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{{#Wiki_filter:.                                         --     .   .   - ._. _-- -
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                            U.S. NUCLEAR REGULATORY COMMISSION
._. _-- -
                                                REGION I
.
                                                                                              I
.
      Docket Nos.:       50-245         50-336       50-423                                 1
,
                                                                                              l
l
'.
U.S. NUCLEAR REGULATORY COMMISSION
REGION I
Docket Nos.:
50-245
50-336
50-423
1
l
Report Nos.:
97-01
97-01
97-01
,
,
      Report Nos.:       97-01          97-01        97-01                                  l
License Nos.:
      License Nos.:      DPR-21         DPR-65       NPF-49
DPR-21
                                                                                              i
DPR-65
                                                                                              I
NPF-49
      Licensee:         Northeast Nuclear Energy Company                                   ;
i
.                         P. O. Box 128                                                       i
Licensee:
                          Waterford, CT 06385
Northeast Nuclear Energy Company
.
P. O. Box 128
i
Waterford, CT 06385
.
.
      Facility:         Millstone Nuclear Power Station, Units 1,2, and 3
Facility:
      Inspection at:     Waterford, CT
Millstone Nuclear Power Station, Units 1,2, and 3
                                                                                              i
Inspection at:
      Dates:             January 1,1997 - March 10,1997                                     )
Waterford, CT
      inspectors:       T. A. Easlick, Senior Resident inspector Unit 1
i
                          D. P. Beaulieu, Senior Resident inspector, Unit 2                   l
Dates:
January 1,1997 - March 10,1997
inspectors:
T. A. Easlick, Senior Resident inspector Unit 1
D. P. Beaulieu, Senior Resident inspector, Unit 2
I
I
                          A. C. Cerne, Senior Resident inspector, Unit 3                     I
A. C. Cerne, Senior Resident inspector, Unit 3
j                         A. L. Burritt, Resident inspector, Unit 1                           l
j
2                         R. J. Arrighi, Resident inspector, Unit 3                           '
A. L. Burritt, Resident inspector, Unit 1
                          L. L. Scholl, Reactor Engineer, Region l
2
                          N. J. Blumberg, Project Engineer, Region i
R. J. Arrighi, Resident inspector, Unit 3
3                        R. J. Urban, Project Engineer, Region I                             ,
'
                                                                                              '
L. L. Scholl, Reactor Engineer, Region l
a                        J. T. Furia, Senior Radiation Specialist, Region I, DRS
N. J. Blumberg, Project Engineer, Region i
                          J. E. Carrasco, Reactor Engineer, Region I, DRS
R. J. Urban, Project Engineer, Region I
i     Approved by:       Jacque P. Durr, Chief
3
                          Inspection Branch
,
                          Special Projects Office, NRR
'
J. T. Furia, Senior Radiation Specialist, Region I, DRS
a
J. E. Carrasco, Reactor Engineer, Region I, DRS
i
Approved by:
Jacque P. Durr, Chief
Inspection Branch
Special Projects Office, NRR
I
I
1
1
7
7
        9704170127 970411
9704170127 970411
        PDR     ADOCK 05000245
PDR
        Q                 PDR
ADOCK 05000245
f
Q
PDR
f
e


              _. -     _ _ .                               - -_               _ . - . . _ _ __                 ___             .___ _
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                                                TABLE OF CONTENTS
TABLE OF CONTENTS
.    EX EC UTIVE S U M M AR Y . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . ii
EX EC UTIVE S U M M AR Y . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . ii
.
4'
4'
      U1.1 Operations .................................................. 1
'
'
              U101             Cond uct of O perations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1
U1.1 Operations
.................................................. 1
U101
Cond uct of O perations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1
U102
Operational Status of. Facilities and Equipment . . . . . . . . . .
1
,
...
U103
Operations Procedures and Documentation
3
,
,
              U102            Operational Status of. Facilities and Equipment . . . . . . . . . . ...                          1
................
              U103            Operations Procedures and Documentation                          ................                3
;
                                                                                                                                        ,
U105
                                                                                                                                        l
Operator Training Qualification . . . . . . . . . . . . . . . . . . . . . . . . . 3
;            U105            Operator Training Qualification . . . . . . . . . . . . . . . . . . . . . . . . . 3
U108
              U108             Miscellaneous Operations issues . . . . . . . . . . . . . . . . . . . . . . . . 5
Miscellaneous Operations issues . . . . . . . . . . . . . . . . . . . . . . . . 5
1
1
i     U 1.ll M ainte na n c e . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 6
i
              U1 M2           Maintenance and Material Condition of Facilities and
U 1.ll M ainte na n c e . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 6
                              Equipment       .......................................                                         6
U1 M2
Maintenance and Material Condition of Facilities and
Equipment
6
.......................................
'
'
U 1.lli Enginee ring . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 7
'
'
      U 1.lli Enginee ring . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 7
U1 E1
              U1 E1           Conduct of Engineering               ..............................                               7
Conduct of Engineering
              U1 E2           Engineering Support of Facilities and Equipment . . . . . . . . . . . . . 9
7
                                                                                                                                        i
..............................
              U1 E8           Miscellaneous Engineering issues . . . . . . . . . . . . . . . . . . . . . . 11                         l
U1 E2
                                                                                                                                        :
Engineering Support of Facilities and Equipment . . . . . . . . . . . . . 9
                                                                                                                                        l
i
    S2.1 Operations       .................................................                                                   12      l
U1 E8
              U2 01           Conduct of Operations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 12                     !
Miscellaneous Engineering issues . . . . . . . . . . . . . . . . . . . . . . 11
,            U2 O2           Operational Status of Facilities and Equipment . . . . . . . . . . . . . 12                             )
S2.1 Operations
;             U2 08           Miscellaneous Operations issues . . . . . . . . . . . . . . . . . . . . . . . 14
12
      U 2.ll M ainte n a n c e . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 16
.................................................
j             U2 M8           Miscellaneous Maintenance issues .....................                                           16
U2 01
      U 2.lli Engine e ring . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17
Conduct of Operations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 12
              U2 E8           Miscellaneous Engineering issues . . . . . . . . . . . . . . . . . . . . . . 17
U2 O2
Operational Status of Facilities and Equipment . . . . . . . . . . . . . 12
)
,
;
U2 08
Miscellaneous Operations issues . . . . . . . . . . . . . . . . . . . . . . . 14
U 2.ll M ainte n a n c e . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 16
j
U2 M8
Miscellaneous Maintenance issues
16
.....................
U 2.lli Engine e ring . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17
U2 E8
Miscellaneous Engineering issues . . . . . . . . . . . . . . . . . . . . . . 17
i
i
4
4
      U3.1 Operations     .................................................                                                   20
U3.1 Operations
              U3 01           Conduct of Operations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 20
20
              U~s 03           Operations Procedures and Documentation                         ...............                 23
.................................................
              U3 07           Quality Assurance in Operations . . . . . . . . . . . . . . . . . . . . . . . 26
U3 01
i     U 3.11 M ain te n a n c e . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 27
Conduct of Operations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 20
              U3 M1           Conduct of Maintenance ............................                                             27
U~s 03
              U3 M8           Miscellaneous Maintenance issues .....................                                           29
Operations Procedures and Documentation
      U 3.Ill Engine e ring . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 31
23
              U3 E8           Miscellaneous Engineering issues . . . . . . . . . . . . . . . . . . . . . . 31
...............
      IV Plant Support     .................................................                                                   35
U3 07
              R1               Radiological Protection and Chemistry Controls ............                                     35
Quality Assurance in Operations . . . . . . . . . . . . . . . . . . . . . . . 26
              R8               Miscellaneous Radiological Protection and Chemistry issues                               ...     39
i
      V. M anage ment M eetings . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 39
U 3.11 M ain te n a n c e . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 27
              X1               Exit Meeting Summary . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 39
U3 M1
                                                                il
Conduct of Maintenance
                                                                                                                                    _
27
............................
U3 M8
Miscellaneous Maintenance issues
29
.....................
U 3.Ill Engine e ring . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 31
U3 E8
Miscellaneous Engineering issues . . . . . . . . . . . . . . . . . . . . . . 31
IV Plant Support
35
.................................................
R1
Radiological Protection and Chemistry Controls
35
............
R8
Miscellaneous Radiological Protection and Chemistry issues
39
...
V. M anage ment M eetings . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 39
X1
Exit Meeting Summary . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 39
il
_


    _ . . . . _ _ _ . _ ._ _-._ _._ _ ___.__._._ _ _._._                                                         ._ _
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. . . . _ _ _ . _ ._ _-._ _._ _ ___.__._._ _ _._._
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                                                                                            .
!
                                                                                                                      'l
                                                                                                                        !
4
4
  s                                                                                                                     !
!
                                                                                                                        ;
s
              -
;
i                                                            EXECUTIVE SUMMARY L
i
!                                                       Millstone Nuclear Power Station' .
EXECUTIVE SUMMARY L
                                            Combined inspection 245/97-01; 336/97-01; 423/97-01                         !
-
                                                                                                                        !
!
              Operations
Millstone Nuclear Power Station'
              *.
.
                                                                                                                        l
Combined inspection 245/97-01; 336/97-01; 423/97-01
                                                                                                                        '
!
                          Numerous inaccurate Personal Qualification Statements (Form 398) were identified
!
                          at all four Connecticut plants following NRC questions on two recent adverse                   :
Operations
                          condition reports. Approximately two thirds of the Personal Qualification                     !
* .
                          Statements submitted for recent license applicants were inaccurate. These                     ;
Numerous inaccurate Personal Qualification Statements (Form 398) were identified
                          applications resulted in the conduct of NRC license examinations and the issuance -           j
'
                          of licenses. In a significant number of cases, the licenses were issued without the.           .
at all four Connecticut plants following NRC questions on two recent adverse
                          candidates fully completing the licensee's training and qualification program, and in         j
:
                          a few cases the reactivity manipulations, specifically required by 10 CFR 55, were             i
condition reports. Approximately two thirds of the Personal Qualification
                          also not complete. This issue is unresolved for'each Millstone unit pending the
!
                          completion of the licensee investigation, resolution of allidentified deficiencies and         .
Statements submitted for recent license applicants were inaccurate. These
                          implementation of programmatic corrective actions. (Section U1.05.1)                           !
;
                                                                                                                        !
applications resulted in the conduct of NRC license examinations and the issuance -
                                                                                                                        '
j
              *          The degraded conditions found in the Unit 1 spent fuel pool are representative of a
of licenses. In a significant number of cases, the licenses were issued without the.
                          icng standing disregard for foreign material exclusion (FME) during the conduct of         .i
.
                          refuelmg fioor activities. Past low standards for FME control allowed the                     ,
candidates fully completing the licensee's training and qualification program, and in
                          accumulation of a large amount of debris, which could potentially have a significant         l
j
                        -impact on the fuel assemblies stored in the pool. Once the recovery organization               !
a few cases the reactivity manipulations, specifically required by 10 CFR 55, were
                          became aware of the extent of the problem, by reviewing video tapes, the                     i
i
                          inspectors noted a good response, including clear direction as to what needed to be           ,
also not complete. This issue is unresolved for'each Millstone unit pending the
                          done in the short term. Based on this information, the acceptability of the degraded         8
completion of the licensee investigation, resolution of allidentified deficiencies and
                          conditions in the spent fuel pool will be unresolved pending NRC review of the               ,
.
                          issues. (Section U1.02.1)                                                                     1
implementation of programmatic corrective actions. (Section U1.05.1)
              *-          At Unit 1, the licensee failed to evaluate and address a violation concerning the             ,
!
                          failure to prevent work which had the potential for draining the reactor vessel during         )
!
                          refueling. Further, the licensee failed to provide a comprehensive closure package -           I
The degraded conditions found in the Unit 1 spent fuel pool are representative of a
                          of a quality consistent =with the process committed to in December 1996. The
'
                        ' manner in which this issue was addressed provides evidence of the licensees ability
*
                          to perform effective reviews and to implement appropriate corrective' actions. As a
icng standing disregard for foreign material exclusion (FME) during the conduct of
                          result of the inspector's concerns with the quality of the completion packages, the
.i
                          licensee withdrew the NRC completion package schedule. A revised schedule was
refuelmg fioor activities. Past low standards for FME control allowed the
                          still in developmcat at the end of the inspection period. (Section U1.08.1)
,
              *            Although the Unit 2 backlog of 798 adverse condition reports (ACRs) that are
accumulation of a large amount of debris, which could potentially have a significant
                          greater than 120 days old indicates that timeliness for completing corrective actions
l
                          remains a concern, the reduction in the backlog of older ACRs from 940 to 798
-impact on the fuel assemblies stored in the pool. Once the recovery organization
                          since the last inspection period is a positive trend which reflects the licensee's
!
                          increased level of effort in this area. Timeliness and effectiveness of corrective             i
became aware of the extent of the problem, by reviewing video tapes, the
                          actions are areas '... which the licensee must demonstrate sustained improved                 l
i
                          performance. (Section U2.02.1)-                                                               l
inspectors noted a good response, including clear direction as to what needed to be
                                                                                                                          1
,
                                                                        iii                                              J
8
                                                                                                                          l
done in the short term. Based on this information, the acceptability of the degraded
                                                                                                                          i
conditions in the spent fuel pool will be unresolved pending NRC review of the
                                                                                                                          l
,
                                                                                                                        j
issues. (Section U1.02.1)
1
At Unit 1, the licensee failed to evaluate and address a violation concerning the
*-
,
failure to prevent work which had the potential for draining the reactor vessel during
refueling. Further, the licensee failed to provide a comprehensive closure package -
of a quality consistent =with the process committed to in December 1996. The
' manner in which this issue was addressed provides evidence of the licensees ability
to perform effective reviews and to implement appropriate corrective' actions. As a
result of the inspector's concerns with the quality of the completion packages, the
licensee withdrew the NRC completion package schedule. A revised schedule was
still in developmcat at the end of the inspection period. (Section U1.08.1)
Although the Unit 2 backlog of 798 adverse condition reports (ACRs) that are
*
greater than 120 days old indicates that timeliness for completing corrective actions
remains a concern, the reduction in the backlog of older ACRs from 940 to 798
since the last inspection period is a positive trend which reflects the licensee's
increased level of effort in this area. Timeliness and effectiveness of corrective
actions are areas '... which the licensee must demonstrate sustained improved
performance. (Section U2.02.1)-
l
iii
J
l
i
j


.
.
  *
A Unit 2 licensee event report discussed that while recovering from a loss of a
        A Unit 2 licensee event report discussed that while recovering from a loss of a
*
        direct current (dc) bus, an operator failed to enter an action statement when three
direct current (dc) bus, an operator failed to enter an action statement when three
        channels of wide range nuclear instrumentation were rendered inoperable. This was
channels of wide range nuclear instrumentation were rendered inoperable. This was
        characterized as a non-cited violation. The primary concern associated with this
characterized as a non-cited violation. The primary concern associated with this
        event was the fact that there was minimal procedural guidance provided to
event was the fact that there was minimal procedural guidance provided to
        operators to recover the loss of a de bus. The licensee is in the process of
operators to recover the loss of a de bus. The licensee is in the process of
        preparing 12 abnormal operating procedures for recovering various de buses and
preparing 12 abnormal operating procedures for recovering various de buses and
        distribution panels. This concern is being tracked by an unresolved item. (Section
distribution panels. This concern is being tracked by an unresolved item. (Section
        U2.02.2)
U2.02.2)
  *
In addition to the physical plant design controls, a longstanding NRC concern at Unit
        In addition to the physical plant design controls, a longstanding NRC concern at Unit
*
        2 is that operating procedures do not reflect the Final Safety Analysis Report
2 is that operating procedures do not reflect the Final Safety Analysis Report
        (FSAR), and an NRC open item has existed since 1993 to address this concern.
(FSAR), and an NRC open item has existed since 1993 to address this concern.
        This inspection report closes the old open item npqt because adequate corrective
This inspection report closes the old open item npqt because adequate corrective
        actions have been taken, but because this concern is being addressed and tracked
actions have been taken, but because this concern is being addressed and tracked
        by more recent items. The issue includes an evaluation of the procedure change
by more recent items. The issue includes an evaluation of the procedure change
        process, as well as the design control process, to ensure future operation is
process, as well as the design control process, to ensure future operation is
        conducted in accordance with the FSAR. (Section U2.08.1)
conducted in accordance with the FSAR. (Section U2.08.1)
  *
The procedure upgrade program has been effective in standardizing procedure
        The procedure upgrade program has been effective in standardizing procedure
*
        formats across the site. Because of the number of individuals involved in the
formats across the site. Because of the number of individuals involved in the
        procedure upgrades and the long period of time to complete the task, the quality of
procedure upgrades and the long period of time to complete the task, the quality of
        procedures vary substantially. As an adjunct to the Demand For Information
procedures vary substantially. As an adjunct to the Demand For Information
        process [10 CFR 50.54(f)], which incorporates a verification of the design and
process [10 CFR 50.54(f)], which incorporates a verification of the design and
        licensing bases, procedure accuracy will be verified. (Section U3 03)
licensing bases, procedure accuracy will be verified. (Section U3 03)
                                                                                                !
The licensee's root cause investigation and corrective action plan for control of high
  *
*
        The licensee's root cause investigation and corrective action plan for control of high
energy line break (HELB) doors were determined to be good. However, the
        energy line break (HELB) doors were determined to be good. However, the
requirement to label the required HELB doors with a minimum number of turns to
        requirement to label the required HELB doors with a minimum number of turns to
ensure proper latching should have been included in the adverse condition report
        ensure proper latching should have been included in the adverse condition report
corrective action plan if it was deemed necessary to prevent recurrence. (Section
        corrective action plan if it was deemed necessary to prevent recurrence. (Section       ;
U3.01.2)
        U3.01.2)                                                                               l
Good' contingency planning and appropriate consideration of the applicable standard
  *    Good' contingency planning and appropriate consideration of the applicable standard
*
        and regulations were in evidence for both planned operational evolutions and           !
and regulations were in evidence for both planned operational evolutions and
        emergent shutdown conditions. Where necessary to improve shutdown risk
emergent shutdown conditions. Where necessary to improve shutdown risk
        margins, temporary modifications or special system lineup were considered and well
margins, temporary modifications or special system lineup were considered and well
        controlled. The licensee development of a standardized approach for disseminating
controlled. The licensee development of a standardized approach for disseminating
        operations policy for interpreting the language and action statement applicability of   l
operations policy for interpreting the language and action statement applicability of
        the Unit 3 technical specifications appeared warranted. The examples noted during       l
the Unit 3 technical specifications appeared warranted. The examples noted during
        this period will be reviewed further as an inspector follow item. (Section U3.01.1)
this period will be reviewed further as an inspector follow item. (Section U3.01.1)
  Maintenance
Maintenance
  *    At Unit 1, the preparation and conduct of work associated with the entry and video
At Unit 1, the preparation and conduct of work associated with the entry and video
        survey of the reactor water cleanup (RWCU) demineralizer room were well
*
        controlled. The inspector noted that good radiological practices were used.
survey of the reactor water cleanup (RWCU) demineralizer room were well
                                                iv
controlled. The inspector noted that good radiological practices were used.
                                                                                              J
iv
J


