ML20084G878: Difference between revisions

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=Text=
=Text=
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    ,*f                                   (',\                               p V               p==%             Q ll dfi Jersey Central Powerr* &, Light Cornpany M AolSoN AVENUE AT PUNCH BOWL Ro AD e MoRRISToWN   N.J. 07960 e 539-6118 December 14, 1971                   c.A
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                                                                                /                   4 l                                                                             ./         ('     ~
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J.il     -    3 Dr. Peter A. Morris, Director                     G-                         ~~
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l                         Division of Reactor Licensing                     2     DEC171971" S United States Atomic Energy Cornmission             '
p==%
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ll dfi Jersey Central Power &, Light Cornpany r*
l Washington D. C. 20545             .
M AolSoN AVENUE AT PUNCH BOWL Ro AD e MoRRISToWN N.J. 07960 e 539-6118 December 14, 1971 c.A 4
                                                                          . 6                g                  -
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J.il 3
Dr. Peter A. Morris, Director G-l Division of Reactor Licensing 2
DEC171971"
~~
l United States Atomic Energy Cornmission ts, mWit D'EMI S
6 g
l Washington D. C. 20545 s tacts 8 g


==Dear Dr. Morris:==
==Dear Dr. Morris:==
O                   /
O
/
M*
M*
l                            
l


