ENS 43949: Difference between revisions

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| event date = 02/01/2008 04:45 EST
| event date = 02/01/2008 04:45 EST
| last update date = 02/01/2008
| last update date = 02/01/2008
| title = Automatic Scram As A Result Of Turbine Trip
| title = Automatic Scram as a Result of Turbine Trip
| event text = Unit 2 automatically scrammed [at] 0445 as a result of an RPS actuation due to a turbine trip.  All rods inserted.  The plant is stable.  No ECCS or SRV actuation occurred.  This report is made pursuant to 50.72(B)(iv)(B).  An investigation into the cause is currently in progress.  
| event text = Unit 2 automatically scrammed [at] 0445 as a result of an RPS actuation due to a turbine trip.  All rods inserted.  The plant is stable.  No ECCS or SRV actuation occurred.  This report is made pursuant to 50.72(B)(iv)(B).  An investigation into the cause is currently in progress.  
Primary plant pressure is 900 psig. with the decay heat path to the condenser via turbine bypass valves.  All safety related systems are operable, and the licensee is investigating a potential issue with the EHC system.   
Primary plant pressure is 900 psig. with the decay heat path to the condenser via turbine bypass valves.  All safety related systems are operable, and the licensee is investigating a potential issue with the EHC system.   

Latest revision as of 22:15, 1 March 2018

ENS 43949 +/-
Where
Limerick Constellation icon.png
Pennsylvania (NRC Region 1)
Reporting
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation
Time - Person (Reporting Time:+-4 h-0.167 days <br />-0.0238 weeks <br />-0.00548 months <br />)
Opened: Mark Crim
05:45 Feb 1, 2008
NRC Officer: Joe O'Hara
Last Updated: Feb 1, 2008
43949 - NRC Website
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