  .
.
.
          The material condition in the room was acceptable and no deficiencies were
.
          identified. (Section U1.M2.1)
The material condition in the room was acceptable and no deficiencies were
    *
identified. (Section U1.M2.1)
          Maintenance and surveillance activities were performed professionally and
Maintenance and surveillance activities were performed professionally and
          thoroughly. All observed maintenance activities were performed with the work       l
*
          package or surveillance procedure present at the job site and personnel were noted
thoroughly. All observed maintenance activities were performed with the work
          to be closely following the procedures. Review of the surveillance procedures     ;
l
          revealed that the requirements of the applicable technical specifications were
package or surveillance procedure present at the job site and personnel were noted
                                                                                            '
to be closely following the procedures. Review of the surveillance procedures
          appropriately incorporated into the implementing procedure. (Section U3.M1.1)
revealed that the requirements of the applicable technical specifications were
    *
'
          The licensee developed a Fix-It-Now (FIN) multi-discipline work team approach to
appropriately incorporated into the implementing procedure. (Section U3.M1.1)
          augment the way maintenance is performed at the unit. This process is in addition
The licensee developed a Fix-It-Now (FIN) multi-discipline work team approach to
          to the normal work control process. The FIN work process is being implemented in
*
          a conservative manner. Any work required on protected train equipment was not
augment the way maintenance is performed at the unit. This process is in addition
          being assigned to the FIN team. All monitored work activities performed by the FIN
to the normal work control process. The FIN work process is being implemented in
          team were performed in accordance with the unit and station procedures. FIN team
a conservative manner. Any work required on protected train equipment was not
          members appeared to be well qualified. (Section U3.M1.1)                           1
being assigned to the FIN team. All monitored work activities performed by the FIN
    *
team were performed in accordance with the unit and station procedures. FIN team
          Plant inspection-tourt revealed improvements in the Unit 3 areas of housekeeping, i
members appeared to be well qualified. (Section U3.M1.1)
          material conditions, and work controls. Field observations raised no new
Plant inspection-tourt revealed improvements in the Unit 3 areas of housekeeping,
          unresolved safety issues, but did highlight the need for additional management
*
          attention to a previously identified concern regarding the control of temporary
material conditions, and work controls. Field observations raised no new
          equipment with the potential to adversely impact safety-related components. This
unresolved safety issues, but did highlight the need for additional management
          " Seismic II/l" issue will be tracked as an inspector follow item and will receive
attention to a previously identified concern regarding the control of temporary
          further evaluation as a "significant item" in the NRC Restart Assessment Plan.
equipment with the potential to adversely impact safety-related components. This
          (U3.M8.1 )
" Seismic II/l" issue will be tracked as an inspector follow item and will receive
    Engineering
further evaluation as a "significant item" in the NRC Restart Assessment Plan.
    *    A review was performed at Unit 1 of the licensee's progress in resolution of the
(U3.M8.1 )
          Unresolved Safety issue (USI) A-46 outliers documented in the Licensee Event
Engineering
          Report (LER) 96-003, Rev. 2. These deficiencies involved inadequate anchorage of
A review was performed at Unit 1 of the licensee's progress in resolution of the
          the emergency diesel generator day tank and the turbine building secondary closed
*
          cooling water air coolers. The regulatory requirements for reportability were met
Unresolved Safety issue (USI) A-46 outliers documented in the Licensee Event
          and the corrective action prescribed in the LER were adequate in general, based on
Report (LER) 96-003, Rev. 2. These deficiencies involved inadequate anchorage of
          the detailed walkdown of the A-46 modifications, the inspector concluded that the
the emergency diesel generator day tank and the turbine building secondary closed
          licensee performed a substantial number of field modifications to accommodate the
cooling water air coolers. The regulatory requirements for reportability were met
          seismic loading on mechanical and electrical equipment identified in the USl A-46
and the corrective action prescribed in the LER were adequate in general, based on
          scope and documented in LER 96-003; this LER is closed. The followup of the
the detailed walkdown of the A-46 modifications, the inspector concluded that the
          licensee's commitments to resolve the A-46 program outliers prior to startup for
licensee performed a substantial number of field modifications to accommodate the
          cycle 16 operation and the assessment of the implication of this event on the
seismic loading on mechanical and electrical equipment identified in the USl A-46
          operation of Unit 1 will be unresolved pending further NRC review. (Section
scope and documented in LER 96-003; this LER is closed. The followup of the
          U 1.E1.1 )
licensee's commitments to resolve the A-46 program outliers prior to startup for
    *    The corrective actions taken by the Unit 1 Cnmponent Engineering
cycle 16 operation and the assessment of the implication of this event on the
          Services / Nondestructive Test Engineering (CES/NTE) concerning the use of test
operation of Unit 1 will be unresolved pending further NRC review. (Section
          equipment was acceptable. The corrective actions appeared to be broad-based. A
U 1.E1.1 )
          majority of the short term corrective actions were complete, and the long term
The corrective actions taken by the Unit 1 Cnmponent Engineering
                                                  v
*
Services / Nondestructive Test Engineering (CES/NTE) concerning the use of test
equipment was acceptable. The corrective actions appeared to be broad-based. A
majority of the short term corrective actions were complete, and the long term
v


    ._   - -                 .--                 .   -     .   -.       .-               - _.     .
._
                                                                                                        '
- -
.--
.
-
.
-.
.-
- _.
.
'
4
4
  .
.
                corrective actions were being tracked for closure., The significance of the UT
corrective actions were being tracked for closure., The significance of the UT
            -
-
                instruments being past their calibration due dates was minimal because they were
instruments being past their calibration due dates was minimal because they were
              . subsequently found to be within tolerance. (Section U1.E2.1)
. subsequently found to be within tolerance. (Section U1.E2.1)
a      *        The NRC is concerned about the operation of the new containment isolation check
The NRC is concerned about the operation of the new containment isolation check
                valve 1-CU-29 at Unit 1, which is operating with lower than expected flow rates
a
                during this extended shutdown. While the use of non-intrusive check valve testing
*
                has verified that the check valve is backseated, this is a short term indication. The
valve 1-CU-29 at Unit 1, which is operating with lower than expected flow rates
                long term effects of the low flow operation have yet to be determined. This issue is
during this extended shutdown. While the use of non-intrusive check valve testing
                unresolved pending the NRC review of the licensee's final determination of the
has verified that the check valve is backseated, this is a short term indication. The
                operability of the valve prior to plant startup. (Section U1.E2.2)
long term effects of the low flow operation have yet to be determined. This issue is
      *        The inspectors found that overlap test reviews performed in 1993 were not               !
unresolved pending the NRC review of the licensee's final determination of the
                adequate. The licensee failed to identify this deficiency and improperly concluded
operability of the valve prior to plant startup. (Section U1.E2.2)
                that the 1993 reviews accomplished the actions requested by NRC Generic Letter
The inspectors found that overlap test reviews performed in 1993 were not
                96-01, " Testing Of Safety-Related Logic Circuits." (Section U3.E8.1)
*
                                                                                                        t
adequate. The licensee failed to identify this deficiency and improperly concluded
      Plant Support
that the 1993 reviews accomplished the actions requested by NRC Generic Letter
      *
96-01, " Testing Of Safety-Related Logic Circuits." (Section U3.E8.1)
                The licensee has demonstrated a significant increase in management attention
t
                towards work control and maintaining occupational exposures as low as is
Plant Support
                reasonably achievable. However, two of the licensee's activities were determined
The licensee has demonstrated a significant increase in management attention
                not to be in compliance with NRC regulations. The Unit 1 violation involves a long-
*
                standing situation (since initial plant start-up), concerning an unmonitored release
towards work control and maintaining occupational exposures as low as is
                pathway in the ventilation system for the radwaste storage building. The violation
reasonably achievable. However, two of the licensee's activities were determined
                at Unit 2 involves a failure to adhere to the licensee's radiation protection program
not to be in compliance with NRC regulations. The Unit 1 violation involves a long-
                concerning proper use of electronic dosimeters. (Section R1)                             !
standing situation (since initial plant start-up), concerning an unmonitored release
                                                                                                        I
pathway in the ventilation system for the radwaste storage building. The violation
                                                                                                        l
at Unit 2 involves a failure to adhere to the licensee's radiation protection program
                                                                                                        I
concerning proper use of electronic dosimeters. (Section R1)
                                                                                                        :
vi
                                                        vi


-                                                     -       -
-
  .
-
                                            Report Details
-
    Summarv of Plant Status                                                                         I
.
    Unit 1 remained in an extended outage for the duration of the inspection period. The
Report Details
    licensee continues to implement configuration management program activities, engineering
Summarv of Plant Status
    reviews, and docketed correspondence assessments to verify compliance with the
Unit 1 remained in an extended outage for the duration of the inspection period. The
    established design and licensing basis of the unit. The successful completion of these
licensee continues to implement configuration management program activities, engineering
    activities is required by NRC order prior to restart of the unit. During this period, the         .
reviews, and docketed correspondence assessments to verify compliance with the
    licensee implemented a major revision to the corrective action procedure. The goal was to       I
established design and licensing basis of the unit. The successful completion of these
    simplify the process, and at the same time make it more responsive towards restart and           l
activities is required by NRC order prior to restart of the unit. During this period, the
    needed organizational improvements. Under the new process, " condition reports" have
.
    replaced " adverse condition reports" to capture both the regulatory defined adverse
licensee implemented a major revision to the corrective action procedure. The goal was to
    condition, as well as other conditions that do not meet managements expectations.
simplify the process, and at the same time make it more responsive towards restart and
                                                                                                      l
needed organizational improvements. Under the new process, " condition reports" have
    The licensee has recently made two changes to the organizational structure at Unit 1. A           ,
replaced " adverse condition reports" to capture both the regulatory defined adverse
    project management group was established to facilitate the implementation of plant               j
condition, as well as other conditions that do not meet managements expectations.
    modifications prior to startup. Additionally, a restart manager was selected to oversee         j
The licensee has recently made two changes to the organizational structure at Unit 1. A
    completion of the Operational Readiness Plan, which will be used to identify and control         i
project management group was established to facilitate the implementation of plant
    the actions necessary to achieve and maintain improved performance. The restart manager         l
j
    will also be responsible for the review of corrective action completion packages, which will
modifications prior to startup. Additionally, a restart manager was selected to oversee
    provide objective evidence of corrective action completion. Section U1.08.1 & U1.E8.1 of
j
    this report provides an assessment of the licensee's progress in the area of completion
completion of the Operational Readiness Plan, which will be used to identify and control
                                                          -
i
    package development. The effectiveness of these changes, as well as the new corrective
the actions necessary to achieve and maintain improved performance. The restart manager
    action program, will be assessed as part of future NRC inspections.
will also be responsible for the review of corrective action completion packages, which will
                                            U1.1 Operations
provide objective evidence of corrective action completion. Section U1.08.1 & U1.E8.1 of
    U101           Conduct of Operations
this report provides an assessment of the licensee's progress in the area of completion
    01.1 General Comments (71707)
-
    Using Inspection Procedure 71707, the inspectors conducted frequent reviews of ongoing
package development. The effectiveness of these changes, as well as the new corrective
    plant operations. The inspectors reviewed operability determinations, availability
action program, will be assessed as part of future NRC inspections.
    determinations, and witnessed the conduct of management review team discussions
U1.1 Operations
    regarding the disposition and closure of condition reports (CRs). During a routine tour of
U101
    the Unit 1 intake structure, the inspector found the material condition of systems and
Conduct of Operations
    components to be adequate. The licensee initiated a material condition improvement
01.1 General Comments (71707)
    project in the Spring of 1996. The inspector observed some material improvement work
Using Inspection Procedure 71707, the inspectors conducted frequent reviews of ongoing
    on-going. Specific events and noteworthy observations are detailed in the sections below.
plant operations. The inspectors reviewed operability determinations, availability
    U102           Operational Status of Facilities and Equipment
determinations, and witnessed the conduct of management review team discussions
    O 2.1 Soent Fuel Pool Cleanliness
regarding the disposition and closure of condition reports (CRs). During a routine tour of
    a.     Inspection Scope (71707)
the Unit 1 intake structure, the inspector found the material condition of systems and
    NRC inspection report 245/96-08, dated December 3,1996, discussed the continued
components to be adequate. The licensee initiated a material condition improvement
    identification of discrepant conditions in the spent fuel pool, indicating a need to accelerate
project in the Spring of 1996. The inspector observed some material improvement work
    the evaluation portion of the spent fuel pool cleanup / recovery plan. At that time, the
on-going. Specific events and noteworthy observations are detailed in the sections below.
U102
Operational Status of Facilities and Equipment
O 2.1 Soent Fuel Pool Cleanliness
a.
Inspection Scope (71707)
NRC inspection report 245/96-08, dated December 3,1996, discussed the continued
identification of discrepant conditions in the spent fuel pool, indicating a need to accelerate
the evaluation portion of the spent fuel pool cleanup / recovery plan. At that time, the


        _m   .                   .   ___         ...           _       . _ . __   ._     _.
_m
                                                                                                          1
.
  -                                                                                                     I
.
___
...
_
. _ . __
._
_.
1
-
,
2
1
-inspectors concluded that all discrepant conditions warrant identification and evaluation in
,
,
                                                                                                          l
the short term to ensure the collective impact of these issues were addressed. On January
                                                        2                                                !
;
                                                                                                          1
10,1997, the inspectors reviewed a video tape surveillance of the spent fuel pool
,    -inspectors concluded that all discrepant conditions warrant identification and evaluation in
conducted on January 3, using an under water camera. The video tapes were reviewed to
      the short term to ensure the collective impact of these issues were addressed. On January           ;
J
      10,1997, the inspectors reviewed a video tape surveillance of the spent fuel pool                 l
evaluate the conditions in the spent fuel pool including the fuel storage racks and stored
      conducted on January 3, using an under water camera. The video tapes were reviewed to             J
fuel bundles.
      evaluate the conditions in the spent fuel pool including the fuel storage racks and stored
b.
      fuel bundles.
Observations and Findinas
      b.       Observations and Findinas
As discussed in NRC report 245/96-08, the earlier video tapes identified improperly seated
      As discussed in NRC report 245/96-08, the earlier video tapes identified improperly seated         )
)
      fuel bundles. In light of the recent video surveys, the licensee determined that the               ;
fuel bundles. In light of the recent video surveys, the licensee determined that the
      improperly seated bundles were caused by one of three conditions: 1) There are 55 fuel             '
improperly seated bundles were caused by one of three conditions: 1) There are 55 fuel
      bundles elevated as a result of their channel fasteners being caught on the spent fue!            ,
      racks; 2) 14 fuel bundles are elevated due to unknown reasons, although it is suspected            )
:      that debris is in the fuel rack preventing proper seating; 3) One additional fuel bundle was      ;
      resting on a 1/4 inch metal tube (suspected to be a boron tube from a control rod blade            ]
      segment) that is lying on the floor liner and bends upward into the bottom of the fuel            1
'
      storage cell. An evaluation was performed to address all relevant issues including: the          J
,      effect of a bundle drop on the fuel bundle itself, the fuel rack, and spent fuel pool liner;
i      seismic response of the fuel racks; the criticality margin; fuel assembly cooling; and water
i      shielding. The licensee concluded that the storage racks that contained elevated fuel            ;
      assemblies were operable, but were not full qualified, since the fuel assemblies were not
'
'
      fully seated. In response to this concern, procedural controls were put in place to ensure
bundles elevated as a result of their channel fasteners being caught on the spent fue!
      that no fuel assemblies are transferred within the spent fuel pool until all fuel is fully       .
,
      seated.
racks; 2) 14 fuel bundles are elevated due to unknown reasons, although it is suspected
      The video tapes also revealed a significant amount of debris on the fuel bundles, fuel           {
)
      racks, and the floor of the fuel pool. The debris included rope, cable, boron tubes, a broom   f 4
:
      head, filter hoses, nuts, and unidentifiable objects. In addition, the bottom of the fuel pool
that debris is in the fuel rack preventing proper seating; 3) One additional fuel bundle was
      was covered by a layer of sediment. Additionally, the viden ^) view identified that the
;
      velocity limiter portion cf '.our control rod blade assemblies vere stored vertically on top of
resting on a 1/4 inch metal tube (suspected to be a boron tube from a control rod blade
      one another without support. The velocity limiter sections were located on the spent fuel         i
]
      pool floor in the space between a spent fuel rack and the control rod blade storage rack.         I
segment) that is lying on the floor liner and bends upward into the bottom of the fuel
      An engineering evaluation of the velocity limiter storage configuration concluded that the
1
      structural integrity of the spent fuel rack, the control rod blade storage rack, and the pool
storage cell. An evaluation was performed to address all relevant issues including: the
      liner would be maintained in the event of an impact caused by the velocity limiters falling
J
      over.
'
      A dent was identified in the spent fuel pool floor liner from an impact of an unknown
effect of a bundle drop on the fuel bundle itself, the fuel rack, and spent fuel pool liner;
      object. The dent was approximately 4 inches in diameter and was relatively uniform and
,
        smooth, with no obvious nicks or gouges. A final operability determination and safety
i
        evaluation concluded that there were no operability or safety issues, and that the dent did       l
seismic response of the fuel racks; the criticality margin; fuel assembly cooling; and water
        not challenge the leak tightness or structural integrity of the fuel pool.                       j
i
        A previously known condition concerning the storage of a damaged, irradiated fuel                 i
shielding. The licensee concluded that the storage racks that contained elevated fuel
        assemble stored in a " damaged fuel container," was roviewed to consider the collective           l
;
        impact of this issue and the other fuel pool discrepan:les. The fuel assemble was
assemblies were operable, but were not full qualified, since the fuel assemblies were not
        damaged in 1974, placed in a storage container in 1976, and moved to its current location
fully seated. In response to this concern, procedural controls were put in place to ensure
'
that no fuel assemblies are transferred within the spent fuel pool until all fuel is fully
.
seated.
The video tapes also revealed a significant amount of debris on the fuel bundles, fuel
{
racks, and the floor of the fuel pool. The debris included rope, cable, boron tubes, a broom
f
4
head, filter hoses, nuts, and unidentifiable objects. In addition, the bottom of the fuel pool
was covered by a layer of sediment. Additionally, the viden ^) view identified that the
velocity limiter portion cf '.our control rod blade assemblies vere stored vertically on top of
one another without support. The velocity limiter sections were located on the spent fuel
i
pool floor in the space between a spent fuel rack and the control rod blade storage rack.
An engineering evaluation of the velocity limiter storage configuration concluded that the
structural integrity of the spent fuel rack, the control rod blade storage rack, and the pool
liner would be maintained in the event of an impact caused by the velocity limiters falling
over.
A dent was identified in the spent fuel pool floor liner from an impact of an unknown
object. The dent was approximately 4 inches in diameter and was relatively uniform and
smooth, with no obvious nicks or gouges. A final operability determination and safety
evaluation concluded that there were no operability or safety issues, and that the dent did
not challenge the leak tightness or structural integrity of the fuel pool.
j
A previously known condition concerning the storage of a damaged, irradiated fuel
i
assemble stored in a " damaged fuel container," was roviewed to consider the collective
impact of this issue and the other fuel pool discrepan:les. The fuel assemble was
damaged in 1974, placed in a storage container in 1976, and moved to its current location