==Subject:==
==Subject:==
Oyster Creek Station Docket No. 50-219 l                                         Failure of Main Steam Isolation Valve NSO3B i                                         to Fully Close l                                                                                                                   'i l                                     The purpose of this letter is to provide you with an interim l                         report regarding the failure of Main Steam Isolation Valve NSO3B to fully j                         close during a surveillance test to measure valve closure time.
Oyster Creek Station Docket No. 50-219 l
I As a result of the manual reactor scram of November 16, 1971, j
Failure of Main Steam Isolation Valve NSO3B i
the main steam line pressure dropped below 850 psig. This event                 -
to Fully Close l
precipitated the automatic closure of the four main steam isolation valves, all of which operated successfully. While performing the I
'i l
The purpose of this letter is to provide you with an interim l
report regarding the failure of Main Steam Isolation Valve NSO3B to fully j
close during a surveillance test to measure valve closure time.
I j
As a result of the manual reactor scram of November 16, 1971, the main steam line pressure dropped below 850 psig. This event precipitated the automatic closure of the four main steam isolation valves, all of which operated successfully. While performing the I
required timing test of the main steam isolation valves before reactor startup, it was observed that the closed indication for inside valve
required timing test of the main steam isolation valves before reactor startup, it was observed that the closed indication for inside valve
_ NSo3B_ failed to_in(tiate. An immediate investigation was begun t6"
_ NSo3B_ failed to_in(tiate. An immediate investigation was begun t6"
                                                                                            ~
~
determine the cause.
determine the cause.
After concluding that the indicator circuit logic was not the cause of the failure, the drywell was deinerted and a physical inspection was made of the operation of valve NS03B.         It was               I fobservedthatthevalveoperatorlackedapproximately1-1/2 inches
After concluding that the indicator circuit logic was not the cause of the failure, the drywell was deinerted and a physical I
[ of travel to accomplish full valve closure. The coupling between-                   A the valve and the operator was then broken and the valve stem dropped the required 1-1/2 inches to achieve full closure, thus i                         locating the problem in the valve operating mechanism.
inspection was made of the operation of valve NS03B.
The dashpot section of the valve operator' was dismantled, and it was found that a cast iron cushion spud had been crushed with
It was fobservedthatthevalveoperatorlackedapproximately1-1/2 inches
                '        the pieces becoming wedged betwssii~tliEb'ottom of 'the dashpot piston
[ of travel to accomplish full valve closure. The coupling between-A the valve and the operator was then broken and the valve stem dropped the required 1-1/2 inches to achieve full closure, thus i
, h                       and the base _of the cylinder. At this time an investigation was made l g, , d' ((,,  O of the remainifig ' components of the operator for possible damage and none was found.
locating the problem in the valve operating mechanism.
The dashpot section of the valve operator' was dismantled, and it was found that a cast iron cushion spud had been crushed with the pieces becoming wedged betwssii~tliEb'ottom of 'the dashpot piston l g,, ' O
, h d ((,,
and the base _of the cylinder. At this time an investigation was made of the remainifig ' components of the operator for possible damage and none was found.
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  'Q t, - }') p b                   The cause of the valve failure is attributed to the spud
k[.
'Q t, - }') p b The cause of the valve failure is attributed to the spud
,Ip fragments becoming vedged between the dashpot and the cylinder bottom.
; h IsI j
; h IsI j
            ,Ip          fragments becoming vedged between the dashpot and the cylinder bottom.
The forces which led to the spud failure appear to be the result of a j',
The forces which led to the spud failure appear to be the result of a k[. j',
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5 . .
5 Dr. Peter A. Morris Page II 7
Dr. Peter A. Morris Page II                                                                           7 December 14, 1971                                                           gofc ,
December 14, 1971 gofc,
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* shock wave applied to the valve plug when it was opened during preparation for reactor startup. This shock wave was produced by not equalizing the pressure across the inside valve before opening it. The shock wave was transmitted to the cast iron cushion spud by the valve stem causing it to fail in compression.
shock wave applied to the valve plug when it was opened during preparation for reactor startup. This shock wave was produced by not equalizing the pressure across the inside valve before opening it.
The shock wave was transmitted to the cast iron cushion spud by the valve stem causing it to fail in compression.
It is suspected that this failure was the result of a single impact shock rather than many small shocks.
It is suspected that this failure was the result of a single impact shock rather than many small shocks.
The remaining three is,olation valves were inspected for
The remaining three is,olation valves were inspected for failed cushion spuds.
* failed cushion spuds. It was found that valve NS03A, also an inside valve, had a cushion spud failure, but it did not hamper the valves closing ability. New cushion spuds were fabricated and installed in valves NS03B and NS03A. The repaired valves were exercised, timed, and proven to operate satisfactorily.
It was found that valve NS03A, also an inside valve, had a cushion spud failure, but it did not hamper the valves closing ability. New cushion spuds were fabricated and installed in valves NS03B and NS03A. The repaired valves were exercised, timed, and proven to operate satisfactorily.
Pieces of the cushion spud are being sent to Hydro-Line )
Pieces of the cushion spud are being sent to Hydro-Line )
Manufacturing Company for more comprehensive analysis as a means
Manufacturing Company for more comprehensive analysis as a means to confirm the cause of its failure.
                                  ~
Based upon this analysis,
to confirm the cause of its failure. Based upon this analysis, the remedial actions described above vill be reevaluated if necessary.
~
the remedial actions described above vill be reevaluated if necessary.
In addition to this, the cushion spuds on all four valve dashpots vill be reexamined at the next refueling outage in April 1972 or at an earlier dat,e if plant conditions become amenable to such an inspection. Further, proper valve operating procedures have been reviewed with all operating personnel.
In addition to this, the cushion spuds on all four valve dashpots vill be reexamined at the next refueling outage in April 1972 or at an earlier dat,e if plant conditions become amenable to such an inspection. Further, proper valve operating procedures have been reviewed with all operating personnel.
We vill advise you of the final results of our evaluation as soon as they are available.
We vill advise you of the final results of our evaluation as soon as they are available.
Twenty-five copies of this letter are enclosed.
Twenty-five copies of this letter are enclosed.
Very truly yours,
Very truly yours,
                                        /d         '
/d Ivan R. Fin ock, Jr.
Ivan R. Fin ock, Jr.
Manager, Nuclear Generating Stations IRF/pk cc: Mr. J. P. O'Reilly, Director Division of Compliance, Region I
Manager, Nuclear Generating Stations IRF/pk cc: Mr. J. P. O'Reilly, Director Division of Compliance, Region I
                -'                        '  ~                           -
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Latest revision as of 04:35, 14 December 2024

Ro:On 711116,MSIV NS03B Failed to Fully Close During Surveillance Test to Measure Valve Closure Time.Cause Attributed to Spud Fragments Becoming Wedged Between Dashpot & Cylinder Bottom
ML20084G878
Person / Time
Site: Oyster Creek
Issue date: 12/14/1971
From: Finfrock I
JERSEY CENTRAL POWER & LIGHT CO.
To: Morris P
US ATOMIC ENERGY COMMISSION (AEC)
Shared Package
ML20084G880 List:
References
NUDOCS 8304270064
Download: ML20084G878 (2)


