ENS 55028: Difference between revisions

From kanterella
Jump to navigation Jump to search
(StriderTol Bot change)
(StriderTol Bot change)
Line 1: Line 1:
{{ENS notification
{{ENS notification
| event number = 55028
| event number = 55028
| facility =  
| facility = Arkansas Nuclear
| Organization =  
| Organization =  
| license number =  
| license number =  
| region =  
| region = 4
| state =  
| state = Arkansas
| city =  
| city =  
| unit =  
| unit = 2
| utype =  
| utype = B, CE
| cfr = <Br>
| cfr = 10 CFR 50.72(b)(2)(iv)(B)  
50.72(B)(2)(Iv)(B)  
<br>50.72(b)(3)(iv)(A)
<Br>50.72(B)(3)(Iv)(A)
| emergency class = Non Emergency
| emergency class =  
| notification date = 12/10/2020 20:43
| notification date = </b> 20:43
| notification by = Danny Watts
| notification by = </B> Danny Watts
| NRC officer = Kerby Scales
| NRC officer = </B> Kerby Scales
| event date = 12/10/2020 16:08 CST
| event date = </b> 12/10/2020 </b>  16:08 CST
| last update date = 12/11/2020
| last update date = </b> 12/11/2020
| title = Automatic Reactor Scram Due to Low Steam Generator Water Level
| title =  
| event text = On December 10, 2020 at 1608 CST, Arkansas Nuclear One, Unit 2 (ANO-2) experienced an automatic reactor scram from 100 percent power due to Low Steam Generator Water Level in 2E-24A Steam Generator.  Emergency Feedwater actuated automatically due to low water level in the A Steam Generator.  Due to inadequate control of the B Main Feedwater Control System, water level in the B Steam generator rose to a level requiring manual trip of the B Main Feedwater pump.  Emergency Feedwater responded as designed to feed both steam generators automatically.
| event text =  
All other systems responded as designed.  All electrical power is being supplied from offsite power and maintaining unit electrical loads as designed.
Unit 2 is currently stable in Mode 3 (Hot Standby) maintaining pressure and temperature via Emergency Feedwater and secondary system steaming.
There are no indications of a radiological release on either unit as a result of this event.
This report satisfies the reporting criteria of both 10 CFR 50.72(b)(2)(iv)(6) for the Reactor Protection System actuation and 10 CFR 50.72(b)(3)(iv)(A) for the actuation of the Emergency Feedwater System.
The Arkansas Nuclear One NRC Senior Resident Inspector has been notified.
* * * UPDATE FROM JOHN LINDSEY TO DONALD NORWOOD AT 1605 EST ON 12/11/2020 * * *
The purpose of this [report] is to provide an update to NRC Event Number 55028.
The cause of the inadequate control of the B Main Feedwater Control System to control B Steam Generator Level was verified to be associated with the failure that led to the A Steam Generator low level condition.
After taking action to trip the B Main Feedwater Pump, Emergency Feedwater was manually actuated for the B Steam Generator and the Emergency Feedwater System was verified to maintain proper automatic control of both Steam Generator levels.
At the time of the initial event notification, plant temperature and pressure control had been transferred from Emergency Feedwater to Auxiliary Feedwater along with secondary system steaming.
The licensee notified the NRC Resident Inspector.
Notified R4DO (Kellar).
| URL = https://www.nrc.gov/reading-rm/doc-collections/event-status/event/2020/20201214en.html#en55028
| URL = https://www.nrc.gov/reading-rm/doc-collections/event-status/event/2020/20201214en.html#en55028
}}
}}


{{ENS-Nav}}[[Category:Power Reactor]]
{{ENS-Nav}}[[Category:Power Reactor]]

Revision as of 01:33, 15 January 2021

ENS 55028 +/-
Where
Arkansas Nuclear Entergy icon.png
Arkansas (NRC Region 4)
Reporting
10 CFR 50.72(b)(2)(iv)(B)
50.72(b)(3)(iv)(A)
Time - Person (Reporting Time:+-1.42 h-0.0592 days <br />-0.00845 weeks <br />-0.00195 months <br />)
Opened: Danny Watts
20:43 Dec 10, 2020
NRC Officer: Kerby Scales
Last Updated: Dec 11, 2020
55028 - NRC Website
Loading map...