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{{#Wiki_filter:-____-_-_ _ ______ _
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*
                                  -
-
                                                                                UNITED STATES
UNITED STATES
                      ' .1 *  ,[pomfo6fDo                      NUCf. EAR REGULATORY COMMISSION
,[pomfo6fD
                                            "
NUCf. EAR REGULATORY COMMISSION
                              [ ''           n
' .1 *
                                              j
o
                                                                                  REGION ll
[ ''
                                                                          101 MARIETTA STREET,N.W.
REGION ll
                              J* ..
"
                                              't~                           ATLANTA, GEORGI A 30323
n
                                *%*****   /                                                                            ,
J ..
                                      Report Nos.:      50-369/88-04 and 50-370/88-04
j
                                      Licensee: Duke Power Company
101 MARIETTA STREET,N.W.
                                                  '422 Scuth Church Street
*
                                                  Charlotte, NC 28242
't~
                                      Facility Name: McGuire Nuclear Station 1 and 2
ATLANTA, GEORGI A 30323
                                      Docket Nos:      50-369 and 50-370                                                .
*%
                                      License Nos:      NPF-9 and NPF-17
/
                                      Inspection Conducted: J uary 21, 1988 - February 26, 1988
*****
                                      Inspector:                                /)2/                d        [
                                                  E Orders,~ Senior Res ent inspector
                                                                    ~
                                                                                                      ' Gate Signed    ,
                                      Accompanying Personnel:      D. Nelson
                                                                      . Croteau
                                      Approved by:                      ~
                                                                          "
                                                                                                      8        [
                                                                                                        / Vate Signed
                                                                                                                        '
                                                        T. 'A.7e'ebles, Seg< ion Chief
                                                        Division of React'or Projects
                                                                                      SUMMARY
,
,
                                      Scope:     This routine unannounced inspection involved the areas of operations
Report Nos.:
                                      safety verification,       surveillance testing, maintenance activities,   and
50-369/88-04 and 50-370/88-04
                                      follow-up on previous inspection findings.
Licensee: Duke Power Company
                                      Results:     In the areas inspected, one violation was identified with two
'422 Scuth Church Street
                                      examples involving a failure to follow procedures and an inadequate procedure
Charlotte, NC 28242
                                      associated with performing equalizing charges on vital batteries and operating
Facility Name: McGuire Nuclear Station 1 and 2
                                      the chemical and volume control system.
Docket Nos:
                                                                                                                        ,
50-369 and 50-370
                                                                                                                        ;
.
                                                                                                                        ;
License Nos:
                                                                *
NPF-9 and NPF-17
                              8803290336 880310                                                                         ,
Inspection Conducted: J uary 21, 1988 - February 26, 1988
                              PDR     ADOCK 05000369                                                                     '
~
                              Q                       DCD
/)2/
                                                                                                                      _]
d
[
Inspector:
E Orders,~ Senior Res ent inspector
' Gate Signed
,
Accompanying Personnel:
D. Nelson
. Croteau
8
[
'
"
Approved by:
T. 'A.7e'ebles, Seg< ion Chief
/ Vate Signed
~
Division of React'or Projects
SUMMARY
Scope:
This routine unannounced inspection involved the areas of operations
,
safety verification,
surveillance testing, maintenance activities,
and
follow-up on previous inspection findings.
Results:
In the areas inspected, one violation was identified with two
examples involving a failure to follow procedures and an inadequate procedure
associated with performing equalizing charges on vital batteries and operating
the chemical and volume control system.
,
;
;
*
8803290336 880310
,
PDR
ADOCK 05000369
'
Q
DCD
_]


  .
.
.
                                    REPORT DETAILS
.
    1. Persons Contacted
REPORT DETAILS
        Licensee Employees
1.
      *T. McConnell, Plant Manager
Persons Contacted
        B. Travis, Superintendent of Operations
Licensee Employees
      *0. Rains, Superintendent of Maintenance
*T. McConnell, Plant Manager
        B. Hamilton, Superintendent of Technical Services
B. Travis, Superintendent of Operations
      *N. McCraw, Compliance Engineer
*0. Rains, Superintendent of Maintenance
      *M. Sample, Superintendent of Integrated Scheduling
B. Hamilton, Superintendent of Technical Services
      *L. Firebaugh, OPS /NPE/MNS
*N. McCraw, Compliance Engineer
      *S. LeRoy, Licensing, General Office
*M. Sample, Superintendent of Integrated Scheduling
        D. Baxter, OPS /MNS/NPD
*L.
      *S. Copp, Planning Engineer
Firebaugh, OPS /NPE/MNS
        R. Banner, Compliance
*S. LeRoy, Licensing, General Office
        J. Snyder, Performance Engineer
D. Baxter, OPS /MNS/NPD
      *N. Athertor., Compliance
*S. Copp, Planning Engineer
      *W. Reesioe, Operations Engineer
R. Banner, Compliance
      *R. White, IAE Engineer
J. Snyder, Performance Engineer
        Other licensee employees contacted included construction craftsmen,
*N. Athertor., Compliance
        technicians, operators, mechanics, security force members, and office
*W. Reesioe, Operations Engineer
        personnel.
*R. White, IAE Engineer
      * Attended exit interview
Other licensee employees contacted included construction craftsmen,
    2. Exit Interview (30703)
technicians, operators, mechanics, security force members, and office
        The inspection findings identified below were summarized on February 26,
personnel.
        1988, with those persons indicated in paragraph 1 above.     A violation,
* Attended exit interview
        described in paragraphs 9 and 11, was identified with two examples. The
2.
        following items we e discussed in detail:
Exit Interview (30703)
              (0 pen) Inspector Followup Item (IFI) 369, 370/88-04-01, Long Term
The inspection findings identified below were summarized on February 26,
              Corrective Actions Associated With Nuclear Service Water Expansion
1988, with those persons indicated in paragraph 1 above.
              Joint Liner Failure (see paragraph 8).
A violation,
              (0 pen) Violation 369, 370/88-04-02, Failure to Follow Procedure and
described in paragraphs 9 and 11, was identified with two examples. The
              Inadequate Procedure Associated with Battery Equalizing Charge and
following items we e discussed in detail:
              Chemical and Volume Control (NV) System (see paragraphs 9 and 11).
(0 pen) Inspector Followup Item (IFI) 369, 370/88-04-01, Long Term
              (Closed) Licensee Identified Violation (LIV) 369/88-04-03, Inoperable
Corrective Actions Associated With Nuclear Service Water Expansion
              Gaseous Activity Monitor Due to Deficient Procedure (see paragraph
Joint Liner Failure (see paragraph 8).
              10).
(0 pen) Violation 369, 370/88-04-02, Failure to Follow Procedure and
        The licensee representatives present offered no dissenting comments, nor
Inadequate Procedure Associated with Battery Equalizing Charge and
        did they identify as proprietary any of the information reviewed by the
Chemical and Volume Control (NV) System (see paragraphs 9 and 11).
        inspectors during the course of their inspection.
(Closed) Licensee Identified Violation (LIV) 369/88-04-03, Inoperable
Gaseous Activity Monitor Due to Deficient Procedure (see paragraph
10).
The licensee representatives present offered no dissenting comments, nor
did they identify as proprietary any of the information reviewed by the
inspectors during the course of their inspection.


