05000313/FIN-2013011-04: Difference between revisions

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| identified by = NRC
| identified by = NRC
| Inspection procedure = IP 93800
| Inspection procedure = IP 93800
| Inspector = A Sanchez, D Allen, D Loveless, G Miller, J Watkins, S Jonesb, Latta G, Werner J, Melfi L, Willoughby N, Okonkw
| Inspector = A Sanchez, D Allen, D Loveless, G Miller, J Watkins, S Jonesb, Lattag Werner, J Melfi, L Willoughby, N Okonkwo
| CCA = N/A for ROP
| CCA = N/A for ROP
| INPO aspect =  
| INPO aspect =  
| description = On August 8, 2012, Unit 2 tripped following a loss of condenser vacuum. Following the trip, main feedwater regulating valve A failed to close and remained approximately 8 percent open, complicating the operator response to the event. The licensee concluded that the valve jacking mechanism had been left in the wrong position following maintenance. An NRC finding associated with this event is documented in NRC inspection report 05000313/2012005; 0500368/2012005 as FIN 05000368/2012005-008 (ADAMS Accession No. ML13045A520). Following the Unit 2 reactor trip on March 31, 2013, operators identified that main feedwater regulating valve A failed to indicate closed. This indication caused the operators to trip main feedwater pump A and manually initiate the emergency feedwater actuation system. Arkansas Nuclear One Unit 2 is a Combustion Engineering designed plant and emergency feedwater is not normally actuated on a non-complicated reactor trip. Operators subsequently placed the auxiliary feedwater system in service, which required operators to manually inhibit the emergency feedwater system, rendering both trains inoperable and requiring entry into Technical Specification 3.0.3 for a short period of time. This again complicated operator response to the trip. The licensee later determined that the regulating valve actually had closed, and the valve indication was in error. The condition was corrected by tightening loose adjustment screws on the valve position indication limit switches. The team concluded that additional inspection was required to assess the effectiveness of the licensee maintenance practices on the main feedwater regulating valves: Unresolved Item URI 05000368/2013011-04, Main Feedwater Regulating Valve Maintenance Practices.  
| description = On August 8, 2012, Unit 2 tripped following a loss of condenser vacuum. Following the trip, main feedwater regulating valve A failed to close and remained approximately 8 percent open, complicating the operator response to the event. The licensee concluded that the valve jacking mechanism had been left in the wrong position following maintenance. An NRC finding associated with this event is documented in NRC inspection report 05000313/2012005; 0500368/2012005 as FIN 05000368/2012005-008 (ADAMS Accession No. ML13045A520). Following the Unit 2 reactor trip on March 31, 2013, operators identified that main feedwater regulating valve A failed to indicate closed. This indication caused the operators to trip main feedwater pump A and manually initiate the emergency feedwater actuation system. Arkansas Nuclear One Unit 2 is a Combustion Engineering designed plant and emergency feedwater is not normally actuated on a non-complicated reactor trip. Operators subsequently placed the auxiliary feedwater system in service, which required operators to manually inhibit the emergency feedwater system, rendering both trains inoperable and requiring entry into Technical Specification 3.0.3 for a short period of time. This again complicated operator response to the trip. The licensee later determined that the regulating valve actually had closed, and the valve indication was in error. The condition was corrected by tightening loose adjustment screws on the valve position indication limit switches. The team concluded that additional inspection was required to assess the effectiveness of the licensee maintenance practices on the main feedwater regulating valves: Unresolved Item URI 05000368/2013011-04, Main Feedwater Regulating Valve Maintenance Practices.  
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Latest revision as of 19:50, 20 February 2018

04
Site: Arkansas Nuclear Entergy icon.png
Report IR 05000313/2013011 Section 4OA5
Date counted Jun 30, 2013 (2013Q2)
Type: URI:
cornerstone Mitigating Systems
Identified by: NRC identified
Inspection Procedure: IP 93800
Inspectors (proximate) A Sanchez
D Allen
D Loveless
G Miller
J Watkins
S Jonesb
Lattag Werner
J Melfi
L Willoughby
N Okonkwo
INPO aspect
'