          . ~-               ..     -             -                   .         .             .     - .
. ~-
    ,
..
  ..
-
-
.
.
.
- .
,
..
i
i
i
i                                                        3
3
        in 1989. The licensee performed a safety evaluation, as part of an operability
in 1989. The licensee performed a safety evaluation, as part of an operability
"i
"i
        determination, that addressed the storage configuration of the damaged fuel container and
determination, that addressed the storage configuration of the damaged fuel container and
its location in the control rod storage rack. Similar to the unseated bundles, criticality,
<
<
          its location in the control rod storage rack. Similar to the unseated bundles, criticality,
seismic response, water shielding, and decay heat removal were evaluated. Based on that
'
'
          seismic response, water shielding, and decay heat removal were evaluated. Based on that
evaluation, the licensee concluded that the storage configuration is safe and does not
          evaluation, the licensee concluded that the storage configuration is safe and does not
constitute an unreviewed safety question. In addition, a procedural restriction was placed
          constitute an unreviewed safety question. In addition, a procedural restriction was placed
in procedure EN 1067, Supplemental Procedure for Inventory and Control of Special
          in procedure EN 1067, Supplemental Procedure for Inventory and Control of Special
Nuclear Material, to prevent storing fuelin locations adjacent to the damaged fuel
          Nuclear Material, to prevent storing fuelin locations adjacent to the damaged fuel
assembly. This was required since the criticality margin for storage of fuel assemblies in
          assembly. This was required since the criticality margin for storage of fuel assemblies in
adjacent rack locations has not been fully evaluated and full qualification has not been
          adjacent rack locations has not been fully evaluated and full qualification has not been
verified,
          verified,
c.
          c.       Conclusions
Conclusions
        The inspectors concluded that the degraded conditions in the spent fuel pool are                   ,
The inspectors concluded that the degraded conditions in the spent fuel pool are
          representative of a long standing lack of concern for fore:gn material exclusion (FME)             '
,
.        during the conduct of refueling floor activities. Past low standards for FME control allowed
representative of a long standing lack of concern for fore:gn material exclusion (FME)
'
during the conduct of refueling floor activities. Past low standards for FME control allowed
.
the accumulation of a large amount of debris, which could potentially have a significant
4
4
          the accumulation of a large amount of debris, which could potentially have a significant
i '
i'
impact en the fuel assemblies stored in the pool. Once the recovery organization became
          impact en the fuel assemblies stored in the pool. Once the recovery organization became
aware of the extent of the problem, by reviewing the video tapes, the inspectors noted a
,
#
#
          aware of the extent of the problem, by reviewing the video tapes, the inspectors noted a          ,
good resoonse, including clear direction as to what needed to be done in the short term.
          good resoonse, including clear direction as to what needed to be done in the short term.         ,
,
;         The appropriate operability determinations and safety evaluations were prepared, and
;
          adverse condition reports were initiated to document the findings.
The appropriate operability determinations and safety evaluations were prepared, and
          In a letter to the NRC dated February 21,1997, the licensee documented the current
adverse condition reports were initiated to document the findings.
          conditions in the spent fuel pool and their future plans for correcting the adverse
In a letter to the NRC dated February 21,1997, the licensee documented the current
conditions in the spent fuel pool and their future plans for correcting the adverse
, conditions. Prior to core reload all unseated fuel assemblies will be properly seated and all
'
'
        , conditions. Prior to core reload all unseated fuel assemblies will be properly seated and all
-
      -
new and reload fuel bundles will be visually inspected from below to check for foreign -
          new and reload fuel bundles will be visually inspected from below to check for foreign -
material before placement in the core. The licensee committed to cleaning up the pool,
          material before placement in the core. The licensee committed to cleaning up the pool,
including removal of debris and various used components, prior to Refueling Outage 16.
          including removal of debris and various used components, prior to Refueling Outage 16.
Based on this information, the acceptability of the degraded conditions in the spent fuel
          Based on this information, the acceptability of the degraded conditions in the spent fuel
_
_         pool will be unresolved (URI 245/97-01-01) pending NRC review of the issues and the
pool will be unresolved (URI 245/97-01-01) pending NRC review of the issues and the
l         completion of the licensee's root cause analysis.
l
          U103           Operations Procedures and Documentation
completion of the licensee's root cause analysis.
          03.1 Operations Procedures
U103
          During May and June,1996, two Unit 1 Operations department staff engineers performed
Operations Procedures and Documentation
          a self assessment of the Procedure Upgrade Program (PUP) for Unit 1 Operations
03.1 Operations Procedures
          procedures. The Unit 1 operations self-assessment contained a significant number of
During May and June,1996, two Unit 1 Operations department staff engineers performed
          negative findings concerning the Unit 1 PUP process for the Operations Department and for
a self assessment of the Procedure Upgrade Program (PUP) for Unit 1 Operations
          the quality of the upgraded procedures produced. The inspector discussed this assessment
procedures. The Unit 1 operations self-assessment contained a significant number of
          with one of the staff engineers and the Unit 1 Operations Manager. Although the
negative findings concerning the Unit 1 PUP process for the Operations Department and for
          assessment applied to Unit 1 only, the Unit 1 Operations Manager stated that he would
the quality of the upgraded procedures produced. The inspector discussed this assessment
          share the self assessment results with other Unit 1 Departments and with the operations
with one of the staff engineers and the Unit 1 Operations Manager. Although the
          managers of the other Millstone units. The licensee's resolution of the problems identified
assessment applied to Unit 1 only, the Unit 1 Operations Manager stated that he would
share the self assessment results with other Unit 1 Departments and with the operations
managers of the other Millstone units. The licensee's resolution of the problems identified


  _. _     _   _         .       . _ _                                                       _   _ _ . _ .
_. _
        ,
_
                                                                                                                    >
_
        '
.
                                                                                                                    )
. _ _
                                                                                                                    i
_
_ _ . _ .
,
>
'
)
i
4
i
.
.
                                                          4                                                        i
)
                                                                                                                    )
in the Unit 1 self assessment are unresolved (URI 97-01-02) pending the NRC's review of
          in the Unit 1 self assessment are unresolved (URI 97-01-02) pending the NRC's review of
the associated corrective actions.
,
,
          the associated corrective actions.
#
#
          U105           Operator Training Qualification
U105
Operator Training Qualification
e
e
!         05.1 Inaccuracies in Personal Qualification Statements Certifications
!
)         a.       Inspection Scope
05.1 Inaccuracies in Personal Qualification Statements Certifications
!         Two adverse condition reports (ACRs) were initiated to address operator license training -
)
          related deficiencies. The ACRs document the failure of license candidates to complete all
a.
;         classes, on the job training (OJT), and on shift watch standing time, along with the failure             l
Inspection Scope
          to comply with procedures resulting in weaknesses in the systematic approach to training.               >
!
i         The issues were identified as a result of preliminary findings and insights gained from an
Two adverse condition reports (ACRs) were initiated to address operator license training -
j         independent root cause investigation to address poor candidate performance during a                     f
related deficiencies. The ACRs document the failure of license candidates to complete all
:         recent Millstone Unit 1 initial license examination. The inspectors reviewed the short term             1
;
!         actions taken in response to these two ACRs. The reviews focused on the accuracy of
classes, on the job training (OJT), and on shift watch standing time, along with the failure
to comply with procedures resulting in weaknesses in the systematic approach to training.
>
i
The issues were identified as a result of preliminary findings and insights gained from an
j
independent root cause investigation to address poor candidate performance during a
f
:
recent Millstone Unit 1 initial license examination. The inspectors reviewed the short term
1
!
actions taken in response to these two ACRs. The reviews focused on the accuracy of
;
;
          Personal Qualification Statements (Form 398) submitted to the NRC staff as an application
Personal Qualification Statements (Form 398) submitted to the NRC staff as an application
:         for an operators license. The Form 398 contains assertions by the applicant, the training                 l
:
,        coordinator and senior management representative on site, that among other things, the                   l
for an operators license. The Form 398 contains assertions by the applicant, the training
          applicant completed the licensee's requirements to be a licensed operator.                              ]
coordinator and senior management representative on site, that among other things, the
,
}
}
i~
applicant completed the licensee's requirements to be a licensed operator.
          b.       Observations and Findinas
]
i
~
b.
Observations and Findinas
i
-
-
                                                                                                                    i
During the review subsequent to the initiation of the ACRs, the licensee identified
          During the review subsequent to the initiation of the ACRs, the licensee identified
numerous discrepancies which resulted in inaccurate Personal Qualification Statements
-
-
          numerous discrepancies which resulted in inaccurate Personal Qualification Statements
;
;          (Form 398). In some cases, the errors resulted in candidates not meeting the licensee's.
(Form 398). In some cases, the errors resulted in candidates not meeting the licensee's.
          minimum program requirements prior to signing of the 398 forms; however, the necessary               e. .
minimum program requirements prior to signing of the 398 forms; however, the necessary
j         training was completed prior to the license examination. In other cases, the candidates
e. .
          were issued licenses without the program requirements being met. The discrepancies
j
          include failure to complete the required on shift watchstanding time, OJT, and the required
training was completed prior to the license examination. In other cases, the candidates
i         number of reactivity manipulations, in addition, several candidates failed to meet the
were issued licenses without the program requirements being met. The discrepancies
include failure to complete the required on shift watchstanding time, OJT, and the required
i
number of reactivity manipulations, in addition, several candidates failed to meet the
*
*
          program prerequisites such as technical degree or additional experience requirements.
program prerequisites such as technical degree or additional experience requirements.
:
At Millstone Unit 1, the four most recent license classes were reviewed by the licensee, in
the two most recent classes,12 of 13 candidates submitted inaccurate 398 forms. In the
i
two prior classes, only 1 of 9 candidate's 398 form was inaccurate. Most of the
}
discrepancies involved the failure to complete required under-instruction watches, but also
included the failure to complete the required OJT. In the worst case, the candidate
completed little more than 3 of the required 13 weeks of OJT specified by the training
program description.
:
:
          At Millstone Unit 1, the four most recent license classes were reviewed by the licensee, in
At Millstone Unit 2, a review of the two most recent license classes revealed 14 out of 16
          the two most recent classes,12 of 13 candidates submitted inaccurate 398 forms. In the
candidates submitted inaccurate 398 forms. These discrepancies generally consisted of
i          two prior classes, only 1 of 9 candidate's 398 form was inaccurate. Most of the
insufficient hours of under-instruction watchstanding, but also included one case of
}          discrepancies involved the failure to complete required under-instruction watches, but also
.
            included the failure to complete the required OJT. In the worst case, the candidate
insufficient reactivity manipulations and two cases in which OJT records appear to be lost.
            completed little more than 3 of the required 13 weeks of OJT specified by the training
            program description.
:          At Millstone Unit 2, a review of the two most recent license classes revealed 14 out of 16
            candidates submitted inaccurate 398 forms. These discrepancies generally consisted of
.          insufficient hours of under-instruction watchstanding, but also included one case of
            insufficient reactivity manipulations and two cases in which OJT records appear to be lost.
4
4
e
e


    .
.
                                                                                                      l
l
  -                                                                                                   :
-
                                                    5
5
      At Millstone Unit 3, the review of the most recent license class revealed 3 of 10 of the
At Millstone Unit 3, the review of the most recent license class revealed 3 of 10 of the
      candidates submitted inaccurate 398 forms. These discrepancies included one missed
candidates submitted inaccurate 398 forms. These discrepancies included one missed
      under-instruction watch, one case of insufficient reactivity manipulations and the failure to
under-instruction watch, one case of insufficient reactivity manipulations and the failure to
      meet the program prerequisites, and one case in which OJT requirements were
meet the program prerequisites, and one case in which OJT requirements were
      accomplished after the assertion that all training program requirements were completed on
accomplished after the assertion that all training program requirements were completed on
      the 398 form.
the 398 form.
      At Connecticut Yankee, the review of the most recent license class revealed 10 out 12
At Connecticut Yankee, the review of the most recent license class revealed 10 out 12
      candidates submitted inaccurate 398 forms. These discrepancies included insufficient
candidates submitted inaccurate 398 forms. These discrepancies included insufficient
      hours of under-instruction watchstanding, insufficient reactivity manipulations in two
hours of under-instruction watchstanding, insufficient reactivity manipulations in two
      cases, and program prerequisites not met in two cases. Additionally, OJT records were
cases, and program prerequisites not met in two cases. Additionally, OJT records were
      lost or signed after the 398 was completed.
lost or signed after the 398 was completed.
                                                                                                      1
On March 3,1997, the licensee issued a letter to the NRC staff to discussing these issues.
      On March 3,1997, the licensee issued a letter to the NRC staff to discussing these issues.     I
Subsequently, the NRC staff issued a confirmatory action letter. The reviews are being
      Subsequently, the NRC staff issued a confirmatory action letter. The reviews are being
'
                                                                                                      '
expanded on Millstone Unit 3 and Connecticut Yankee. Millstone Unit 2 is still evaluating
      expanded on Millstone Unit 3 and Connecticut Yankee. Millstone Unit 2 is still evaluating       ;
if review scope expansion is warranted and Millstone Unit 1 is preparing a position that
      if review scope expansion is warranted and Millstone Unit 1 is preparing a position that       '
'
      additional expansion is not necessary. The licensee has removed numerous individuals
additional expansion is not necessary. The licensee has removed numerous individuals
      from watchstanding duties and requested the withdrawal of two licenses. However, in the         l
from watchstanding duties and requested the withdrawal of two licenses. However, in the
      case of Millstone Unit 2, some licensed operators removed frorn watchstanding duties have       I
case of Millstone Unit 2, some licensed operators removed frorn watchstanding duties have
      been restored to an active status following the completion of missed requirements. The
been restored to an active status following the completion of missed requirements. The
      licensee believes the majority of the discrepancies can be attributed to unclear
licensee believes the majority of the discrepancies can be attributed to unclear
      expectations on program requirements, the failure to maintain the programs currer t using       i
expectations on program requirements, the failure to maintain the programs currer t using
      the systems approach to training, and poor record keeping practices. All of the fctors are   ~!
the systems approach to training, and poor record keeping practices. All of the fctors are
      the result of inadequate management oversight.
~!
      c.     Conclusion
the result of inadequate management oversight.
      The licensee identified numerous inaccurate Personal Qualification Statements (Form 398)
c.
      following NRC questions on two recent ACRs. Approximately two thirds of the Personal
Conclusion
      Qualification Statements submitted for recent license applicants were inaccurate. These
The licensee identified numerous inaccurate Personal Qualification Statements (Form 398)
      applications resulted in the conduct of NRC license examinations and the issuance of
following NRC questions on two recent ACRs. Approximately two thirds of the Personal
      licensees. In a significant number of cases, the licenses were issued without the
Qualification Statements submitted for recent license applicants were inaccurate. These
      candidates completing the licensee's training and qualification program, and in a few cases
applications resulted in the conduct of NRC license examinations and the issuance of
      the reactivity manipulations, specifically required by 10 CFR 55, were also not complete.
licensees. In a significant number of cases, the licenses were issued without the
      This issue is unresolved (URI 245,336,423/97-01-03) pending the completion of the
candidates completing the licensee's training and qualification program, and in a few cases
      licensee's investigation, resolution of allidentified deficiencies and implementation of
the reactivity manipulations, specifically required by 10 CFR 55, were also not complete.
      programmatic corrective actions.
This issue is unresolved (URI 245,336,423/97-01-03) pending the completion of the
      U108           Miscellaneous Operations issues (92700)
licensee's investigation, resolution of allidentified deficiencies and implementation of
      08.1 (Undate) Violation 50-245/95-42-01: Failure to Prevent Work Which Had the
programmatic corrective actions.
              Potential for Drainina the Reactor Vessel Durina Fuel Movements
U108
      This violation concerned the failure to prevent work which had the potential for draining
Miscellaneous Operations issues (92700)
      the reactor vessel while fuel removal was in progress. In addition, the licensee does not
08.1 (Undate) Violation 50-245/95-42-01: Failure to Prevent Work Which Had the
      have a formal process to ensure all applicable technical specifications are properly
Potential for Drainina the Reactor Vessel Durina Fuel Movements
      implemented during refueling. Further, based on the inspector's review of the licensing
This violation concerned the failure to prevent work which had the potential for draining
the reactor vessel while fuel removal was in progress. In addition, the licensee does not
have a formal process to ensure all applicable technical specifications are properly
implemented during refueling. Further, based on the inspector's review of the licensing
 