                                                          . . - _ - - . .         .           . . . _ - - .
. . - _ - - . .
          -
.
                ,
. . .
      ,
_ - -
    ..   .
.
  ,
-
                                                        2
,
            3.   Unresolved Items
,
                  An unresolved item (UNR) is a matter about which more information is
..
                  required to determine whether it is acceptable or may involve a violation
.
                  or deviation. There were no unresolved items identified in this report.
,
            4.   Plant Operations (71707, 71710)                                                             .
2
                  'The inspection staff reviewed plant operations during the report period to
3.
                  verify conformance with applicable regulatory requirements. Control room
Unresolved Items
                  logs, shift supervisors' logs, shift turnover records and equipment
An unresolved item (UNR) is a matter about which more information is
                  removal and restoration records were routinely perused. Interviews were
required to determine whether it is acceptable or may involve a violation
                  conducted with plant operations, maintenance, chemistry, health physics,
or deviation. There were no unresolved items identified in this report.
                  and performance personnel.
4.
                  Activities within the control room were monitored during shifts and at
Plant Operations (71707, 71710)
                  shift changes. Actions and/or activities observed were conducted as
.
                  prescribed in applicable station administrative directives. The complement
'The inspection staff reviewed plant operations during the report period to
                  of licensed personnel on each shift met or exceeded the minimum required
verify conformance with applicable regulatory requirements. Control room
                  by Technical Specifications.
logs, shift supervisors' logs, shift turnover records and equipment
                  Plant tours taken during the reporting period included, but were not
removal and restoration records were routinely perused. Interviews were
                  limited to, the turbine buildings, the auxiliary building, Units 1 and 2
conducted with plant operations, maintenance, chemistry, health physics,
                  electrical equipment rooms, Units 1 and 2 cable spreading rooms, and the
and performance personnel.
                  station yard zone inside the protected area.
Activities within the control room were monitored during shifts and at
                  During the plant tours, ongoing activities, housekeeping, security,
shift changes. Actions and/or activities observed were conducted as
                  equipment status and radiation control practices were observed,
prescribed in applicable station administrative directives. The complement
                  a.   Unit 1 Operations
of licensed personnel on each shift met or exceeded the minimum required
                        Unit 1 operated at full power for the entire reporting period except
by Technical Specifications.
Plant tours taken during the reporting period included, but were not
limited to, the turbine buildings, the auxiliary building, Units 1 and 2
electrical equipment rooms, Units 1 and 2 cable spreading rooms, and the
station yard zone inside the protected area.
During the plant tours, ongoing activities, housekeeping, security,
equipment status and radiation control practices were observed,
a.
Unit 1 Operations
Unit 1 operated at full power for the entire reporting period except
for a reduction to 30% on February 2 to correct high sodium levels in
'
'
                          for a reduction to 30% on February 2 to correct high sodium levels in
the steam generators.
                        the steam generators. The chemistry problem was corrected and full-
The chemistry problem was corrected and full-
                        power was restored the following day.             The high sodium levels were         '
power was restored the following day.
i                       attributed to a leaking turbine building heating water system (YH)
The high sodium levels were
                        converter allowing sodium into the condensate makeup system.
'
                  b.   Unit 2 Operations
i
;                       Unit 2 operated at full power for the entire reporting period with no
attributed to a leaking turbine building heating water system (YH)
;                         significant problems.
converter allowing sodium into the condensate makeup system.
                        No violation or deviations were identified.
b.
            5.   Surveillance Testing (61726)
Unit 2 Operations
l                 Selected surveillance tests were analyzed and/or witnessed by the
;
                  inspector to ascertain procedural and performance adequacy and conformance
Unit 2 operated at full power for the entire reporting period with no
                  with applicable Technical Specifications.
;
significant problems.
No violation or deviations were identified.
5.
Surveillance Testing (61726)
l
Selected surveillance tests were analyzed and/or witnessed by the
inspector to ascertain procedural and performance adequacy and conformance
with applicable Technical Specifications.
l
l
I
I
I
I


        - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _.__ _ - - .                                             _ _ _ _ _ - ..             _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ ______
- _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _.__ _ - - .
                                                                                                                                                                                                          i
_ _ _ _ _ - ..
                                                                '
_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _
                                                                                  '
_
                                                        -
______
                                                          .
i
                                  .
'
                          ,
'
-
.
.
,
'
'
                                                                                                                                        3
3
,
,
w
w
i                                                                                   Selected tests were witnessed to ascertain that current written approved
i
,                                                                                    procedures were available and in use, that test equipment in use was
Selected tests were witnessed to ascertain that current written approved
                                                                                    calibrated, that test prerequisites were met, that system restoration was
procedures were available and in use, that test equipment in use was
-                                                                                    completed and test results were adequate.
,
                                                                                    Detailed below are selected tests which were either reviewed or witnessed:
calibrated, that test prerequisites were met, that system restoration was
                                                                                            PROCE0VRE                                   EQUIPMENT / TEST
completed and test results were adequate.
                                                                                    PT/2/A/4401/05A           KC Train A Heat Exchanger Perform Test
-
Detailed below are selected tests which were either reviewed or witnessed:
PROCE0VRE
EQUIPMENT / TEST
PT/2/A/4401/05A
KC Train A Heat Exchanger Perform Test
.
PT/0/A/4350/28A
125 Volt Vital Battery Weekly Inspector
'
'
.                                                                                  PT/0/A/4350/28A            125 Volt Vital Battery Weekly Inspector
PT/2/A/4201/01
                                                                                    PT/2/A/4201/01             Containment Sump Recirc Test
Containment Sump Recirc Test
.                                                                                   PT/0/A/4350/28B           125 V0LT VITAL BATTERY Quarterly
.
4
PT/0/A/4350/28B
                                                                                                                Inspection
125 V0LT VITAL BATTERY Quarterly
                                                                                    PT/0A/4601/08B             SSPS Train B PT
4
i                                                                                   PT/2/A/4401/01A           KC Train A Performance Test
Inspection
i                                                                                   PT/2/A/4350/04             4 KV Sequence Undervoltage
PT/0A/4601/08B
]                                                                                    PT/2/A/4252/01            Auxiliary Feedwater #2 Performance Test-
SSPS Train B PT
                                                                                    PT/2/A/4601/01            Protective System Channel 1 Function
i
                                                                                                                Test
PT/2/A/4401/01A
:                                                                                    PT/2/A/4208/04A            NS Train 2A Heat Exchanger Test
KC Train A Performance Test
                                                                                    PT/2/A/4401/05B            KC Train B Heat Exchanger Performance
i
.                                                                                                              Test
PT/2/A/4350/04
                                                                                    PT/0/A/4601/078            Reactor Trip Breaker Response Time
4 KV Sequence Undervoltage
                                                                                                                Testing
                                                                                    PT/2/A/4403/08            RN Train A Flow Balance
                                                                                    PT/2/A/4252/01B            Motor Driven Aux. Feedwater Pump 2B Performance
                                                                                                                Test
                                                                                    PT/1/A/4200/28            Slave Relay Test
                                                                                    PT/1/A/4601/02            Protective System Channel II
                                                                                                                Functional Test
                                                                                    PT/1/A/4403/018            RN Train B Performance Test
                                                                                    PT/1/A/4150/17A            Unit 1 Pressurizer Heater
;                                                                                                              Capacity Test
?                                                                                    PT/1/A/4208/03A            Train A NS Heat Exchanger
                                                                                                                Perf. Test
l                                                                                    PT/1/A/4403/02              RN Valve Stroke Timing
,
                                                                                    PT/1/A/4206/01B            NI Pump 28 Performance Test
                                                                                    PT/1/A/4350/23A            Hydrogen Mitigation Test
]
]
;                                                                       6.           Maintenance Observations (62703)
PT/2/A/4252/01
                                                                                    Routine maintenance activities were reviewed and/or witnessed by the
Auxiliary Feedwater #2 Performance Test-
j                                                                                   resident inspection staff to ascertain procedural and performance adequacy
PT/2/A/4601/01
j                                                                                   and conformance with applicable Technical Specifications.
Protective System Channel 1 Function
I                                                                                   The selected activities witnessed were examined to ascertain that, where
Test
                                                                                    applicable, current written approved procedures were available and in use,
:
                                                                                    that prerequisites were met, that equipment restoration was completed and
PT/2/A/4208/04A
                                                                                    maintenance results were adequate.
NS Train 2A Heat Exchanger Test
"
PT/2/A/4401/05B
                                                                                    No violations or deviations were identified.
KC Train B Heat Exchanger Performance
,
Test
  d
.
                                                                                                                                                                                                        ~
PT/0/A/4601/078
    - -                   ,.wv-~-,                                         ,,s--     , - - ,   , . , . -,n_
Reactor Trip Breaker Response Time
Testing
PT/2/A/4403/08
RN Train A Flow Balance
PT/2/A/4252/01B
Motor Driven Aux. Feedwater Pump 2B Performance
Test
PT/1/A/4200/28
Slave Relay Test
PT/1/A/4601/02
Protective System Channel II
Functional Test
PT/1/A/4403/018
RN Train B Performance Test
PT/1/A/4150/17A
Unit 1 Pressurizer Heater
;
Capacity Test
?
PT/1/A/4208/03A
Train A NS Heat Exchanger
Perf. Test
l
PT/1/A/4403/02
RN Valve Stroke Timing
,
PT/1/A/4206/01B
NI Pump 28 Performance Test
]
PT/1/A/4350/23A
Hydrogen Mitigation Test
;
6.
Maintenance Observations (62703)
Routine maintenance activities were reviewed and/or witnessed by the
j
resident inspection staff to ascertain procedural and performance adequacy
j
and conformance with applicable Technical Specifications.
I
The selected activities witnessed were examined to ascertain that, where
applicable, current written approved procedures were available and in use,
that prerequisites were met, that equipment restoration was completed and
maintenance results were adequate.
"
No violations or deviations were identified.
,
d
- -
,.wv-~-,
,,s--
a-
, - - ,
, . , .
-,n_
~


