltage. With all breakers open, the 'A' Emergency Diesel Generator auto started and loaded onto the bus. All leads had previously been removed from the bus per the procedure. The 'A' Emergency Diesel Generator is operating as designed and is available to supply Unit 2 'A' ESS Bus if required. The auto start of a Emergency Diesel Generator is reportable as an event that results in the valid actuation of a system designed to mitigate the consequences of significant events per 10CFR50.72(b)(3)(iv)(A). The licensee notified the NRC Resident Inspector.Emergency Diesel Generator
ENS 4060221 March 2004 17:32:00Information OnlyThree Injuried Noncontaminated Contractors Were Transported to the Hospital.On 3/21/04 at 12:32 hrs a bucket truck working at the Unit 1 Cooling Tower came in contact with a 230KV transmission line causing the loss of one off site power supply to the plant. The 500 KV offsite circuit remained energized during the event. A contract employee at the base of the truck was thrown due to the electrical short. A contract employee in the bucket of the truck was able to lower the bucket to the ground. A first aid crew was dispatched to the location and an Ambulance was requested. The Ambulance entered the site at 12:50 and at 13:02 the individuals were transported to the local hospital. Due to the electrical transient in the plant, a contract employee performing grinding activities lost control of the grinder and injured his middle finger. This individual received first aid and was transported to the local hospital by his supervisor. The individual injured in the plant was surveyed by Health Physics prior to leaving the site and no contamination was found. The Local Law Enforcement Agency was notified of the Emergency vehicle being dispatched to the site. The State Emergency Operations Center will be notified of the Emergency vehicle entering the site. The NRC Resident Inspector and local agencies were notified and the state will be notified.
ENS 4060523 March 2004 12:46:0010 CFR 50.72(b)(3)(ii)(A), Seriously DegradedIndication of Crack Failure on Rcs Pressure Boundary Penetration

Unit 1 is currently in a refueling outage in Mode 5. During a routine inservice inspection of the reactor vessel, an indication was discovered on the N1B penetration. This is associated with the suction for B Loop of Reactor Recirculation. At 0746 on 3/23/2004, the Control Room was notified that the evaluation was completed and the indication was determined to be unacceptable under the ASME Section XI Code. Based on guidance provided in NUREG-1022, Rev. 2, this material defect in the primary coolant boundary constitutes a seriously degraded condition and is reportable under 10CFR50.72(b)(3)(ii)(A). A final evaluation of the flaw and a repair plan is being developed. The licensee informed the NRC Resident Inspector.

          • RETRACTED ON 4/29/04 AT1018 FROM HUFFORD TO LAURA*****

On March 23, 2004, PPL Susquehanna, LLC reported a material defect discovered on the N1B penetration associated with the suction for the B Loop of Reactor Recirculation. The defect was discovered during routine inservice inspection of the reactor vessel. At the time of the report, the indication was believed to exceed the acceptability standards of ASME Section XI, IWB-3640. Accordingly, an ENS call was made pursuant to the reporting requirements of 10CFR50.72(b)(3)(ii)(A). Engineering analysis subsequently determined that the dimensional characteristics of the flaw were within the acceptability requirements of ASME Section Xl. This analysis conclusion provides the basis for retraction of the ENS report of March 23. Although hypothetical flaw growth calculations demonstrated that the flaw size would remain within the allowable envelope of ASME Section Xl, IWB-3641-1 over the next operating cycle, and continued operation without repair of the observed flaw was justified, PPL Susquehanna, LLC performed a weld repair of the defect during the recently completed refueling outage. Notified the R1DO (R. Barkley)

ENS 4061628 March 2004 11:37:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News ReleaseOffsite Notification Due to Three Car AccidentOn 3/28/04 at 0637, Plant Security was notified of a three car accident at the entrance to the site involving 1) an employee leaving the site, 2) a south bound vehicle on US Route 11, and 3) an employee entering the site. There were no reported injuries. Local law enforcement (LLEA) was contacted and investigated the incident. Because of the involvement of a LLEA and potential media or general public interest in the event, the Pennsylvania Emergency Management Agency (PEMA) was notified of the incident at 0812 hours. Based on the notification to a government agency and possible public interest, this event was determined to be reportable under 10CFR50.72(b)(2)(xi). The Licensee notified the NRC Resident Inspector.
ENS 406425 April 2004 05:30:0010 CFR 50.72(b)(3)(v)(A), Loss of Safety Function - Shutdown the ReactorLoss of Safety Function for Emergency Diesel Generators During Surveillance Testing

At 0030 (ET) during setup for Unit 1 Division 1 LOCA/LOOP Surveillance testing, the controlling procedure required making the Loss of Power instrumentation for the 1A and 1C ESS buses inoperable. The specification has a 1 hour time limit for restoration, or the associated Diesel Generators must be declared inoperable. Due to delays during the setup of equipment the time requirements were not met, and the associated Diesel Generators were declared inoperable at 0130. The Susquehanna Safety Analysis requires three operable Diesel Generators to safely shutdown. Therefore, this condition is reportable for Unit 2 under 10CFR50.72(b)(3)(v). Unit 1 is in Mode 5 and therefore not impacted. The Loss of Power instruments were restored, and the Diesel Generators declared operable at 0223. The licensee notified the NRC Resident Inspector.

