05000327/LER-1980-007-01, Engineering Found That Incorrect Valve Operator Weights Were Used for Seismic Analysis of Component Cooling Water Sys Valves.Caused by Incorrect Weights Shown on Drawings

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Engineering Found That Incorrect Valve Operator Weights Were Used for Seismic Analysis of Component Cooling Water Sys Valves.Caused by Incorrect Weights Shown on Drawings
ML19340B253
Person / Time
Site: Sequoyah 
Issue date: 10/14/1980
From: Cottle W, Kirk G
TENNESSEE VALLEY AUTHORITY
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19340B248 List:
References
LER-80-007-01X, LER-80-7-1X, NUDOCS 8010210703
Download: ML19340B253 (2)


LER-1980-007, Engineering Found That Incorrect Valve Operator Weights Were Used for Seismic Analysis of Component Cooling Water Sys Valves.Caused by Incorrect Weights Shown on Drawings
Event date:
Report date:
3271980007R01 - NRC Website

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.I o i:l l With Unit 1 in Mode 6 following initial core loading, notification was received ggl from TVA Division of Engineering Design that incorrect (non-conservative) valve 1o,A t{ operator weights were used in the seismic analysis for component cooling water [ol3; j valves FCV-70-133,'134, and 183 (T.S.6.9.1.12.h).

There was no effect upon public jc sjl health or safety. Previous occurrences - none.

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Tennessee Valley Authority Sequoyah Nuclear Plant LER SUPPLEMENTAL INFORMATION UPDATED REPORT - PREVIOUS REPORT DAT; 3-28-80 SQRO-50-327/80007 Rev. 2 Technical Specification Involved 6.9.1.12.h Reported Under Technical Specification 6.9.1.12.h Date of Occurrence:

3/15/80 Time of Occurrence: 0900 EST Unit 1 Identification and Description of Occurrence:

Notification was received frem TVA Division of Engineering Design that

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incorrect (non-conservative) valve operator weights were used in the seismic analysis for component cooling water valves FCV-70-133,134, and 183.

Conditions Prior to Occurrence:

Unit 1 in Mode 6 following init'ial core loading.

Action specified in the Technical Specification Surveillance Requirements =et h

due to inocerable eaufreent. Describe.

j ii/A fpparent Cause of Occurrence:

Iacorrect valve operator weight used in seismic analysis due to error on vax e vendor drawings.

Analysis of Occurrence:

There was no effect upon public health or safety.

Corrective Astion:

The seismic ana.ysis was rerun using the correct valve op-rator weights.

No physical changes were required.

Failure Data:

N/A