ENS 51809: Difference between revisions
Jump to navigation
Jump to search
StriderTol (talk | contribs) (Created page by program invented by Mark Hawes) |
StriderTol (talk | contribs) (Created page by program invented by StriderTol) |
||
Line 16: | Line 16: | ||
| event date = 03/20/2016 21:54 EDT | | event date = 03/20/2016 21:54 EDT | ||
| last update date = 03/21/2016 | | last update date = 03/21/2016 | ||
| title = Technical Specification (Ts) Required Shutdown Due | | title = Technical Specification (Ts) Required Shutdown Due to Pressure Boundary Leakage | ||
| event text = During a planned Unit 1 shutdown for a refueling outage, a 0.5 gpm 'pressure boundary leak' was identified on a 1 inch pipe connected to the '1A' RHR-Shutdown Cooling return line by the drywell leak inspection team during a drywell inspection at approximately 15% power. The leak exceeded the TS 3.4.3.2 'Operational Leakage' LCO of no pressure boundary leakage. TS action 'a' was entered which requires to be in at least Hot Shutdown within 12 hours and Cold Shutdown within the next 24 hours. Therefore, the event is reportable within 4 hours per 10CFR50.72(b)(2)(i) due to the initiation of a plant shutdown required by the plant's TS. | | event text = During a planned Unit 1 shutdown for a refueling outage, a 0.5 gpm 'pressure boundary leak' was identified on a 1 inch pipe connected to the '1A' RHR-Shutdown Cooling return line by the drywell leak inspection team during a drywell inspection at approximately 15% power. The leak exceeded the TS 3.4.3.2 'Operational Leakage' LCO of no pressure boundary leakage. TS action 'a' was entered which requires to be in at least Hot Shutdown within 12 hours and Cold Shutdown within the next 24 hours. Therefore, the event is reportable within 4 hours per 10CFR50.72(b)(2)(i) due to the initiation of a plant shutdown required by the plant's TS. | ||
The event is also reportable within 8 hours per 10CFR50.72(b)(3)(ii) due to an event that resulted in the condition of the nuclear power plant, including its principal safety barriers, being seriously degraded. | The event is also reportable within 8 hours per 10CFR50.72(b)(3)(ii) due to an event that resulted in the condition of the nuclear power plant, including its principal safety barriers, being seriously degraded. |
Latest revision as of 20:45, 1 March 2018
Where | |
---|---|
Limerick Pennsylvania (NRC Region 1) | |
Reporting | |
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown 10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded | |
LER: | 05000352/LER-2016-003 |
Time - Person (Reporting Time:+-2.05 h-0.0854 days <br />-0.0122 weeks <br />-0.00281 months <br />) | |
Opened: | John Harkins 23:51 Mar 20, 2016 |
NRC Officer: | Vince Klco |
Last Updated: | Mar 21, 2016 |
51809 - NRC Website
| |