  • * * * RETRACTION FROM R. FRY TO M. RIPLEY 1419 ET ON 05/27/04 * * * *

The following is a retraction of ENS Notification #40642 AND #40646: On April 5, 2004, PPL Susquehanna, LLC reported three events to the NRC associated with Unit 1 Division 1 LOCA/LOOP surveillance testing. In each case, the safety function of two (out of 4) emergency diesel generators was brought into question during the testing. In two of these events, the E (substituting for A) and C diesel generators were administratively declared inoperable per Technical Specifications. This was necessary because Loss of Power instrumentation for the 1A and 1C buses, rendered inoperable in support of the test procedure, was not restored within 1 hour. In the third event, the E (for A) and C emergency diesel generators were, again, declared inoperable when two ESW pump start timers failed to meet acceptance criteria thus bringing the proper start sequencing of emergency loads into question. Because the Susquehanna Safety Analysis requires three diesel generators to safely shutdown an operating unit, the potential compromise of the diesel generator safety function was a concern for Unit 2 in each instance. (NOTE: Unit 1 was in Refueling Mode 5 and was, therefore, not impacted by these events.) Accordingly, Control Room personnel conservatively initiated ENS reporting under 10CFR50.72(b)(3)(v) in response to the apparent loss of safety function for Unit 2. Subsequent engineering analysis has concluded that, although the declaration of diesel generator inoperability was correct and in accordance with Technical Specifications, fulfillment of these administrative actions did not result in an actual loss of safety function during any of the above described events. Details of the analysis show that the diesel generators were available to supply emergency power to the ESS buses and/or that sufficient redundant equipment was available to fulfill the safety function needs of Unit 2. These analysis conclusions provide the basis for retraction of the ENS reports made on April 5, 2004." The licensee notified the NRC Resident Inspector. Notified R1DO (R. Conte)

Emergency Diesel Generator
ENS 406465 April 2004 15:40:0010 CFR 50.72(b)(3)(v)(A), Loss of Safety Function - Shutdown the Reactor
10 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual Heat
10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Loss of Safety Function for Emergency Diesel Generators During Surveillance Testing

At 1040 hrs during setup for Unit 1 Division 1 LOCA/LOOP Surveillance testing, the controlling procedure required making the Loss of Power instrumentation for the 1A and 1C ESS buses inoperable. The specification has a 1 hour time limit for restoration, or the associated Diesel Generators must be declared inoperable. Due to delays during the setup of equipment the time requirements were not met, and the 'E' (Substituting for 'A') and 'C' Diesel Generators were declared inoperable at 1140 hrs. The Loss of Power instruments were restored, and the Diesel Generators declared operable at 1206 hrs. Unit 1 is in Mode 5 requiring only 2 diesel generators operable, therefore not impacted by the Loss of Power instrumentation inoperability. Also during the surveillance, two pump start timers failed to meet the required acceptance criteria. The 'A' ESW Pump timer actuated at 47.86 seconds (criteria; 36 sec. to 44 sec) and the 'C' ESW Pump timer actuated at 50.38 seconds (criteria: 39.6 sec. to 48.4 sec). With failure of the timers, proper loading on the Diesel Generators is not assured, and they were declared inoperable until the associated pump control breakers were opened. The 'E' Diesel Generator was declared inoperable at 1448 hrs, when the data analysis identified that the 'A' ESW pump timer did not meet acceptance criteria. The 'E' Diesel Generator was returned to operable at 1453 hrs when the DC Knife switches for the 'A' ESW pump were open. The 'C' Diesel Generator was declared inoperable at 1524 hrs, when the data analysis identified that the 'C' ESW pump timer did not meet acceptance criteria. The 'C' Diesel Generator was restored to operable at 1706 hrs after supported systems were realigned to prevent further loss of safety function and the DC Knife switches for the 'C' ESW pump were open. The Susquehanna safety analysis requires three operable Diesel Generators to safely shutdown the plant. Therefore with only two operable Diesel Generators, the condition requires an 8 hr ENS notification in accordance with 10CFR50.72(b)(3)(v)and (vi). All times referenced above are EDT. The licensee informed the NRC Resident Inspector.

* * * RETRACTION FROM R. FRY TO M. RIPLEY 1419 ET ON 05/27/04 * * * *

The following is a retraction of ENS Notification #40642 AND #40646: On April 5, 2004, PPL Susquehanna, LLC reported three events to the NRC associated with Unit 1 Division 1 LOCA/LOOP surveillance testing. In each case, the safety function of two (out of 4) emergency diesel generators was brought into question during the testing. In two of these events, the E (substituting for A) and C diesel generators were administratively declared inoperable per Technical Specifications. This was necessary because Loss of Power instrumentation for the 1A and 1C buses, rendered inoperable in support of the test procedure, was not restored within 1 hour. In the third event, the E (for A) and C emergency diesel generators were, again, declared inoperable when two ESW pump start timers failed to meet acceptance criteria thus bringing the proper start sequencing of emergency loads into question. Because the Susquehanna Safety Analysis requires three diesel generators to safely shutdown an operating unit, the potential compromise of the diesel generator safety function was a concern for Unit 2 in each instance. (NOTE: Unit 1 was in Refueling Mode 5 and was, therefore, not impacted by these events.) Accordingly, Control Room personnel conservatively initiated ENS reporting under 10CFR50.72(b)(3)(v) in response to the apparent loss of safety function for Unit 2. Subsequent engineering analysis has concluded that, although the declaration of diesel generator inoperability was correct and in accordance with Technical Specifications, fulfillment of these administrative actions did not result in an actual loss of safety function during any of the above described events. Details of the analysis show that the diesel generators were available to supply emergency power to the ESS buses and/or that sufficient redundant equipment was available to fulfill the safety function needs of Unit 2. These analysis conclusions provide the basis for retraction of the ENS reports made on April 5, 2004." The licensee notified the NRC Resident Inspector. Notified R1DO (R. Conte)

