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 Issue dateTitleTopic
ML17317B2648 June 1979LER 79-019/01T-0 on 790519:cracks Found in 16-inch Feedwater Elbows Adjacent to Nozzle Welds Caused Buildup of Nonradioactive Water in Containment Sump.Caused Being Determined.Elbows in Generators Being ReplacedLiquid penetrant
ML17317B2758 June 1979LER 79-019/01X-1 on 790519:small Leaks Found in Feedwater Piping to Steam Generator.No Further Description
ML17317B32513 July 1979LER 79-034/03L-0 on 790613:several Valves Exhibited Excessive Leakage Causing as-found Leak Rate to Exceed Limit.Caused by Leakage from Check Valves.Check Valves Replaced
ML17317B33013 July 1979LER 79-020/03L-0 on 790615:several Valves Exhibited Excessive Leakage,Causing as-found Leak Rate to Exceed Limit.Major Source of Leak Attributed to Check Valves.Caused by Sand Deposits on Seating Surfaces & Pitted Seats
ML17317B34919 July 1979LER 79-021/03L-0 on 790622:starting Time Exceeded Tech Specs During Test on Hydrogen Skimmer Recirculation Fan.Design Change Installed 781118 After Repeated Occurences & 10 Tests Satisfactorily Performed
ML17317B37425 July 1979LER 79-022/03L-0 on 790706:bistable 2PB-934B Tripped at Value Exceeding Tech Spec Limit by 0.104 Psi During Surveillance Test on Containment Pressure Protection.Caused by Drifting of Bistable Trip Set Point.Bistable Replaced
ML17317B39827 July 1979LER 79-023/03L-0 on 790629:in Mode 4,during Startup from Cold Shutdown,East Engineered Safety Features Ventilation Sys Fire Protection Spray for Charcoal Filter Operated at 2,230.Caused by Grounded Manual Actuation StationFire Watch
ML17317B40731 July 1979LER 79-024/03L-0 on 790702:south Boric Acid Storage Tank & Boron Injection Tank Were Out of Spec While Unit Was in Hot Standby.Caused by Normal Fluctuation.Boric Acid Was Transferred to TankBoric Acid
ML17317B40831 July 1979LER 79-025/03L-0 on 790702:safety Valve Was Lifted on Steam Generator 3,which Brought Reactor to sub-critical Condition. Operation of Safety Valve Was within Allowed Setpoints.Gag Removed & High Power Trips Reset
ML17317B41231 July 1979LER 79-034/03L-0 on 790705:during Plant Tour,Two Ice Condenser Intermediate Deck Doors Were Found Frozen Shut. Cause Not Determined.No Further Action Planned.Formerly Numbered Incorrectly as LER 79-034/03L-0
ML17317B41331 July 1979LER 79-035/03L-0 on 790705:while Cleanup of Demineralized Water Sys Was in Process,Rcs Passed from Operational Mode 5 to Mode 4 & Isolation Valves Closed.Caused by Breakdown of Communication Between Cleanup Crew & Reactor Operator
ML17317B4308 August 1979LER 79-025/03L-0 on 790709:while Reviewing Axial Power Distribution Monitoring Sys Printouts,Discovered Two Occasions in Which Results of Only One Detector Scan Printed Out.Cause Under Investigation
ML17317B4338 August 1979LER 79-037/03L-0 on 790709:position of Certain Control Bank C Rods Exceeded 12-step Limit Imposed by Tech Specs. Caused by Drifting of Rod Signal Conditioning Module
ML17317B43431 July 1979LER 79-036/03L-0 on 790709:two Ice Condenser Intermediate Deck Doors Found Frozen Shut.Cause Not Determined.Ice Chipped Off & Doors Returned to Operable Status
ML17317B4708 August 1979LER 79-026/03L-0 on 790723:while Studying Computer Printout for Axial Power Distribution,Discovered One Detector Scan Printed Out.Problem Under Investigation.Operations Personnel Closely Monitoring Printouts
ML17317B47115 August 1979Updated LER 78-065/03X-1 on 781229:previous Rept of Inoperable Pressurizer Level Channel Is No Longer Considered RO Due to Recent Tech Spec Change Deleting All Pressurizer Low Level Operability Requirements
ML17317B47215 August 1979LER 79-027/03L-0 on 790723,previously Issued as LER 79-025/03L-0:while Reviewing Computer Printout,Discovered K 0900 Address Not Reset to 0 Prior Ro Scanning Core.Temporary Change Sheet Issued