,
.
.. ,_ __
_ - - . . _
_
_ __
___
_
_
_
 
_
          .. ,_ __                        _      _ __                        _  _      ___       . _ _ _ .
___
    , .                    _ - - . . _                        ___    _
. _ _ _
    .
.
.
d
d
-
-
                                                          6
6
.
.
bases for the current Technical Specification 3.5.F 7, it did not appear that the conditions
j
.
.
          bases for the current Technical Specification 3.5.F 7, it did not appear that the conditions          j
;
;        . initially established and reviewed by the NRC were appropriately maintained during                 s"
. initially established and reviewed by the NRC were appropriately maintained during
          subsequent amendments.
s"
;         The licensee developed a process for preparation of corrective action completion packages
subsequent amendments.
:         and a schedule for providing them to the NRC, as a result of a previous NRC request. The
;
          inspector reviewed the first corrective action completion package prepared to address the
The licensee developed a process for preparation of corrective action completion packages
          three issues discussed above. The documentation package contained a root cause analysis               !
:
and a schedule for providing them to the NRC, as a result of a previous NRC request. The
inspector reviewed the first corrective action completion package prepared to address the
three issues discussed above. The documentation package contained a root cause analysis
-(RCA), license event report, and a violation response, which were developed to address the
3
3
        -(RCA), license event report, and a violation response, which were developed to address the
issues. However, these documents were not consistent with each other and generally did
          issues. However, these documents were not consistent with each other and generally did
not address the cited violation. The identified causes and many of the corrective actions,
          not address the cited violation. The identified causes and many of the corrective actions,
address maintenance and planning issues that led to the unplanned draining of a small
          address maintenance and planning issues that led to the unplanned draining of a small
amount of reactor water during maintenance on a recirculation discharge valve. The RCA
i        amount of reactor water during maintenance on a recirculation discharge valve. The RCA
i
appears to have been performed prior to the licensee's acknowledgment of the technical
'
'
          appears to have been performed prior to the licensee's acknowledgment of the technical                ,
,
          specification compliance issue. The majority of the corrective actions specified, involve             I
specification compliance issue. The majority of the corrective actions specified, involve
          improvements to the shutdown risk program; however, the inspector determined that these
I
improvements to the shutdown risk program; however, the inspector determined that these
actions would not preclude a recurrence of the technical specification non-compliance.
'
'
          actions would not preclude a recurrence of the technical specification non-compliance.
The violation response discussed the development of mode change checklists and
          The violation response discussed the development of mode change checklists and
j-
j-
enhanced logs; however, these actions, which may address technical specification
'
'
          enhanced logs; however, these actions, which may address technical specification
compliance, were not implemented by the end of the inspection period.
          compliance, were not implemented by the end of the inspection period.
The licensee did not address the adequacy of Technical Specification 3.5.F.7, nor verify
          The licensee did not address the adequacy of Technical Specification 3.5.F.7, nor verify
:
:         that the conditions initially established and reviewed by the NRC were appropriately
that the conditions initially established and reviewed by the NRC were appropriately
          maintained during subsequent amendments. The license event report was submitted 3                     !
maintained during subsequent amendments. The license event report was submitted 3
months after the event without a detailed reason for the delay and no corrective actions
i
4
4
'
'
          months after the event without a detailed reason for the delay and no corrective actions              i
were specified for the late reporting.
                                                                                                                '
          were specified for the late reporting.
2
2
          This item will remain open pending resolution of this item. The licensee failed to                 0
This item will remain open pending resolution of this item. The licensee failed to
;         appropriately evaluate and address these issues for more than a year since the event.
0
;
appropriately evaluate and address these issues for more than a year since the event.
!
!
          Further, the licensee failed to provide a closure package consistent with the process
Further, the licensee failed to provide a closure package consistent with the process
          committed to in December 1996. The manner in which this issue was addressed provides
committed to in December 1996. The manner in which this issue was addressed provides
          evidence of the licensees ability to perform effective reviews and to implement appropriate
evidence of the licensees ability to perform effective reviews and to implement appropriate
          corrective actions. As a result of the inspector's concerns with the quality of the
corrective actions. As a result of the inspector's concerns with the quality of the
..        completion packages, the licensee withdrew the NRC completion package schedule. A
completion packages, the licensee withdrew the NRC completion package schedule. A
          revised schedule was stillin development at the end of the inspection period.
..
                                                  U1.ll Maintenance
revised schedule was stillin development at the end of the inspection period.
          U1 M2           Maintenance and Material Condition of Facilities and Equipment
U1.ll Maintenance
U1 M2
Maintenance and Material Condition of Facilities and Equipment
i
i
i
i        M2.1 RWCU Demineralizer Room Material Condition
M2.1 RWCU Demineralizer Room Material Condition
;         a.       insoection Scope (71750)
;
'
a.
insoection Scope (71750)
'
'
          The inspector observed activities associated with the entry into, and video survey of, the
The inspector observed activities associated with the entry into, and video survey of, the
          reactor water cleanup (RWCU) demineralizer room. The purpose of the entry was to                   -i
'
i         determine the material condition of the infrequently accessed room. A remote controlled
reactor water cleanup (RWCU) demineralizer room. The purpose of the entry was to
;       robot was used, which supported both a video camera and radiation detection equipment.
-i
  .
i
determine the material condition of the infrequently accessed room. A remote controlled
;
robot was used, which supported both a video camera and radiation detection equipment.
.


.
.
                                                7
7
  b.     Observations and Findinas
b.
                                                                                              '
Observations and Findinas
  The health physics (HP) department was well prepared for this activity since preparations
The health physics (HP) department was well prepared for this activity since preparations
  and staging were completed the day before. This allowed potential problems to be
'
  identified and corrected prior to the start of work. In particular, it was identified in
and staging were completed the day before. This allowed potential problems to be
  advance that the robot would need to be lifted into the room through the access in the
identified and corrected prior to the start of work. In particular, it was identified in
  wall, and preparations were made to account for this. Positive control over personnel
advance that the robot would need to be lifted into the room through the access in the
  access, was observed with only people that were needed for the activity permitted in the
wall, and preparations were made to account for this. Positive control over personnel
  area. The workers' awareness of radiological hazards was evident. HP supervision and
access, was observed with only people that were needed for the activity permitted in the
  the system engineer provided oversight of this activity. The video survey indicated that     l
area. The workers' awareness of radiological hazards was evident. HP supervision and
                                                                                              '
the system engineer provided oversight of this activity. The video survey indicated that
  the room was in good condition and the structural integrity of the piping and three
the room was in good condition and the structural integrity of the piping and three
  domineralizer tanks was intact. There was no indication of any system leakage and
'
  radiation levels in the general area were normal.
domineralizer tanks was intact. There was no indication of any system leakage and
  c.     Conclusions
radiation levels in the general area were normal.
  Based on the above review, the inspector determined that the preparation and conduct of
c.
  work associated with the entry and video survey of the RWCU demineralizer room was
Conclusions
  well controlled. The inspector noted that good radiological practices were used. The
Based on the above review, the inspector determined that the preparation and conduct of
  material condition in the room was acceptable and no deficiencies were identified.
work associated with the entry and video survey of the RWCU demineralizer room was
                                        U1.Ill Enaineerina
well controlled. The inspector noted that good radiological practices were used. The
  U1 E1         Conduct of Engineering
material condition in the room was acceptable and no deficiencies were identified.
  E1.1   Unresolved Safety issue USl A-46 " Seismic Qualification of Eauipment in Operatina
U1.Ill Enaineerina
          Plants."
U1 E1
  a.     Insoection Scope (37550)
Conduct of Engineering
  The scope of this inspection was to review the licensee's progress in resolving the outliers
E1.1
  identified during the implementation of the Unresolved Safety issue (USI) A-46 " Seismic
Unresolved Safety issue USl A-46 " Seismic Qualification of Eauipment in Operatina
  Qualification of Equipment in Operating Plants."
Plants."
  b.     Observations
a.
  The inspector reviewed the Licensee Event Report (LER) 96-003, Rev. 2 that documented
Insoection Scope (37550)
  deficiencies involving inadequate anchorage of the emergency diesel generator (EDG) day
The scope of this inspection was to review the licensee's progress in resolving the outliers
  tank and the turbine building secondary closed cooling water (TBSCCW) air coolers.
identified during the implementation of the Unresolved Safety issue (USI) A-46 " Seismic
  Backaround
Qualification of Equipment in Operating Plants."
  in December 1980, The NRC staff initiated an Unresolved Safety issue, (USI) A-46,
b.
  " Seismic Qualification of Equipment in Operating Plants," related to seismic adequacy of
Observations
  mechanical and electrical equipment in older nuclear plants. After technical research by
The inspector reviewed the Licensee Event Report (LER) 96-003, Rev. 2 that documented
  the Seismic Qualification Utility Group (SQUG) and the NRC regarding this issue, the NRC
deficiencies involving inadequate anchorage of the emergency diesel generator (EDG) day
tank and the turbine building secondary closed cooling water (TBSCCW) air coolers.
Backaround
in December 1980, The NRC staff initiated an Unresolved Safety issue, (USI) A-46,
" Seismic Qualification of Equipment in Operating Plants," related to seismic adequacy of
mechanical and electrical equipment in older nuclear plants. After technical research by
the Seismic Qualification Utility Group (SQUG) and the NRC regarding this issue, the NRC


  .,__ _           _     _               - _ _     .-     .           _ . _ . _   _     . _ _ _ . . . . _ _
.,__ _
#
_
                                    .re i
_
                                                                                                                ,
- _ _
  .
.-
'
.
                                                          7
_ . _ . _
          b.     Observations and Findinas
_
. _ _ _ . . .
. _
_
#
.re i
,
.
'
7
b.
Observations and Findinas
i
i
          The health physics (HP) department was well prepared for this activity since preparations
The health physics (HP) department was well prepared for this activity since preparations
          and staging were completed the day before. This allowed potential problems to be
and staging were completed the day before. This allowed potential problems to be
"
identified and corrected prior to the start of work. In particular, it was identified in
          identified and corrected prior to the start of work. In particular, it was identified in
"
          advance that the robot would need to be lifted into the room through the access in the
advance that the robot would need to be lifted into the room through the access in the
          wall, and preparations were made to account for this. Positive control over personnel-
wall, and preparations were made to account for this. Positive control over personnel-
,       access, was observed with only people that were needed for the activity permitted in the             j
,
]'        area. The workers' awareness of radiological hazards was evident. HP supervision and
access, was observed with only people that were needed for the activity permitted in the
          the system engineer provided oversight of this activity. The video survey indicated that               l
j
,        the room was in good condition and the structural integrity of the piping and three                     I
]
l         demineralizer tanks was intact. There was no indication of any system leakage and                       l
area. The workers' awareness of radiological hazards was evident. HP supervision and
l        radiation levels in the general area were normal.
'
          c.     Conclusions
the system engineer provided oversight of this activity. The video survey indicated that
l
the room was in good condition and the structural integrity of the piping and three
,
l
demineralizer tanks was intact. There was no indication of any system leakage and
l
radiation levels in the general area were normal.
c.
Conclusions
t.
t.
          Based on the above review, the inspector determined that the preparation and conduct of
Based on the above review, the inspector determined that the preparation and conduct of
j         work associated with the entry and video survey of the RWCU demineralizer room was
j
          well controlled. -The inspector noted that good radiological practices were used. - The
work associated with the entry and video survey of the RWCU demineralizer room was
well controlled. -The inspector noted that good radiological practices were used. - The
material condition in the room was acceptable and no deficiencies were identified.
,
,
          material condition in the room was acceptable and no deficiencies were identified.
;
;
I
I
                                                U1.Ill Enaineerina                                             '
U1.Ill Enaineerina
'
I
I
          U1 El         Conduct of Engineering
U1 El
          E1.1   Unresolved Safety issue USI A-46 " Seismic Qualification of Eauioment in Ooeratina           ,
Conduct of Engineering
                  Plants."
E1.1
Unresolved Safety issue USI A-46 " Seismic Qualification of Eauioment in Ooeratina
,
Plants."
I
I
          a.     Inspection Scope (37550)
a.
l         The scope of this inspection was to review the licensee's progress in resolving the outliers
Inspection Scope (37550)
          identified during the implementation of the Unresolved Safety issue (USl) A-46 " Seismic
l
i         Qualification of Equipment in Operating Plants."
The scope of this inspection was to review the licensee's progress in resolving the outliers
          b.     Observations
identified during the implementation of the Unresolved Safety issue (USl) A-46 " Seismic
;         The inspector reviewed the Licensee Event Report (LER) 96-003, Rev. 2 that documented
i
          deficiencies involving inadequate anchorage of the emergency diesel generator (EDG) day
Qualification of Equipment in Operating Plants."
          tank and the turbine building secondary closed cooling water (TBSCCW) air coolers,
b.
                                                                                                                i
Observations
          Beckaround
;
          in December 1980, The NRC staff initiated an Unresolved Safety issue, (USI) A-46,
The inspector reviewed the Licensee Event Report (LER) 96-003, Rev. 2 that documented
          " Seismic Qualification of Equipment in Operating Plants," related to seismic adequacy of
deficiencies involving inadequate anchorage of the emergency diesel generator (EDG) day
          mechanical and electrical equipment in older nuclear plants. After technical research by
tank and the turbine building secondary closed cooling water (TBSCCW) air coolers,
          the Seismic Qualification Utility. Group (SQUG) and the NRC regarding this issue, the NRC
i
                                                                                                                !
Beckaround
in December 1980, The NRC staff initiated an Unresolved Safety issue, (USI) A-46,
" Seismic Qualification of Equipment in Operating Plants," related to seismic adequacy of
mechanical and electrical equipment in older nuclear plants. After technical research by
the Seismic Qualification Utility. Group (SQUG) and the NRC regarding this issue, the NRC


              .           -       . .   _     .   . . - _ . . .   -               -     . -   - - -
.
  .
-
. .
_
.
.
. - _ . .
.
-
-
. -
- - -
.
1
1
8
4
4
>
>
                                                      8
*
*
      published a detailed approach for resolving USl A-46, in Generic Letter 87-02, "Verif!:ation
published a detailed approach for resolving USl A-46, in Generic Letter 87-02, "Verif!:ation
  -
of Seismic Adequacy of Mechanical and Electrical Equipment in Operating Reactors, USl A-
      of Seismic Adequacy of Mechanical and Electrical Equipment in Operating Reactors, USl A-
-
      4 6. "
4 6. "
:
:
      The Generic Letter procedure set forth an approach for verifying seismic adequacy of
The Generic Letter procedure set forth an approach for verifying seismic adequacy of
i
i
      equipment using earthquake experience data supplemented by test results and analyses, as
equipment using earthquake experience data supplemented by test results and analyses, as
,     necessary. Licensees subject to USl A-46 were encouraged to participate in the generic                 '
,
necessary. Licensees subject to USl A-46 were encouraged to participate in the generic
'
'
      program to accomplish seismic verification of equipment. As a result, SQUG developed the
'
      " Generic Implementation Procedure (GIP) for seismic verification of Nuclear Plant
program to accomplish seismic verification of equipment. As a result, SQUG developed the
      equipment."                                                                                           l
" Generic Implementation Procedure (GIP) for seismic verification of Nuclear Plant
equipment."
l
;
;
      USl A-46 Proaram at MS1
USl A-46 Proaram at MS1
:
:
      At Millstone Unit 1, the USl A-46 program was conducted to address the concerns
At Millstone Unit 1, the USl A-46 program was conducted to address the concerns
      expressed in GL 87-02 regarding the seismic adequacy of safety related electrical and                 d
expressed in GL 87-02 regarding the seismic adequacy of safety related electrical and
      mechanical equipment. The resolution of the seismic adequacy issue appeared to be
d
      conducted in accordance with the SOUG approach, using the generic implementation plan
mechanical equipment. The resolution of the seismic adequacy issue appeared to be
      (GlP) as approved by the NRC in Supplemental Safety Evaluation Report (SSER) No.2.
conducted in accordance with the SOUG approach, using the generic implementation plan
                                                                                                            I
(GlP) as approved by the NRC in Supplemental Safety Evaluation Report (SSER) No.2.
      Supplement 1 to GL 87-02, transmitted May 22,1992 includes SSER-2 which reviews the                   l
I
      GIP, requires the licensee to identify within 120 days a schedule for implementation and             '
Supplement 1 to GL 87-02, transmitted May 22,1992 includes SSER-2 which reviews the
      any anticipated deviation from the GIP methods. The inspector verified that the licensee
l
      met this requirement by reviewing the licensee's letter dated September 21,1992. In this
GIP, requires the licensee to identify within 120 days a schedule for implementation and
      letter the licensee identified a schedule for MS1, which stated that the submittal of the
'
      final report will take place six months after refueling outage 15, which is stillin progress.
any anticipated deviation from the GIP methods. The inspector verified that the licensee
      The inspector noted that the implementation of the USI A-46 review program has resulted
met this requirement by reviewing the licensee's letter dated September 21,1992. In this
    'in the identification of outlier conditions which challenged the operability of the plant     ,
letter the licensee identified a schedule for MS1, which stated that the submittal of the
      components. These outliers were reported in an LER. The LER described the proposed
final report will take place six months after refueling outage 15, which is stillin progress.
      corrective action, which includes resolution of all outlier conditions prior to start up from
The inspector noted that the implementation of the USI A-46 review program has resulted
      Refueling Outage (RFO) 15.
'in the identification of outlier conditions which challenged the operability of the plant
      The LER selected for this inspection addresses operability concerns involving inadequate
,
      anchorage of the EDG day tank and the TBSCCW air coolers. These operability concerns
components. These outliers were reported in an LER. The LER described the proposed
      were properly documented as LER,96-003, Rev. 2. The inspector reviewed the LER 96-
corrective action, which includes resolution of all outlier conditions prior to start up from
      003, to ensure that regulatory requirements for reportability were met. The licensee has
Refueling Outage (RFO) 15.
      properly identified this design deficiency as a USl A-46 program outlier, and has properly
The LER selected for this inspection addresses operability concerns involving inadequate
      characterized it as being reportable in accordance with 10 CFR 50.72 and 10 CFR 50.73.
anchorage of the EDG day tank and the TBSCCW air coolers. These operability concerns
      The inspector found the LER's event described in a chronological sequence and the
were properly documented as LER,96-003, Rev. 2. The inspector reviewed the LER 96-
      prescribed corrective action appeared to be appropriate.
003, to ensure that regulatory requirements for reportability were met. The licensee has
      Conclusion
properly identified this design deficiency as a USl A-46 program outlier, and has properly
      in terms of reportability, the proper characterizations were given to the outliers of the USl
characterized it as being reportable in accordance with 10 CFR 50.72 and 10 CFR 50.73.
      A-46 program. The licensee prepared the LERs documenting these outliers in accordance
The inspector found the LER's event described in a chronological sequence and the
      with established regulatory requirements. Based on these inspection results, LER 50-               .
prescribed corrective action appeared to be appropriate.
      245/96-003 is closed. The followup of the licensee's commitments to resolve the A-46
Conclusion
      program outliers prior to startup for cycle 16 operation and the assessment of the
in terms of reportability, the proper characterizations were given to the outliers of the USl
A-46 program. The licensee prepared the LERs documenting these outliers in accordance
with established regulatory requirements. Based on these inspection results, LER 50-
.
245/96-003 is closed. The followup of the licensee's commitments to resolve the A-46
program outliers prior to startup for cycle 16 operation and the assessment of the


