ENS 43132: Difference between revisions
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| event date = 01/29/2007 23:10 EST | | event date = 01/29/2007 23:10 EST | ||
| last update date = 02/01/2007 | | last update date = 02/01/2007 | ||
| title = Automatic Reactor Scram | | title = Automatic Reactor Scram on Low Reactor Pressure Vessel (Rpv) Water Level | ||
| event text = On 1/29/07 with Hope Creek reactor startup in progress, in mode 1 at 22% Reactor power, Secondary Condensate Pump Minimum Flow Control Valves began to cycle. Reactor water level reached 39" (RPV level 7) and then lowered to 30" (RPV level 4). Manual control of the Reactor Feed pumps was taken, however, RPV water level continued to lower to 15" (Reactor scram on RPV water level is 12.5") at which time the reactor mode switch was locked in shutdown. There were no ECCS injections and all ECCS systems are operable. Initial review of the event indicates that all systems operated as expected with the exception of the Secondary Condensate pump minimum flow valves and the 'A' IRM failed to insert. Current plant conditions as of 1/30/07 at 0010 are: Hope Creek is in mode 3 at 565 psig. The Main Steam Line Isolation valves are open. 'B' and 'C' Primary Condensate Pumps, 'B' and 'C' Secondary Condensate Pumps, and 'A' Rx Feed Pump are feeding the vessel. All control rods have fully inserted on the scram and Main Turbine Bypass valves are removing decay heat. | | event text = On 1/29/07 with Hope Creek reactor startup in progress, in mode 1 at 22% Reactor power, Secondary Condensate Pump Minimum Flow Control Valves began to cycle. Reactor water level reached 39" (RPV level 7) and then lowered to 30" (RPV level 4). Manual control of the Reactor Feed pumps was taken, however, RPV water level continued to lower to 15" (Reactor scram on RPV water level is 12.5") at which time the reactor mode switch was locked in shutdown. There were no ECCS injections and all ECCS systems are operable. Initial review of the event indicates that all systems operated as expected with the exception of the Secondary Condensate pump minimum flow valves and the 'A' IRM failed to insert. Current plant conditions as of 1/30/07 at 0010 are: Hope Creek is in mode 3 at 565 psig. The Main Steam Line Isolation valves are open. 'B' and 'C' Primary Condensate Pumps, 'B' and 'C' Secondary Condensate Pumps, and 'A' Rx Feed Pump are feeding the vessel. All control rods have fully inserted on the scram and Main Turbine Bypass valves are removing decay heat. | ||
The licensee will inform the LAC (Lower Alloways Creek Township) and has informed the NRC Resident Inspector. | The licensee will inform the LAC (Lower Alloways Creek Township) and has informed the NRC Resident Inspector. |
Latest revision as of 22:17, 1 March 2018
Where | |
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Hope Creek New Jersey (NRC Region 1) | |
Reporting | |
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation | |
Time - Person (Reporting Time:+-3.35 h-0.14 days <br />-0.0199 weeks <br />-0.00459 months <br />) | |
Opened: | Bernie Litkett 00:49 Jan 30, 2007 |
NRC Officer: | Steve Sandin |
Last Updated: | Feb 1, 2007 |
43132 - NRC Website
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