ENS 51965: Difference between revisions

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| event date = 05/30/2016 09:30 PDT
| event date = 05/30/2016 09:30 PDT
| last update date = 05/30/2016
| last update date = 05/30/2016
| title = Manual Opening Of Reactor Trip Breakers Due To Rod Position Error Greater Than 12 Steps
| title = Manual Opening of Reactor Trip Breakers Due to Rod Position Error Greater than 12 Steps
| event text = On 5/30/2016 at 0930 [PDT], Unit 2 was in its 19th refueling outage in Mode 4 (hot shutdown, reactor subcritical).  Routine post-maintenance testing of digital rod position indication (DRPI) was in progress in accordance with Surveillance Test Procedure (STP) R-1C.  Rod Shutdown Bank A was being withdrawn.  With Shutdown Bank A Group 1 demand indicating 14 steps, and Group 2 demand indicating 13 steps, Bank A DRPI indicated 12 steps but control rod B4 DRPI indication remained at Step 0.  With the bank demand position exceeding rod B4's DRPI indication by greater than 12 steps,  Operators manually opened the Reactor Trip Breakers, placing all the rods in a known position due to an inoperable DRPI system.  All systems actuated as required and rods fully inserted.
| event text = On 5/30/2016 at 0930 [PDT], Unit 2 was in its 19th refueling outage in Mode 4 (hot shutdown, reactor subcritical).  Routine post-maintenance testing of digital rod position indication (DRPI) was in progress in accordance with Surveillance Test Procedure (STP) R-1C.  Rod Shutdown Bank A was being withdrawn.  With Shutdown Bank A Group 1 demand indicating 14 steps, and Group 2 demand indicating 13 steps, Bank A DRPI indicated 12 steps but control rod B4 DRPI indication remained at Step 0.  With the bank demand position exceeding rod B4's DRPI indication by greater than 12 steps,  Operators manually opened the Reactor Trip Breakers, placing all the rods in a known position due to an inoperable DRPI system.  All systems actuated as required and rods fully inserted.
                                                                              
                                                                              

Latest revision as of 21:45, 1 March 2018

ENS 51965 +/-
Where
Diablo Canyon Pacific Gas & Electric icon.png
California (NRC Region 4)
Reporting
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Time - Person (Reporting Time:+2.68 h0.112 days <br />0.016 weeks <br />0.00367 months <br />)
Opened: Russ Cruzen
19:11 May 30, 2016
NRC Officer: Jeff Herrera
Last Updated: May 30, 2016
51965 - NRC Website
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