                                  _        _            .--    _ __ _ _                ._
    ,
  .
,
,
                                                        9
_
      implication of this event on the operation of Unit 1.will be unresolved pending further.NRC.   .
_
      . review (URI 50-245/97-01-04)
.--
_ __ _ _
._
.
9
,
implication of this event on the operation of Unit 1.will be unresolved pending further.NRC.
.
. review (URI 50-245/97-01-04)
Review of the Corrective Action for the EDG Day Tank
,
,
      Review of the Corrective Action for the EDG Day Tank
Since the EDG system is an emergency ac power system and the EDG day tank is a safety
,      Since the EDG system is an emergency ac power system and the EDG day tank is a safety
,
      related component, the inspector focused his review on the licensee's corrective action
related component, the inspector focused his review on the licensee's corrective action
      - package. In the package, the Design Change Notice (DCN) designed and installed the
- package. In the package, the Design Change Notice (DCN) designed and installed the
      seismic restraint that consists of a box frame around the tank supported by the block
seismic restraint that consists of a box frame around the tank supported by the block
      wall's structural reinforcements.
wall's structural reinforcements.
f
f
      The design modification package was found to be complete, and the frame was designed
The design modification package was found to be complete, and the frame was designed
l     in accordance with the American Institute of Steel Construction (AISC) Manual for Steel
l
      Construction, 9th Edition. However, key design parameters in the calculation were not
in accordance with the American Institute of Steel Construction (AISC) Manual for Steel
      properly referenced making it difficult for an independent auditor to determine whether or     l
Construction, 9th Edition. However, key design parameters in the calculation were not
l     not these parameters are correct. These key design parameters questioned by the
properly referenced making it difficult for an independent auditor to determine whether or
        inspector included acceleration values, friction values between the day tank and the
l
      concrete base pad; the calculated reaction of the block wall; and the shear capacity of the
l
        block wall. All the inspector's questions and observations were properly resolved by thea     .
not these parameters are correct. These key design parameters questioned by the
d      licensee.
inspector included acceleration values, friction values between the day tank and the
concrete base pad; the calculated reaction of the block wall; and the shear capacity of the
block wall. All the inspector's questions and observations were properly resolved by thea
.
licensee.
d
1
1
        Conclusion
Conclusion
                                                                                                    .
.
      The inspector determined that,the modification package was complete and the frame
The inspector determined that,the modification package was complete and the frame
        properly designed.
properly designed.
        Walkdown of the Modifications
Walkdown of the Modifications
        The inspector and the licensee design engineer walked down the modifications for the EDG
The inspector and the licensee design engineer walked down the modifications for the EDG
        day tank and the TBSCCW air coolers, with the following details.
day tank and the TBSCCW air coolers, with the following details.
        With regard to the EDG day tank, the general area was inspected and the framing to
With regard to the EDG day tank, the general area was inspected and the framing to
        distribute the tank's load appeared to be structurally sound. The tank was inspected and it
distribute the tank's load appeared to be structurally sound. The tank was inspected and it
        was noted that the impact on the block wall (T-27B) was minimal and limited to shear in
was noted that the impact on the block wall (T-27B) was minimal and limited to shear in
        the plane of the block wall. The inspector also noted that these block walls had been
the plane of the block wall. The inspector also noted that these block walls had been
        previously upgraded in response to NRC Bulletin 80-11. Outside the EDG day tank along
previously upgraded in response to NRC Bulletin 80-11. Outside the EDG day tank along
        the hallways the inspector noted that proper seismic bracing and anchorage was evident
the hallways the inspector noted that proper seismic bracing and anchorage was evident
        on the following:
on the following:
        *      Several modifications to vital electrical equipment (switchgear, load centers and
Several modifications to vital electrical equipment (switchgear, load centers and
                motor control centers) were installed.
*
        *      Modification to vital batteries consisted of shim material which was installed to
motor control centers) were installed.
                address A-46 outlier conditions.
Modification to vital batteries consisted of shim material which was installed to
        *      Modifications to prevent seismic interaction between lighting fixtures and vital
*
                equipment were installed.
address A-46 outlier conditions.
Modifications to prevent seismic interaction between lighting fixtures and vital
*
equipment were installed.


                                                                                  --         -    -.
--
  _
-
  '
-.
                                                                                                          i
_
                                                        10
                                                                                                          )
      *        . At the turbine building, elevation 14'-6" the inspector noted that the TBSCCW air      l
            . coolers identified in the USl A-46 program scope were modified to accommodate
              -
                seismic bracing and anchorage. in the EDG room, more air coolers and other              i
                components (air-start tanks, motor control center, and control panel) were              j
                seismically anchored or braced to address USl A-46 outliers.
      Conclusion                                                                                        !
      Based on the detailed walkdown of the A-46 modifications, the inspector concluded that
      the licensee has performed a substantial number of field modifications to accommodate the
      seismic loading on mechanical and electrical equipment identified in the USl A 46 scope.
      U1 E2              Engineering Support of Facilities and Equipment
                                                                                                          !
                                                                                                        '
      E2.1      Adverse Condition Report (ACR) Review
                                                                                                        i
      a.        Inspection Scope (37550)                                                                i
                                                                                                        1
'
'
      The inspector reviewed an ACR issued on August 16,1996, to assess whether appropriate             )
i
      corrective actions were identified and implemented to prevent recurrence of the adverse
10
      condition. The ACR (M1-96-0427) reviewed by the inspector concerned Component                     l
)
      Engineering Services / Nondestructive Test Engineering (CES/NTE) ultrasonic test (UT)             I
. At the turbine building, elevation 14'-6" the inspector noted that the TBSCCW air
      instruments that had exceeded their calibration due dates.
*
                                                                                                        ]
. coolers identified in the USl A-46 program scope were modified to accommodate
      b.       Observations and Findinos
-
      Six CES/NTE UT instruments were found to have exceeded their yearly calibration due
seismic bracing and anchorage. in the EDG room, more air coolers and other
      dates, with four of them having been possibly used during examinations at Unit 1. As           "
i
    ' stated on the ACR,'the person who previously handled the CES/NTE material and test
components (air-start tanks, motor control center, and control panel) were
      equipment (M&TE) program no longer workea for the company, and none of the job
j
      functions were replaced or reassigned. As a result, there was no ownership of the
seismically anchored or braced to address USl A-46 outliers.
      CES/NTE M&TE program.
Conclusion
      The six instruments in question were sent offsite to a vendor for calibration. All six were       I
Based on the detailed walkdown of the A-46 modifications, the inspector concluded that
      found to be within tolerance when they were received. Additionally, before and after each
the licensee has performed a substantial number of field modifications to accommodate the
      examination was performed, the instruments were calibrated in accordance with procedure
seismic loading on mechanical and electrical equipment identified in the USl A 46 scope.
      NU-UT-1, using a step wedge or calibration blocx The missed yearly calibrations are               j
U1 E2
      performed to verify instrument operability only, and do not represent a quality related           ;
Engineering Support of Facilities and Equipment
                                                                                                          i
'
      calibration. In other words, the calibrations done during examinations might be sufficient
E2.1
      to preclude sending these instruments offsite for yearly calibrations. Since these yearly
Adverse Condition Report (ACR) Review
      calibrations are not required by the ASME Code, the licensee will determine whether to
i
      suspend them.
a.
      The inspector reviewed Quality Assurance Audit Package A-60607, " Measuring & Test                 i
Inspection Scope (37550)
      Equipment," an audit that was conducted from August 26,1996 through September 18,
i
        1996. This audit evaluated the key elements and processes of the M&TE program and               ;
1
      determined that the program at Millstone and Connecticut Yankee was ineffective in
The inspector reviewed an ACR issued on August 16,1996, to assess whether appropriate
)
'
corrective actions were identified and implemented to prevent recurrence of the adverse
condition. The ACR (M1-96-0427) reviewed by the inspector concerned Component
l
Engineering Services / Nondestructive Test Engineering (CES/NTE) ultrasonic test (UT)
instruments that had exceeded their calibration due dates.
]
b.
Observations and Findinos
Six CES/NTE UT instruments were found to have exceeded their yearly calibration due
dates, with four of them having been possibly used during examinations at Unit 1. As
"
' stated on the ACR,'the person who previously handled the CES/NTE material and test
equipment (M&TE) program no longer workea for the company, and none of the job
functions were replaced or reassigned. As a result, there was no ownership of the
CES/NTE M&TE program.
The six instruments in question were sent offsite to a vendor for calibration. All six were
found to be within tolerance when they were received. Additionally, before and after each
examination was performed, the instruments were calibrated in accordance with procedure
NU-UT-1, using a step wedge or calibration blocx The missed yearly calibrations are
j
performed to verify instrument operability only, and do not represent a quality related
i
calibration. In other words, the calibrations done during examinations might be sufficient
to preclude sending these instruments offsite for yearly calibrations. Since these yearly
calibrations are not required by the ASME Code, the licensee will determine whether to
suspend them.
The inspector reviewed Quality Assurance Audit Package A-60607, " Measuring & Test
i
Equipment," an audit that was conducted from August 26,1996 through September 18,
1996. This audit evaluated the key elements and processes of the M&TE program and
;
determined that the program at Millstone and Connecticut Yankee was ineffective in
 
_
_
_.
,
1
.
l
11
fulfilling its mission and did not fully comply with 10 CFR 50 Appendix B criteria. in
- < .
response to this audit, ACR M1-96-0614 was written to address the adverse condition.'
1
i
i
To address the ACRs and audit report, CES/NTE developed a corrective action plan and
dedicated an individual to implement the plan and take ownership of the CES/NTE M&TE
program. Additionally, the licensee ensured that all CES/NTE quality related equipment
currently being used at Millstone and Connecticut Yankee was in calibration.
c.
Conclusion
The inspector concluded that the corrective actions taken by CES/NTE associated with the
ACRs and the QA audit was acceptable. The corrective actions appeared to be broad-
based. A majority of the short term corrective actions were complete, and the long term
corrective actions were being tracked for closure. The safety significance of the UT
j
instruments being past their calibration due dates was minimal because they were
subsequently found to be within tolerance.
E2.2 Containment isolation Check Valve.1-CU-29
a.
Inspection Scope (37551)
'
The inspector reviewed adverse condition report (ACR) 96-0539, which documents an
issue concerning the design specifications of the new containment isolation check valve 1-
1
CU-29. The valve was replaced with a smaller size valve for better flow characteristics,
and to allow testing and maintenance during this outage.
]
b.
Observations and Findinas
i
!
The replacement valve was a specially designed 6" check valve with a 4.5" disc. The disc
'
size was selected based on two flow conditions other than normal operations: 1) shutdown
flow conditions occurring approximately 10% of the time (70 days per operating cycle)
with a minimum system flow of 300 gpm; 2) and startup flow condition, occurring about
1
0.2% of the time with a system flow rate of 100-200 gpm. Due to the current extended
outage, it is not known if the shutdown flow rate will affect the valve. In fact, the RWCU
system is unable to produce the 300 gpm used in selecting the disc size due to the flow
restriction created by the pressure control valve 1-CU-10. During the followup of this
issue, the inspector noted that the actual system flow rate is approximately 190-200 gpm
using the auxiliary cleanup pump, it is not known what effects, if any, will be created by
i
operating the valve at these lower flow rates for this extended period.
In a effort to determine if the valve disc was fluttering or banging into the backseat due to
the low flow conditions, the licensee employed Liberty Technologies to perform non-
intrusive check valve testing. Liberty Technologies performed both acoustic and magnetic
testing on CU-29. Their report stated that the test results provide positive indication of full
opening during the flow initiation test. Acoustic data recorded during steady state flow
indicated no anomalous behavior (such as excessive trim wear or rattling). The report also
'
noted that due to large valve body signal strength from the magnetic sensors during the
--


                                                                                                    _ _.
,
  ,
_
                                                                                                          1
_
.                                                                                                        l
                                                                                                        l
                                                  11                                                    l
    fulfilling its mission and did not fully comply with 10 CFR 50 Appendix B criteria. in    -<.
    response to this audit, ACR M1-96-0614 was written to address the adverse condition.'                1
                                                                                                          i
                                                                                                          i
    To address the ACRs and audit report, CES/NTE developed a corrective action plan and
    dedicated an individual to implement the plan and take ownership of the CES/NTE M&TE
    program. Additionally, the licensee ensured that all CES/NTE quality related equipment
    currently being used at Millstone and Connecticut Yankee was in calibration.
    c.      Conclusion
    The inspector concluded that the corrective actions taken by CES/NTE associated with the
    ACRs and the QA audit was acceptable. The corrective actions appeared to be broad-
    based. A majority of the short term corrective actions were complete, and the long term
    corrective actions were being tracked for closure. The safety significance of the UT                  j
    instruments being past their calibration due dates was minimal because they were
    subsequently found to be within tolerance.
    E2.2 Containment isolation Check Valve.1-CU-29
                                                                                                        I
    a.      Inspection Scope (37551)                                                                    '
    The inspector reviewed adverse condition report (ACR) 96-0539, which documents an                    :
    issue concerning the design specifications of the new containment isolation check valve 1-          1
    CU-29. The valve was replaced with a smaller size valve for better flow characteristics,            !
    and to allow testing and maintenance during this outage.
                                                                                                        ]
    b.      Observations and Findinas                                                                  i
                                                                                                        !
    The replacement valve was a specially designed 6" check valve with a 4.5" disc. The disc            '
    size was selected based on two flow conditions other than normal operations: 1) shutdown
    flow conditions occurring approximately 10% of the time (70 days per operating cycle)
    with a minimum system flow of 300 gpm; 2) and startup flow condition, occurring about                1
    0.2% of the time with a system flow rate of 100-200 gpm. Due to the current extended                :
    outage, it is not known if the shutdown flow rate will affect the valve. In fact, the RWCU
    system is unable to produce the 300 gpm used in selecting the disc size due to the flow
    restriction created by the pressure control valve 1-CU-10. During the followup of this
    issue, the inspector noted that the actual system flow rate is approximately 190-200 gpm
    using the auxiliary cleanup pump, it is not known what effects, if any, will be created by            i
    operating the valve at these lower flow rates for this extended period.
                                                                                                          l
    In a effort to determine if the valve disc was fluttering or banging into the backseat due to
    the low flow conditions, the licensee employed Liberty Technologies to perform non-
    intrusive check valve testing. Liberty Technologies performed both acoustic and magnetic
    testing on CU-29. Their report stated that the test results provide positive indication of full
    opening during the flow initiation test. Acoustic data recorded during steady state flow
    indicated no anomalous behavior (such as excessive trim wear or rattling). The report also          '
    noted that due to large valve body signal strength from the magnetic sensors during the
                          --
 
    _    _
  ,
.
.
                                                      12
12
      valve opening and steady state tests were insufficient to provide useful results. However, .
valve opening and steady state tests were insufficient to provide useful results. However, .
they determined the acoustic data was a sufficient basis for the conclusions documented.
-
-
      they determined the acoustic data was a sufficient basis for the conclusions documented.
A member of the engineering staff informed the inspector that ACR 96-0539 was currently
      A member of the engineering staff informed the inspector that ACR 96-0539 was currently
open and under review. Engineering needs to determine a method for ascertaining the
      open and under review. Engineering needs to determine a method for ascertaining the
actual impact of the lower flow operation on the valve. Localleak rate testing is being
      actual impact of the lower flow operation on the valve. Localleak rate testing is being
considered as a possible method to determine if any valve degradation has occurred,
      considered as a possible method to determine if any valve degradation has occurred,
c.
      c.     Conclusions
Conclusions
      The NRC is concerned about the operation of CU-29 with lower than expected flow rates
The NRC is concerned about the operation of CU-29 with lower than expected flow rates
      during this extended shutdown. While the use of non-intrusive check valve testing has
during this extended shutdown. While the use of non-intrusive check valve testing has
      verified that the check valve is backseated, this is a short term indication. The long term
verified that the check valve is backseated, this is a short term indication. The long term
      effects of the lower flow operation have yet to be determined. This issue is unresolved
effects of the lower flow operation have yet to be determined. This issue is unresolved
      -(URI 245/97-01-05) pending the NRC review of the licensee's finial determination of the
-(URI 245/97-01-05) pending the NRC review of the licensee's finial determination of the
      operability of the valve prior to plant startup.
operability of the valve prior to plant startup.
      U1 E8           Miscellaneous Engineering issues
U1 E8
      E8.1   Closecut Documentation Packaae Review
Miscellaneous Engineering issues
      The inspector reviewed the contents of a corrective action documentation package for NRC
E8.1
      unresolved item 96-04-07 (safety relief valve electric lift modification). The inspector
Closecut Documentation Packaae Review
      noted that the package included a draft licensee response to an NRC request for additional
The inspector reviewed the contents of a corrective action documentation package for NRC
      information associated with the license amendment. Per previous arrangements the
unresolved item 96-04-07 (safety relief valve electric lift modification). The inspector
      licensee documentation packages were to be complete and contain only approved
noted that the package included a draft licensee response to an NRC request for additional
      documents. The package was returned to the licensee and no inspection was performed at
information associated with the license amendment. Per previous arrangements the
      this time.
licensee documentation packages were to be complete and contain only approved
documents. The package was returned to the licensee and no inspection was performed at
this time.


.
.
.
                                                  13
.
                                          Report Details
13
  Summary of Unit 2 Status
Report Details
  Unit 2 entered the inspection period with the core off-loaded. The unit was initially shut
Summary of Unit 2 Status
  down on February 20,1996, to address containment sump screen concerns and has
Unit 2 entered the inspection period with the core off-loaded. The unit was initially shut
  remained shut down to address an NRC Demand for Information [10 CFR 50.54(f)] letter
down on February 20,1996, to address containment sump screen concerns and has
  requiring an assertion by the licensee that future operations are conducted in accordance
remained shut down to address an NRC Demand for Information [10 CFR 50.54(f)] letter
  with the regulations, the license, and the Final Safety Analysis Report.
requiring an assertion by the licensee that future operations are conducted in accordance
                                          U2.1 Operations
with the regulations, the license, and the Final Safety Analysis Report.
  U201           Conduct of Operations
U2.1 Operations
  01.1 General Comments (71707)
U201
  Using Inspection Procedure 71707, the inspectors conducted frequent reviews of ongoing
Conduct of Operations
  plant operations to ensure that licensee's controls were effective in achieving continued
01.1 General Comments (71707)
  safe operation of the faciiity while shut down. The inspectors observed that proper control
Using Inspection Procedure 71707, the inspectors conducted frequent reviews of ongoing
  room staffing was maintained, access to the control room was properly controlled, and
plant operations to ensure that licensee's controls were effective in achieving continued
  operator behavior was commensurate with the plant configuration and plant activities in
safe operation of the faciiity while shut down. The inspectors observed that proper control
  progress. In general, the conduct of operations was professional and safety-conscious.
room staffing was maintained, access to the control room was properly controlled, and
  Operations Management has recently placed greater attention on improving performance
operator behavior was commensurate with the plant configuration and plant activities in
  associated with operator response to control room alarms with a focus on communications
progress. In general, the conduct of operations was professional and safety-conscious.
  and use of alarm response procedures. The NRC has noted the improvements in this area,     i
Operations Management has recently placed greater attention on improving performance
  particularly regarding control room operators communicating to the unit supervisors what
associated with operator response to control room alarms with a focus on communications
  alarms were received and ensuring a mutual understanding of why the alarm was received.
and use of alarm response procedures. The NRC has noted the improvements in this area,
  The licensee discovery of potential discrepancies in the personal qualification statements
i
  (NRC Form 398) of certain Unit 2 licensed operators has been assessed for immediate
particularly regarding control room operators communicating to the unit supervisors what
  impact and determined to require further evaluation. This is considered an unresolved       ,
alarms were received and ensuring a mutual understanding of why the alarm was received.
  issue as described in Section U1.05.1 of this inspection report.
The licensee discovery of potential discrepancies in the personal qualification statements
  The inspector toured the Unit 2 intake structure and found the material condition of
(NRC Form 398) of certain Unit 2 licensed operators has been assessed for immediate
  systems and components to be acceptable, in the Spring of 1996, the licensee instituted a
impact and determined to require further evaluation. This is considered an unresolved
  corrective action plan to address material deficiencies. A number of items have been
,
  corrected, which has improved the material condition of the intake structure.
issue as described in Section U1.05.1 of this inspection report.
  U2 O2         Operational Status of Facilities and Equipment
The inspector toured the Unit 2 intake structure and found the material condition of
    02.1 Adverse Condition Report Backloa
systems and components to be acceptable, in the Spring of 1996, the licensee instituted a
    a.     Insocction Scope
corrective action plan to address material deficiencies. A number of items have been
  The NRC evaluated the timeliness in which the licensee completed corrective actions
corrected, which has improved the material condition of the intake structure.
    associated with Unit 2 adverse condition reports (ACRs).
U2 O2
Operational Status of Facilities and Equipment
02.1 Adverse Condition Report Backloa
a.
Insocction Scope
The NRC evaluated the timeliness in which the licensee completed corrective actions
associated with Unit 2 adverse condition reports (ACRs).


