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 Entered dateSiteRegionReactor typeEvent description
ENS 399701 July 2003 05:04:00MonticelloNRC Region 3GE-3

On June 30, 2003 at approximately 1545 (CDT) it was identified that a High Energy Line Break (HELB) door separating Divisional Motor Control Centers was not latched as required. It was determined that this condition existed for a maximum of 15 minutes. This condition is being reported as an event or condition that could have prevented the fulfillment of a safety function in accordance with 10 CFR 50.72(b)(3)(v). The licensee notified the NRC Resident Inspector and the State Emergency Management Agency.

  • * *RETRACTION on 08/27/03 at 1215 EDT from R. Sand to John MacKinnon * * *

Because plant safety was not significantly degraded, this event is not reportable under the unanalyzed condition criteria based on: (1) the door in either event was in an uncontrolled condition for less than one minute, (2) the door was not materially affected, only operated improperly, (3) the PRA significance of the event was low, and (4) the HELB Barrier door was not open for a period than is allowed by station procedural guidance. R3DO (C. Miller) notified. The station continues to review the events in the station's corrective action program. The NRC Resident Inspector was notified of this retraction by the licensee.

ENS 4000822 July 2003 21:10:00MonticelloNRC Region 3GE-3

A High Energy Line Break (HELB) door was not latched as required. This condition is being reported as an event that could have prevented the fulfillment of a safety function in accordance with 10CFR50.72(b)(3)(v)(A). The door is currently closed. The HELB door which separates two critical Motor Control Center (MCC) areas was unlatched for less than two (2) minutes. The licensee will inform the state representative and has informed the NRC resident inspector.

  • * * RETRACTION on 08/27/03 at 1216 EDT by R. Sand to John MacKinnon * * *

Because plant safety was not significantly degraded, this event is not reportable under the unanalyzed condition criteria based on: (1) the door in either event was in an uncontrolled condition for less than one minute, (2) the door was not materially affected, only operated improperly, (3) the PRA significance of the event was low, and (4) the HELB Barrier door was not open for a period longer than is allowed by station procedural guidance. R3DO (C. Miller) notified. The station continues to review the event in the station's corrective action program. The NRC Resident Inspector was notified of this retraction by the licensee.

ENS 4011829 August 2003 21:08:00PilgrimNRC Region 1GE-3During performance of routine operability testing, the High Pressure Coolant Injection System (HPCI) tripped and restarted due to an as yet undetermined cause. The trip and restart sequence occurred twice in close succession approximately 20 minutes into a normal run before the operator took action to manually trip the turbine. Investigation into the cause of the malfunction is on-going. The HPCI system has been declared inoperable in accordance with Technical Specifications. The operability of all other Emergency Core Cooling System components has been verified. There was never any actual coolant injection by the HPCI system during this event. The NRC Resident Inspector has been notified by the licensee. The State of Massachusetts will also be notified.
ENS 401386 September 2003 22:11:00PilgrimNRC Region 1GE-3

While operating at 100% power, the plant sustained a loss of the 480 bus "B1". As a result of the loss of power, HPCI has been isolated due to the inability to auto isolate on a primary containment isolation signal. The SBGT was initiated to restore building ventilation. The Reactor Water Clean Up System was manually isolated due to the loss of power. The "A" recirculation pump tripped as a result of the loss of power. The loss of the 480V bus is being investigated at this time. The NRC Resident Inspector was notified.

          • UPDATE ON 9/6/03 AT 1805 FROM McDONNELL TO LAURA*****

Due to the loss of power to the RCIC quadrant coolers, the RCIC system is inoperable but available. The NRC Resident Inspector was notified.

ENS 4014610 September 2003 21:02:00MonticelloNRC Region 3GE-3

Potential break of Fire Water Main in Admin Bldg could cause both divisions of Safe Shutdown equipment to be inoperable by flooding the battery rooms for #11 & 12 125VDC Batteries. Vulnerable section of piping has been isolated to eliminate the flooding concern. Fire Protection compensatory actions have been established in accordance with the site Fire Protection Program. The licensee informed the NRC resident inspector.

  • * * RETRACTION FROM PFEFFER TO GOTT AT 1242 ON 11/7/03 * * *

Monticello is retracting the event reported based on evaluations which indicate that the fire main is not considered a potential flooding source. Additional evaluations are ongoing, and issues will be entered into the station's corrective action program. The licensee has notified the NRC Resident Inspector. Notified R3DO (Hills)

ENS 4020930 September 2003 23:11:00DresdenNRC Region 3GE-3Dresden Unit 2 automatically scrammed on low reactor vessel water level after "2C" reactor feed pump tripped (1 of 2 running). All systems responded as required (all rods fully inserted). Investigation into reactor feed pump trip cause has begun. The NRC Resident Inspector will be notified of this event by the licensee.
ENS 402111 October 2003 11:12:00PilgrimNRC Region 1GE-3At approximately 0430 on October 1, 2003 with the reactor Mode Switch in Refuel, reactor water level 210" above Top of Active Fuel, and reactor water temperature less than 110F, investigations and walkdowns were being performed to identify potential sources of drywell leakage. Drywell leakage was well within Technical Specification limits. During these walkdowns a small leak in a cap of a nozzle of the reactor pressure vessel boundary, nozzle N10, located at reactor vessel height 440" was identified. This location is 84" above Top of Active Fuel. This is a cut and capped 4" Control Rod Drive return line. The leak appears to be on the cap weld. This notification is being made per 10 CFR 50.72(b)3(ii)(A). All required ECCS systems are presently operable. Investigation is continuing. The (NRC) resident inspector has been notified.
ENS 402277 October 2003 06:20:00DresdenNRC Region 3GE-3The Unit 2 HPCI system has been declared INOPERABLE due to the failure of a pressure suppression pool high-level switch during surveillance and being unable to maintain the HPCI pump suction lined up to the pressure suppression pool in standby lineup. Per technical specification 3.3.5.1. required action D.2.2. with the high level switch INOPERABLE the HPCI system must have the pump suction aligned to the suppression pool with in 24 hours or declare the HPCI system INOPERABLE when the required action completion time can not be met. The function of the suppression pool high-level switch causes the HPCI pump suction to automatically realign to the suppression pool when the suppression pool reaches the high level set point during an accident. When the pump suction swap to the suppression pool was performed the HPCI gland seal leak off pump began to run automatically. Further investigation determined that there was an unknown input into the HPCI gland seal leak off condenser (GSLO). Normally the GSLO does not have an input while in standby lineup and therefore does not normally operate while the pump suction is aligned to the Pressure Suppression Pool. The GSLO pump would have a discharge flow path with the HPCI system running and therefore would have the ability to maintain its design function. However in the standby line (-up) with the pump suction aligned to the suppression pool the GSLO pump did not have a discharge flow path. This inability to pump the GSLO condenser required the suction be realigned to the condensate storage tank and with the combination of a failed suppression pool high-level switch requires declaration of INOPERABITY of the HPCI system. This is a 14 day LCO. This is a single train system and reportable under SAF 1.8 Event or Condition That Could Have Prevented Fulfillment of a Safety Function. The INOPERABLE HPCI system function can be manually initiated from the main control room. Investigation and troubleshooting into the unknown HPCI GSLO input has been, initiated in parallel with the repairs to the failed suppression high level switch. The licensee intended on notifying the NRC Resident Inspector.
ENS 4031110 November 2003 16:04:00DresdenNRC Region 3GE-3