Emergency Diesel Generator
ENS 4069521 April 2004 20:35:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Scram in Response to High Main Turbine Vibration During StartupAt 1635 on 04/21/2004, Susquehanna Unit 1 was returning to service from its 13th Refueling and Inspection Outage which included main turbine replacement. During start-up turbine testing with the generator off line, several main turbine bearings experienced high vibration. In response to these high vibrations, the reactor was manually scrammed from approximately 17% power. The main steam line isolation valves were manually closed and main condenser vacuum was broken in order to more rapidly slow the main turbine speed. All control rods fully inserted on the SCRAM, a level 3 containment isolation signal was received as expected. RCIC was manually initiated to control reactor water level. Lowest reactor water level reached was approximately 3" narrow range. There were no radioactive releases. This RPS actuation is reportable under 10CFR50.72(b)(2)(iv)(B) as an 'Unplanned RPS Actuation with the Reactor Critical.' The RPS Actuation and the RCIC injection are reportable per 10CFR50.72(b)(3)(iv)(A) 'Unplanned Actuations of Systems that Mitigate the Consequences of Significant Events.' Investigation into the high main turbine bearing vibrations is ongoing. The main turbine was tripped prior to the manual scram and no SRVs have lifted due to low decay heat level. The electric plant is in a normal lineup. The licensee notified the NRC Resident Inspector and the PEMA representative.Main Turbine
Main Steam Line
Main Condenser
Control Rod
ENS 4071128 April 2004 17:07:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release
10 CFR 50.72(a)(1)(i), Emergency Class Declaration
Unusual Event Decleared Due to an Electrical Failure in a Non-Vital Load Center Located in the Unit 2 Reactor BuildingOn 04/28/04 at 1325 EDT, Susquehanna declared an Unusual Event due to an electrical failure in a power distribution panel at a non-vital load center located in the Unit 2 Reactor Building. The affected load center supplies electrical power to the Main Condenser Vacuum system causing plant operations to be reduced to 80% reactor power. Unit 1 has not been affected by this incident and Unit 2 remains stable at 80% reactor power. The licensee terminated the Unusual Event at 1552 and is investigating the cause of the incident which appears to have been a phase-to-phase fault on the 13.8 KV load center feeder cable. Currently, load center 2B250 is being fed through an alternate feeder so that associated systems can be placed back in service. Unit 2 is making preparations to return to full power. There were no personnel injuries nor radioactive releases as a result of this event. The licensee notified the NRC Resident Inspector, Luzerne and Columbia county emergency management agencies, the Pennsylvania Emergency Management Agency and has issued a press release. Notified the following of the termination of the Unusual Event: R1DO(Barkley), DIRO (Frant), NRR (Marsh), DHS (E. McDonald) and FEMA (D. Barden).Main Condenser
ENS 4073321 March 2004 16:32:0010 CFR 50.73(a)(1), Submit an LERInvalid Actuation of Containment Isolation Signals in More than One SystemThe following information was obtained from the licensee via facsimile: On 03/21/04 at 12:32 hours (EST), a JLG Manlift working on the Unit 1 Cooling Tower came into contact with a 230 KV transmission line, causing the loss of one of two off-site power supplies to the plant (Startup Transformer T-10 and its associated loads). The other Startup Transformer (T-20) assumed the extra electrical load, as designed, and restored power to the station. At the time of this event, Unit 1 was in Mode 5 and Unit 2 was in Mode 1. Both Units continued in Modes 5 and 1, respectively. As a result of the loss of the T-10 transformer, the following Unit 2 Primary Containment Isolation (Valves)(PCIVs) closed on loss of logic power: Containment Atmosphere Control PCIVs HV-25740A, HV-25750A, HV-25776A, HV25780A, HV-25736A, and HV-25742A, HV-25752A, HV-25774A, HV-25782A, HV-25734A. Drywell Sump PCIVs HV-261108 A1 and A2 closed. Reactor Building Chilled Water PCIVs HV-28791 A1 and A2 and HV-28792 A1 and A2 closed. Recirculation Sample PCIV HV-243F019 closed. All isolation signals were successfully reset and the T-10 line was subsequently restored. The Unit 2 electrical transient event resulted in general containment isolation signals affecting containment isolation valves in more than one system and is therefore being reported per 10 CFR 50.73(a)(1) and 10 CFR 50.73(a)(2)(iv)(A). A voluntary ENS Phone Notification to the NRC, related to this event, was previously made on 03/21/04, due to notification of the Pennsylvania Emergency Management Agency (PEMA), because an emergency vehicle entered plant property. The above listed systems' Division 1 containment isolation valve actuations were completed and functioned successfully on loss of logic power. The licensee has informed the NRC Resident Inspector of this notification.Primary containment