  .
.
  .
.
                                                  14
14
    b.     Observetions and Findinas
b.
Observetions and Findinas
Timeliness for completion of corrective actions has been a longstanding concern at
'
Millstone. Having an ACR backlog in itself is not a reflection of poor performance because
as the threshold for writing ACRs decreases, the ACR backlog willincrease accordingly.
The concern is the number of ACRs that are not closed in a timely manner. To help
provide the NRC some sense of the licensee's progress in addressing the timeliness
concern, the licensee was asked to provide the number of ACRs having outstanding
corrective actions that are greater than 120 days old. Although the NRC does not consider
120 days a level of excellence nor is it acceptable when addressing immediate safety
concerns, it does provide some understanding of licensee management effectiveness in
addressing the corrective action timeliness issue.
Several months ago, the NRC raised a concern that the licensee's ACR database did not
allow them to determine the number of ACRs having outstanding corrective actions. The
1
licensee's previous understanding, as documented in NRC Inspection Report (IR) 50-
336/96-09, was that the ACR data entries had been corrected to provide reliable ACR
'
'
    Timeliness for completion of corrective actions has been a longstanding concern at
backlog numbers. However, additional licensee reviews of the ACR database indicate that
    Millstone. Having an ACR backlog in itself is not a reflection of poor performance because
the number of ACRs greater than 120 days old as of December 31',1997, was 940 ACRs,
    as the threshold for writing ACRs decreases, the ACR backlog willincrease accordingly.
i
    The concern is the number of ACRs that are not closed in a timely manner. To help
no_t 732 ACRs as stated in IR 50-336/96-09. The increase of 208 ACRS is based on a
    provide the NRC some sense of the licensee's progress in addressing the timeliness
licensee review of previously closed ACRs that they decided to reopen based on
    concern, the licensee was asked to provide the number of ACRs having outstanding
incomplete closure documentation. At the end of the current inspection period (February
    corrective actions that are greater than 120 days old. Although the NRC does not consider
24,1997), there were 798 ACRs greater than 120 days old that have not been closed.
    120 days a level of excellence nor is it acceptable when addressing immediate safety      !
DEPARTMENT
    concerns, it does provide some understanding of licensee management effectiveness in      I
ACRs OLDER
    addressing the corrective action timeliness issue.
THAN 120 DAYS
    Several months ago, the NRC raised a concern that the licensee's ACR database did not
Operations
    allow them to determine the number of ACRs having outstanding corrective actions. The      1
56
    licensee's previous understanding, as documented in NRC Inspection Report (IR) 50-        l
Design Engineering
    336/96-09, was that the ACR data entries had been corrected to provide reliable ACR        '
211
    backlog numbers. However, additional licensee reviews of the ACR database indicate that
;
    the number of ACRs greater than 120 days old as of December 31',1997, was 940 ACRs,       i
Technical Support (System Engineering)
    no_t 732 ACRs as stated in IR 50-336/96-09. The increase of 208 ACRS is based on a
254
    licensee review of previously closed ACRs that they decided to reopen based on
Work Planning
    incomplete closure documentation. At the end of the current inspection period (February
28
    24,1997), there were 798 ACRs greater than 120 days old that have not been closed.
Maintenance
                                  DEPARTMENT                     ACRs OLDER
55
                                                                THAN 120 DAYS
_
                    Operations                                         56
l&C
                    Design Engineering                                 211                     ;
42
                    Technical Support (System Engineering)             254
Safety / Licensing
                    Work Planning                                       28
25
                    Maintenance                                         55
Other
                                                                                _
127
                    l&C                                               42
TOTAL
                    Safety / Licensing                                 25
798
                    Other                                             127
c.
                    TOTAL                                             798
Conclusion
    c.     Conclusion
Although the backlog of 798 adverse condition reports (ACRs) that are greater than 120
    Although the backlog of 798 adverse condition reports (ACRs) that are greater than 120
days old indicates that timeliness for completing corrective actions continues to be a
    days old indicates that timeliness for completing corrective actions continues to be a


,
,
                                                                              >
>
                                                  15
15
  concern, the reduction in this backlog of older ACRs from 940 to 798 since the last.
concern, the reduction in this backlog of older ACRs from 940 to 798 since the last.
  inspection period is a positive trend which reflects the licensee's increased level of effort in
inspection period is a positive trend which reflects the licensee's increased level of effort in
  this area. As discussed in NRC Inspection Report 50-336/96-04, timeliness and
this area. As discussed in NRC Inspection Report 50-336/96-04, timeliness and
  effectiveness of corrective actions is an area in which the licensee must demonstrate
effectiveness of corrective actions is an area in which the licensee must demonstrate
  sustained improved performance.
sustained improved performance.
  U2 08         Miscellaneous Operations issues (92700)
U2 08
  08.1 (Closed) Violation 50-336/94-17-10: O_peration Outside System Desian Parameters
Miscellaneous Operations issues (92700)
  a.     inspection Scope
08.1 (Closed) Violation 50-336/94-17-10: O_peration Outside System Desian Parameters
  The sc-ope of this inspection included a review of Violation 50-336/94-17-10.
a.
  b.     Observations and Findinas
inspection Scope
  This violation involved the failure to correctly translate design basis temperature limits of
The sc-ope of this inspection included a review of Violation 50-336/94-17-10.
  the service water (SW) and reactor building closed cooling water (RBCCW) 2ystems into
b.
  operating procedures. As a result, on May 24,1993, a reactor trip occurred when the SW
Observations and Findinas
  and RBCCW system temperature limits were exceeded during a main condenser thermal               j
This violation involved the failure to correctly translate design basis temperature limits of
  backwashing evolution. This violation was previously reviewed in NRC Inspection Report           ;
the service water (SW) and reactor building closed cooling water (RBCCW) 2ystems into
  50-336/96-05 which concluded that the violation could not be closed because although             '
operating procedures. As a result, on May 24,1993, a reactor trip occurred when the SW
  the specific procedures regarding thermal backweshing were adequately aabemd, the
and RBCCW system temperature limits were exceeded during a main condenser thermal
  corrective actions were too narrow in that they failed to address the possibility eat other
j
  plant procedures did not insure operation was in accordance with the plant's oesign basis.
backwashing evolution. This violation was previously reviewed in NRC Inspection Report
  c.     Conclusion
50-336/96-05 which concluded that the violation could not be closed because although
  Violation 50-336/94-17-10, which resulted from a 1993 unresolved item, reflects that the
'
  failure to operate the plant in accordance with the design basis had been a longstanding
the specific procedures regarding thermal backweshing were adequately aabemd, the
  NRC concern. The licensee failure to address this type of concern eventually culminated in
corrective actions were too narrow in that they failed to address the possibility eat other
  their current extended shutdown and 10 CFR 50.54(f) effort which is intended to ensure           i
plant procedures did not insure operation was in accordance with the plant's oesign basis.
  the plant is designed and operated in accordance with the licensing and design basis.           I
c.
  There are several outstanding violations including Escalated Enforcement items 50-336/96-         '
Conclusion
  06-05 & 96-08-06 which also address plant operation that is inconsistent with the
Violation 50-336/94-17-10, which resulted from a 1993 unresolved item, reflects that the
  licensing basis. Therefore, Violation 50-336/94-17-10 is being closed nql because
failure to operate the plant in accordance with the design basis had been a longstanding
  adequate corrective actions have been taken but because this concern is being addressed         ;
NRC concern. The licensee failure to address this type of concern eventually culminated in
  and tracked by more recent items.                                                                 '
their current extended shutdown and 10 CFR 50.54(f) effort which is intended to ensure
  08.2 (Closed) LER 50-336/96-15, (Open) Unresolved item 50-336/96-01-04: Failure to
i
          Enter Action Statement Reaardina the Number of Operable Nuclear instrument
the plant is designed and operated in accordance with the licensing and design basis.
          Channels
There are several outstanding violations including Escalated Enforcement items 50-336/96-
  a.     inspection Scooe
'
  The scope of this inspection included a review of Licensee Event Report 50-336/96-15.
06-05 & 96-08-06 which also address plant operation that is inconsistent with the
licensing basis. Therefore, Violation 50-336/94-17-10 is being closed nql because
adequate corrective actions have been taken but because this concern is being addressed
and tracked by more recent items.
'
08.2 (Closed) LER 50-336/96-15, (Open) Unresolved item 50-336/96-01-04: Failure to
Enter Action Statement Reaardina the Number of Operable Nuclear instrument
Channels
a.
inspection Scooe
The scope of this inspection included a review of Licensee Event Report 50-336/96-15.


  .
.
  .
.
                                                    16
16
      b.     Observations and Findinas
b.
      On March 12,1996, while the unit was shut down, the "B" train vital de bus was
Observations and Findinas
      inadvertently deenergized due to operator error. The resultant loss of various vital and non
On March 12,1996, while the unit was shut down, the "B" train vital de bus was
      vital power supplies overflowed the reactor building closed cooling water surge tank
inadvertently deenergized due to operator error. The resultant loss of various vital and non
      through a failed open make-up valve, and challenged the operators to recover from this
vital power supplies overflowed the reactor building closed cooling water surge tank
      complex event. The event was complicated by the fact that there was minimal procedural
through a failed open make-up valve, and challenged the operators to recover from this
      guidance for operators to use to recover the bus. One train of shutdown cooling remained
complex event. The event was complicated by the fact that there was minimal procedural
;    in operation throughout the event and normal power was restored within four hours.
guidance for operators to use to recover the bus. One train of shutdown cooling remained
      During the recovery, operators were required by procedure to deenergize bus VA-40, a
in operation throughout the event and normal power was restored within four hours.
      vital 120 Volt ac instrument panel which supplies channel "D" of the reactor protection
;
      system (RPS). Operators were aware that a loss of RPS channel "D" would cause the
During the recovery, operators were required by procedure to deenergize bus VA-40, a
      channel "D" wide range nuclear instrument to be inoperable. Prior to the loss of the "B"
vital 120 Volt ac instrument panel which supplies channel "D" of the reactor protection
      train vital de bus, in an unrelated situation, channel "B" and "C" wide range nuclear
system (RPS). Operators were aware that a loss of RPS channel "D" would cause the
      instruments had been declared inoperable. The action statement for Technical
channel "D" wide range nuclear instrument to be inoperable. Prior to the loss of the "B"
      Specification (TS) 3.3.1.1 is applicable when less than two channels of wide range nuclear
train vital de bus, in an unrelated situation, channel "B" and "C" wide range nuclear
      instruments are operable. The action statement requires the immediate verification of
instruments had been declared inoperable. The action statement for Technical
      shutdown margin and at least once every 4 hours thereafter. The operators did not
Specification (TS) 3.3.1.1 is applicable when less than two channels of wide range nuclear
    ~ recognize the need to erter the TS 3.3.1.1 limiting condition for operation when bus VA .
instruments are operable. The action statement requires the immediate verification of
      40 was deenergized.
shutdown margin and at least once every 4 hours thereafter. The operators did not
      LER 50-336/96-15 stated that a contributing cause for failing to enter the TS 3.3.1.1
~ recognize the need to erter the TS 3.3.1.1 limiting condition for operation when bus VA .
      action statement was that the shift was occupied with the restoration of the deenergized
40 was deenergized.
      dc bus and was considering the effects of deenergizing loads on plant operatico. The
LER 50-336/96-15 stated that a contributing cause for failing to enter the TS 3.3.1.1
      licensee's corrective actions included training of operators to not only consider the effects
action statement was that the shift was occupied with the restoration of the deenergized
      of their actions on plani operations, but they must also assess TS requirements, in
dc bus and was considering the effects of deenergizing loads on plant operatico. The
      addition, operating procedures were changed to remind operators to determine if TSs are
licensee's corrective actions included training of operators to not only consider the effects
      affected when deenergizing an electrical bus.
of their actions on plani operations, but they must also assess TS requirements, in
      c.     Conclusion
addition, operating procedures were changed to remind operators to determine if TSs are
      The failure of operators to enter the action statement for TS 3.3.1.1 when three channels
affected when deenergizing an electrical bus.
      of wide range nuclear instrumentation were inoperable is considered a violation. This
c.
      licensee-identified and corrected violation is being treated as a Non-Cited Violation,
Conclusion
      consistent with Section Vll.B.1 of the NRC Enforcement Policy. The primary concern
The failure of operators to enter the action statement for TS 3.3.1.1 when three channels
      associated with tnis event was the fact that there was minimal procedural guidance
of wide range nuclear instrumentation were inoperable is considered a violation. This
      provided to operators to recover the loss of de bus. The licensee is in the process of
licensee-identified and corrected violation is being treated as a Non-Cited Violation,
      preparing 12 abnormal operating procedures for recovering various dc buses and
consistent with Section Vll.B.1 of the NRC Enforcement Policy. The primary concern
      distribution panels. This concern is being tracked by Unresolved Item 50-336/96-01-04.
associated with tnis event was the fact that there was minimal procedural guidance
                                                                                                    l
provided to operators to recover the loss of de bus. The licensee is in the process of
                                                                                                    !
preparing 12 abnormal operating procedures for recovering various dc buses and
                                                                                                    I
distribution panels. This concern is being tracked by Unresolved Item 50-336/96-01-04.
I


,
,
                                                                                            !
.
.
                                                17
17
                                        U2.ll Maintenance
U2.ll Maintenance
                                                                                            i
i
  U2 M8         Miscellaneous Maintenance issues (92903)                                   l
U2 M8
                                                                                            l
Miscellaneous Maintenance issues (92903)
  M8.1 (Closed) Unresolved item 50-336/96-04-09: Troubleshootina Controls                     '
M8.1 (Closed) Unresolved item 50-336/96-04-09: Troubleshootina Controls
                                                                                            i'
'
  a,     lnspection Scope
i
  in April 1996, the NRC resident inspectors identified programmatic concerns regarding the U
a,
  conduct of troubleshooting. The concerns centered around the practice of performing
lnspection Scope
  " troubleshooting" under the guise of " investigating" to avoid implementing the
'
  administrative requirements for the performance of troubleshooting that are contained in
in April 1996, the NRC resident inspectors identified programmatic concerns regarding the
  procedure WC-1, " Work Control Process." This issue was unresolved pending licensee
U
  changes to WC-1.                                                                           i
conduct of troubleshooting. The concerns centered around the practice of performing
                                                                                            !
" troubleshooting" under the guise of " investigating" to avoid implementing the
  b.     Observations and Findinas
administrative requirements for the performance of troubleshooting that are contained in
  in July 1996, the licensee issued Attachment 5.2 to procedure WC-1. This attachment
procedure WC-1, " Work Control Process." This issue was unresolved pending licensee
  provides guidelines to be used in conjunction with a work order when a formal           .
changes to WC-1.
  troubleshooting plan is not required by Attachment 5 of WC-1.                             '
b.
  The inspector reviewed the instructions contained in WC-1 and reviewed several work       I
Observations and Findinas
  orders that performed troubleshooting since the issuance of the change to WC-1.
in July 1996, the licensee issued Attachment 5.2 to procedure WC-1. This attachment
  c.     Conclusions
provides guidelines to be used in conjunction with a work order when a formal
  The inspector found that Attachment 5.2 of WC-1 contains appropriate directions to
.
  ensure that all troubleshooting work is documented, supervision is consulted prior to       .
troubleshooting plan is not required by Attachment 5 of WC-1.
  performing repair or replacement of components and retest requirements are determined
'
  following the completion of the troubleshooting. No problems were identified during the
The inspector reviewed the instructions contained in WC-1 and reviewed several work
  review of the troubleshooting work orders. This item is closed.
I
                                                                                            I
orders that performed troubleshooting since the issuance of the change to WC-1.
  M8.2 (Closed) Unresolved item 50-336/96-06-06: Hioh Pressure Safety Iniectiori Check
c.
          Valve Backflow Testino
Conclusions
  a.     Insoection Scope (92903)
The inspector found that Attachment 5.2 of WC-1 contains appropriate directions to
  The inspectors identified that the licensee had unnecessarily relaxed the frequency of
ensure that all troubleshooting work is documented, supervision is consulted prior to
  backflow testing of high pressure safety injection system (HPSI) pump discharge check
.
  valves. The licensee agreed to revise the surveillance procedure to perform quarterly
performing repair or replacement of components and retest requirements are determined
  backflow testing. This issue was unresolved pending NRC review of the planned
following the completion of the troubleshooting. No problems were identified during the
  procedure changes,
review of the troubleshooting work orders. This item is closed.
  b.     Observations and Findinas
I
  The licensee revised procedure SP 21136, " Safety injection and Containment Spray
M8.2 (Closed) Unresolved item 50-336/96-06-06: Hioh Pressure Safety Iniectiori Check
  System Valves Operational Readiness Test," to include quarterly backflow testing of the
Valve Backflow Testino
  HPSI pump discharge check valves.
a.
Insoection Scope (92903)
The inspectors identified that the licensee had unnecessarily relaxed the frequency of
backflow testing of high pressure safety injection system (HPSI) pump discharge check
valves. The licensee agreed to revise the surveillance procedure to perform quarterly
backflow testing. This issue was unresolved pending NRC review of the planned
procedure changes,
b.
Observations and Findinas
The licensee revised procedure SP 21136, " Safety injection and Containment Spray
System Valves Operational Readiness Test," to include quarterly backflow testing of the
HPSI pump discharge check valves.