On 11/10/2003 at 07:20 CST it was discovered, during a control room panel walk-down, that Dresden U2 had primary containment valves 2-1601-56 Torus Purge valve and 2-1601-21 DW (drywell) Purge valve open simultaneously. This valve alignment created a flow path from the Drywell to the Torus, effectively bypassing the pressure suppression function of the torus water volume during a LOCA (Loss of Coolant Accident) condition. This condition placed U2 containment in an unanalyzed condition, not capable of performing the intended design function, which is to mitigate the consequences of a LOCA. The proper valve alignment was restored at 07:26 CST which restored U2 primary containment to operable status per TS (Tech. Spec) 3.6.1.1. A review of plant data identified that this valve arrangement, which bypassed primary containment, had been in effect when U2 entered Mode 2 (Startup) from Mode 4 (Cold Shutdown) at 12:01 on Nov 9, 2003. In addition, this valve line-up existed for a duration greater than that allowed by TS 3.6.1.1 A.1 and B.1 (1 hour). The NRC Resident Inspector was notified of this event by the licensee.

        • Retraction on 12/31/03 at 1430 EST by J. Welch taken by MacKinnon ****

Dresden has performed an engineering evaluation that bounds the plant conditions that existed while the two valves were simultaneously open. The evaluation concluded that the valves would have automatically closed in sufficient time to prevent exceeding the design limits of the primary containment during a postulated Design Basis Accident. Therefore, Dresden retract the ENS call associated with this event. This event will be the subject of an Licensee Event Report in accordance with the requirements of 10 CFR 50.73(a)(2)(i)(B), 'Any event or condition which was prohibited by the plant's Technical Specifications.'" R3DO (Ken Riemer) notified. The NRC Resident Inspector was notified of the above retraction by the Licensee.

ENS 4038812 December 2003 01:25:00DresdenNRC Region 3GE-3Manual scram was inserted during a Stator Cooling Runback that was not expected. Cause of the Stator Cooling Runback is under investigation. Group 2 & 3 Primary Containment Isolation System (PCIS) isolations occurred as expected due to reactor level drop during the scram. All other systems operated as expected. All controls rods were fully inserted during the manual scram. The MSIVs are open with decay heat being removed via steam to the main condenser using the turbine bypass valves. The condensate and feedwater system is in operation maintaining reactor vessel water level. Current Reactor Pressure is 880 psig and Reactor Level +30 inches. The electrical plant lineup is stable and in a normal lineup for this condition. The manual scram of this unit had no affect on the other unit onsite which is in a refueling outage. The licensee has notified the NRC Resident Inspector.
ENS 4044814 January 2004 15:00:00PilgrimNRC Region 1GE-3

At 1049 EST on January 14, 2004 the Control Room was notified that 78% (87 out of 112) Emergency Sirens failed a 'Quiet Test.' The Quiet test is a status check between the Emergency Offsite Facility and each individual siren. Further investigation revealed that 53 sirens would not operate as required and 34 were experiencing some degree of degradation. Indications point toward amplifier problems within each affected siren. Efforts are ongoing to troubleshoot and repair the effected sirens. Contingency plans are in place for alternate notification. The resident inspector has been notified. This condition was discovered during routine monthly testing. The sirens were upgraded about a year ago using equipment supplied by Federal Signal.

* * * UPDATE ON 1/20/04 AT 1422 EST FROM RANDY HAISLET TO GERRY WAIG * * *

The following was received via facsimile: This is a follow up to event report 40448 concerning a loss of 53 sirens. As of this morning, 105 of the 112 sirens are considered operable. Six of the 7 inoperable sirens are due to rotational problems. The remaining siren is inoperable due to the impact of a vehicle on it's pole. Work is currently on going to restore these sirens. The siren failures reported in event report are believed to be the result of a manufacturing defect which resulted in temperature sensitivity. A temporary means of heating the subject equipment has been put in place. Investigation is continuing. Notified R1DO (Clifford Anderson)

ENS 4046823 January 2004 13:53:00DresdenNRC Region 3GE-3

Dresden Unit 2 is performing a Technical Specification required shutdown due to the loss of the (120 VAC) Essential Service Bus normal electrical feed. This is reportable per 10CFR 50.72(b)(2)(i), SAF 1.2 "Plant Shutdown Required by Technical Specification". The loss of the feed occurred at 02:10 (CST) on 01/23/04 and power swapped to the backup feed. Technical Specification 3.8.7. A. was entered and repairs began on the uninterruptible power supply. Repairs were unsuccessful and Unit 2 shut down began at 12:20 (CST) with unit required to be hot shutdown by 22:10 (CST) 01/23/04 and cold shutdown by 22:10 (CST) 01/24/04. Repairs will continue in parallel will unit shutdown. The licensee notified the NRC Resident Inspector.

      • UPDATE on 01/23/04 at 1742 EST by G. Morrow taken by John MacKinnon****

Unit 2 ESS BUS normal feed was restored to OPERABLE, unit shutdown was secured and preparations for load increase are in progress. Preliminary troubleshooting data taken on the ESS UPS show the most likely cause of the UPS power supply transfer was a static switch component that caused the UPS to swap to the emergency supply. The troubleshooting shows the malfunction that caused the initial power supply transfer to the ESS Emergency supply via the ABT at 0210 this morning originated in the static switch circuitry. The static switch is bypassed in the current configuration and therefore the power supply to the ESS bus is assured. The voltage sensing relays investigated during the troubleshooting on the output of the inverter show no indication that an inverter failure initiated the bus transfer. Operations will continue to monitor the output of the inverter. Troubleshooting of the UPS static switch will continue to determine the cause of the malfunction. R3DO (Roger Lanksbury) notified NRC Resident Inspector was notified of this update by the licensee.

