ENS 51809: Difference between revisions

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| event date = 03/20/2016 21:54 EDT
| event date = 03/20/2016 21:54 EDT
| last update date = 03/21/2016
| last update date = 03/21/2016
| title = Technical Specification (Ts) Required Shutdown Due To Pressure Boundary Leakage
| title = Technical Specification (Ts) Required Shutdown Due to Pressure Boundary Leakage
| event text = During a planned Unit 1 shutdown for a refueling outage, a 0.5 gpm 'pressure boundary leak' was identified on a 1 inch pipe connected to the '1A' RHR-Shutdown Cooling return line by the drywell leak inspection team during a drywell inspection at approximately 15% power.  The leak exceeded the TS 3.4.3.2 'Operational Leakage' LCO of no pressure boundary leakage.  TS action 'a' was entered which requires to be in at least Hot Shutdown within 12 hours and Cold Shutdown within the next 24 hours.  Therefore, the event is reportable within 4 hours per 10CFR50.72(b)(2)(i) due to the initiation of a plant shutdown required by the plant's TS.
| event text = During a planned Unit 1 shutdown for a refueling outage, a 0.5 gpm 'pressure boundary leak' was identified on a 1 inch pipe connected to the '1A' RHR-Shutdown Cooling return line by the drywell leak inspection team during a drywell inspection at approximately 15% power.  The leak exceeded the TS 3.4.3.2 'Operational Leakage' LCO of no pressure boundary leakage.  TS action 'a' was entered which requires to be in at least Hot Shutdown within 12 hours and Cold Shutdown within the next 24 hours.  Therefore, the event is reportable within 4 hours per 10CFR50.72(b)(2)(i) due to the initiation of a plant shutdown required by the plant's TS.
The event is also reportable within 8 hours per 10CFR50.72(b)(3)(ii) due to an event that resulted in the condition of the nuclear power plant, including its principal safety barriers, being seriously degraded.
The event is also reportable within 8 hours per 10CFR50.72(b)(3)(ii) due to an event that resulted in the condition of the nuclear power plant, including its principal safety barriers, being seriously degraded.

Latest revision as of 20:45, 1 March 2018

ENS 51809 +/-
Where
Limerick Constellation icon.png
Pennsylvania (NRC Region 1)
Reporting
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown

10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded
LER: 05000352/LER-2016-003
Time - Person (Reporting Time:+-2.05 h-0.0854 days <br />-0.0122 weeks <br />-0.00281 months <br />)
Opened: John Harkins
23:51 Mar 20, 2016
NRC Officer: Vince Klco
Last Updated: Mar 21, 2016
51809 - NRC Website
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