, . --
,
                                                                                                  i
. --
                                                                                                  !
i
'
18
i
c.
Conclusions
'
'
                                                                                                  l
The NRC concluded that the licensee had appropriately resolved the check valve testing
                                                                                                  1
concern in Revision 10 of procedure SP 21136 and the associated data forms. This item is
                                                  18
closed.
                                                                                                  i
U2.lll Enaineerina
  c.      Conclusions                                                                            '
'
  The NRC concluded that the licensee had appropriately resolved the check valve testing
U2 E8
  concern in Revision 10 of procedure SP 21136 and the associated data forms. This item is       I
Miscellaneous Engineering issues
  closed.
i
                                                                                                  l
E8.1 LClosed) Unresolved item 50-336/95-07-06: Condensate Storaae Tank Siohon Break
                                          U2.lll Enaineerina                                     '
a.
  U2 E8         Miscellaneous Engineering issues
Inspection Scope (92903)
                                                                                                  i
On February 10,1995, the licensee discovered that the condensate storage tank (CST)
  E8.1 LClosed) Unresolved item 50-336/95-07-06: Condensate Storaae Tank Siohon Break
level had dropped to approximately 30% due to a heat exchanger tube leak. At the time of
  a.     Inspection Scope (92903)
the event the plant was defueled and no minimum tank volume was require by the plant.
  On February 10,1995, the licensee discovered that the condensate storage tank (CST)
technical specifications. During an investigation of the inadvertent loss of CST inventory
  level had dropped to approximately 30% due to a heat exchanger tube leak. At the time of
the licensee discovered that a siphon break (a 1/2 inch hole) in the tank recirculation piping
  the event the plant was defueled and no minimum tank volume was require by the plant.
was missing. This issue was unresolved pending further review of how the plant design
  technical specifications. During an investigation of the inadvertent loss of CST inventory
change process missed the removal of the siphon break,
  the licensee discovered that a siphon break (a 1/2 inch hole) in the tank recirculation piping
b.
  was missing. This issue was unresolved pending further review of how the plant design
Observations and Findinas
  change process missed the removal of the siphon break,
Plant information Report (PIR) 2-95-174 documented the licensee's investigation of the
  b.     Observations and Findinas
missing siphon break. The licensee's review concluded that the section of piping, in which
  Plant information Report (PIR) 2-95-174 documented the licensee's investigation of the
the siphon break was located, may have been removed and replaced during a modification
  missing siphon break. The licensee's review concluded that the section of piping, in which
performed in 1992 to install a CST nitrogen blanketing system. The modification included
  the siphon break was located, may have been removed and replaced during a modification
the addition of a stiffener beam on the internal tank wall that required the recirculation loop
  performed in 1992 to install a CST nitrogen blanketing system. The modification included
suction piping to be modified to provide clearance for the beam.
  the addition of a stiffener beam on the internal tank wall that required the recirculation loop
The interference problem between the stiffener and the recirculation piping was not
  suction piping to be modified to provide clearance for the beam.
identified during the initial modification design. When the problem was identified a design
  The interference problem between the stiffener and the recirculation piping was not
change notice (DCN) was processed to provide details on how to modify the piping.
  identified during the initial modification design. When the problem was identified a design
However, the drawing provided with this DCN did not depict the existence of the siphon
  change notice (DCN) was processed to provide details on how to modify the piping.
break hole.
  However, the drawing provided with this DCN did not depict the existence of the siphon
The work description in the work order that modified the piping was to " fabricate and
  break hole.
installinternal piping to the CST per drawing #25203-13006 Sheet 44". Although only
  The work description in the work order that modified the piping was to " fabricate and
the section of piping at the elevation of the stiffener beam was affected, the work order
  installinternal piping to the CST per drawing #25203-13006 Sheet 44". Although only
did not preclude the replacement of the section of piping that contained the siphon break
  the section of piping at the elevation of the stiffener beam was affected, the work order
hole, nor did the drawing provide the details necessary to drill the hole in the event the
  did not preclude the replacement of the section of piping that contained the siphon break
piping was replaced.
  hole, nor did the drawing provide the details necessary to drill the hole in the event the
The cause of the event appears to be inadequate attention to detail during the preparation
  piping was replaced.
of the DCN and the associated drawing since other drawings (the system piping and
  The cause of the event appears to be inadequate attention to detail during the preparation
  of the DCN and the associated drawing since other drawings (the system piping and


                                                                                      -         _
-
                                                                                                  I
_
  .
I
                                                  19
.
    instrumentation drawing and the original piping isometric drawing) showed the existence of
19
    a siphon break hole.
instrumentation drawing and the original piping isometric drawing) showed the existence of
    The licensee briefed the design engineering staff on this event and the need to pay
a siphon break hole.
    particular attention to less obvious design attributes such as siphon breakers when
The licensee briefed the design engineering staff on this event and the need to pay
    developing design changes. Also, since the time of this event, the licensee has
particular attention to less obvious design attributes such as siphon breakers when
    implemented programmatic improvements to the design control process to improve the
developing design changes. Also, since the time of this event, the licensee has
    effectiveness of the process.
implemented programmatic improvements to the design control process to improve the
    The inspector noted that the plant technical specifications require the maintenance of a
effectiveness of the process.
    minimum volume of 150,000 gallons of water in the CST when in modes 1,2 or 3 and the
The inspector noted that the plant technical specifications require the maintenance of a
    volume is verified every 12 hours. These requirements reduce the possibility of a
minimum volume of 150,000 gallons of water in the CST when in modes 1,2 or 3 and the
    significant, undetected loss of CST inventory when the plant is in operation.
volume is verified every 12 hours. These requirements reduce the possibility of a
    c.     Conclusion                                                                             l
significant, undetected loss of CST inventory when the plant is in operation.
    The inspector concluded that the licensee had taken appropriate actions to resolve this
c.
    issue. However, the inspector noted that the licensee evaluation could have been more
Conclusion
    thorough in that the investigator did not review the associated work order until questioned
l
    by the inspector. A review of the work order was necessary to determine if the event may
The inspector concluded that the licensee had taken appropriate actions to resolve this
    have been a result of poor work controls, which has been a problem in the past at this site.
issue. However, the inspector noted that the licensee evaluation could have been more
    This item is closed.
thorough in that the investigator did not review the associated work order until questioned
    E8.2 LClosed) Unresolved item 50-336/95-11-03: 10 CFR 21 Reportability Review
by the inspector. A review of the work order was necessary to determine if the event may
    a.     Inspection Scone (92903)
have been a result of poor work controls, which has been a problem in the past at this site.
    Following the licensee identification of several design problems that affected replacement
This item is closed.
    components of the engineered safeguards actuation system (ESAS) cabinets, the NRC
E8.2 LClosed) Unresolved item 50-336/95-11-03: 10 CFR 21 Reportability Review
    inspectors questioned if the findings had been reviewed for reportability under the
a.
    requirements of 10 CFR 21, " Reporting of Defects and Noncompliance." At the time of
Inspection Scone (92903)
    the inspection in 1995, no formal review had been initiated and the issue was unresolved
Following the licensee identification of several design problems that affected replacement
    pending further actions to be taken by NU, and NRC review of the licensee actions.
components of the engineered safeguards actuation system (ESAS) cabinets, the NRC
    b.     Observations and Findinas
inspectors questioned if the findings had been reviewed for reportability under the
    in June 1995, the licensee performed an assessment of the design problems experienced
requirements of 10 CFR 21, " Reporting of Defects and Noncompliance." At the time of
    with the ESAS system during the previous two refueling outages. The assessment
the inspection in 1995, no formal review had been initiated and the issue was unresolved
    identified four significant design problems that were related to defects in the components
pending further actions to be taken by NU, and NRC review of the licensee actions.
    provided by the vendor. The four problems were assessed for reportability in engineering
b.
    evaluation M2-EV-97-0004, Revision 0, " Evaluation of URI 95-11-03, Reportability of
Observations and Findinas
    ESAS Design Deficiencies."
in June 1995, the licensee performed an assessment of the design problems experienced
    Three of the four issues had been reported to the NRC in Licensee Event Reports (LERs)
with the ESAS system during the previous two refueling outages. The assessment
    94-12-00, 95-18-00 and 95-21-00. The issue associated with LER 94-12-00 had also
identified four significant design problems that were related to defects in the components
    been reported by the vendor ~(Eaton Corporation) in accordance 10 CFR 21. The fourth
provided by the vendor. The four problems were assessed for reportability in engineering
    issue was documented in ACR 00506 and the licensee had determined that the issue was
evaluation M2-EV-97-0004, Revision 0, " Evaluation of URI 95-11-03, Reportability of
    not reportable.
ESAS Design Deficiencies."
Three of the four issues had been reported to the NRC in Licensee Event Reports (LERs)
94-12-00, 95-18-00 and 95-21-00. The issue associated with LER 94-12-00 had also
been reported by the vendor ~(Eaton Corporation) in accordance 10 CFR 21. The fourth
issue was documented in ACR 00506 and the licensee had determined that the issue was
not reportable.
,
,


                                                                                              _. _
_.
_
.,
.,
                                                                                                      i
i
                                                                                                      !
!
  .
.
                                                                                                      i
20
                                                  20
The engineering evaluation notea that problems reported in an LER did not require
    The engineering evaluation notea that problems reported in an LER did not require                 ;
additional reporting in accordance with 10 CFR 21. The bases for an LER fulfilling the
    additional reporting in accordance with 10 CFR 21. The bases for an LER fulfilling the           {
{
    licensee's reporting obligations under 10 CFR 21 is contained in 10 CFR 21.2(c).                 '
licensee's reporting obligations under 10 CFR 21 is contained in 10 CFR 21.2(c).
    The inspector also noted in discussions with the licensee that the components that were
'
    'the subject of LERs 95-018 and 95-021 were designs that were unique to Millstone Unit 2.         l
The inspector also noted in discussions with the licensee that the components that were
      c.   Conclusion
'the subject of LERs 95-018 and 95-021 were designs that were unique to Millstone Unit 2.
    The inspector reviewed the licensee evaluation, LERs and ACR and found that the licensee
c.
      appropriately evaluated and reported the failures to the NRC. This item is closed.
Conclusion
                                                                                                      1
The inspector reviewed the licensee evaluation, LERs and ACR and found that the licensee
                                                                                                      ,
appropriately evaluated and reported the failures to the NRC. This item is closed.
                                                                                                      1
,
                                                                                                      l
1
                                                                                                      1
l
                                                                                                      I
1
                                                                                                      l
l
                                                                                                      j
j
                                                                                                  - .
- .


                                                                        __ __         _         _ __ __
__ __
_
_
__ __
&
&
i
i
n.
n.
,
21
                                                  21
,
.
.
                                          Reoort Details
Reoort Details
  Summary of Unit 3 Status
Summary of Unit 3 Status
  Unit 3 remained in cold shutdown (mode 5) status throughout the inspection period. The                 ;
Unit 3 remained in cold shutdown (mode 5) status throughout the inspection period. The
  licensee continued its implementation of the Millstone Unit 3 Recovery Plan and the                     '
;
  configuration management program activities in support of the milestones leading to the
licensee continued its implementation of the Millstone Unit 3 Recovery Plan and the
  readiness for the unit restart. In accordance with commitments made to the NRC with
'
  regard to corrective action progress and documentation of the completed work items, the
configuration management program activities in support of the milestones leading to the
  licensee provided the first set of corrective action completion packages for NRC review.               ;
readiness for the unit restart. In accordance with commitments made to the NRC with
; To date, the presentation of such packages to the NRC has been timely,. relative to the
regard to corrective action progress and documentation of the completed work items, the
  scheduled workload. This documentation has also provided evidence of progress in the
licensee provided the first set of corrective action completion packages for NRC review.
  resolution of open NRC inspection items, as well as an indication of the licensee efforts to
;
  demonstrate corrective action program effectiveness. NRC review of the available closure
;
                                                                                                            )
To date, the presentation of such packages to the NRC has been timely,. relative to the
packages will continue as an ongoing process, with the individual technical issues
scheduled workload. This documentation has also provided evidence of progress in the
  discussed, as appropriate, in the following report sections and in future NRC inspection                 l
resolution of open NRC inspection items, as well as an indication of the licensee efforts to
  reports.
demonstrate corrective action program effectiveness. NRC review of the available closure
  On January 22,1997, the appointment of Mr. M. H. Brothers, then the Unit 3 Director, to
)
packages will continue as an ongoing process, with the individual technical issues
,
discussed, as appropriate, in the following report sections and in future NRC inspection
reports.
On January 22,1997, the appointment of Mr. M. H. Brothers, then the Unit 3 Director, to
the position of Vice President-Millstone Unit 3, was announced, in this new position, Mr.
-
-
  the position of Vice President-Millstone Unit 3, was announced, in this new position, Mr.
j
Brothers fills the role of Recovery Officer for the unit. On January 28,1997, Mr. Brothers
Brothers fills the role of Recovery Officer for the unit. On January 28,1997, Mr. Brothers
  announced the appointment of Mr. G. D. Hicks, who had been serving on the Carolina
announced the appointment of Mr. G. D. Hicks, who had been serving on the Carolina
  Power & Light Recovery Team for Unit 3, to the position of Unit 3 Director, in an acting
Power & Light Recovery Team for Unit 3, to the position of Unit 3 Director, in an acting
  capacity. Both of these managerial changes became effective on February 3,1997. The
capacity. Both of these managerial changes became effective on February 3,1997. The
  inspector noted that Mr. Hicks' qualifications to assume the Unit 3 Director position had
inspector noted that Mr. Hicks' qualifications to assume the Unit 3 Director position had
  been reviewed by both the licensing department and the Nuclear Safety & Oversight
been reviewed by both the licensing department and the Nuclear Safety & Oversight
  organization. -The inspector also reviewed section 6.3.1 of the unit technical specifications
organization. -The inspector also reviewed section 6.3.1 of the unit technical specifications
and American National Standard, ANSI N18.1-1971, regarding " Plant Managers" and -
?
d
d
  and American National Standard, ANSI N18.1-1971, regarding " Plant Managers" and -                    ?
identified no qualification concerns or other questions regarding these licensee
  identified no qualification concerns or other questions regarding these licensee
management changes.
  management changes.
:
:
                                          U3.1 ODer8tions
U3.1 ODer8tions
  U3 01           Conduct of Operations
U3 01
  01.1 General Comments (71707)
Conduct of Operations
  Using inspection Procedure 71707, the inspectors conducted frequent reviews of ongoing
01.1 General Comments (71707)
    plant operations. During a walkdown of the Unit 3 intake structure, the inspector observed
Using inspection Procedure 71707, the inspectors conducted frequent reviews of ongoing
    large scale painting and materialimprovement work in progress. Various degrees of work
plant operations. During a walkdown of the Unit 3 intake structure, the inspector observed
    activity have been on-going in the intake structure since the licensee instituted a material
large scale painting and materialimprovement work in progress. Various degrees of work
    condition improvement project in the Spring of 1996. The inspector noted that adverse
activity have been on-going in the intake structure since the licensee instituted a material
    condition report M3-97-0370, dated February 1,1997, was written to report that station
condition improvement project in the Spring of 1996. The inspector noted that adverse
    air and instrument air supply piping in the intake structure was in poor extemal condition.
condition report M3-97-0370, dated February 1,1997, was written to report that station
    The licensee is planning to replace or paint the piping. In general, the conduct of
air and instrument air supply piping in the intake structure was in poor extemal condition.
    operations was professional and safety-conscious; specific events and noteworthy
The licensee is planning to replace or paint the piping. In general, the conduct of
i observations are detailed in the sections below.
operations was professional and safety-conscious; specific events and noteworthy
i
observations are detailed in the sections below.
e
e