ENS 407664 April 2004 18:57:0010 CFR 50.73(a)(1), Submit an LER60 -Day Report: Invalid Actuation of the "E" Emergency Diesel GeneratorOn 04/04/04 at 14:57 hours, the "E" Emergency Diesel Generator unexpectedly started in the emergency mode of operation during performance of Unit 1 LOCA/LOOP surveillance testing. The diesel generator started in response to a false loss of offsite power signal that occurred after an electrical test jumper was incorrectly installed in panel 1A201. While the procedure directed installation of the jumper across the field side of states links T5-10 and T5-12, the jumper was instead installed across the panel side of the links. When link T5-10 was opened per procedural direction, a false LOOP signal was sent to the "E" diesel generator start circuit. The "E" emergency diesel generator successfully started and properly responded to the complete train actuation signal. The diesel was shutdown following the incident. No other plant equipment was affected by this jumper use error. At the time of this event, Unit 1 was in Mode 5 and Unit 2 was in Mode 1. Both Units continued in Modes 5 and 1, respectively. Surveillance testing was successfully completed on 04/05/04. The consequences of this event were limited to the unplanned start of the "E" emergency diesel generator. The diesel generator started and functioned in accordance with its design. This event comprises an invalid actuation of an emergency AC electrical power system and is therefore being reported in accordance with 10 CFR 50.73(a)(2)(iv)(A) as a 60- day telephone notification per the provision of 10 CFR 50.73 (a)(1). The NRC Resident Inspector was notified of the 60- day report notification by the licensee.Emergency Diesel Generator
ENS 4077726 May 2004 20:00:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News ReleaseOff Site NotificationThis event is being reported under 10CFR50.72(b)(2)(xi) as an item of public interest and an event for which other government agencies have been notified. At 1600 on 5/26/2004, the operations Shift Manager was notified by the Security Shift Supervisor that an individual (truck driver) had been arraigned by a LLEA (Local Law Enforcement Agency) judge for prohibited items (drug paraphernalia) which were discovered during a routine entrance search of personnel and vehicles. The items were discovered outside the protected area (and) were determined to not pose a threat or attempted threat. The LLEA was called and responded to the site access area and removed the individual to the local barracks, where he was subsequently arraigned on a misdemeanor. The individual's name has been removed from the Susquehanna LLC visitors list. The Manager of Nuclear Security briefed NRC Region #1 Inspector, Dana Caran, concerning the incident. The licensee notified the NRC Resident Inspector.
ENS 4094813 August 2004 12:00:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessLoss of the Safety Parameter Display System (Spds) for Greater than 8 HoursAt 08:00 on 8/13/04 Computer Maintenance personnel discovered the Unit 1 SPDS computer was not updating properly. A review into the history identified that the SPDS computer had stopped updating at 21:00 on 8/12/04. The Control Room was notified. The computer group was successful in resetting the SPDS computer and is now properly operating. Since the Unit 1 SPDS computer system was unavailable for greater than 8 hours, this is considered a loss of Emergency Assessment Capability and therefore reportable under 10CFR50.72(b)(3)(xiii). The licensee informed the NRC Resident Inspector.Safety Parameter Display System
ENS 4095615 August 2004 00:45:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessLoss of Safety Parameter Display SystemAt 2045 (EDT) on 08/14/2004, Computer Maintenance personnel discovered the Unit 2 SPDS computer was not updating properly. A review of history identified that the SPDS computer had stopped updating at 1109 (EDT) on 8/14/2004. The Control Room was notified. Computer Maintenance was successful in resetting the SPDS computer at 2100 (EDT), and it is now properly operating. Since the Unit 2 SPDS computer system was unavailable for greater than 8 hours, this is considered a Loss of Emergency Assessment Capability and reportable under 10CFR50.72(b)(3)(xiii). The licensee notified the NRC Resident Inspector.Safety Parameter Display System
ENS 4097020 August 2004 16:15:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialRailroad Access Process Radiation Monitors Actuation Capability Was Inadvertently DefeatedAt 12:15 PM on 8/20/04, it was discovered that actions performed on 7/16/04 in support of Dry Fuel Storage activities to defeat the Railroad Access Area Radiation Monitor alarm horn had also defeated the actuation capability of the Railroad Access Process Radiation monitors. Per Technical Specifications, the process monitors are required to be operable "during movement of irradiated fuel assemblies within the Railroad Access Shaft, and above the Railroad Access Shaft with the Railroad Access Shaft Equipment Hatch open." Contrary to the Tech Spec requirement, two loaded Dry Fuel Storage Casks were lowered in the Railroad Shaft, one on 8/2/04 and the second on 8/16/04, with the radiation monitors inoperable. During this period the automatic isolation and re-alignment of Reactor Building Zone lll, automatic start of Reactor Building Recirculation Fans, and the automatic starts of SGTS and CREOASS would not have actuated from a HI-HI Radiation condition in the Railroad Access Shaft. Actual radiological conditions observed during the transfer of the casks in the railroad shaft would not have resulted in the need for system actuation. All other instruments in the Reactor Building ventilation system which actuate these systems were operable as required by Tech Specs. The jumpers which defeated the actuation capability were removed on 8/20/04 at 1400 (hrs.). This event is considered reportable under 50.72(b)(3)(v)(C) as a loss of safety function. The NRC Resident Inspector was notified.Reactor Building Ventilation
ENS 410299 September 2004 08:24:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessLoss of Emergency Assessment Capability