                                                  - . - - - - - - - _ - _ - _ -- _   _   ._
- . - - - - - - - _ - _ - _
                                                                                                      - - - - _ _ _ _ ,
-- _
                  '
_
            .
._
      -
- - - - _ _ _ _ ,
  .,-.
                                                  4
        7.  Follow-up on Previous Inspection Findings (92702)
              The following previously identified items were reviewed to asccitain that
              the licensee's responses, where applicable, and licensee actions were in
              compliance with regulatory requirements and corrective actions have been
              completed. Selective verification included record revie.. . observations,
                                                                                    .
              and discussions with licensee personnel.
              (CLOSED) Violation 50-369/86-08-02, Failure to follow procedures during
              criticality and removal of equipment from service.              Adequate corrective
              actions have been taken.
              (CLOSED)  Violation 50-369/86-30-01, Failure to comply with TS 6.8.1 -
              OP/1/A/6200/04-ND flow with no KC resulting in water hammers.                    This
              incident was discussed with licensed personnel stressing procedural
              compliance and use of alternate methods to verify plant conrutions.
              Safety related hangers were checked for damage by the licensee and no
              damage was found. Adequate corrective actions have been taken.
'
'
              (CLOSED) Violation 50-369, 370/86-04-01, Failure to have an operable ECCS
.
              flowpath. This violation involved inoperability of both safety injection
-
              pumps since suction from the volume control tank would not automatically
.,-.
              transfer to the refueling water storage tank. Department Directive 2.8.2
4
              (T) Rev. O and Station Directive 2.8.2 Rev. I were instituted prov ding         i
7.
              guidance on determining operability. A functional review was performed to
Follow-up on Previous Inspection Findings (92702)
              determine the design purpose of each motor operated valve (MOV) which
The following previously identified items were reviewed to asccitain that
              receives an Engineerei Safety Features signal and the information was
the licensee's responses, where applicable, and licensee actions were in
              incorporated in the Technical Specification Reference Manual as an aid to
compliance with regulatory requirements and corrective actions have been
              determine operability.   A Technical Specification interpretation was
completed.
              incorporated referencing the use of the Station Directive and Technical
Selective verification included record revie.. . observations,
              Specification Reference Manual in determining operability. The Department
.
and discussions with licensee personnel.
(CLOSED) Violation 50-369/86-08-02, Failure to follow procedures during
criticality and removal of equipment from service.
Adequate corrective
actions have been taken.
(CLOSED)
Violation 50-369/86-30-01, Failure to comply with TS 6.8.1 -
OP/1/A/6200/04-ND flow with no KC resulting in water hammers.
This
incident was discussed with licensed personnel stressing procedural
compliance and use of alternate methods to verify plant conrutions.
Safety related hangers were checked for damage by the licensee and no
damage was found. Adequate corrective actions have been taken.
(CLOSED) Violation 50-369, 370/86-04-01, Failure to have an operable ECCS
'
flowpath. This violation involved inoperability of both safety injection
pumps since suction from the volume control tank would not automatically
transfer to the refueling water storage tank. Department Directive 2.8.2
(T) Rev. O and Station Directive 2.8.2 Rev. I were instituted prov ding
i
guidance on determining operability. A functional review was performed to
determine the design purpose of each motor operated valve (MOV) which
receives an Engineerei Safety Features signal and the information was
incorporated in the Technical Specification Reference Manual as an aid to
determine operability.
A Technical Specification interpretation was
incorporated referencing the use of the Station Directive and Technical
Specification Reference Manual in determining operability. The Department
[
[
              Directive, Station Directive, Technical Specification Reference Manual,
Directive, Station Directive, Technical Specification Reference Manual,
              and Technical Specification interpretation were reviewed by the inspector.
and Technical Specification interpretation were reviewed by the inspector.
              Adequate corrective actions have been taken.
Adequate corrective actions have been taken.
1             (CLOSED)   Inspector Followup Item 50-370/84-32-02, Need for operational
1
              procedure regarding degraded Standby Shutdown Facility (SSF). The
(CLOSED)
              licensee has attached a note to T.S. 3.7.14 which states the shift
Inspector Followup Item 50-370/84-32-02, Need for operational
              supervisor is to ensure security is informed as SSF components are
procedure regarding degraded Standby Shutdown Facility (SSF).
              declared inoperable and also when those components are returned to
The
              operable status.
licensee has attached a note to T.S. 3.7.14 which states the shift
              (CLOSED)   Inspector Followup Item 369-84-17-01 and 370-84-14-01,
supervisor is to ensure security is informed as SSF components are
              Environmental Qualification Requirement NM/ Duke Agreement. From July 28
declared
              through August 1, 1986 NRC representatives reviewed the licensees
inoperable and also when those components are returned to
              implementation of a program required by 10 CFR 50.49 for establishing and
operable status.
              maintaining the environmental qualification (EQ) of electrical equipment.
(CLOSED)
              The findings indicated that a program had been implemented to meet the
Inspector
              requirements of 10 CFR 50.49 except for certain deficiencies documented in
Followup
              Inspection Report 50-369, 370/86-20. These deficiencies are being tracked
Item 369-84-17-01 and 370-84-14-01,
Environmental Qualification Requirement NM/ Duke Agreement. From July 28
through August 1,
1986 NRC representatives reviewed the
licensees
implementation of a program required by 10 CFR 50.49 for establishing and
maintaining the environmental qualification (EQ) of electrical equipment.
The findings indicated that a program had been implemented to meet the
requirements of 10 CFR 50.49 except for certain deficiencies documented in
Inspection Report 50-369, 370/86-20. These deficiencies are being tracked
as followup items to 50-369, 370/86-20. Based on the inspection findings
;
;
              as followup items to 50-369, 370/86-20. Based on the inspection findings
i
i            and separate followup items being tracked, this item is c'osed.
and separate followup items being tracked, this item is c'osed.
!
!
                                                                                                    .
.