ML17317B47315 August 1979Updated LER 79-022/03X-1 on 790323:to Prevent Recurrence of Nearly Simultaneous Bus Failures,Battery Equalizing Charge Has Been Reduced from 280 to 275 Volts.Addl Design Change Requested to Provide Overvoltage Alarm to Alert Operators
ML17317B47415 August 1979Updated LER 79-030/03X-1 on 790417:design Change Coupled W/Relay Degradation Caused Relay to React Slower During Sequence.Design Change RFC-DC-12-2384 Installed as Preventive Measure
ML17317B47515 August 1979Updated LER 79-039/03L-0 on 790720:control Sys Repaired to Deliver Larger Quantity of Acid to Rcs.No Further Action Planned
ML17317B49626 July 1979LER 79-040/03L-0 on 790726:during Moderator Coefficient Test,Reactor Power Decreased from 79% to 58% in 43 Minutes. Iodine Isotopic Analysis Not Performed in Required Time. Caused by Poor Communication Between Operator & Supervisor
ML17318A26013 September 1979LER 79-042/03L-0:on 790814,pressurizer Pressure Transmitters Isolated.Caused by Instrument Drift.Investigation in Progress.Transmitters Recalibr
ML17318A26113 September 1979LER 79-043/03L-0:on 790201,axial Power Distribution Monitoring Sys Detector Alarm Setpoint Was Set Nonconservatively.Setpoint Reset.Personnel Received Addl Training
ML17318A27518 September 1979LER 79-044/03L-0:on 790825,cable Penetration in Floor of Hot Shutdown Panel Found to Have Fire Barrier Seal Removed. Removed by Contractor for Design Change.Continuous Fire Watch StationedFire Barrier
Continuous fire watch
ML17318A3181 October 1979LER 79-045/03L-0:on 790831,ice Condenser Intermediate Deck Door Found Frozen Shut.Caused by Condensation as Result of Increased Influx of Humid Air.Ice Was Chipped Away & Door Freed
ML17318A41413 November 1979LER 79-002/03X-1:on 790127,injection of Boric Acid Caused Increase of Neutron Flux in Reactor Core.Axial Flux Difference Exceed Limits & Alarm Did Not Function Properly. Caused by Hardware FailureBoric Acid
ML17318A46428 November 1979LER 79-057/03L-0:on 791029,while Shifting to RHR,motor- Operated Containment Isolation Valve Failed to Open Completely & Would Not Close.Caused by Corrosion of Valve Operator Torque Switch Due to Condensation in Conduit
ML17318A46828 November 1979LER 79-039/03L-0:on 791031,containment Air Particulate Detector Tripped on Low Flow While Plant Was in Mode 6. Caused by Flow Trip Switch in Nonvertical Position.Proper Air Particulate Flow Established
ML17318A47126 November 1979LER 79-056/03L-0 on 791027,opening Torque on Two Ice Condenser Lower Inlet Doors Exceeded Max Tech Spec Limit. Caused by Door Springs Slightly Stiffer than Doors on Other Bays.Spring Tension Bolts Adjusted
ML17318A47628 November 1979LER 79-038/01T-0:on 791114,boron Injection Flow Path Was Inadvertantly Made Inoperable to Perform Surveillance Testing.Caused by Charging Line Being Out of Svc for Sys Mod.Fuel Element Altered
ML17318A57922 January 1980LER 79-054/03L-0:on 791226,during Surveillance Test on Automatic Load Sequence Timing Relays,Four Timers Found to Exceed Tolerance.Caused by Original Setpoint Valve Value Differing from Design Value.Test Procedure Modified
ML17318A64517 March 1980LER 80-010/03L-0:on 800216,during Surveillance Test,Suction Valve VMO-102 for Containment Equalization Fan HV-CEQ-2 Failed to Open,Making Air Recirculation Sys Inoperable. Caused by Maladjusted Torque Switch in Motor Operator
ML17318A7974 June 1980Updated LER 80-001/03X-1:on 800119,w/approx 10% Power Level, Steam Generators Fed Too Much Feedwater Flow Resulting in Temp & Pressure Drop.Caused by Attempt to Recover Low Steam Generator Level
ML17319A45619 June 1980LER 80-024/03L-0:on 800520,w/turbine Drive Auxiliary Feedwater Pump in Nonrunning Standby Position,Alarm Received That Pump Tripped.Probably Caused by Control Linkage Disconnecting from Throttle Valve