At 04:24 EDT, the Control Room Super Particulate Iodine Noble Gas (SPING), Stack Monitoring System, terminal and the associated terminal in the Technical Support Center (TSC) began printing transmit and receive errors. As a result, all SPINGs were declared inoperable and associated Technical Requirements actions entered for alternate sampling. Review by Nuclear Regulatory Affairs and Shift Supervisor considers the occurrence a loss of Emergency Assessment Capability and is therefore reportable under 10 CFR 50.72(b)(3)(xiii). Licensee is taking samples every 4 hours.

The NRC Resident Inspector was notified of this event by the licensee.

ENS 4121522 November 2004 20:10:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialPortion of Primary Instrument Lines Not Aligned to Secondary ContainmentAt 15:10 on 11/22/2004 Operations was notified of a condition that could have prevented the ability of Secondary Containment to control and monitor the release of radioactive material. Three primary system instrument lines have approximately a 20-foot run in an area that is not normally aligned to Secondary Containment. This area has been realigned to Secondary Containment until an analysis of this design can be completed. This has been determined to be reportable under 10CFR50.72(b)(3)(v)(C). Unit 1 is at 15% power with the main generator off line for unrelated repairs. The licensee notified the NRC Resident Inspector.Secondary containment
ENS 4128122 December 2004 20:00:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News ReleaseOffsite Notification Made to Pennsylvania Emergency Management Agency (Pema)An ambulance was called to the site because a plant employee, not in the power plant but in an onsite office building, complained of chest pains. The individual was taken by the ambulance to Berwick Hospital. PEMA was notified of this by the licensee. The NRC Resident Inspector was notified of this event by the licensee.
ENS 413909 February 2005 14:20:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentBoth Trains of the Control Structure Emergency Outside Air Supply System Inoperable

At 09:20 am, on February 9th, the control room declared both trains of Control Structure Emergency Outside Air Supply System (CREOASS) inoperable. The control room was notified of an inoperable boundary door that was not closed and latched and therefore would not have allowed CREOASS to perform its safety function of maintaining the Control Structure at a positive pressure if required. The door was closed and locked (at 11:15) to restore the habitability boundary. The door has since been repaired (adjustment of latch mechanism). Initial investigation determined that the door had been unlocked at approximately 09:20 this morning by an elevator vendor to perform maintenance. This is being reported as an event or condition that could have prevented the fulfillment of the safety function required to mitigate the consequences of an accident. CREOASS was not called upon to function during the period that the door was not operable. The licensee notified the NRC Resident Inspector.

  • * * RETRACTION FROM LICENSEE (ROBINSON) TO NRC (HUFFMAN) @ 1328 EDT ON 4/8/05 * * *

The following information was provided by the licensee (licensee text in quotes): On 2/9/2005, PPL Susquehanna LLC reported a loss of safety function for the Control Room Emergency Outside Air Supply System (CREOASS) based on one of the Control Structure Habitability boundary doors being found partially open. Positive air pressure generated by the Control Structure HVAC System prevented the door closure mechanism from maintaining the door closed. The door was closed to restore the habitability boundary. The event was reported as a condition that could have prevented the fulfillment of the safety function required to mitigate the consequences of an accident. The Safety Function of the CREOASS is to provide adequate radiation protection to permit occupancy of the Control Room under accident conditions for the duration of the accident. The CREOASS accomplishes this by: 1) filtering the outside make-up air supply and 2) maintaining a positive pressure in the control structure habitability boundary to limit unfiltered air in leakage into the boundary. A subsequent engineering evaluation concluded that with the door closure mechanism providing a resistive force, CREOASS would have been able to maintain a positive pressure within the boundary and perform its safety function as described above. In conclusion, the reported condition did not result in a loss of safety function under 10CFR50.72 (b)(3)(v)(D) and is therefore being retracted. The NRC Resident Inspector and R1DO (Noggle) have been notified.

HVAC
ENS 414624 March 2005 20:10:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release
10 CFR 50.72(a)(1)(i), Emergency Class Declaration
Unusual Event Declared

The following information was obtained from the licensee via facsimile (licensee text in quotes): At 3:10 PM EST PPL Susquehanna, LLC, declared a Notification of Unusual Event (classification OU4) for a Fire within Protected Area Boundary not Extinguished within 15 Minutes of Detection. The fire occurred in the turbine building of unit 2 which is currently in a refueling outage. Activation of the Emergency plan is reportable under 10CFR50.72(a)(3). There were no open flames observed, only smoke. The source of the smoke was weld slag that fell into a bucket of material. Due to the temporary ventilation system installed, the smoke spread throughout the turbine building prompting the licensee to call away a fire. The licensee is investigating the area at this time. There are no personnel injuries or equipment damage at this time. The licensee will inform the NRC Operations Center when the NOUE is terminated.

  • * * UPDATE FROM PRESTON PRATT TO MIKE RIPLEY @ 1614 EST ON 3/4/05 * * *

The licensee has terminated the Unusual Event. The source of the smoldering material was discovered and extinguished. The licensee has notified the NRC Resident Inspector. The Headquarters Operations Officer notified DHS (Frost), IRD (Wilson), NRR (Reis), FEMA (Sweitzer), and R1DO (Holody).

  • * * UPDATE FROM R. FRY TO M. RIPLEY 2015 EST 03/04/05 * * *

At 16:30 PM EST PPL Susquehanna, LLC, authorized a press release as a result of a Notification of Unusual Event (classification OU4) for a Fire within Protected Area Boundary not Extinguished within 15 Minutes of Detection. The fire occurred in the Turbine Building of Unit 2 which is currently in a refueling outage. The press release was issued at 17:15 EST. Any event or situation related to the health and safety of the public or onsite personnel, or protection of the environment, for which a news release is planned or notification to other government agencies has been or will be made is reportable under 10 CFR 50.72(b)(2)(xi). The licensee notified the NRC Resident Inspector. Notified R1 DO (D. Holody)

ENS 414636 March 2005 20:00:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentPost-Accident Monitoring Instrumentation Inoperable

The following information was provided by the licensee via facsimile (licensee text in quotes): At 1500, on March 6, 2005, the Control Room declared both required divisions for three functions (Primary Containment Pressure, Primary Containment Hydrogen and Oxygen Analyzer, and Drywell Atmosphere Temperature) of Post Accident Monitoring Instrumentation (a Safety System) inoperable. The control room was notified of 'Non Quality' (non-Q) parts installed in both required divisions of a Post Accident Monitoring Instrumentation Recorder. The appropriate LCO Conditions were entered for one or more functions with two required channels inoperable. This equipment has passed all surveillance requirements and has been functional since installation. Plans are being developed to replace the non-qualified parts. This is being reported as an event or condition that could have prevented fulfillment of a safety function required to mitigate the consequences of an accident in accordance with 10CFR50.72(b)(3)(v)(D). The licensee notified the NRC Resident Inspector.