                                                            _ . _ _ _ _ _ _ _ _ - _ _ _ _ . _ _ _ _ _ - _ - _               _ __ _ __ _ _ _
_ . _ _ _ _ _ _ _ _ - _ _ _ _ . _ _ _ _ _ - _ - _
          '
_ __ _ __ _ _ _
      '
'
    .
'
  ,
.
                                                                                                                                                1
,
                                                  5
1
        8.   Nuclear Service Water Pump Damage
5
            On January 19, 1988 during the performance of PT/1/A/4403/08, Nuclear
8.
            Service Water (RN) Train B Flow Balance, it was detected that adequate
Nuclear Service Water Pump Damage
            flow could not be achieved through the containment spray (NS) nor the
On January 19, 1988 during the performance of PT/1/A/4403/08, Nuclear
            component cooling (KC) heat exchangers. The required flow rates were 6000
Service Water (RN) Train B Flow Balance, it was detected that adequate
            GPM for=the KC heat exchanger and 3800 GPM for the NS heat exchanger. The
flow could not be achieved through the containment spray (NS) nor the
            actual flow rates were 5900 GPM and 3600 GPM respectively.
component cooling (KC) heat exchangers. The required flow rates were 6000
            Based on the test results, site personnel requested that Corporate Design
GPM for=the KC heat exchanger and 3800 GPM for the NS heat exchanger. The
            Engineering provide a justification for continued operation (JCO). The
actual flow rates were 5900 GPM and 3600 GPM respectively.
            JCO, which was provided that evening, justified continued safe operation
Based on the test results, site personnel requested that Corporate Design
            with flow rates of 5600 and 3500 GPM respectively.                                               The calculations
Engineering provide a justification for continued operation (JCO).
The
JCO, which was provided that evening, justified continued safe operation
with flow rates of 5600 and 3500 GPM respectively.
The calculations
supporting the JC0 were reviewed by the resident inspection staff.
4
4
            supporting the JC0 were reviewed by the resident inspection staff.
In as much as the flow rates through the KC and NS heat exchangers had
            In as much as the flow rates through the KC and NS heat exchangers had
dropped rather dramatically since the previous test perfermed on
            dropped rather dramatically since the previous test perfermed on
October.29, 1987 at which time the respective flow rates were 6448 and
            October.29, 1987 at which time the respective flow rates were 6448 and
4001 GPM, the test group decided to perform a head curve test on the pun;p.
            4001 GPM, the test group decided to perform a head curve test on the pun;p.
This took place on January 26, 1988. The results of the head curve test
            This took place on January 26, 1988. The results of the head curve test
indicated that the pump had lost a significant amount of capacity as can
            indicated that the pump had lost a significant amount of capacity as can
be seen on the Attachment. Accordingly, the pump, associated train and
            be seen on the Attachment. Accordingly, the pump, associated train and
supported equipment were declared inoperable.
            supported equipment were declared inoperable.
The pump was torn down for inspection and possible impeller replacement.
            The pump was torn down for inspection and possible impeller replacement.
Upon disassembling the pump, the maintenance technicians found a large
            Upon disassembling the pump, the maintenance technicians found a large
                      '
            piece (approximately 1/8" x 8" x 36") of stainless steel sheet metal in
            the pump throat.
            The. metal was determined to be the liner from an expansion joint located
            immddiately upstream of the putnp. The expansion joint war repaired,
            the pump impeller was replaced and the train was tested / returned to
            service on January 29, within the allowed 72 hour action statement time
'
'
            frame.
piece (approximately 1/8" x 8" x 36") of stainless steel sheet metal in
        \
the pump throat.
!           All other RN pumps were visually inspected to verify that the expansion
The. metal was determined to be the liner from an expansion joint located
immddiately upstream of the putnp.
The expansion joint war repaired,
the pump impeller was replaced and the train was tested / returned to
service on January 29, within the allowed 72 hour action statement time
\\
frame.
'
!
All other RN pumps were visually inspected to verify that the expansion
(
(
            joints were intact. Longer term plans include inspection of the weld
joints were intact.
,            attaching the liner to the expansion joint or replacement of the joint
Longer term plans include inspection of the weld
            with piping.
attaching the liner to the expansion joint or replacement of the joint
,
l
with piping.
l
This issue will be carried as an inspector follow-up item (IFI 369,
l
l
l            This issue will be carried as an inspector follow-up item (IFI 369,
370/88-04-01).
l            370/88-04-01).
I
I           No violations or deviations were identified.
No violations or deviations were identified.
        9.   Vital Battery Equalizing Charge
9.
:           An assured vital 125 volt direct current (VDC) power supply is provided to
Vital Battery Equalizing Charge
            both units by four battery banks consisting of 59 lead-calcium battery
:
An assured vital 125 volt direct current (VDC) power supply is provided to
both units by four battery banks consisting of 59 lead-calcium battery
cells each. The batteries are continuously charged or "floated" on the
l
l
            cells each. The batteries are continuously charged or "floated" on the
l
l
;
;
)
)
'                                                                                                                                             _;
'
_;