ENS 4047424 January 2004 03:22:00DresdenNRC Region 3GE-3At 0322 EST on 01/24/03, Licensee reported that at 0037 CST on 01/24/03, the Unit 3 reactor auto scrammed from 96% power due to an auto main turbine trip while performing weekly main turbine testing. All control rods inserted completely. Steam is being dumped to the main condenser. PCIS Group 2 (Containment Ventilation System) and Group 3 (Shutdown Cooling System) isolated as expected due to reactor vessel level decrease following the scram. Reactor vessel level is being maintained at normal level (30 inches) with the reactor feedwater system. Reactor pressure is 900 psig and moderator temperature is 530 degrees F. All systems functioned as expected. Unit 3 is in Condition 3 (Hot Shutdown). The cause of the main turbine trip is under investigation. This event had no effect on Unit 2. The licensee notified the NRC Resident Inspector.
ENS 4048126 January 2004 20:20:00MonticelloNRC Region 3GE-3

V-ERF-11 ('A' Emergency Filtration Train (EFT) recirculation fan) was found to have an improper alteration affecting the fan's shaft speed, and 'A' EFT was declared inoperable. Concurrently, the #12 Emergency Diesel Generator (EDG) was inoperable for planned maintenance, making 'B' EFT inoperable. This condition is a loss of safety function during a design basis accident, and impacts the ability of the plant to mitigate the consequences of an accident. The licensee notified the NRC Resident Inspector.

  • * * UPDATE ON 1/26/04 AT 2112 EST FROM RASK TO GOTT * * *

At 1958 CST the licensee declared the #12 EDG operable and thus the #12 ("B") EFT was also operable. Additionally, at 2010 the licensee declared the #11 ("A") EFT operable. Notified R3DO (Burgess).

  • * * RETRACTION AT 1043 ON 3/23/04 BLAKESLEY TO GOTT * * *

Based on further investigation V-ERF-11 ('A' Emergency Filtration Train (EFT) recirculation fan) would have been able to provide the required flow and would have fulfilled its required safety functions with the improper alterations. Therefore the event was not reportable. Notified R3DO ( O'Brien).

ENS 4049130 January 2004 14:35:00DresdenNRC Region 3GE-3Unit 3 experienced an automatic reactor scram due to a main turbine trip. The main turbine tripped due to low oil pressure, the cause of which is under investigation. Primary Containment Isolation System Group 2 and 3 isolations occurred as expected due to the reactor water level decrease following the scram. After reactor water level was restored to normal (+30 inches), level continued to increase to the reactor feed pump high level trip setpoint. Reactor level was subsequently restored to normal and the reactor feed pumps were restarted and are currently supplying the reactor. Decay heat is being removed by the main steam system via auxiliary loads. All other systems responded as expected. Current reactor pressure is 850 psi, and level is stable at 30 inches. The NRC Senior Resident Inspector is in the control room.
ENS 404941 February 2004 09:54:00DresdenNRC Region 3GE-3During the Unit 3 scram on 01/30/04 the response of the feedwater level control system caused the RPV (Reactor Pressure Vessel) level to increase higher than expected. RPV level rose above the HPCI steam line. Calculations showed approximately 60 gallons of water entered the steam line. This response could adversely affect the HPCI system should the same type of event occur and FWLC (Feedwater Level Control) respond the same way on Unit 2. Based on this information and no reasonable assurance that the same response will not occur, the Unit 2 HPCI system is conservatively being declared inoperable. HPCI remains available. Entering Tech Spec 3.5.1 Required Action F.1 (Isolation Condenser is OPERABLE) and F.2 (Restore HPCI to Operable status within 14 days). A modification is being prepared to change the response of FWLC to preclude this adverse response during a transient. The NRC Resident Inspector will be notified.
ENS 4051813 February 2004 11:49:00MonticelloNRC Region 3GE-3At 0730, Monticello Nuclear Generating Plant became aware of the loss of incoming phone call capability. Investigation determined loss of ENS, HPN (FTS) lines were inoperable as well as the State of MN dedicated line. Commercial incoming calls (inoperable) out calls were operable. By 0930 CST all phone system were restored and determined operable. NRC Operations Center was notified of inoperable ENS phone via backup commercial line. NRC Resident Inspector was notified of this by the licensee.
ENS 4054726 February 2004 08:38:00PilgrimNRC Region 1GE-3The High Pressure Coolant Injection (HPCI) system had been removed from service to perform planned maintenance and testing. During post-maintenance testing, the HPCI gland seal condensate pump tripped due to a blown control power fuse. The maintenance scope did not include the pump or its power supply. The fuse was replaced and the surveillance completed satisfactorily. Investigation into the cause of the failure is ongoing. HPCI remains inoperable in support of additional pre-planned testing. The licensee notified the State and the NRC Resident Inspector.
ENS 4058511 March 2004 21:22:00MonticelloNRC Region 3GE-3Monticello Nuclear Generating plant is making a voluntary report with regard to the Technical Support Center (TSC) not meeting design criteria Subsection 8.2-1.f of Supplement 1 to NUREG-0737. This specifies that the TSC will be provided with radiological protection necessary to assure that the radiation exposure to any person working in the TSC would not exceed 5 REM whole body (or its equivalent part of the body) for the duration of the accident. During review of the calculations associated with an on-going Alternative Source Term project, plant staff identified the potential for a radiation shine path to exist from the reactor building to the TSC during a DBA (Design Basis Accident) - Loss of Coolant Accident (LOCA), that could result in radiation levels reaching a point dictating evacuation of the TSC under existing emergency plan procedures. As required by NUREG-0696 and confirmed by the plant staff, existing procedural guidance directs personnel to evacuate to the back-up TSC (located in the EOF) if the TSC cannot be occupied continuously. The NRC resident has been informed of this discovery.' The licensee is continuing their assessment and will determine the appropriate corrective actions.
ENS 4062530 March 2004 10:40:00Quad CitiesNRC Region 3GE-3At 0740 hours (CST) during testing of the turbine thrust bearing wear detector, a main turbine trip occurred. This resulted in an automatic reactor scram due to turbine stop valve closure. Following the scram all Group II (Primary Containment) and Group III (Reactor Water Cleanup) isolations occurred as expected. All essential equipment functioned as required. Unit 2 remains in Mode 3 with reactor water level in the normal level band. An investigation into the Unit 2 turbine trip is in progress. Unit 1 was unaffected by the event and remains at 85% power. All control rods fully inserted. Decay heat is being removed via steam to the main condenser using the bypass valves. The Licensee notified the NRC Resident inspector.
ENS 4067113 April 2004 00:46:00DresdenNRC Region 3GE-3High Pressure Coolant Injection System Incapable of Performing its intended Safety Function. This report is being made in accordance with 10 CFR 50.72(b)(3)(v) due the High Pressure Coolant Injection System being incapable of performing its intended safety function. At 1810 hours (CDT) during performance of the functional test of the level instrumentation for the automatic realignment of the High Pressure Coolant Injection system (HPCI) suction sources, plant maintenance person identified that logic circuitry leads had been lifted. The leads not being connected would prevent the automatic realignment of the HPCI suction from its non-safety related source, the Condensate Storage Tank (CST), to its safety related source, the Suppression Pool. Based on preliminary information, the leads were lifted during scheduled maintenance activities on the HPCI system in March. The applicable Technical Specification specified that HPCI be declared inoperable within an hour. Actions were immediately taken to restore the automatic function. The leads were re-landed and the TS condition exited at 1853 hours. The inability of the system to automatically realign due to a CST low level or a Suppression Pool high level is considered to be a condition that would prevent the fulfillment of the safety function of the HPCI system. The licensee is still investigating the cause. The NRC Resident Inspector was notified.
ENS 4070224 April 2004 09:00:00DresdenNRC Region 3GE-3This report is being made in accordance with 10 CFR 50.72 (b)(2)(iv)(B) . On 04/24/2004 at 06:03 (CDT), Dresden Unit 2 experienced an automatic Scram from 20% Reactor power due to Main Steam Isolation Valve closure, cause is under investigation. There were no Electromatic Relief or Safety Relief Valve actuations and the Isolation Condenser was initiated manually for pressure control. There were no ECCS initiations. PCIS Group 2 and Group 3 Isolations occurred as expected due to normal reactor water level decrease following the scram. All other systems responded as expected. All control rods fully inserted on the automatic scram. The electric plant is in a normal lineup and being supplied from offsite power. The licensee notified the NRC Resident Inspector.
ENS 4070324 April 2004 15:30:00DresdenNRC Region 3GE-3

