ML20054K479

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Application to Amend License DPR-62,revising Tech Specs Re MAPLHGR Penalty Which Is 8.5% Reduction in MAPLHGR Values.Info Supersedes Values Submitted 820520.Criticality Presently Scheduled for 820710
ML20054K479
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 06/28/1982
From: Howe P
CAROLINA POWER & LIGHT CO.
To: Vassallo D
Office of Nuclear Reactor Regulation
Shared Package
ML20054K480 List:
References
NUDOCS 8207020239
Download: ML20054K479 (2)


Text

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GP&L Carohna Power A L.tght Company JUN ts 1982 Office of Nuclear Reactor Regulation ATTN: Mr. D. B. Vassallo, Chief Operating Reactors Branch No. 2 United States Nuclear Regulatory Commission Washington, D.C. 20555 BRUNSWICK STEA'i ELECTRIC PLANT, UNIT NO. 2 DOCKET No. 50-324 LICENSE NO. DPR-62 FUEL CYCLE No. 5 - RELOAD LICENSING SUPPLEMENTAL INFORMATION

Dear Mr. Vassallo:

Summary:

In accordance with the Code of Federal Regulations, Title 10, Parts 50.90 and 2.101, Carolina Power & Light Company (CP&L) hereby requests revisions to the Technical Specifications (TS) for the Brunswick Staan Electric Plant (BSEP) Unit No. 2. The attached changes supersede comparable TS pages requested by our letter dated May 20, 1982.

Discussion:

Subsequent to the aforementioned submittal, core spray sparger inspections were conducted. As discussed in our June 14-15, 1982 meeting with NRC staff members, a Maximum Average Planar Linear lleat Generation Rate (MAPLilGR) reduction would be imposed in accordance with the Emergency Core Cooling System (ECCS) information presented in the meeting. The enclosed TS changes, as requested by the NRC, reflect the imposed MAPLHGR penalty which is a uniform 8.5 percent reduction in MAPLilGR values f rom those submitted in our May 20, 1982 request. In the near future, CP&L will be forwarding the ECCS and structural analyses to support information provided to the Staff in the June 14-15, 1982 necting. At a later date, CP&L plans to provide a revised

" rapid" REFLOOD aaalysis which, upon NRC approval, should eliminate the MAPLHGR penalty.

Brunswick Unit No. 2 criticality is presently scheduled for July 10, 1982. We request the Staff review be conducted to support issuance of the TS revisions to allow return to power in accordance with this schedule. We will keep your staff apprised of any changes to the schedule.

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Administrative In our May 20, 1982 submittal, CP&L remitted a $4,000 check as payment of the Class III amendment foe; therefore, additional fees are not required with this subnittal.

Should you require additional information, please contact our staf f.

Yours very truly, O . usW P. W. Howe Vice President Technical Services MSG /mf (097C3T1) cc: Messrs. J. P. O'Reilly (NRC-RII)

J. A. Van Vliet (NRC)

P. W. Howe, having been first duly sworn, did depose and say that the information contained herein is true and correct to his own personal knowledge or based upon information and belief.

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