ENS 46641
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ENS Event | |
---|---|
14:10 Feb 25, 2011 | |
Title | Manual Scram Due to Recirculation Pump Trip |
Event Description | Limerick Unit 2 was manually scrammed from 100% power on 2/25/11 at 0910 EST in accordance with plant procedure OT-112 'Recirculation Pump Trip', when both the '2A' and '2B' recirculation pumps tripped. Preliminary indication of why the recirculation pumps tripped is due to main generator stator water coolant runback. The cause of the stator water coolant runback is currently under investigation at this time.
All control rods inserted as required. No ECCS or RCIC initiations occurred. No primary or secondary containment isolations occurred. The plant is currently in HOT SHUTDOWN maintaining normal Reactor Water Level with Feedwater in service. Primary plant pressure and temperature is 600 psia and approximately 485 degrees F. All unit safety related equipment is operable and available, if needed. The decay heat path is via turbine bypass valves. There is no affect on Unit 1. The licensee informed Montgomery, Chester, Burks Counties and the Pennsylvania Emergency Management Agency (PEMA). The licensee intends to issue a press release. The NRC Resident Inspector has been notified. |
Where | |
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Limerick Pennsylvania (NRC Region 1) | |
Reporting | |
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation | |
LER: | 05000353/LER-2011-002 |
Time - Person (Reporting Time:+-2.37 h-0.0988 days <br />-0.0141 weeks <br />-0.00325 months <br />) | |
Opened: | John Weissinger 11:48 Feb 25, 2011 |
NRC Officer: | Joe O'Hara |
Last Updated: | Feb 25, 2011 |
46641 - NRC Website
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Unit 2 | |
---|---|
Reactor critical | Critical |
Scram | Yes, Manual Scram |
Before | Power Operation (100 %) |
After | Hot Shutdown (0 %) |
WEEKMONTHYEARENS 549962020-11-13T07:45:00013 November 2020 07:45:00
[Table view]10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Scram Due to High Reactor Pressure Signal ENS 540982019-06-04T05:45:0004 June 2019 05:45:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Scram During Rapid Plant Shutdown ENS 519682016-06-01T13:00:0001 June 2016 13:00:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Scram Due to Unexpected Core Flow Change ENS 516142015-12-19T12:02:00019 December 2015 12:02:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Scram Due to Low Reactor Water Level ENS 508472015-02-24T02:40:00024 February 2015 02:40:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Scram on Reactor High Pressure Signal ENS 498712014-03-05T04:34:0005 March 2014 04:34:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Unit 1 Manually Scrammed During a Rapid Shutdown in Response to a Turbine Ehc Failure ENS 481172012-07-18T12:15:00018 July 2012 12:15:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration Unusual Event Declared Due to Flashover in the Load Center Transformer Cabinet ENS 478502012-04-19T11:53:00019 April 2012 11:53:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(xiii), Loss of Emergency Preparedness Manual Reactor Scram Following Loss of Recirculation Pumps ENS 469192011-06-03T14:21:0003 June 2011 14:21:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Scram Following a Turbine Trip ENS 469032011-05-29T09:02:00029 May 2011 09:02:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Trip Due to Low Pressure in Ehc System ENS 466412011-02-25T14:10:00025 February 2011 14:10:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Scram Due to Recirculation Pump Trip ENS 460422010-06-24T00:51:00024 June 2010 00:51:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Scram Following Loss of Both Recirculation Pumps ENS 440882008-03-22T23:39:00022 March 2008 23:39:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Turbine Trip Resulting in a Reactor Scram ENS 439492008-02-01T09:45:0001 February 2008 09:45:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Scram as a Result of Turbine Trip ENS 433152007-04-24T06:10:00024 April 2007 06:10:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge Automatic Reactor Scram with Eccs Injection on Lowering Reactor Vessel Water Level ENS 420542005-10-13T02:24:00013 October 2005 02:24:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Scram Due to Reactor High Pressure Signal ENS 418482005-07-18T13:52:00018 July 2005 13:52:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Scram ENS 408322004-06-22T17:13:00022 June 2004 17:13:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Scram Following an Electrical Yard Manipulation 2020-11-13T07:45:00 | |
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