This report is being made in accordance with 10 CFR 50.72(b)(3)(v)(B). On 04/24/2004 at 06:03 (CDT), Dresden Unit 2 was using the Isolation Condenser to control reactor pressure following a Unit Scram. The isolation condenser operated properly until 10:50 (CDT) when the Isolation Condenser 2-1301-3 valve could not be opened to the full open position. ISO Condenser was declared INOPERABLE and Technical Specification Limiting Condition of Operation 3.5.3. Condition 'A' was ENTERED. High Pressure Coolant Injection has been administratively verified OPERABLE. Reactor Pressure is being maintained 550-1000 psig and being maintained with Reactor Water Clean Up Flow and Gland Seal System. Investigation into the cause of the valve failure is in-progress. Unit 2 had been operating approximately 30 days prior to the scram reported previously in EN #40702. The licensee informed the NRC Resident Inspector.

  • * * RETRACTION ON 6/23/04 AT 2036 EDT FROM GLEN MORROW TO ARLON COSTA * * *

On April 24, 2004, Dresden made an ENS call due to the failure of Isolation Condenser valve 2-1301-3 to fully open and the subsequent determination that the Isolation Condenser was inoperable. The ENS call was made based on the decision that this was required by 10CFR50.72(b)(3)(v)(B), 'Any event or condition that at the time of discovery could have prevented fulfillment of the safety function of structures or systems that are needed to remove residual heat.' Isolation Condenser System operation is not credited in Dresden's accident analyses. Transients and Events treated as transients are listed under section 15.0.2.1 of the UFSAR. Accidents are described and analyzed under section 15.0.2.2 of the UFSAR. The isolation condenser is not credited for fulfilling safety function of removal of residual heat of any accident as described in section 15.0.2.2, Accidents. In accordance with the guidance contained in NUREG 1022, 'Event Reporting Guidelines 10CFR50.72 and 10CFR50.73,' Section 3.2.7, 'Event or Condition That Could Have Prevented Fulfillment of a Safety Function,' a functional failure of the Isolation Condenser System is not reportable under 10CFR50.72(b)(3)(v)(B). Therefore, Dresden is retracting this ENS call. This Isolation Condenser System event will be described in a Licensee Event Report in accordance with 10CFR50.73(a)(2)(i)(B), 'Any event or condition which was prohibited by the plant's Technical Specifications' The licensee notified the NRC Resident Inspector. Notified R3DO (Kozak).

ENS 4071228 April 2004 18:50:00DresdenNRC Region 3GE-3During routine alignment of the Control Room HVAC system it was determined the 2/3-5741-053B damper failed to close as required. The damper is required to close to isolate outside air to the control room for accident conditions. Because of the damper failure the Control Room Emergency Ventilation System (CREVS) was declared inoperable at 1209 on 4/28/04. The CREVS is a single train system utilized to mitigate the consequences of an accident and this event is reportable under 10 CFR 50.72(b)(3)(v)(D). (Exelon Reportability Manual Section - SAF 1.8) The licensee notified the NRC Resident Inspector.
ENS 4071328 April 2004 18:50:00DresdenNRC Region 3GE-3On 4/28/04 at 1536 (CDT), Dresden Unit 2 experienced a trip of the 2A Recirc MG set and associated recirc pump. This placed the unit in the immediate scram region of the power to flow map. The Unit NSO manually scrammed the reactor in accordance with the immediate operator actions of DOA 202.01. Troubleshooting is in progress to determine the cause of the 2A Recirc MG set trip. There were no Electromatic Relief or Safety Relief Valve actuations. There were no ECCS initiations. PCIS Group 2 and Group 3 Isolations occurred as expected due to normal reactor water level decrease following the scram. All systems responded as expected following the reactor scram. This report is being made in accordance with 10 CFR 50.72 (b)(2)(iv)(B) for an actuation of the RPS and 10 CFR 50.72(b)(3)(iv)(A) for Group 2 and 3 actuations. All control rods fully inserted, the electrical grid is stable, ECCS and the EDGs remain operable. The licensee notified the NRC Resident Inspector.
ENS 407275 May 2004 15:29:00DresdenNRC Region 3GE-3

Unit 3 scrammed as a result of a loss of offsite power. An unusual event was declared and the state was notified at 1352 (EST). A Group I, II, and III (isolation) was received. The Isolation Condenser was manually initiated for reactor pressure control. HPCI (High Pressure Coolant Injection) was manually initiated to control reactor water level. All systems operated as expected. The Unit 3 and 2/3 emergency diesel generators automatically started and closed on to their respective busses. The reason for the loss of offsite power is not know at this time. Switchyard work was in progress at the time of the event. All control rods fully inserted into the core during the reactor scram. The licensee notified the NRC Resident Inspector.