Text

c,

',*f

(',\\

pQ V

p==%

ll dfi Jersey Central Power &, Light Cornpany r*

M AolSoN AVENUE AT PUNCH BOWL Ro AD e MoRRISToWN N.J. 07960 e 539-6118 December 14, 1971 c.A 4

/

l

./

('

~

J.il 3

Dr. Peter A. Morris, Director G-l Division of Reactor Licensing 2

DEC171971"

~~

l United States Atomic Energy Cornmission ts, mWit D'EMI S

6 g

l Washington D. C. 20545 s tacts 8 g

Dear Dr. Morris:

O

/

M*

l

Subject:

Oyster Creek Station Docket No. 50-219 l

Failure of Main Steam Isolation Valve NSO3B i

to Fully Close l

'i l

The purpose of this letter is to provide you with an interim l

report regarding the failure of Main Steam Isolation Valve NSO3B to fully j

close during a surveillance test to measure valve closure time.

I j

As a result of the manual reactor scram of November 16, 1971, the main steam line pressure dropped below 850 psig. This event precipitated the automatic closure of the four main steam isolation valves, all of which operated successfully. While performing the I

required timing test of the main steam isolation valves before reactor startup, it was observed that the closed indication for inside valve

_ NSo3B_ failed to_in(tiate. An immediate investigation was begun t6"

~

determine the cause.

After concluding that the indicator circuit logic was not the cause of the failure, the drywell was deinerted and a physical I

inspection was made of the operation of valve NS03B.

It was fobservedthatthevalveoperatorlackedapproximately1-1/2 inches

[ of travel to accomplish full valve closure. The coupling between-A the valve and the operator was then broken and the valve stem dropped the required 1-1/2 inches to achieve full closure, thus i

locating the problem in the valve operating mechanism.

The dashpot section of the valve operator' was dismantled, and it was found that a cast iron cushion spud had been crushed with the pieces becoming wedged betwssii~tliEb'ottom of 'the dashpot piston l g,, ' O

, h d ((,,

and the base _of the cylinder. At this time an investigation was made of the remainifig ' components of the operator for possible damage and none was found.

dR - 0?!

k[.

'Q t, - }') p b The cause of the valve failure is attributed to the spud

,Ip fragments becoming vedged between the dashpot and the cylinder bottom.

h IsI j

The forces which led to the spud failure appear to be the result of a j',

f JV) ' lIII f

- )e 5455 83042{006471121405000219 g

l DR A OCg PDR

}

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5 Dr. Peter A. Morris Page II 7

December 14, 1971 gofc,

el' V

shock wave applied to the valve plug when it was opened during preparation for reactor startup. This shock wave was produced by not equalizing the pressure across the inside valve before opening it.

The shock wave was transmitted to the cast iron cushion spud by the valve stem causing it to fail in compression.

It is suspected that this failure was the result of a single impact shock rather than many small shocks.

The remaining three is,olation valves were inspected for failed cushion spuds.

It was found that valve NS03A, also an inside valve, had a cushion spud failure, but it did not hamper the valves closing ability. New cushion spuds were fabricated and installed in valves NS03B and NS03A. The repaired valves were exercised, timed, and proven to operate satisfactorily.

Pieces of the cushion spud are being sent to Hydro-Line )

Manufacturing Company for more comprehensive analysis as a means to confirm the cause of its failure.

Based upon this analysis,

~

the remedial actions described above vill be reevaluated if necessary.

In addition to this, the cushion spuds on all four valve dashpots vill be reexamined at the next refueling outage in April 1972 or at an earlier dat,e if plant conditions become amenable to such an inspection. Further, proper valve operating procedures have been reviewed with all operating personnel.

We vill advise you of the final results of our evaluation as soon as they are available.

Twenty-five copies of this letter are enclosed.

Very truly yours,

/d Ivan R. Fin ock, Jr.

Manager, Nuclear Generating Stations IRF/pk cc: Mr. J. P. O'Reilly, Director Division of Compliance, Region I

~

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_ _ _