                                                                                        .___ ____ __-__
.___ ____ __-__
. ..
. ..
      o
o
          '
'
        .
.
    .
.
                                                    6
6
            Vital DC buses and assume load without interruption upon loss of a battery
Vital DC buses and assume load without interruption upon loss of a battery
            charger or associated alternating current (AC) power source. The normal
charger or associated alternating current (AC) power source. The normal
            float voltage is 2.23 VDC per cell or approximately 132 VDC for each bank.
float voltage is 2.23 VDC per cell or approximately 132 VDC for each bank.
            Periodically, whenever battery parameters such as individual cell voltage
Periodically, whenever battery parameters such as individual cell voltage
            or specific gravity decrease to undesirable limits, an equalizing charge
or specific gravity decrease to undesirable limits, an equalizing charge
            is performed to return the bank to optimum condition. Vendor manual MCM
is performed to return the bank to optimum condition. Vendor manual MCM
            1356.01-3 recommends an initial maximum equalizing charge voltage of 2.39
1356.01-3 recommends an initial maximum equalizing charge voltage of 2.39
            VDC per cel'. (141 VDC per bank). Instrumentation and Electrical (IAE)
VDC per cel'. (141 VDC per bank).
            procedure IP/0/A/3061/08, Water Addition and Equalize Charging for Vital
Instrumentation and Electrical (IAE)
            Batteries, appropriately states 141 VDC as the initial equalizing charge
procedure IP/0/A/3061/08, Water Addition and Equalize Charging for Vital
            voltage reduced by 2.39 volts for each jumpered cell. Some individual
Batteries, appropriately states 141 VDC as the initial equalizing charge
            cells have retained undesirable low voltages following equalizing charge.
voltage reduced by 2.39 volts for each jumpered cell.
            Therefore, the licensee, with verbal vendor concurrence, has increased the
Some individual
            equalize charge voltage up to 150 volts to correct the individual cell
cells have retained undesirable low voltages following equalizing charge.
            problems.   However, the IAE procedure specifies 141 VDC not 150 VDC.
Therefore, the licensee, with verbal vendor concurrence, has increased the
            On February 10, 1988, the inspector observed an indicated voltage of 148
equalize charge voltage up to 150 volts to correct the individual cell
            VDC during an equalize charge on battery EVCB that had been in progress
problems.
            since February 9. When questioned about the increased voltage, the IAE
However, the IAE procedure specifies 141 VDC not 150 VDC.
            Technician     performing   the   charge acknowledged   tne   procedural
On February 10, 1988, the inspector observed an indicated voltage of 148
            non-compliance but stated that the IAE engineer authorized the higher
VDC during an equalize charge on battery EVCB that had been in progress
            voltage. The IAE engineer had been acting on the belief that the
since February 9. When questioned about the increased voltage, the IAE
              procedure allowed him to specify a higher voltage. IAE considers the
Technician
              higher voltage justified based on verbal communication with the battery
performing
              vendor.
the
              Several NRC concerns arise:
charge
              The IAE technician chose to ignore the procedure instructions based on
acknowledged
              verbal instructions from the IAE engineer. The NRC considers this to be a
tne
              failure to follow the procedure; a change to the procedure should have
procedural
              been made. Whea warranted, methods are available to properly change
non-compliance but stated that the IAE engineer authorized the higher
              procedures. Station Directive 4.2.1, Handling of Station Procedures,
voltage.
              contains detailed instructions on when and how to make major changes to
The IAE engineer had been acting on the belief that the
              existing procedures.     This process includes a safety evaluation, second
procedure allowed him to specify a higher voltage.
              review, and approval which was essentially short circuited by the IAE
IAE considers the
              personnel in this case. The practice of increasing the equalizing charge
higher voltage justified based on verbal communication with the battery
              voltage has previously taken place on other batteries thereby providing
vendor.
              ample opportunity for the need for a procedure change to be detected and
Several NRC concerns arise:
              properly implemented.     This is violation 369, 370/88-04-02.
The IAE technician chose to ignore the procedure instructions based on
              Other recent events were caused by licensee personnel not complying with
verbal instructions from the IAE engineer. The NRC considers this to be a
              procedures.     On August 28, 1987, IAE technicians failed to return a
failure to follow the procedure; a change to the procedure should have
              Residual Heat Removal Pump recirculation flow instrument to service due in
been made.
              part to not following their procedure (Inspection Report 50-369,
Whea warranted, methods are available to properly change
              370/87-41). On September 16, 1C87, technicians caused a Unit 1 blackout
procedures.
              due to testing of lockout relays beyond the scope of their procedures
Station Directive 4.2.1, Handling of Station Procedures,
              (Inspection Report 50-369,       370/87-41).   On December 28,   1987, IAE
contains detailed instructions on when and how to make major changes to
                                                                                                        l
existing procedures.
                                                                                                          l
This process includes a safety evaluation, second
                                                                              _
review, and approval which was essentially short circuited by the IAE
                                                                                                        ;
personnel in this case. The practice of increasing the equalizing charge
voltage has previously taken place on other batteries thereby providing
ample opportunity for the need for a procedure change to be detected and
properly implemented.
This is violation 369, 370/88-04-02.
Other recent events were caused by licensee personnel not complying with
procedures.
On August 28, 1987, IAE technicians failed to return a
Residual Heat Removal Pump recirculation flow instrument to service due in
part to not following their procedure (Inspection Report 50-369,
370/87-41). On September 16, 1C87, technicians caused a Unit 1 blackout
due to testing of lockout relays beyond the scope of their procedures
(Inspection Report 50-369,
370/87-41).
On December 28,
1987, IAE
l
l
_
;


                                      .-. _
.-.
        .
_
              .
.
      .
.
    *
.
  .
*
                                                      7
.
                technicians actuated a reactor trip signal while conducting a test in the
7
                Solid State Protection System by performing a procedure step expressly
technicians actuated a reactor trip signal while conducting a test in the
                forbidden dt.e to the conditions of the system at the time. (Inspection
Solid State Protection System by performing a procedure step expressly
                Report 50-369/370-87-43). Although each event is unique with respect to
forbidden dt.e to the conditions of the system at the time.
                procedure compliance, collectively they raise concerns about the
(Inspection
                licensee's procedure work ethic in general. Each of these events resulted
Report 50-369/370-87-43). Although each event is unique with respect to
                in an NRC violation, yet the procedure compliance problem persists.
procedure compliance, collectively they raise concerns about the
                Future NRC inspections will closely monitor licensee corrective actions
licensee's procedure work ethic in general. Each of these events resulted
                associated with these violations and performance in the area of auherence
in an NRC violation, yet the procedure compliance problem persists.
                to procedures.
Future NRC inspections will closely monitor licensee corrective actions
          10.   Licensee Event Report (LER) Followup (90712, 92700)
associated with these violations and performance in the area of auherence
                The following LERs were reviewed to determine whether reporting
to procedures.
                requirements have been met, the cause appears accurate, the corrective
10.
                actions appear appropriate, generic applicability has been considered, and
Licensee Event Report (LER) Followup (90712, 92700)
                whether the event is related to previous events.         Selected LERs were
The following LERs were reviewed to determine whether reporting
                chosen for more detailed followup in verifying the nature, impact, and
requirements have been met, the cause appears accurate, the corrective
                cause of the event as well as corrective actions taken.
actions appear appropriate, generic applicability has been considered, and
                (CLOSED)   LER 369/86-10.   Inoperable gaseous activity monitor due to
whether the event is related to previous events.
                defective procedure.     As corrective action, Procedure IP/0/A/3010/06,
Selected LERs were
                Reactor Protection System Response Time Test, was revised to require
chosen for more detailed followup in verifying the nature, impact, and
                installing wiring and hardware to maintain the isolation capability of
cause of the event as well as corrective actions taken.
                gaseous activity monitor 1 EMF-39L with both trains of the Solid State
(CLOSED)
                Protection System removed from service. TS 3.3.3.9 requires 1 EMF-39 to be
LER 369/86-10.
                operable at all times but this monitor was inoperable on June 3,1986,
Inoperable gaseous activity monitor due to
                during performance of IP/0/A/3010/06. This item is identified as a
defective procedure.
                Licensee Identified Violation (LIV 369/88-04-03) for violatior. of T. S.
As corrective action, Procedure IP/0/A/3010/06,
i               3.3.3.9.
Reactor Protection System Response Time Test, was revised to require
l               (CLOSED)   LER 369/86-11. D/G 1A auto-started due to a Unit 1 Train A
installing wiring and hardware to maintain the isolation capability of
l               blackout actuation caused by a design deficiency. Under-voltage relays in
gaseous activity monitor 1 EMF-39L with both trains of the Solid State
!               the blackout circuit were designed to pickup at a voltage which was too
Protection System removed from service. TS 3.3.3.9 requires 1 EMF-39 to be
operable at all times but this monitor was inoperable on June 3,1986,
during performance of IP/0/A/3010/06.
This item is identified as a
Licensee Identified Violation (LIV 369/88-04-03) for violatior. of T. S.
i
3.3.3.9.
l
(CLOSED)
LER 369/86-11. D/G 1A auto-started due to a Unit 1 Train A
l
blackout actuation caused by a design deficiency. Under-voltage relays in
!
the blackout circuit were designed to pickup at a voltage which was too
high.
The licensee replaced the relays with relays of a icwer pickup
'
'
                high. The licensee replaced the relays with relays of a icwer pickup
'
'
voltage.
                voltage.
I
I         11. Chemical and Volume Control (NV) System Operation
11. Chemical and Volume Control (NV) System Operation
                On February 3,1988, the Unit 1 diaphram on 1NV-474 ruptured causing a
On February 3,1988, the Unit 1 diaphram on 1NV-474 ruptured causing a
                spill when removing the cation bed demineralizer from service in the NV
spill when removing the cation bed demineralizer from service in the NV
                system.   Investigation revealed that two steps had been reversed for no
system.
                apparent reason during the last procedure change of OP/1/A/6200/01,
Investigation revealed that two steps had been reversed for no
                Chemical and Volume Control System. Reversal of the steps caused the NV
apparent reason during the last procedure change of OP/1/A/6200/01,
                system flow to be totally secured while removing the cation bed from
Chemical and Volume Control System.
!               service causing possible overpressurization of the low pressure section of
Reversal of the steps caused the NV
l               the NV system including the mixed bed demineralizers (300 psig design) and
system flow to be totally secured while removing the cation bed from
!
service causing possible overpressurization of the low pressure section of
l
the NV system including the mixed bed demineralizers (300 psig design) and
letdown heat exchanger (600 psig design) and causing the 1NV-474 diaphram
i
i
                letdown heat exchanger (600 psig design) and causing the 1NV-474 diaphram
to rupture. The actual pressure applied to the system is not known. This
                to rupture. The actual pressure applied to the system is not known. This
event constitutes a violation of TS 6.8.1. for an inadequate procedure and
                event constitutes a violation of TS 6.8.1. for an inadequate procedure and
is another example of violation 369,
                is another example of violation 369, 370/88-04-02 discussed in
370/88-04-02 discussed in
                paragraph 9.
paragraph 9.
:
:
:
:
!
!