  • * * UPDATE ON 05/05/04 AT 1746 FROM D. GRONEK TO W. GOTT * * *

At 1601 Dresden Station Unit 3 terminated from an Unusual Event for a loss of offsite power. Bus 8 in the 345 KV switchyard was restored from circuit breaker 4-8. Transformer 32 was energized and supplied to Bus 33 and 33-1. Bus 34 remains energized from the Unit 3 SBO diesel generator. Bus 34-1 remains powered from the Unit 3 emergency diesel generator. Actions are being taken to restore those busses to the normal offsite power source. Plant cooldown is in progress and the unit is proceeding to Mode 4. Reactor water level is being maintained by HPCI and reactor pressure is being controlled with HPCI and the Isolation Condenser. LPCI is running in the torus cooling mode of operation. The LCO action requirement for secondary containment inoperability was exited at 1630. The licensee notified the State and the NRC Resident Inspector. Notified DHS (McIntire), FEMA (M. Eaches), DIRO (Nieh), R3DO (Lipa) and NRR EO (Lyons).

ENS 407358 May 2004 07:07:00DresdenNRC Region 3GE-3While performing a unit start-up, SRM 24 was declared inoperable due to erratic indications. SRM 22 was already inoperable which resulted in falling below the Technical Specification 3.3.1.2 mode 2 requirement of 3 operable SRMs. The cause of the erratic indications on SRM 24 is unknown at this time. All control rods were fully inserted at 0527 CDT. The license plans to go to a cold shutdown condition to investigate the erratic source range monitor. The NRC Resident Inspector was notified of this event by the licensee.
ENS 4074613 May 2004 22:12:00DresdenNRC Region 3GE-3At 1915 CST, Dresden personnel identified that the ENS phone was not operational, either with outgoing or incoming calls. The NRC Ops Center was contacted via the normal commercial phone system and informed of the situation. Call back from the NRC via the commercial phone line failed as Dresden is currently not receiving outside phone calls due to the failure. A call back method through BPO (Bulk Power Operations) has been established. The phone problem appears to be not at the Dresden Site, SBC (local phone provider) is initiating repairs. Current off-site communications are being augmented via personal cellular telephones. The licensee notified the NRC Resident Inspector.
ENS 4084428 June 2004 03:07:00DresdenNRC Region 3GE-3

The Station declared an Unusual Event (at 01:30 CDT) due to a felt earthquake and confirmation from other sites. The site seismic recorder did not register an event. No damage has been noted at this time. Inspections will continue. The licensee notified the NRC Resident Inspector and State authorities. NOTE: See related EN#40845 and EN#40846.

  • * * UPDATE ON 06/28/04 @ 0726 BY RILEY RUFFIN TO C GOULD * * *

Plant walk downs were performed and no damage was observed during the walk downs. The UE was terminated at 0555 CDT. The licensee notified the NRC Resident Inspector, the State and local authorities. Notified by e-mail: Susan Frant (IRO), Thomas Kozak (R3 DO), Frank Gillespie (NRR EO), Pat Hiland (Reg3), and Geoffrey Grant (R3). Also notified FEMA (Erwin Casto) and DHS (Andy Akers).

ENS 4084628 June 2004 03:19:00Quad CitiesNRC Region 3GE-3

On June 28, 2004 at 0147 CDT, the Control Room was notified that an earthquake was felt on site by Security Personnel. Both units 1 & 2 remain on line and stable with no abnormalities and no physical or structural damage identified. The Plant seismograph DID NOT trigger. An unusual event was declared at 0151 CDT. The licensee notified the NRC Resident Inspector, State and local authorities. NOTE: See related EN#40844 and EN#40845.

  • * * UPDATE ON 6/28/04 0436 EDT FROM RON RUSTIK TO ARLON COSTA * * *

On June 28, 2004 at 0318 CDT, the Unusual Event has been terminated. A complete tour of all plant vital and protected areas was performed with no physical or structural damage verified. Security performed an inspection of outside areas of plant property and noted nothing unusual. The licensee notified the NRC Resident Inspector, State and local authorities. Notified by e-mail: Susan Frant (IRO), Thomas Kozak (R3 DO), Frank Gillespie (NRR EO), Pat Hiland (Reg3), and Geoffrey Grant (R3). Also notified FEMA (Erwin Casto) and DHS (Andy Akers).