  • * * UPDATE ON 03/30/05 @ 1128 BY JIM HUFFORD TO CHAUNCEY GOULD * * * RETRACTION

The following information was provided by the licensee via facsimile (licensee text in quotes): On March 6, 2005, PPL Susquehanna, LLC reported a perceived loss of safety function for three functions of Post Accident Monitoring Instrumentation on Unit 1. The notification was made pursuant to the reporting requirements of 10CFR50,72(b)(3)(v)(d). Engineering analysis has subsequently determined that the use of non-Q fuse holders in the Quality application did not adversely affect the safety-related functions which they supported. The fuse holders were removed, subjected to testing, and determined to be electrically and functionally equivalent 'to Quality fuse holders maintained at the station. This analysis conclusion provides the basis for retraction of the ENS report of March 6. The NRC Resident Inspector was notified. The Reg 1 RDO (Jim Trapp) was informed.

Primary containment
ENS 4150621 March 2005 03:30:0010 CFR 50.72(b)(3)(ii)(A), Seriously DegradedPressure Boundary Leakage Discovered During Hydro TestThe following information was obtained from the licensee via fax (licensee text in quotes): At 22:30 on 3/20/2005, the Control Room was notified by the test director that ASME CLASS I Boundary System Leakage Hydrostatic Pressure Test (SE-200-002) had failed. The reason was a leak identified on Reactor Recirc Pump B Discharge Valve, HV243F031B. The leak is coming from the Stub Tube Weld Leakoff Connection for the valve. It is leaking approx. 10 drops per minute. Technical Requirement 3.4.2 was entered. It was determined to be unacceptable under the ASME Section XI Code. Based on guidance provided in NUREG-1022, Rev. 2, this material defect in the primary coolant boundary constitutes a seriously degraded condition and is reportable under 10CFR50.72(b)(3)(ii)(A). A final evaluation of the flaw and a repair plan is being developed. The NRC Resident was notified.05000388/LER-2005-001
ENS 4158510 April 2005 15:50:0010 CFR 50.72(b)(2)(i), Tech Spec Required ShutdownTechnical Specification Required Shutdown Due to Failed 125V Dc Battery Charger

At 0352 the 2C 125VDC battery charger failed. Fuses internal to the charger were found blown. Technical Specifications require restoration of the charger within 2 hrs or enter Mode 3 within the next 12 hrs and Mode 4 within the next 36 hrs. Investigation has not been able to restore the charger, and therefore the shutdown of the unit has commenced. Loads are currently being carried by the batteries, and personnel are monitoring battery voltage. Initial investigation has not identified any generic issues or any indication of tampering. This event is a Technical Specification required shutdown, and is reportable as a four hour ENS Notification under 10 CFR 50.72(b)(2)(i). Additionally, this is a voluntary notification due to an anticipated press release associated with the downpower towards unit shutdown. There is evidence of degraded insulation on wires inside the affected battery charger. Battery loads are very small with an initial estimate of battery life at 80 hours. All safety systems are operable. There is no impact on Unit 1. Unit 2 is expected to reach Mode 3 at 1720 on 4/10/05. The NRC Resident Inspector has been notified. State (FEMA) will be notified.

  • * * UPDATE PROVIDED BY LICENSEE (HUFFORD) TO NRC (HELD) AT 2030 ON 4/10/05 * * *

At 17:28 the plant completed a normal reactor shutdown and entered Mode 3 in accordance with plant procedures to fulfill the requirements of Technical Specification 3.8.4. There were no ECCS initiations and lowest water level was approximately -4 inches. The licensee reported that the 2C battery charger was back in service but remained in the LCO due to battery requirements. They are also completing engineering evaluations for extent of condition. The NRC Resident Inspector was notified. R1DO (Noggle) notified.

  • * * UPDATE PROVIDED BY LICENSEE (KLINEFELTER) TO NRC (HELD) AT 1710 ON 4/12/05 * * *

At 16:28 on April 12th, 2005 Susquehanna Unit 2 entered Mode 2 (Start-up) following the completion of repairs to the failed 125VDC battery charger and inspection to the remaining 3 Unit 2 125VDC battery chargers. A courtesy call was made (to) the Pennsylvania Emergency Management Agency. An informational press release will be made. The NRC Resident Inspector was notified by the licensee. R1DO (White) was notified.