      _ -__ _       _ _ _ _ _ _         -.                     . - - _ _ -__ _
_ -__ _
_ _ _ _ _ _
-.
. - - _ _ -__ _
_
_
                                                                                          MCGUIRE NUCLEAR STATION
MCGUIRE NUCLEAR STATION
                                                                                                                      RN PUMP 1B HEAD CURVES
RN PUMP 1B HEAD CURVES
                                230                                                                   ;
230
                                                                                                      !
;
                                                                                                      i
!
                                220 - - -                       - - - - - - -                         --                                               - --~ - - - - - - - - - - - - - - - --
i
                m                                                               ' ~~
220 -
                x                                                                         ~.
- -
                w                                                                                 -..
- - - - - - -
                F
--
                <              210             ---- -                               -
- --~ - - - - - - - - - - - - - - - --
                                                                                    86-H-  -  - f ~: ' '                   ~.
m
                                                                                                                                  -- --- --                     ---
' ~~
                                                                                                                                                                        !
x
                                                                                                                                                                                    - - - - - - - - - - -                                                                                           --
~.
                S                                                                                                                        ''
w
                u
.
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-.
                                                                                                      I
F
                                                                                                                                                ._  ,
210
                                                                                                                                                          -
---- -
                                                                                                                                                                        I
-
                o              200           - - - - - - -
- - f ~: ' '
                                                                                                -- f ---- -- - - - - - -
-- --- --
                                                                                                                                                              -
---
                                                                                                                                                                '
- - - - - - - - - - -
                                                                                                                                                                    k ;---                               - - - - - - - -                     - - - - - -                                   ---
--
    s           F
<
    5
86-H-
    r
''
                W
I
                W
!
                                                                                    88-HEAD
~.
                                                                                                      i
S
                                                                                                                                                                                                  '
N
                                                                                                                                                                                                                                            l
i
    I
._
    <
u
                b               19 0 -t-- ---
I
                                                                    - - -- - - - - - - - - f -
,
                                                                                                                                    - - -           - - -
-
                                                                                                                                                                  -t---
o
                                                                                                                                                                        i
200
                                                                                                                                                                                          - - - - - -
- - - - - - -
                                                                                                                                                                                                                    '
-- f ---- -- - - - - - -
                                                                                                                                                                                                                              ,.,-                       RIG HEAD - --- -
k ;---
    -           o                                                                                                                                                       I                                                           ,
- - - - - - - -
    N           6                                                                                     !                                   \                             i                                                               .
- - - - - -
                3-             180 -h---- -- --                                             -
---
                                                                                                      j-
'
                                                                                                                -                 - - - - -
-
                                                                                                                                              '\
s
                                                                                                                                              -          --
F
                                                                                                                                                                        1
5
                                                                                                                                                                        t          -                  - -- 87-HE D--;N  - - - -         o                    -- --               --                 -
W
                                                                                                                                                                                                                                                          '
88-HEAD
                o
'
                -
l
                                        !                                                            :                                                                                                                                     !
W
                                        i                                                                                                                                                                                                   i               s
i
                2                       l                                                             j                                                                                                                                     i                 -
r
                <
b
                z              170 -h -                                             -
19 0
                                                                                                -r-           - - - - - - - - - - - -
-t-- ---
                                                                                                                                                                      -t-
- - -- - - - - - - - - f -
                                                                                                                                                                                  --                                         - - - --~ - - - - - - - '
- - -
                                                                                                                                                                                                                                                                        s
- - -
                                                                                                                                                                                                                                                                                -    --- --
-t---
                >                       :                                                                                                                               ;                                                                                                   -
- - - - - -
, . , -
RIG HEAD - --- -
I
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- ---
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-- ---- -- c
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l
l
                Q                        !                                                                                                                              !                                                                    i                                N
H
                  J                                                                                                                                                      '                                                                                                        '
;
                                                                                                                                                                                                                                            l                                      '
.
                4              160 -                      - - -                  -
:
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i
                                                                                                                                                    - - - I -- -                                       -                 --
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                                                                                                                                                                                                                                  -----t------~---                                     -
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                                    6000                                                         8000                                                           10000                                                                 12000                                                     14000
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Latest revision as of 12:33, 11 December 2024

Insp Repts 50-369/88-04 & 50-370/88-04 on 880121-0226. Violation Noted.Major Areas Inspected:Operations,Safety Verification,Surveillance Testing,Maint Activities & Followup on Previous Insp Findings
ML20148H178
Person / Time
Site: McGuire, Mcguire  
Issue date: 03/08/1988
From: William Orders, Peebles T
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20148H159 List:
References
50-369-88-04, 50-369-88-4, 50-370-88-04, 50-370-88-4, NUDOCS 8803290336
Download: ML20148H178 (9)


See also: IR 05000369/1988004

Text

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UNITED STATES

,[pomfo6fD

NUCf. EAR REGULATORY COMMISSION

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REGION ll

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j

101 MARIETTA STREET,N.W.

't~

ATLANTA, GEORGI A 30323

  • %

/

,

Report Nos.:

50-369/88-04 and 50-370/88-04

Licensee: Duke Power Company

'422 Scuth Church Street

Charlotte, NC 28242

Facility Name: McGuire Nuclear Station 1 and 2

Docket Nos:

50-369 and 50-370

.

License Nos:

NPF-9 and NPF-17

Inspection Conducted: J uary 21, 1988 - February 26, 1988

~

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d

[

Inspector:

E Orders,~ Senior Res ent inspector

' Gate Signed

,

Accompanying Personnel:

D. Nelson

. Croteau

8

[

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Approved by:

T. 'A.7e'ebles, Seg< ion Chief

/ Vate Signed

~

Division of React'or Projects

SUMMARY

Scope:

This routine unannounced inspection involved the areas of operations

,

safety verification,

surveillance testing, maintenance activities,

and

follow-up on previous inspection findings.

Results:

In the areas inspected, one violation was identified with two

examples involving a failure to follow procedures and an inadequate procedure

associated with performing equalizing charges on vital batteries and operating

the chemical and volume control system.

,

8803290336 880310

,

PDR

ADOCK 05000369

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DCD

_]

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.

REPORT DETAILS

1.

Persons Contacted

Licensee Employees

  • T. McConnell, Plant Manager

B. Travis, Superintendent of Operations

  • 0. Rains, Superintendent of Maintenance

B. Hamilton, Superintendent of Technical Services

  • N. McCraw, Compliance Engineer
  • M. Sample, Superintendent of Integrated Scheduling
  • L.

Firebaugh, OPS /NPE/MNS

  • S. LeRoy, Licensing, General Office

D. Baxter, OPS /MNS/NPD

  • S. Copp, Planning Engineer

R. Banner, Compliance

J. Snyder, Performance Engineer

  • N. Athertor., Compliance
  • W. Reesioe, Operations Engineer
  • R. White, IAE Engineer

Other licensee employees contacted included construction craftsmen,

technicians, operators, mechanics, security force members, and office

personnel.

  • Attended exit interview

2.

Exit Interview (30703)

The inspection findings identified below were summarized on February 26,

1988, with those persons indicated in paragraph 1 above.