ML17319A46323 June 1980LER 80-010/03L-0:on 800522,during Ice Condenser Insp,Eight Intermediate Deck Doors Were Found Frozen & Considered Inoperable Per Tech Spec.Caused by Condensation on Top Deck Door Divider Beam.Design Change Requested
ML17319A46725 June 1980LER 80-011/03L-0:on 800531,w/unit in Shutdown Mode, Containment Atmosphere Air Particulate & Gaseous Radiation Monitoring Sys Pump Tripped on Low Flow.Caused by Inaccurate Flowmeter.Flowmeter Replaced
ML17319A51114 July 1980LER 80-027/03L-0:on 800613,during Piping Mod,Hand Shutoff Valve in Suction Line to Motor Driven Auxiliary Feed Pump 1 Was Closed to Stop Leakage Interfering W/Welding.Pump Was Inoperable Until Completion of Welding
ML17319A73526 February 1981Updated LER 80-024/03X-1:on 800520,alarm Indicated Auxiliary Feedwater Pump Tripped in Nonrunning Auto Standby Position. Caused by Turbine Control Linkage Unlatching from Trip & Throttle Valve,Possibly Due to Lumber on Trip Linkage
ML17319A76612 March 1981LER 81-002/03L-0:on 810215,west Motor Driven Auxiliary Feed Pump Was Removed from Svc to Repair Emergency Leakoff Line Check valve,FW-160.Caused by Dirt Causing Valve to Stick. Valve Cleaned
ML17319A77613 March 1981LER 81-003/03L-0:on 810212,during Normal Operations,Control Room Cable Vault Left Unattended W/No Fire Watch Posted While Access Door Was Sealed for Testing.Caused by Misunderstanding of Tech Spec 3.7.10.Personnel ReinstructedFire Watch
ML17319A78823 March 1981Updated LER 80-019/03X-1:on 800811,surveillance Requirement Tech Spec 4.8.1.1a Not Performed.Caused by Operator Error. Operator Reprimanded.Procedures Revised to Include Breaker Alignment & to Require Signoff on Completion
ML17319A79217 March 1981LER 81-003/03L-0:on 810217 & 0301,ESW Pump 2-E Found Inoperable.Caused by Closed Inlet & Outlet Slide Gate Valves to Strainers on Discharge of ESW Pumps Due to Defective Agastat Timer.Timer Replaced & Backwash Sys Cycled
ML17319A8001 April 1981LER 81-004/03L-0:on 810308,ISI Data Review for Ba Transfer Pump 3 Was Not Reviewed within 96-h Time Limit.Caused by Test Data Being Inadvertently Overlooked by Technical Inservice Insp Coordinator.Card File Developed
ML17319A8021 April 1981LER 80-029/03L-0:on 801217,during NRC Audit of Surveillance Records of Essential Svc Water Sys,Operations Dept Procedure 01-OHP 4030.STP.022,Revision 5,found Deficient in Meeting Tech Spec Requirements.Caused by Personnel Error
ML17319A82327 April 1981LER 81-008/03L-0:on 810407,during Fire Protection Spray Sys Surveillance Test,Eight Spray Nozzles for Engineered Safety Features Vent Charcoal Filter 2-HV-AES-1 & 14 Nozzles for 2-HV-AES-2 Were Found Partially Plugged.Sys Flushed
ML17319A82527 April 1981LER 81-009/03L-0:on 810408,during Fire Protection Spray Sys Surveillance Test,Eight Spray Nozzles for Engineered Safety Feature Charcoal Filter 1-HV-AES-1 Were Found Partially Plugged.Caused by Buildup of Debris in Nozzles.Sys Flushed
ML17319A82829 April 1981LER 81-009/03L-0:on 810331,after Entering Mode 6 & Floodup of Reactor Cavity,Routine Analysis of RCS Indicated Chloride Concentration of 0.26 Ppm.Cause Is Undetermined. Contamination Was Reduced by Purification
ML17319A8415 May 1981LER 81-010/03L-0:on 810411,snubbers 1 & 29 Were Found Inoperable.Caused by Fluid Leak on 29 Due to Separation of Joint at End Seal O-ring.O-ring Replaced.Snubber 1 Upside Down Due to Loose Extension Rod Locknut.Locknut Tightened
ML17319A8425 May 1981LER 81-011/03L-0:on 810411,steam Line Pressure Transmitter MPP-210 Was Found Exceeding Allowable Value for Differential Pressure Between Steam Lines.Caused by Instrument Drift. Transmitter Recalibr
ML17319A8435 May 1981LER 81-012/03L-0:on 810413,cracks Found in Divider Barrier Seal.Cause Unknown.Defective Portions Replaced