ENS 4163125 April 2005 02:30:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessSpds (Safety Parameter Display System) Is Down for Planned MaintenanceAt 2130 hours on 04/24/2005 the Unit 1 SPDS system will be removed from service for planned maintenance (cable rework). The duration of work is expected to be 32 hours (scheduled for completion at 0530 hours on 04/26/2005). ERDS will remain operable during the work window but several points will not be available. For example 23 of 58 ERDS points will be unavailable while SPDS is out of service. However, the ERDS system will still be operable and transmit the remaining points. Loss of Emergency Assessment Capability - A review of the ability of the Emergency organization to function without SPDS was performed. Alternate sources for many of the points in SPDS were identified and are contained on an Emergency Plan format in PICSY (plant integrated computer system). Those points not available from PICSY can be obtained from the control room. With these compensatory actions and the communications in place between the facilities, there will not be a major loss of emergency assessment capability. Since the Unit 1-SPDS computer system will be unavailable for greater than 8 hours, this is considered a Loss of Emergency Assessment Capability and reportable under 10CFR50.72(b)(3)(xiii). The NRC Resident Inspector was notified.Safety Parameter Display System
ENS 4164026 April 2005 11:31:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessSpds (Safety Parameter Display System) Is Down for Planned Maintenance

At 0731 hours (EDT) on 04/26/2005 the Unit 2 SPDS system was removed from service for planned maintenance. The duration of work is expected to be 48 hours (scheduled for completion at 0700 hours (EDT) on 04/28/2005). ERDS will remain operable during the work window but several points will not be available. For example 23 of 58 ERDS points will be unavailable while SPDS is out of service. However, the ERDS system will still be operable and transmit the remaining points. Loss of Emergency Assessment Capability - A review of the ability of the emergency organization to function without SPDS was performed. Alternate sources for many of the points in SPDS were identified and are contained on an Emergency Plan format in PICSY (plant integrated computer system). Those points not available from PICSY can be obtained from the control room. With these compensatory actions and the communications in place between the facilities, there will not be a major loss of emergency assessment capability. Since the Unit 2 SPDS computer system will be unavailable for greater than 8 hours, this is considered a Loss of Emergency Assessment Capability and reportable under 10CFR50.72(b)(3)(xiii). The NRC Resident Inspector has been notified.

  • * * UPDATE ON 4/28/05 AT 1412 EDT FROM RON FRY TO A. COSTA * * *

This is a followup courtesy notification to EN#4160. The Unit 2 SPDS system as noted below (above) has been restored to normal at 13:52 (EDT) on 4/28/05 The licensee notified the NRC Resident Inspector. Notified R1DO (Barkley).

Safety Parameter Display System
ENS 4164628 April 2005 11:19:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release
10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Unit 2 Manual Reactor Scram Due to Loss of Main Transformer CoolingAt approximately 0700 U2 B Main Transformer cooling was lost. Unit 2 reactor power was reduced from 100% to 75%. Attempts to restore the 2B Main Transformer cooling were unsuccessful, and Unit 2 was manually scrammed from 75% reactor power. RPV water level decreased to -30" due to the SCRAM and was restored by normal Feedwater and RCIC injection. The Main Condenser remained available as a heat sink and there were no SRV lifts. The low water level did result in receiving the Level 2 Division 2 containment isolation signal (-38"), and all expected isolations and initiations did occur. This event requires a 4 hour ENS notification in accordance with 10CFR50.72(b)(2)(iv)(B) for an RPS actuation when critical, and an 8 hour ENS notification per 10CFR50.72(b)(3)(iv)(A) for the injection from RCIC and receipt of the level 2 Containment Isolation signal. Additionally, a press release to the public will be issued, and requires a 4 hour ENS notification in accordance with 10CFR50.72(b)(2)(xi). All rods fully inserted during the manual scram. The electrical system is in a normal shutdown lineup. Secondary containment ventilation was momentarily disrupted in unit-1 and successfully restored. The licensee notified the NRC Resident Inspector and will be notifying the state and media concerning this event.Feedwater
Secondary containment
Main Transformer
Main Condenser
05000388/LER-2005-003
ENS 417466 June 2005 16:33:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release
10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Scram Due to Apparent Generator Load RejectionAt approximately 1233 hours, the Susquehanna Unit Two reactor automatically scrammed due to an apparent generator load reject. All rods inserted, and both reactor recirculation pumps tripped. Reactor water level lowered to -6" causing level 3 (setpoint +13") isolations, and was restored to normal level (+35") by the feedwater system. All isolations at this level occurred as expected. Two steam relief valves opened, then reclosed. Pressure was subsequently controlled via turbine bypass valve operation. All safety systems operated as expected. Some balance of plant loads shutdown apparently due to a voltage perturbation. A reactor recirculation pump was restarted to re-establish forced core circulation. The reactor is currently stable in condition 3. An investigation into the cause of the shutdown is underway. Unit One continued power operation. The NRC resident inspectors were notified. A press release will occur. The licensee will be notifying the State of Pennsylvania.Feedwater
Reactor Recirculation Pump
05000388/LER-2005-005
ENS 4191814 August 2005 23:10:00Information OnlyFire Alarm in Training Building Due to Loss of PowerThis is a Voluntary Report based on a State Notification that does not meet the criteria of 10CFR50.72(b)(2)(xi). At approximately 19:10 hours, the Susquehanna Control Room was notified that offsite fire departments had responded to the Susquehanna Learning Center. This was due to a fire alarm received by the corporate office from the building due to a loss of power to the facility. Offsite fire department personnel along with our Training department inspected the building and found no indications of fire. The Susquehanna Learning Center is located outside of the protected area and approximately one eighth mile from the main access road on State Route 11. Pennsylvania Emergency Management Agency was advised. The loss of power to the training building was the result from lightning in the area. The licensee notified the NRC Resident Inspector.
ENS 420343 October 2005 16:48:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News ReleaseOffsite Notification Made to Pennsylvania Emergency Management Agency (Pema)At 12:48 PM EST, the Main Control Room was notified that an individual needed medical assistance at the South Building. The individual was experiencing chest pains. An ambulance was requested to the site, and arrived on site at 13:17 PM. The individual is not contaminated and was transported offsite to a local hospital at 13:35 PM. PEMA was notified of the incident. This requires a voluntary report due to the offsite notification on an emergency vehicle responding to the site. The NRC Resident Inspector was notified of this voluntary notification.
ENS 4208126 October 2005 14:20:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessLoss of Power at the Emergency Operations Facility

