ENS 46337: Difference between revisions
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| event date = 10/17/2010 05:12 EDT | | event date = 10/17/2010 05:12 EDT | ||
| last update date = 10/18/2010 | | last update date = 10/18/2010 | ||
| title = Automatic Reactor Trip Due | | title = Automatic Reactor Trip Due to 4 Kv Group Bus Undervoltage Condition | ||
| event text = On 10/17/10 at 0512 [EDT], Unit 2 experienced an [automatic] reactor trip due to 4 kV group bus under voltage. While restoring the voltage regulator to automatic, following a swap to manual at 0123 [EDT] on 10/17/10 while 500 kV line 5014 was being restored to service, the reactor tripped after placing the voltage regulator in automatic. | | event text = On 10/17/10 at 0512 [EDT], Unit 2 experienced an [automatic] reactor trip due to 4 kV group bus under voltage. While restoring the voltage regulator to automatic, following a swap to manual at 0123 [EDT] on 10/17/10 while 500 kV line 5014 was being restored to service, the reactor tripped after placing the voltage regulator in automatic. | ||
The crew entered EOP [Emergency Operating Procedure] Trip 1, and then EOP Trip 2 as required. The plant was stabilized at no load conditions. All rods fully inserted on the trip, and all systems responded as designed with RCS [Reactor Coolant System] temperature being controlled via 21 RCP [Reactor Coolant Pump] and the steam dump system. 22, 23, and 24 RCP's tripped on group bus under voltage. The AFW [Auxiliary Feed Water] Pumps started in response to low steam generator levels. 23 AFW was subsequently tripped per procedure since 21 and 22 AFW pumps were in service feeding 21-24 steam generators. | The crew entered EOP [Emergency Operating Procedure] Trip 1, and then EOP Trip 2 as required. The plant was stabilized at no load conditions. All rods fully inserted on the trip, and all systems responded as designed with RCS [Reactor Coolant System] temperature being controlled via 21 RCP [Reactor Coolant Pump] and the steam dump system. 22, 23, and 24 RCP's tripped on group bus under voltage. The AFW [Auxiliary Feed Water] Pumps started in response to low steam generator levels. 23 AFW was subsequently tripped per procedure since 21 and 22 AFW pumps were in service feeding 21-24 steam generators. |
Latest revision as of 22:08, 1 March 2018
Where | |
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Salem ![]() New Jersey (NRC Region 1) | |
Reporting | |
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
Time - Person (Reporting Time:+-2.57 h-0.107 days <br />-0.0153 weeks <br />-0.00352 months <br />) | |
Opened: | Jack Osborne 06:38 Oct 17, 2010 |
NRC Officer: | Dong Park |
Last Updated: | Oct 18, 2010 |
46337 - NRC Website
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