ENS 4088119 July 2004 21:27:00DresdenNRC Region 3GE-3On 7/18/04 at 02:15, Dresden personnel were informed that a pontoon boat in the Kankakee River was near the Dresden Station intake log boom, outside the owner controlled area, and that two individuals had fallen off the boat. Immediate rescue efforts by local law enforcement and rescue agencies rescued one individual, and the second individual was not found. At 04:46, rescue efforts were halted due to excessive fog in the area. On 7/19/04 at 18:04, the dead body of the second individual was discovered surfaced in the middle of the Kankakee River. The dead body subsequently went under the surface and was drawn into the Dresden owned intake log boom. The body was removed from the owner controlled area by Coal City rescue, the Grundy County Sheriff, Grundy County Coroner, and Dresden Station security. The individual was deceased prior to entering the owner controlled area and did not drown on-site. This report is being made in accordance with 10CFR50.72(b)(2)(xi) because of the other government notifications made and potential media involvement. The NRC Resident has been informed.
ENS 4088621 July 2004 11:11:00MonticelloNRC Region 3GE-3Both control room ventilation systems were inoperable due to a seal failure on the in service control room ventilation unit. A 24 hour Limiting Condition of Operation (LCO) was entered at 0512 CDT. (V-EAC-14A) "A" CRV tripped and "B" CRV was isolated for planned maintenance. "B" CRV (V-EAC-14B) was unisolated and restored to service at 0545 CDT (33 minutes later) and the 24 hour LCO exited at 0600 CDT. The plant remains in a 30 day LCO for one train of the CRV being inoperable. Control room temperatures increased slightly during CRV inoperability and are within normal operating band at this time (Temp increased 5 degrees F). State and Local were notified of this by the licensee. The NRC Resident Inspector was notified of this event by the licensee.
ENS 4090930 July 2004 12:51:00PilgrimNRC Region 1GE-3The following information was obtained from the licensee via facsimile: During a surveillance of the Reactor Core Isolation Cooling system (RCIC), the RCIC turbine failed to achieve design pressure and flow. Other safety systems, including the High Pressure Coolant Injection (HPCI) system, are available. This failure is believed to be due to a RCIC flow controller problem. Investigation is continuing. Design pressure/flow is 1250 psig/400 gpm. Actual pressure/flow was 1220 psig/350 gpm. The licensee has notified the NRC Resident Inspector.
ENS 4091231 July 2004 01:28:00Quad CitiesNRC Region 3GE-3On July 30, 2004 at approximately 2125 hours CDT, Instrument Maintenance personnel were performing the Unit One Reactor Low Pressure (RHR/LPCI) Calibration and Functional Test. At this time, the technicians determined that two out of the four "Reactor Steam Dome Pressure - Low" switches in LPCI loop select logic were out of tolerance high. These switches delay completion of the LPCI loop select logic during Single Loop Reactor Recirculation Pump operations (SLO) until the reactor pressure is less than 900 psig. With these switches out of tolerance high, LPCI loop select logic sensitivity was degraded, increasing the potential to select the wrong loop for injection during periods of SLO. At the time of discovery, both Reactor Recirculation pumps were in operation. Both switches were recalibrated immediately upon discovery to within Technical Specification tolerances. The NRC Resident Inspector was notified of this event by the licensee.
ENS 409244 August 2004 16:57:00MonticelloNRC Region 3GE-3A licensed employee was determined to be under the influence of alcohol during a for cause test. The employee's access to the plant has been terminated. Contact the Headquarters Operations Officer for additional details. The licensee notified the NRC Resident Inspector.
ENS 410051 September 2004 17:12:00MonticelloNRC Region 3GE-3Unanalyzed condition due to missing fire barrier and inadequate separation involving power supply cables for RHR and Core Spray pumps. During a review of the site Appendix R program, NMC Engineering personnel discovered that the credited Monticello Division I RHR Pump and Core Spray Pump power cables pass through a Division II fire area. A fire in this room could potentially damage both divisions of post-fire safe shutdown equipment. This condition is reportable under 10CFR50.72(b)(3)(ii)(B) as an unanalyzed condition that significantly degrades plant safety due to the lack of required separation of post-fire safe shutdown trains. As a compensatory action an hourly fire watch has been established in accordance with the Monticello Fire Protection Program. The licensee informed the NRC Resident Inspector. The licensee is continuing their evaluation to determine the extent of the condition.
ENS 411068 October 2004 22:58:00Quad CitiesNRC Region 3GE-3At 2120 (hrs. CDT) on October 8, 2004, while performing the 'Control Room Emergency Ventilation System Test,' which verifies the integrity of the control room envelope, it was determined that the positive pressure requirement of greater than or equal to 0.125 inches water gauge for the control room envelope in Technical Specification Surveillance Requirement 3.7.4.4 could not be met for all specified test points. As a result, Control Room Emergency Ventilation System was declared inoperable and Technical Specification 3.7.4, Condition A was entered. Recently completed surveillance testing has demonstrated that a positive pressure ranging from 0.056 to 0.301 inches water gauge is being maintained in the control room envelope; therefore it is expected that the safety function is being met. However, this notification is being made in accordance with 10 CFR 50.72(b)(3)(v)(D) because the Control Room Emergency Ventilation System is a single train safety system and the Technical Specification requirement is not met. The affect of the failure to meet the Technical Specification requirements on the ability to perform the safety function is continuing to be evaluated. The licensee notified the NRC resident inspector.
ENS 4113919 October 2004 23:37:00Quad CitiesNRC Region 3GE-3

On October 19, 2004 at approximately 1830 hours CDT, Unit One was performing QCOS 2300-05, Quarterly HPCI Pump Operability Test. This was being performed to prove operability following maintenance work on various valves and the turning motor gear unit. At this time when the HPCI turbine was rolled, the HPCI Signal Converter Trouble alarm was received. The HPCI Flow Controller demand controlled at approximately 7250 gpm instead of controlling at the desired 5600 gpm. HPCI was determined not to be operable and was shutdown per procedure. Due to the unexpected behavior of the HPCI Flow Controller, at this time it is not certain if the HPCI will meet its safety function. Therefore, we are reporting this event under 10 CFR 50.72 (b)(3)(v). Licensee entered Tech Spec 3.5.1.(f) 14 day Limiting Condition of Operation (LCO) for HPCI. Reactor Core Isolation Cooling (RICI) is operable. All other Emergency Core Cooling Systems (ECCS) and the Emergency Diesel Generators (EDG) are fully operable if needed. The NRC Resident Inspector was notified of this event by the licensee.

  • * * RETRACTION J. DAVIS TO W. GOTT AT 1819 ON 10/28/04 * * *

The purpose of this report is to retract the ENS report made on October 19, 2004 at 2237 CDT (ENS #41139). The initial report was made following HPCI operability testing in accordance with QCOS 2300-05, Quarterly HPCI Pump Operability Test. When the HPCI turbine was rolled, the HPCI Signal Converter Trouble alarm was received. The HPCI Flow Controller failed to control at the desired 5600 gpm (instead, the system ramped to 7250 gpm). Due to the unexpected behavior, it was not certain at the time if HPCI could have met its design basis requirements. However, a subsequent review of this event has determined that HPCI would have performed its safety function. The Signal Converter failed in a manner that prevented automatic flow control, but did not prevent HPCI from initiating and ramping to full flow (i.e., the turbine high speed stop). In this condition, HPCI would have met corresponding Technical Specifications and Accident Analysis requirements. The circuit board was replaced and the Signal Converter and flow controller feedback loop were re-calibrated. The Unit 1 HPCI turbine's automatic flow control was successfully tested on October 20, 2004. The Licensee notified the NRC Resident Inspector. Notified R3DO (R. Garner)

ENS 4122525 November 2004 16:50:00Quad CitiesNRC Region 3GE-3

On November 25, as of 1545 hours, the Station's Plant Process Computer (PPC) had been in a failed state for greater than eight hours. Previous to this, at 0745 hours, the PPC experienced an unexpected hardware failure. This computer feeds the Safety Parameter Display System (SPDS) for both Units. This failure is considered a major loss of emergency assessment capability. Troubleshooting and repairs are in progress. This failure affects the transmission of ERDS data and applicable emergency response personnel have been notified of the change in their reporting status if an emergency event is declared due to the loss of ERDS. The licensee notified the NRC Resident Inspector.

  • * * UPDATE PROVIDED BY DARIN TO JEFF ROTTON AT 1205 EST ON 11/26/04 * * *

At 1040 CST on 11/26/04, Information Technology personnel restored the Station's PPC to the point where the SPDS and ERDS are both fully functional for both units. The licensee notified the NRC Resident Inspector.

