ENS 43949: Difference between revisions
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StriderTol (talk | contribs) (Created page by program invented by Mark Hawes) |
StriderTol (talk | contribs) (Created page by program invented by StriderTol) |
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| event date = 02/01/2008 04:45 EST | | event date = 02/01/2008 04:45 EST | ||
| last update date = 02/01/2008 | | last update date = 02/01/2008 | ||
| title = Automatic Scram | | title = Automatic Scram as a Result of Turbine Trip | ||
| event text = Unit 2 automatically scrammed [at] 0445 as a result of an RPS actuation due to a turbine trip. All rods inserted. The plant is stable. No ECCS or SRV actuation occurred. This report is made pursuant to 50.72(B)(iv)(B). An investigation into the cause is currently in progress. | | event text = Unit 2 automatically scrammed [at] 0445 as a result of an RPS actuation due to a turbine trip. All rods inserted. The plant is stable. No ECCS or SRV actuation occurred. This report is made pursuant to 50.72(B)(iv)(B). An investigation into the cause is currently in progress. | ||
Primary plant pressure is 900 psig. with the decay heat path to the condenser via turbine bypass valves. All safety related systems are operable, and the licensee is investigating a potential issue with the EHC system. | Primary plant pressure is 900 psig. with the decay heat path to the condenser via turbine bypass valves. All safety related systems are operable, and the licensee is investigating a potential issue with the EHC system. |
Latest revision as of 21:15, 1 March 2018
Where | |
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Limerick Pennsylvania (NRC Region 1) | |
Reporting | |
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation | |
Time - Person (Reporting Time:+-4 h-0.167 days <br />-0.0238 weeks <br />-0.00548 months <br />) | |
Opened: | Mark Crim 05:45 Feb 1, 2008 |
NRC Officer: | Joe O'Hara |
Last Updated: | Feb 1, 2008 |
43949 - NRC Website
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