ENS 45265: Difference between revisions

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| event date = 08/15/2009 16:06 CDT
| event date = 08/15/2009 16:06 CDT
| last update date = 08/15/2009
| last update date = 08/15/2009
| title = Automatic Reactor Scram Due To A Turbine Trip
| title = Automatic Reactor Scram Due to a Turbine Trip
| event text = At 1606 CDT on August 15, 2009, LaSalle Unit 2 automatically scrammed due to a turbine trip.  The turbine trip occurred during weekly turbine trip testing.  Two safety relief valves actuated [and reseated] in the relief mode on the turbine trip.  The reactor water cleanup system isolated during the transient (not being reported as there was no isolation in multiple systems).  The plant is stable with reactor pressure control to the main condenser via the main steam isolation valves. The plant is planning to remain in hot shutdown pending [turbine] electro-hydraulic (EHC) system troubleshooting and repair.
| event text = At 1606 CDT on August 15, 2009, LaSalle Unit 2 automatically scrammed due to a turbine trip.  The turbine trip occurred during weekly turbine trip testing.  Two safety relief valves actuated [and reseated] in the relief mode on the turbine trip.  The reactor water cleanup system isolated during the transient (not being reported as there was no isolation in multiple systems).  The plant is stable with reactor pressure control to the main condenser via the main steam isolation valves. The plant is planning to remain in hot shutdown pending [turbine] electro-hydraulic (EHC) system troubleshooting and repair.
All control rods fully inserted during the scram.  The site is aligning the ring bus for the normal shutdown electrical lineup.  Reactor water level is being maintained using the main feedwater system and decay heat is being removed via the turbine bypass valves.   
All control rods fully inserted during the scram.  The site is aligning the ring bus for the normal shutdown electrical lineup.  Reactor water level is being maintained using the main feedwater system and decay heat is being removed via the turbine bypass valves.   

Latest revision as of 21:11, 1 March 2018

ENS 45265 +/-
Where
LaSalle Constellation icon.png
Illinois (NRC Region 3)
Reporting
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation
Time - Person (Reporting Time:+-1 h-0.0417 days <br />-0.00595 weeks <br />-0.00137 months <br />)
Opened: Michael Findley
20:06 Aug 15, 2009
NRC Officer: Mark Abramovitz
Last Updated: Aug 15, 2009
45265 - NRC Website
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