Due to an electrical fault in the Susquehanna Emergency Operations Facility (EOF), the power to the building has been removed. Testing and repairs are underway and expectations are that power will be restored in approximately 6 hours. The EOF is located approximately 30 miles from the Susquehanna plant and the loss of power does not effect plant operation. Until repairs are complete communications and accident assessments will be made in the on site Technical Support Center (TSC). The Pennsylvania Emergency Management Agency, Luzerne and Columbia Counties have been notified by the Susquehanna Emergency Planning Organization. The NRC and PEMA will be notified upon power restoration. The licensee notified the NRC Resident Inspector.

  • * * UPDATE ON 10/26/05 AT 1500 EDT FROM JIM HUFFORD TO ARLON COSTA * * *

As of approximately 1300 hours on 10/26/2005, power was restored to the Susquehanna Emergency Operations Facility (EOF) and the facility is considered operable. The NRC Resident Inspector will be updated. Notified the R1DO (Silk).

ENS 4209329 October 2005 03:32:0010 CFR 50.72(b)(2)(i), Tech Spec Required ShutdownTechnical Specification Required Shutdown Due to Inoperable Control Rods

On 10/28/2005, Susquehanna Unit 1 operators began the process of shutting down the unit for a maintenance outage to address control cell friction. It was expected that during this evolution, "slow to settle" control rods would be encountered, and rather than delay the continuance of the shutdown to perform operability testing, it was determined that these control rods would conservatively be declared inoperable. Based on previous testing data and trending analysis of operability testing performed during the cycle, PPL (Pennsylvania Power and Light) believes that the subject control rods would have passed operability tests. Accordingly, at 2332 EDT, Technical Specification 3.1.3.f was entered which requires the unit to be taken to Mode 3 in 12 hours when nine or more control rods are inoperable. Entry into this specification was also required per 3.1.3.e when it was determined that four inoperable rods resided within one Banked Position Withdrawal Sequence (BPWS) group. The inoperable control rods are fully inserted and disarmed, shutdown margin requirements are met, and the control rod system was always fully capable of performing its safety function. At the time when the ninth control rod was declared inoperable, Unit One was operating at 18% power. Unit Two is continuing operation at 100% power. PPL is reporting this event as a Technical Specification required shutdown per 10CFR 50.72(b)(2)(i). The NRC Resident Inspector was notified by the licensee. Unit 2 is not affected by this problem and will continue to operate at 100% power.

  • * * UPDATE FROM LICENSEE (ILLIADIS) TO NRC HUFFMAN AT 1011 EDT ON 10/29/05 * * *

At 0744 the plant reached All Rods In and at 0805 entered Mode 3 in accordance with plant procedures to fulfill the requirement of Technical Specification 3.1.3. As stated in the original EN# 42093, it was expected that during this evolution, "slow to settle"' control rods would be encountered, and rather than delay the continuance of the shutdown to perform operability testing, it was determined that these control rods would conservatively be declared inoperable. This action was taken on a total of 41 control rods that failed to settle at position 00 during the shutdown. There are 4 additional control rods that were declared inoperable previously during the cycle and subsequently settled to 00. Of the 41 control rods that failed to settle at the time of the shutdown, 6 have settled to 00 at the time of this update. Based on previous testing data and trending analysis of operability testing performed during the cycle, PPL continues to believe that the subject control rods would have passed operability tests. The inoperable control rods are fully inserted, shutdown margin requirements are met, and the control rod system was always fully capable of performing its safety function. There were no ECCS initiations and no challenges to containment. The licensee notified the NRC Resident Inspector. R1DO (Silk) notified.

Control Rod
ENS 421832 December 2005 05:49:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessSafety Parameter Display System (Spds) Failure on Unit Two

At 0049 hours on 12/2/2005 the Unit 2 (safety parameter display system) SPDS system failed. The cause of the failure is under investigation and is expected to exceed 8 hours. ERDS remains operable but several points are not available. For example 23 of 58 ERDS points are unavailable while SPDS is out of service, The ERDS system can transmit the remaining points. Loss of Emergency Assessment Capability - A review of the ability of the Emergency organization to function without SPDS was performed. Alternate sources for many of the points in SPDS were identified and are contained on an Emergency Plan format in PICSY (plant integrated computer system). Those points not available from PICSY can be obtained from the control room. With these compensatory actions and the communications in place between the facilities, there will not be a major loss of emergency assessment capability. Since the Unit 2 SPDS computer system will be unavailable for greater than 8 hours, this is considered a Loss of Emergency Assessment Capability and reportable under 10CFR50.72(b)(3)(xiii). The NRC Resident Inspector was notified by the licensee.

  • * * UPDATE (Gordy Robinson verbal notification to Joe O'Hara at 0719 EST on 12/2/2005): * * *
As of 0530 EDT on 12/02/05, Unit 2 SPDS was restored to Operable status following replacement of the CPU Board for the Remote Data Concentrator (RDC).  NRC Resident was notified."  R1DO (Todd Jackson) notified.
Safety Parameter Display System