ENS 4126715 December 2004 14:00:00MonticelloNRC Region 3GE-3The oil plug on the HPCI booster pump bearing was discovered to be loose at approximately 2100 (CST) on 12/14/2004. Upon discovery, the plug was re-tightened. The plug may or may not have fallen out had the HPCI system initiated. HPCI is operable, but subsequent evaluation has determined this to be reportable because, at the time of discovery, HPCI operation could not be assured. Event investigation is on-going. The licensee will notify the NRC Resident Inspector.
ENS 413693 February 2005 23:48:00Quad CitiesNRC Region 3GE-3The licensee provided the following report via facsimile: On February 3, 2005 at 1819 hours, Quad Cities Nuclear Power Station (QCNPS) confirmed a vulnerability with a 4160 VAC relaying and metering current transformer (CT) associated with the Unit and Reserve Auxiliary Transformers (i.e., the UAT and RAT) on both Unit 1 and Unit 2. Although the CT is currently fully operable, failure of the CT circuitry could cause the neutral overcurrent relay to trip and lockout the circuit breakers supplying feeds to safety related buses 13 (23) and 14 (24), isolating them from their normal and emergency power sources. Emergency power (i.e., the emergency diesel generator) would still be available to supply power to safety related buses 13-1 (23-1) and 14-1 (24-1), but the Residual Heat Removal Service Water (RHRSW) system may be without a source of power. If this failure occurred during a LOCA, then the RHRSW pumps may not be started within the ten minute requirement. A modification is in progress to eliminate this vulnerability. This event is being reported as a potential loss of safety function (10CFR50.72(b)(3)(v)(B)) and as a degraded or unanalyzed condition (10CFR50.72(b)(3)(ii)(B)). The NRC Resident Inspector has been notified. See similar events #41362 (Crystal River), #41366 (LaSalle), and #41370 (Dresden).
ENS 413704 February 2005 00:23:00DresdenNRC Region 3GE-3The licensee provided the following report via facsimile: On February 3, 2005 at 1915 hours, DNPS confirmed a vulnerability with a 4160 VAC relaying and metering current transformer (CT) associated with the Unit and Reserve Auxiliary Transformers (i.e., the UAT and RAT) on both Units. Although the CT is currently fully operable, failure of the CT circuitry will cause the neutral overcurrent relay to trip (and lockout) the main, reserve and tie feed breakers. These combined protective relay trips will act to trip and lock out the circuit breakers supplying feeds to buses 23 (33) and 24 (34), essentially isolating them from their normal and emergency power sources. Emergency power (i.e., the emergency diesel generator) would still be available to safety related buses 23-1 (33-1) and 24-1 (34-1), but the Containment Cooling Service Water (CCSW) system would remain without a power source. If this failure occurred during a LOCA, then the CCSW pumps may not be able to be started within ten minutes. A modification is in progress to eliminate this vulnerability. This event is being reported as a potential loss of safety function (10CFR50.72(b)(3)(v)(B)) and a degraded or unanalyzed condition (10CFR50.72(b)(3)(ii)(B)). The NRC Resident Inspector has been notified. See similar events #41362 (Crystal River), #41366 (LaSalle), and #41369 (Quad Cities).
ENS 413744 February 2005 17:25:00MonticelloNRC Region 3GE-3The following information was obtained from the licensee via facsimile: On February 4, 2005, at 1337 hours, Monticello Nuclear Generating Plant discovered a potential vulnerability with 4160 VAC current sensing and protective relaying circuitry that could result in bus lockouts of both safeguards buses (#15 and #16) if a specific equipment fault were to occur. The 1AR Auxiliary Reserve Transformer source to each of the safeguards buses have current transformers used for over-current protective relaying that have common connections to facilitate a single watt-hour meter. The lack of neutral over-current trip relaying limits the event vulnerability to a case (most likely fire) of an outside voltage source contacting one or more CT phase legs that forces current through the over-current trip relays. If this forced current is of sufficient magnitude through both division over-current relays, both safeguards buses will receive lockout signals. This would make both safeguards buses unavailable. Since the 1AR transformer is not required at this time, it has been isolated from the safeguards buses, and their associated over-current relaying isolated to preclude occurrence of this event. This event is being reported as a potential loss of safety function (10CFR50.72(b)(3)(v)(A, B, C, and D)) and as a degraded or unanalyzed condition (10CFR50.72(b)(3)(ii)(B)), The NRC Resident Inspector has been notified. See similar events #41362 (Crystal River), #41366 (LaSalle) #41369 (Quad Cities) and #41370 (Dresden).
ENS 4140813 February 2005 22:16:00PilgrimNRC Region 1GE-3The following text report was received from the licensee via facsimile: The High Pressure Coolant Injection (HPCI) system was declared inoperable on 2-13-05 at 19:00 EST due to loss of position indication to MO-2301-8 (HPCI injection valve #2) in the control room and at the system alternate shutdown panel. The other ECCS (Emergency Core Cooling) Systems remain operable. Position indication was restored after control power fuses were replaced. HPCI was returned to operable status at 21:50 EST, 2-13-05. The licensee has notified the NRC Resident Inspector and will be notifying Massachusetts Emergency Management Agency.
ENS 4143623 February 2005 19:20:00MonticelloNRC Region 3GE-3

The licensee provided via facsimile the following report:

During an extent of condition review of the corrective actions associated (with) Event Notification #41374, the Monticello Nuclear Generating Plant (MNGP) engineering staff made the following discovery.  On February 22, 2005 at 12:00 hours, MNGP discovered a potential vulnerability with Alternate Shutdown System (ASDS) isolation design which could result in Bus 16 being locked out in the event of a Control Room or Cable Spreading Room fire.  The Monticello Appendix R Safe Shutdown Analysis for Control Room/Cable Spreading Room fire assumes a loss of control of Division I and II equipment from the Control Room, however, safe shutdown is achieved remotely from the ASDS panel.  ASDS design is such that a Control Room/Cable Spreading Room fire would not impede the ability to safely shutdown and maintain the plant in a shutdown condition.  

Contrary to the ASDS design, it was discovered that an un-isolated metering circuit from the 1AR transformer could result in Bus 16 being locked out in the event of a Control Room or Cable Spreading Room fire. The bus lockout relay from the 1AR transformer is not isolated by the ASDS transfer switches, therefore, this condition could result in failure of Bus 16 to re-energize during the implementation of the Shutdown Outside Control Room procedure. Since the Bus 16 feeder breaker from the 1AR transformer is not required at this time, it has been isolated from the safeguards bus to preclude occurrences of this event. The event is being reported as a potential loss of safety function (10CFR50.72(b)(v)(A,B and D) and as a degraded or unanalyzed condition (10CFR50.72(b)(3)(ii)(B)). The licensee informed NRC Resident Inspector.