A violation,

described in paragraphs 9 and 11, was identified with two examples. The

following items we e discussed in detail:

(0 pen) Inspector Followup Item (IFI) 369, 370/88-04-01, Long Term

Corrective Actions Associated With Nuclear Service Water Expansion

Joint Liner Failure (see paragraph 8).

(0 pen) Violation 369, 370/88-04-02, Failure to Follow Procedure and

Inadequate Procedure Associated with Battery Equalizing Charge and

Chemical and Volume Control (NV) System (see paragraphs 9 and 11).

(Closed) Licensee Identified Violation (LIV) 369/88-04-03, Inoperable

Gaseous Activity Monitor Due to Deficient Procedure (see paragraph

10).

The licensee representatives present offered no dissenting comments, nor

did they identify as proprietary any of the information reviewed by the

inspectors during the course of their inspection.

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2

3.

Unresolved Items

An unresolved item (UNR) is a matter about which more information is

required to determine whether it is acceptable or may involve a violation

or deviation. There were no unresolved items identified in this report.

4.

Plant Operations (71707, 71710)

.

'The inspection staff reviewed plant operations during the report period to

verify conformance with applicable regulatory requirements. Control room

logs, shift supervisors' logs, shift turnover records and equipment

removal and restoration records were routinely perused. Interviews were

conducted with plant operations, maintenance, chemistry, health physics,

and performance personnel.

Activities within the control room were monitored during shifts and at

shift changes. Actions and/or activities observed were conducted as

prescribed in applicable station administrative directives. The complement

of licensed personnel on each shift met or exceeded the minimum required

by Technical Specifications.

Plant tours taken during the reporting period included, but were not

limited to, the turbine buildings, the auxiliary building, Units 1 and 2

electrical equipment rooms, Units 1 and 2 cable spreading rooms, and the

station yard zone inside the protected area.

During the plant tours, ongoing activities, housekeeping, security,

equipment status and radiation control practices were observed,

a.

Unit 1 Operations

Unit 1 operated at full power for the entire reporting period except

for a reduction to 30% on February 2 to correct high sodium levels in

'

the steam generators.

The chemistry problem was corrected and full-

power was restored the following day.

The high sodium levels were

'

i

attributed to a leaking turbine building heating water system (YH)

converter allowing sodium into the condensate makeup system.

b.

Unit 2 Operations

Unit 2 operated at full power for the entire reporting period with no

significant problems.

No violation or deviations were identified.

5.

Surveillance Testing (61726)

l

Selected surveillance tests were analyzed and/or witnessed by the

inspector to ascertain procedural and performance adequacy and conformance

with applicable Technical Specifications.

l

I

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- _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _.__ _ - - .

_ _ _ _ _ - ..

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

_

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i

Selected tests were witnessed to ascertain that current written approved

procedures were available and in use, that test equipment in use was

,

calibrated, that test prerequisites were met, that system restoration was

completed and test results were adequate.

-

Detailed below are selected tests which were either reviewed or witnessed:

PROCE0VRE

EQUIPMENT / TEST

PT/2/A/4401/05A

KC Train A Heat Exchanger Perform Test

.

PT/0/A/4350/28A

125 Volt Vital Battery Weekly Inspector

'

PT/2/A/4201/01

Containment Sump Recirc Test

.

PT/0/A/4350/28B

125 V0LT VITAL BATTERY Quarterly

4

Inspection

PT/0A/4601/08B

SSPS Train B PT

i

PT/2/A/4401/01A

KC Train A Performance Test

i

PT/2/A/4350/04

4 KV Sequence Undervoltage

]

PT/2/A/4252/01

Auxiliary Feedwater #2 Performance Test-

PT/2/A/4601/01

Protective System Channel 1 Function

Test

PT/2/A/4208/04A

NS Train 2A Heat Exchanger Test

PT/2/A/4401/05B

KC Train B Heat Exchanger Performance

Test

.

PT/0/A/4601/078

Reactor Trip Breaker Response Time

Testing

PT/2/A/4403/08

RN Train A Flow Balance

PT/2/A/4252/01B

Motor Driven Aux. Feedwater Pump 2B Performance

Test

PT/1/A/4200/28

Slave Relay Test

PT/1/A/4601/02

Protective System Channel II

Functional Test

PT/1/A/4403/018

RN Train B Performance Test

PT/1/A/4150/17A

Unit 1 Pressurizer Heater

Capacity Test

?

PT/1/A/4208/03A

Train A NS Heat Exchanger

Perf. Test

l

PT/1/A/4403/02

RN Valve Stroke Timing

,

PT/1/A/4206/01B

NI Pump 28 Performance Test

]

PT/1/A/4350/23A

Hydrogen Mitigation Test

6.

Maintenance Observations (62703)

Routine maintenance activities were reviewed and/or witnessed by the

j

resident inspection staff to ascertain procedural and performance adequacy

j

and conformance with applicable Technical Specifications.

I

The selected activities witnessed were examined to ascertain that, where

applicable, current written approved procedures were available and in use,

that prerequisites were met, that equipment restoration was completed and

maintenance results were adequate.

"

No violations or deviations were identified.

,

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- . - - - - - - - _ - _ - _

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- - - - _ _ _ _ ,

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4

7.

Follow-up on Previous Inspection Findings (92702)

The following previously identified items were reviewed to asccitain that

the licensee's responses, where applicable, and licensee actions were in

compliance with regulatory requirements and corrective actions have been

completed.

Selective verification included record revie.. . observations,

.

and discussions with licensee personnel.

(CLOSED) Violation 50-369/86-08-02, Failure to follow procedures during

criticality and removal of equipment from service.

Adequate corrective

actions have been taken.

(CLOSED)

Violation 50-369/86-30-01, Failure to comply with TS 6.8.1 -

OP/1/A/6200/04-ND flow with no KC resulting in water hammers.

This

incident was discussed with licensed personnel stressing procedural

compliance and use of alternate methods to verify plant conrutions.

Safety related hangers were checked for damage by the licensee and no

damage was found. Adequate corrective actions have been taken.

(CLOSED) Violation 50-369, 370/86-04-01, Failure to have an operable ECCS

'

flowpath. This violation involved inoperability of both safety injection

pumps since suction from the volume control tank would not automatically

transfer to the refueling water storage tank. Department Directive 2.8.2

(T) Rev. O and Station Directive 2.8.2 Rev. I were instituted prov ding

i

guidance on determining operability. A functional review was performed to

determine the design purpose of each motor operated valve (MOV) which

receives an Engineerei Safety Features signal and the information was

incorporated in the Technical Specification Reference Manual as an aid to

determine operability.

A Technical Specification interpretation was

incorporated referencing the use of the Station Directive and Technical

Specification Reference Manual in determining operability. The Department

[

Directive, Station Directive, Technical Specification Reference Manual,

and Technical Specification interpretation were reviewed by the inspector.

Adequate corrective actions have been taken.

1

(CLOSED)

Inspector Followup Item 50-370/84-32-02, Need for operational

procedure regarding degraded Standby Shutdown Facility (SSF).

The

licensee has attached a note to T.S. 3.7.14 which states the shift

supervisor is to ensure security is informed as SSF components are

declared

inoperable and also when those components are returned to

operable status.

(CLOSED)

Inspector

Followup

Item 369-84-17-01 and 370-84-14-01,

Environmental Qualification Requirement NM/ Duke Agreement. From July 28

through August 1,

1986 NRC representatives reviewed the

licensees

implementation of a program required by 10 CFR 50.49 for establishing and

maintaining the environmental qualification (EQ) of electrical equipment.

The findings indicated that a program had been implemented to meet the

requirements of 10 CFR 50.49 except for certain deficiencies documented in

Inspection Report 50-369, 370/86-20. These deficiencies are being tracked

as followup items to 50-369, 370/86-20. Based on the inspection findings

i

and separate followup items being tracked, this item is c'osed.

