ENS 46337: Difference between revisions

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| event date = 10/17/2010 05:12 EDT
| event date = 10/17/2010 05:12 EDT
| last update date = 10/18/2010
| last update date = 10/18/2010
| title = Automatic Reactor Trip Due To 4 Kv Group Bus Undervoltage Condition  
| title = Automatic Reactor Trip Due to 4 Kv Group Bus Undervoltage Condition  
| event text = On 10/17/10 at 0512 [EDT], Unit 2 experienced an [automatic] reactor trip due to 4 kV group bus under voltage. While restoring the voltage regulator to automatic, following a swap to manual at 0123 [EDT] on 10/17/10 while 500 kV line 5014 was being restored to service, the reactor tripped after placing the voltage regulator in automatic.   
| event text = On 10/17/10 at 0512 [EDT], Unit 2 experienced an [automatic] reactor trip due to 4 kV group bus under voltage. While restoring the voltage regulator to automatic, following a swap to manual at 0123 [EDT] on 10/17/10 while 500 kV line 5014 was being restored to service, the reactor tripped after placing the voltage regulator in automatic.   
The crew entered EOP [Emergency Operating Procedure] Trip 1, and then EOP Trip 2 as required.  The plant was stabilized at no load conditions.  All rods fully inserted on the trip, and all systems responded as designed with RCS [Reactor Coolant System] temperature being controlled via 21 RCP [Reactor Coolant Pump] and the steam dump system.  22, 23, and 24 RCP's tripped on group bus under voltage.  The AFW [Auxiliary Feed Water] Pumps started in response to low steam generator levels.  23 AFW was subsequently tripped per procedure since 21 and 22 AFW pumps were in service feeding 21-24 steam generators.  
The crew entered EOP [Emergency Operating Procedure] Trip 1, and then EOP Trip 2 as required.  The plant was stabilized at no load conditions.  All rods fully inserted on the trip, and all systems responded as designed with RCS [Reactor Coolant System] temperature being controlled via 21 RCP [Reactor Coolant Pump] and the steam dump system.  22, 23, and 24 RCP's tripped on group bus under voltage.  The AFW [Auxiliary Feed Water] Pumps started in response to low steam generator levels.  23 AFW was subsequently tripped per procedure since 21 and 22 AFW pumps were in service feeding 21-24 steam generators.  

Latest revision as of 22:08, 1 March 2018

ENS 46337 +/-
Where
Salem PSEG icon.png
New Jersey (NRC Region 1)
Reporting
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation

10 CFR 50.72(b)(3)(iv)(A), System Actuation
Time - Person (Reporting Time:+-2.57 h-0.107 days <br />-0.0153 weeks <br />-0.00352 months <br />)
Opened: Jack Osborne
06:38 Oct 17, 2010
NRC Officer: Dong Park
Last Updated: Oct 18, 2010
46337 - NRC Website
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