ENS 4144124 February 2005 22:39:00MonticelloNRC Region 3GE-3A trip of the "A" RPS M-G set resulted in an "A" Group 2 isolation and startup of the standby gas treatment system. There was a preliminary report of a possible fire/smoke smell in the vicinity of the M-G set. However, when an operator reported to the location there was no observed fire. The fire brigade was also dispatched but found no fire or smoke in the M-G set area. The licensee is preparing to place the RPS on its alternate power supply. This will allow the Group 2 isolations and standby gas treatment system actions to be reset. The cause of the M-G set trip is still under investigation. The licensee will be notifying the NRC Resident Inspector as well as state and local authorities.
ENS 414688 March 2005 11:41:00MonticelloNRC Region 3GE-3The following information was provided by the licensee (licensee text in quotes) During isolation of the 'A' Safety Relief Valve, the 12 Residual Heat Removal (RHR) Pump tripped while in service for shutdown cooling. The isolation and shutdown cooling were subsequently restored such that shutdown cooling was lost for approximately 13 minutes. Several Control Room alarms were received at approximately 0454 (CST) while the isolation was being hung. The Control Room Supervisor investigated the alarms and the Reactor Operator identified that the 12 RHR Pump had tripped. The isolation was lifted and shutdown cooling was restored at approximately 0507 (CST). Operators observed that reactor water temperature and level remained stable at 99 degrees F and 651 inches (above the bottom of the vessel), respectively, during the event. The isolation being hung apparently caused a loss of position indication for the RHR pump inlet valve. With no position indication, the pump logic sensed a loss of suction flow path, which caused the RHR pump to trip. The event is under investigation. The NRC resident has been notified.
ENS 4151724 March 2005 07:59:00DresdenNRC Region 3GE-3The licensee provided the following information via email (licensee text in quotes): On 3/24/05 at approximately 0529 Unit 2 received a Group 1 isolation on main steam line high flow. All Group 1 valves closed as required and the reactor scrammed. The Isolation Condenser was manually initiated to control reactor pressure. Group 2 and 3 Containment Isolations occurred as expected. Investigation as to the cause of the Group 1 isolation is in progress. All systems responded as required with no abnormalities noted. The licensee also indicated that a Main Turbine Generator EHC transient occurred at the time of the isolation. All control rods fully inserted, the electrical grid is stable, and decay heat is being removed via the Isolation Condenser System. The licensee notified the NRC Resident Inspector.
ENS 4152424 March 2005 17:50:00Quad CitiesNRC Region 3GE-3

The following information was obtained from the licensee via facsimile (licensee text in quotes): Minimum Switchyard Voltage Requirements Not Met On March 24, 2005, at 0930 hours, Quad Cities was notified that the switchyard voltage was below that required to ensure that offsite power would remain available following a design basis accident. Both sources of off-site power were declared inoperable. The appropriate Technical Specification required actions were taken for both units. The ability of the Emergency Diesel Generators to perform their design function is not affected by this condition. This event is being reported in accordance with 10 CFR 50.72(b)(3)(v)(D) as a condition that could have prevented the fulfillment of a safety function given the predicted post-LOCA switchyard voltage. A preliminary engineering assessment indicates that one source of offsite power was available. Additional confirmatory reviews are being performed to determine if the safety function was preserved. At this time, grid/switchyard voltage has been restored. Minimum switchyard voltage required is 348.4 KV. The analyzed minimum voltage which prompted notification to the NRC was 347.5 KV. Switchyard voltage at the time of this report was ~359 KV. The licensee has notified the NRC Resident Inspector.

  • * * RETRACTION FROM C. STEFFES TO M. RIPLEY 1556 EDT 04/13/05 * * *

The purpose of this report is to retract the following ENS reports: 1) ENS # 41524 on March 24, 2005; 2) ENS # 41562 on April 4, 2005; and 3) ENS # 41587 on April 11, 2005. These reports were made following notification to Quad Cities that the switchyard voltage was below the required value necessary to ensure that offsite power would remain available following a design basis accident. For each event, both sources of offsite power were declared inoperable, the appropriate Technical Specification required actions were taken for both units, and an ENS notification was made for a condition that could have prevented fulfillment of a safety function. The events occurred when Unit 1 was in a refueling outage and Unit 2 was operating at 85% power. Subsequent Engineering analysis has determined that with a unit shutdown, and the large 4 Kv loads on that unit not running, the required minimum post-accident switchyard voltage is reduced to 339.3 kV (for the shutdown unit). Given the new minimum post-accident switchyard voltage, it was confirmed that there was a source of off-site power available to the Station. Specifically for all three events, the projected post-accident switchyard voltage (which ranged between 343 kV to 347.5 kV) was higher than the required minimum post-accident switchyard voltage (339.3 kV) for the shutdown unit. As a result, there was no condition present that could have prevented fulfillment of a safety function, and thus these events are not reportable. The licensee notified the NRC Resident Inspector. Notified R3 DO (J. Madera)

ENS 4153128 March 2005 01:12:00Quad CitiesNRC Region 3GE-3

The following information was obtained from the licensee via facsimile (licensee text in quotes): At 1930, Unit 1 experienced a loss of 480 VAC busses 18 and 19. This caused a loss of power to the Control Room Emergency Ventilation System (CREVS) and the CREVS Air Conditioning System (CREVS AC). This event also caused a loss of power to the U1 equipment that was supporting the Alternate Decay Heat Removal (ADHR) mode of operation. Power was restored to Bus 19 at 2001 and Bus 18 at 2013. The restoration of Bus 18 also restored power to CREVS and CREVS AC. All systems supporting ADHR were restored by 2015. At the time of the occurrence, the estimated time to boil without decay heat removal capability was 571 minutes. All isolations and actuations occurred as expected. The cause of the bus trips is being investigated. This Event is being reported under 50.72 (b)(3)(v)(B) and 50.72 (b)(3)(v)(D). The licensee stated at the time of the event, Busses 18 and 19 were cross-tied and the feeder breaker to Bus 18 tripped open. The breaker was changed out and power to Busses 18 and 19 restored. The cause of the Bus 18 feeder breaker trip has not yet been determined. The licensee has notified the NRC Resident Inspector.

  • * * UPDATE FROM THE LICENSEE (OSELAND) TO NRC (HUFFMAN) AT 0312 EST ON 3/28/05 * * *

The licensee stated that the Alternate Decay Heat Removal pumps from Unit 2 remained in service so that all decay heat removal was not lost. The Unit 1 primary coolant system temperature increase during the 45 minute duration of this event was approximately 1 degree. R3DO (Kozak) has been notified.