!

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_ __ _ __ _ _ _

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5

8.

Nuclear Service Water Pump Damage

On January 19, 1988 during the performance of PT/1/A/4403/08, Nuclear

Service Water (RN) Train B Flow Balance, it was detected that adequate

flow could not be achieved through the containment spray (NS) nor the

component cooling (KC) heat exchangers. The required flow rates were 6000

GPM for=the KC heat exchanger and 3800 GPM for the NS heat exchanger. The

actual flow rates were 5900 GPM and 3600 GPM respectively.

Based on the test results, site personnel requested that Corporate Design

Engineering provide a justification for continued operation (JCO).

The

JCO, which was provided that evening, justified continued safe operation

with flow rates of 5600 and 3500 GPM respectively.

The calculations

supporting the JC0 were reviewed by the resident inspection staff.

4

In as much as the flow rates through the KC and NS heat exchangers had

dropped rather dramatically since the previous test perfermed on

October.29, 1987 at which time the respective flow rates were 6448 and

4001 GPM, the test group decided to perform a head curve test on the pun;p.

This took place on January 26, 1988. The results of the head curve test

indicated that the pump had lost a significant amount of capacity as can

be seen on the Attachment. Accordingly, the pump, associated train and

supported equipment were declared inoperable.

The pump was torn down for inspection and possible impeller replacement.

Upon disassembling the pump, the maintenance technicians found a large

'

piece (approximately 1/8" x 8" x 36") of stainless steel sheet metal in

the pump throat.

The. metal was determined to be the liner from an expansion joint located

immddiately upstream of the putnp.

The expansion joint war repaired,

the pump impeller was replaced and the train was tested / returned to

service on January 29, within the allowed 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> action statement time

\\

frame.

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All other RN pumps were visually inspected to verify that the expansion

(

joints were intact.

Longer term plans include inspection of the weld

attaching the liner to the expansion joint or replacement of the joint

,

l

with piping.

l

This issue will be carried as an inspector follow-up item (IFI 369,

l

370/88-04-01).

I

No violations or deviations were identified.

9.

Vital Battery Equalizing Charge

An assured vital 125 volt direct current (VDC) power supply is provided to

both units by four battery banks consisting of 59 lead-calcium battery

cells each. The batteries are continuously charged or "floated" on the

l

l

)

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6

Vital DC buses and assume load without interruption upon loss of a battery

charger or associated alternating current (AC) power source. The normal

float voltage is 2.23 VDC per cell or approximately 132 VDC for each bank.

Periodically, whenever battery parameters such as individual cell voltage

or specific gravity decrease to undesirable limits, an equalizing charge

is performed to return the bank to optimum condition. Vendor manual MCM

1356.01-3 recommends an initial maximum equalizing charge voltage of 2.39

VDC per cel'. (141 VDC per bank).

Instrumentation and Electrical (IAE)

procedure IP/0/A/3061/08, Water Addition and Equalize Charging for Vital

Batteries, appropriately states 141 VDC as the initial equalizing charge

voltage reduced by 2.39 volts for each jumpered cell.

Some individual

cells have retained undesirable low voltages following equalizing charge.

Therefore, the licensee, with verbal vendor concurrence, has increased the

equalize charge voltage up to 150 volts to correct the individual cell

problems.

However, the IAE procedure specifies 141 VDC not 150 VDC.

On February 10, 1988, the inspector observed an indicated voltage of 148

VDC during an equalize charge on battery EVCB that had been in progress

since February 9. When questioned about the increased voltage, the IAE

Technician

performing

the

charge

acknowledged

tne

procedural

non-compliance but stated that the IAE engineer authorized the higher

voltage.

The IAE engineer had been acting on the belief that the

procedure allowed him to specify a higher voltage.

IAE considers the

higher voltage justified based on verbal communication with the battery

vendor.

Several NRC concerns arise:

The IAE technician chose to ignore the procedure instructions based on

verbal instructions from the IAE engineer. The NRC considers this to be a

failure to follow the procedure; a change to the procedure should have

been made.

Whea warranted, methods are available to properly change

procedures.

Station Directive 4.2.1, Handling of Station Procedures,

contains detailed instructions on when and how to make major changes to

existing procedures.

This process includes a safety evaluation, second

review, and approval which was essentially short circuited by the IAE

personnel in this case. The practice of increasing the equalizing charge

voltage has previously taken place on other batteries thereby providing

ample opportunity for the need for a procedure change to be detected and

properly implemented.

This is violation 369, 370/88-04-02.

Other recent events were caused by licensee personnel not complying with

procedures.

On August 28, 1987, IAE technicians failed to return a

Residual Heat Removal Pump recirculation flow instrument to service due in

part to not following their procedure (Inspection Report 50-369,

370/87-41). On September 16, 1C87, technicians caused a Unit 1 blackout

due to testing of lockout relays beyond the scope of their procedures

(Inspection Report 50-369,

370/87-41).

On December 28,

1987, IAE

l

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7

technicians actuated a reactor trip signal while conducting a test in the

Solid State Protection System by performing a procedure step expressly

forbidden dt.e to the conditions of the system at the time.

(Inspection

Report 50-369/370-87-43). Although each event is unique with respect to

procedure compliance, collectively they raise concerns about the

licensee's procedure work ethic in general. Each of these events resulted

in an NRC violation, yet the procedure compliance problem persists.

Future NRC inspections will closely monitor licensee corrective actions

associated with these violations and performance in the area of auherence

to procedures.

10.

Licensee Event Report (LER) Followup (90712, 92700)

The following LERs were reviewed to determine whether reporting

requirements have been met, the cause appears accurate, the corrective

actions appear appropriate, generic applicability has been considered, and

whether the event is related to previous events.

Selected LERs were

chosen for more detailed followup in verifying the nature, impact, and

cause of the event as well as corrective actions taken.

(CLOSED)

LER 369/86-10.

Inoperable gaseous activity monitor due to

defective procedure.

As corrective action, Procedure IP/0/A/3010/06,

Reactor Protection System Response Time Test, was revised to require

installing wiring and hardware to maintain the isolation capability of

gaseous activity monitor 1 EMF-39L with both trains of the Solid State

Protection System removed from service. TS 3.3.3.9 requires 1 EMF-39 to be

operable at all times but this monitor was inoperable on June 3,1986,

during performance of IP/0/A/3010/06.

This item is identified as a

Licensee Identified Violation (LIV 369/88-04-03) for violatior. of T. S.

i

3.3.3.9.

l

(CLOSED)

LER 369/86-11. D/G 1A auto-started due to a Unit 1 Train A

l

blackout actuation caused by a design deficiency. Under-voltage relays in

!

the blackout circuit were designed to pickup at a voltage which was too

high.

The licensee replaced the relays with relays of a icwer pickup

'

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voltage.

I

11. Chemical and Volume Control (NV) System Operation

On February 3,1988, the Unit 1 diaphram on 1NV-474 ruptured causing a

spill when removing the cation bed demineralizer from service in the NV

system.

Investigation revealed that two steps had been reversed for no

apparent reason during the last procedure change of OP/1/A/6200/01,

Chemical and Volume Control System.

Reversal of the steps caused the NV

system flow to be totally secured while removing the cation bed from

!

service causing possible overpressurization of the low pressure section of

l

the NV system including the mixed bed demineralizers (300 psig design) and

letdown heat exchanger (600 psig design) and causing the 1NV-474 diaphram

i

to rupture. The actual pressure applied to the system is not known. This

event constitutes a violation of TS 6.8.1. for an inadequate procedure and

is another example of violation 369,

370/88-04-02 discussed in

paragraph 9.

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