  , _ ,_ . _ _ _ . . -             . _ _ ~         . -. _ _ . _ _.. _ ._ _ _ _ _ _ _ _ . _ . _ _ _ _ _ _ . _
, _ ,_ . _ _ _ . . -
                                                                                                                        '
. _ _ ~
                                                                                                                        '
. -. _ _ . _ _.. _ ._ _ _ _ _ _ _ _ . _ . _ _ _ _ _ _ . _
i
'
    .
i
'
.
1
1
.
.
j                                                                             22
j
22
i
i
!               < Over the course of this inspection, the inspectors witnessed and/or reviewed a number of             l
!
b                 ,. operational activities, and noted the following observations and assessments of operations         !
< Over the course of this inspection, the inspectors witnessed and/or reviewed a number of
!                   performance:
b
                                                                                                                        ;
,. operational activities, and noted the following observations and assessments of operations
                    *      Good contingency planning (e.g., preparation for field flashing the "B" emergency _
!
f                           diesel generator during the Battery 2 outage) was in evidence.                           -t
!
                                                                        ~
performance:
;
Good contingency planning (e.g., preparation for field flashing the "B" emergency _
*
f
diesel generator during the Battery 2 outage) was in evidence.
-t
'
'
                    *      Appropriate regulatory provisions (e.g', a technical specification [TS] " bases"           -
Appropriate regulatory provisions (e.g', a technical specification [TS] " bases"
j                           change to allow operation of the safety injection pumps in mode 5 to fill an               ,
~
:                           accumulator) were considered and dispositioned to address emergent operational             ;
*
                            conditions.                                                                                 j
-
j
change to allow operation of the safety injection pumps in mode 5 to fill an
,
:
accumulator) were considered and dispositioned to address emergent operational
;
conditions.
j
m
m
[                   *-      Consideration of how the incore flux mapping results affect the quadrant power tilt         I
[
                            ratio (OPTR) was found to be consistent with both the TS definition for QPTR and
Consideration of how the incore flux mapping results affect the quadrant power tilt
f                           the Westinghouse position statement on " core tilt".                                     j
I
*-
ratio (OPTR) was found to be consistent with both the TS definition for QPTR and
f
the Westinghouse position statement on " core tilt".
j
:
-
Evaluation of the calibration provisions for the range and accuracy of digital
l
-
-
                                                                                                                        :
*
-                  *       Evaluation of the calibration provisions for the range and accuracy of digital              l
j-
j-                         instrumentation utilized in the performance of operational surveillances was               i
instrumentation utilized in the performance of operational surveillances was
j-   >
i
                            determined to meet the NRC guidance discussed.in NUREG-1482.                         4
j-
                                                                                                                        ,
>
                                                                                                                        ;
determined to meet the NRC guidance discussed.in NUREG-1482.
4
,
i
i
j                   *      Reductions in the range of reactor coolant system operating temperatures (i.e., T-
;
                            avg) to maintain margins relative to nil ductility transition (NDT) considerations were
j
!'                         implemented consistent with both TS 3.4.10 and ASME Code requirements.
Reductions in the range of reactor coolant system operating temperatures (i.e., T-
*
avg) to maintain margins relative to nil ductility transition (NDT) considerations were
!'
implemented consistent with both TS 3.4.10 and ASME Code requirements.
!-
!-
.                  *      The implementation of temporary modifications (e.g., a bypass-jumper for cross-           j
The implementation of temporary modifications (e.g., a bypass-jumper for cross-
i                           tying trains in the auxiliary feedwater system flow paths) was determined to be
j
j,                         conservative in providing additional heat sinks (i.e., two steam generators) for
*
;                         mshutdown risk considerations.
.
i                                                           .                                                           i
i
;                   *      The licensee discovery of potential discrepancies in the personal qualification-             )
tying trains in the auxiliary feedwater system flow paths) was determined to be
l                           statements (NRC Form 398) of certain Unit 3 licensed operators has been assessed             !
j,
                            for immediate impact and determined to require further evaluation. (NOTE: See               j
conservative in providing additional heat sinks (i.e., two steam generators) for
                            unresolved item associated with similar Unit 1 activities - Section U1.05.1 of this         i
;
h                           inspection report)                                                                           !
mshutdown risk considerations.
4                   Additionally, during control room inspections and reviews of TS limiting condition for
i
.
i
;
The licensee discovery of potential discrepancies in the personal qualification-
)
*
l
statements (NRC Form 398) of certain Unit 3 licensed operators has been assessed
for immediate impact and determined to require further evaluation. (NOTE: See
j
unresolved item associated with similar Unit 1 activities - Section U1.05.1 of this
i
h
inspection report)
4
Additionally, during control room inspections and reviews of TS limiting condition for
-
-
                    operability (LCO) action statements, the inspector raised a question regarding the
operability (LCO) action statements, the inspector raised a question regarding the
!                   applicability of actions for single system / train inoperability when more than one system or
!
applicability of actions for single system / train inoperability when more than one system or
train is determined to be inoperable. Examples where the need for interpretation of the
i
4
4
                    train is determined to be inoperable. Examples where the need for interpretation of the            i
LCO actions might be appropriate for multiple system or component unavailability were
$                  LCO actions might be appropriate for multiple system or component unavailability were
$
I                   identified in TS 3.7.7 and 3.7.1.2. The inspector also noted recent correspondence (i.e., a         !
I
identified in TS 3.7.7 and 3.7.1.2. The inspector also noted recent correspondence (i.e., a
'
'
                    memorandum dated January 17,1997) from the Unit 3 licensing staff providing a                       ,
memorandum dated January 17,1997) from the Unit 3 licensing staff providing a
;                   clarification of TS terminology, e.g., how to interpret "at least once per 7 days". The             ;
,
j                   inspector determined that the licensee needed to further develop its approach to
;
clarification of TS terminology, e.g., how to interpret "at least once per 7 days". The
;
j
inspector determined that the licensee needed to further develop its approach to
4'
4'
                    promulgating such interpretive guidance. While no TS violations or technical concerns
promulgating such interpretive guidance. While no TS violations or technical concerns
j                   were evident in the areas of TS compliance questioned by the inspector, a standardized
j
g                  method for disseminating Unit 3 policy in the interpretation of TS language and LCO
were evident in the areas of TS compliance questioned by the inspector, a standardized
j'                 actions appears prudent. The inspector discussed this issue with cognizant licensee
method for disseminating Unit 3 policy in the interpretation of TS language and LCO
gj'
actions appears prudent. The inspector discussed this issue with cognizant licensee
.'
.'
,                                                                                                                      i
\\
                                                                                                                        \
i
,
&
&
"
"
                                                        ,                                                         _
,
_


  ,
,
  .
.
                                                  23
23
    personnel and intends to review this matter further as an inspector followup item. (IFl
personnel and intends to review this matter further as an inspector followup item. (IFl
    423/97-01-06)
423/97-01-06)
    01.2 Control of Hiah Enerav Line Break (HELB) Doors
01.2 Control of Hiah Enerav Line Break (HELB) Doors
    a.     Insoection Scooe (71707)
a.
    On several occasions during this inspection period the licensee identified that HELB doors
Insoection Scooe (71707)
    were open or not fully latched. These conditions were reported in accordance with 10 CFR
On several occasions during this inspection period the licensee identified that HELB doors
    50.72 as a condition that could have prevented a safety system from functioning as
were open or not fully latched. These conditions were reported in accordance with 10 CFR
    required. The inspector reviewed the licensee's corrective actions to assess the
50.72 as a condition that could have prevented a safety system from functioning as
    effectiveness of the licensee's root cause determination and whether appropriate corrective
required. The inspector reviewed the licensee's corrective actions to assess the
    actions were identified and implemented to prevent recurrence of the adverse condition.           ;
effectiveness of the licensee's root cause determination and whether appropriate corrective
actions were identified and implemented to prevent recurrence of the adverse condition.
*
*
                                                                                                      I
b.
    b.     Observations and Findinas                                                               ,
Observations and Findinas
    On January 10,1997, the licensee reported that the HELB door to the "A" train 4160 volt           l
,
    switchgear room was open. The door had been opened to facilitate battery 301 A-1                 ,
On January 10,1997, the licensee reported that the HELB door to the "A" train 4160 volt
    replacement. Within the next few days, four additional occurrences of an open or                   ;
switchgear room was open. The door had been opened to facilitate battery 301 A-1
    improperly latched HELB door were identified, including one by the resident inspector. All         l
,
    the doors had a HELB sign affixed on both sides of the door.
replacement. Within the next few days, four additional occurrences of an open or
    As a result of these incidents, a level "B" adverse condition report (ACR) was gererated         i
improperly latched HELB door were identified, including one by the resident inspector. All
    and an event review team assembled. As an immediate corrective action, a work stand           -
the doors had a HELB sign affixed on both sides of the door.
    down was held within all departments and licensee management briefed employees on the             ;
As a result of these incidents, a level "B" adverse condition report (ACR) was gererated
    control of plant doors. During the next several days, several other ACRs regarding HELB           !
i
    issues were generated; including doors not being appropriately labeled in the field or on
and an event review team assembled. As an immediate corrective action, a work stand
    prints.
-
                                                                                                      !
down was held within all departments and licensee management briefed employees on the
    The licensee's root cause investigation detarmined that the cause of the events was a             :
control of plant doors. During the next several days, several other ACRs regarding HELB
    failure to develop and implement a HELB door control program, which resulted in a lack of
issues were generated; including doors not being appropriately labeled in the field or on
    understanding of the HELB requirements associated with the plant design basis. Corrective         l
prints.
    actions included: develop a door control program, insert a door control training module in
The licensee's root cause investigation detarmined that the cause of the events was a
    general employee training, and simplify and label all HELB doors. Although not specifically
failure to develop and implement a HELB door control program, which resulted in a lack of
    stated in the corrective action plan, the licensee indicated that door labels would specify
understanding of the HELB requirements associated with the plant design basis. Corrective
    the number of turns required to latch the doors.
actions included: develop a door control program, insert a door control training module in
    As part of the investigation, the licensee concluded that the HELB door issue was not a
general employee training, and simplify and label all HELB doors. Although not specifically
    reportable condition with the plant in modes 5 or 6. Final Safety Analysis Report, Section
stated in the corrective action plan, the licensee indicated that door labels would specify
    3.6.1 states that a high energy system is a fluid system that operates during normal plant
the number of turns required to latch the doors.
    operating conditions. Normal plant conditions are defined as startup, operation at power,
As part of the investigation, the licensee concluded that the HELB door issue was not a
    hot standby, or reactor cooldown to cold shutdown conditions. Therefore, those
reportable condition with the plant in modes 5 or 6. Final Safety Analysis Report, Section
    conditions that were identified while in mode 5 were retracted. However, the licensee
3.6.1 states that a high energy system is a fluid system that operates during normal plant
    concluded that the status of HELB doors should be considered in the shutdown risk
operating conditions. Normal plant conditions are defined as startup, operation at power,
    program since a rupture of the hot water heating line in the service building could result in
hot standby, or reactor cooldown to cold shutdown conditions. Therefore, those
    the loss of safety-related equipment located in the switchgear room, independent of the
conditions that were identified while in mode 5 were retracted. However, the licensee
    plant mode.
concluded that the status of HELB doors should be considered in the shutdown risk
program since a rupture of the hot water heating line in the service building could result in
the loss of safety-related equipment located in the switchgear room, independent of the
plant mode.


      .
.
    .
.
                                                      24
24
        The inspector toured the plant and verified that HELB doors 'nere properly latched.
The inspector toured the plant and verified that HELB doors 'nere properly latched.
        Applicable HELB doors were labeled to indicated the required number of turns to properly
Applicable HELB doors were labeled to indicated the required number of turns to properly
        latch the door. The inspector also verified that a training module was being developed for
latch the door. The inspector also verified that a training module was being developed for
        inclusion in the general employee training. The other corrective actions are scheduled to
inclusion in the general employee training. The other corrective actions are scheduled to
        be complete prior to the unit entering mode 4.
be complete prior to the unit entering mode 4.
        c.     Conclusion
c.
        The licensee's root cause investigation and corrective action plan for control of HELB doors
Conclusion
        were determined to be good. However, the requirement to label the required HELB doors
The licensee's root cause investigation and corrective action plan for control of HELB doors
        with a minimum number of turns to ensure prope- U.ching should have been included in
were determined to be good. However, the requirement to label the required HELB doors
        the ACR corrective action plan if it was deemed necessary to prevent recurrence.
with a minimum number of turns to ensure prope- U.ching should have been included in
        U3 03           Operations Proceduies and Documentation
the ACR corrective action plan if it was deemed necessary to prevent recurrence.
        a.     Inspection Scope
U3 03
                                                                                                      i
Operations Proceduies and Documentation
        The purpose of this inspection was to determine the adequacy of the procedure upgrade         ;
a.
        program (PUP) as it applies to Unit 3. The licensee started the PUP in 1992 to standardize     !
Inspection Scope
        procedure format for all units on the site and to improve the technical adequacy of all       j
i
        procedures. The process was a third iteration of previous procedure improvement             'i
The purpose of this inspection was to determine the adequacy of the procedure upgrade
        programs which were started in the late 1980's. This inspection was performed from             j
program (PUP) as it applies to Unit 3. The licensee started the PUP in 1992 to standardize
        August 1996 through February 24,1997.
procedure format for all units on the site and to improve the technical adequacy of all
        The onsite inspection included interviews with the site PUP group, Unit 3 procedure
j
        coordinators and procedure writers, station oversight group, station quality assurance, and
procedures. The process was a third iteration of previous procedure improvement
        Unit 1 operations personnel. Documents reviewed included, but were not limited to,
'i
        document control (DC) procedures: DC-1, " Administration of Millstone Procedures and
programs which were started in the late 1980's. This inspection was performed from
        Forms"; DC-2, " Developing and Revising Millstone Procedures and Forms"; DC-3,
j
        " Verification and Validation of Millstone Procedures and Forms"; and a sample uf Unit 3
August 1996 through February 24,1997.
        procedures which had already been upgraded. in addition, the inspector reviewed the
The onsite inspection included interviews with the site PUP group, Unit 3 procedure
        Millstone Unit 3 PUP self assessment of their Operations Department (conducted March-         '
coordinators and procedure writers, station oversight group, station quality assurance, and
,      May,1996); Millstone Unit 1 PUP self assessment of their Operations Department                 I
Unit 1 operations personnel. Documents reviewed included, but were not limited to,
        (conducted May-June,1996); Station oversight audit conducted during September 1996;
document control (DC) procedures: DC-1, " Administration of Millstone Procedures and
        and various procedure related adverse condition reports (ACRs).
Forms"; DC-2, " Developing and Revising Millstone Procedures and Forms"; DC-3,
        Although the focus of this inspection was Unit 3, the Unit 1 self assessment was reviewed
" Verification and Validation of Millstone Procedures and Forms"; and a sample uf Unit 3
        and discussed with Unit 1 personnel who performed the assessment and the Unit 1
procedures which had already been upgraded. in addition, the inspector reviewed the
        Operations Manager. The inspector considered its potential applicability to Unit 3.
Millstone Unit 3 PUP self assessment of their Operations Department (conducted March-
'
May,1996); Millstone Unit 1 PUP self assessment of their Operations Department
,
,
        b.     Observations and Findinas
(conducted May-June,1996); Station oversight audit conducted during September 1996;
        At the start of this inspection, there was a station wide Procedure Upgrade Group to
and various procedure related adverse condition reports (ACRs).
        provide overall control of the program. This group developed and maintaineci the station
Although the focus of this inspection was Unit 3, the Unit 1 self assessment was reviewed
        DC procedures for control of the program, the overall status of upgraded procedures,
and discussed with Unit 1 personnel who performed the assessment and the Unit 1
        coordinators for each Millstone Unit, and the hiring of contractors, as necessary, to write
Operations Manager. The inspector considered its potential applicability to Unit 3.
        the procedures. The actual upgrade of procedures was the responsibility of each
b.
        department within each unit. Since the licensee's reorganization in October 1996, the
Observations and Findinas
  __
,
At the start of this inspection, there was a station wide Procedure Upgrade Group to
provide overall control of the program. This group developed and maintaineci the station
DC procedures for control of the program, the overall status of upgraded procedures,
coordinators for each Millstone Unit, and the hiring of contractors, as necessary, to write
the procedures. The actual upgrade of procedures was the responsibility of each
department within each unit. Since the licensee's reorganization in October 1996, the


.
.
.
                                                  25
.
  station PUP group has been decentralized. The group now controls the station
25
  administrative procedures including the PUP DC procedures. It has no control of the
station PUP group has been decentralized. The group now controls the station
  production of upgraded procedures. Despite the changes in PUP control, the quality and
administrative procedures including the PUP DC procedures. It has no control of the
  quantity of upgraded procedures has depended on the individual technical departments in
production of upgraded procedures. Despite the changes in PUP control, the quality and
  each unit.
quantity of upgraded procedures has depended on the individual technical departments in
  A review of the program as it applies to Unit 3 noted the following:
each unit.
                                                                                                1
A review of the program as it applies to Unit 3 noted the following:
  *      The program has been effective in standardizing procedure formats. The document
The program has been effective in standardizing procedure formats. The document
          control procedures are lengthy and cumbersome to use, but appear to be                 I
*
          comprehensive. The quality of the upgraded procedures appears to depend on the       l
control procedures are lengthy and cumbersome to use, but appear to be
          producers of the procedures and the adequacy of the performance verification and     l
comprehensive. The quality of the upgraded procedures appears to depend on the
          validation (V&V) process rather than on any apparent process deficiency.             l
producers of the procedures and the adequacy of the performance verification and
                                                                                                l
validation (V&V) process rather than on any apparent process deficiency.
                                                                                                1
1
  *      The V&V process can be by table top review, procedure walkdowns, or by               i
The V&V process can be by table top review, procedure walkdowns, or by
          procedure performance. All three methods are used, but the table top review by a     I
i
          technical peer is the most common form of validation for Operations and               ;
*
          Maintenance Department procedures. Instrument & Control procedure technicians       !
procedure performance. All three methods are used, but the table top review by a
          stated that when possible their V&V process consisted of procedure walkdowns. -
technical peer is the most common form of validation for Operations and
  *      In general, management involvement in the upgrade process seems to be minimal.
Maintenance Department procedures. Instrument & Control procedure technicians
          Some department managers have more involvement than others. There is heavy
stated that when possible their V&V process consisted of procedure walkdowns. -
          reliance on the procedure coordinators for each department. For example, the Unit   ,
In general, management involvement in the upgrade process seems to be minimal.
          3 operations manager authorized his procedure coordinator to act on his behalf for
*
          procedure review and approval.                                                       ,
Some department managers have more involvement than others. There is heavy
                                                                                                I
reliance on the procedure coordinators for each department. For example, the Unit
  *      The inspector noted that during the five years that the PUP has been in place, there
,
          had been no Quality Assurance (QA) audits of the program itself. Unit 3 Operations
3 operations manager authorized his procedure coordinator to act on his behalf for
          Department had performed a self assessment of the PUP process in May 1996, but
procedure review and approval.
          this assessment was fairly limited. As a result of this NRC inspection, the licensee I
,
          performed two further assessments of the PUP program as it relates to Unit 3.       )
The inspector noted that during the five years that the PUP has been in place, there
                                                                                                1
*
          An assessment of the verification and validation process by Nuclear Oversight for   !
had been no Quality Assurance (QA) audits of the program itself. Unit 3 Operations
          Unit 3 was performed in September 1996. This assessment noted some
Department had performed a self assessment of the PUP process in May 1996, but
          weaknesses and problems in the V&V process. Another assessment was performed
this assessment was fairly limited. As a result of this NRC inspection, the licensee
          on the PUP program for Units 1,2 and 3, November 13-16,1996, by the Region
performed two further assessments of the PUP program as it relates to Unit 3.
          One Procedere Working Group. This group is composed of persons from other NRC
An assessment of the verification and validation process by Nuclear Oversight for
          Region i nuclear utilities. This assessment also noted strengths and weaknesses.
Unit 3 was performed in September 1996. This assessment noted some
          Both assessments noted deficiencies in the PUP program but did not conclude that
weaknesses and problems in the V&V process. Another assessment was performed
          the program was seriously flawed.
on the PUP program for Units 1,2 and 3, November 13-16,1996, by the Region
  *      On February 19,1997, the licensee forwarded to the inspector three recent QA
One Procedere Working Group. This group is composed of persons from other NRC
          audits and fourteen quality control surveillance activities performed in the last
Region i nuclear utilities. This assessment also noted strengths and weaknesses.
          quarter of 1996 and the first quarter of 1997. These audits and surveillance
Both assessments noted deficiencies in the PUP program but did not conclude that
          indicated that procedures are routinely reviewed as part of that activity and, where
the program was seriously flawed.
          appropriate, procedure deficiencies are identified. Also forwarded were recent
On February 19,1997, the licensee forwarded to the inspector three recent QA
          adverse condition reports identifying procedure problems.
*
audits and fourteen quality control surveillance activities performed in the last
quarter of 1996 and the first quarter of 1997. These audits and surveillance
indicated that procedures are routinely reviewed as part of that activity and, where
appropriate, procedure deficiencies are identified. Also forwarded were recent
adverse condition reports identifying procedure problems.


    ..
..
            .
.
      .
.
                                                      26
26
        *  As part of the PUP, the licensee developed the procedure basis document. The
As part of the PUP, the licensee developed the procedure basis document. The
  *
*
            Intent'of this document was to duplicate the procedure and to add blocks at certain
Intent'of this document was to duplicate the procedure and to add blocks at certain
            points to indicate the source or basis for key technical information such as the Final
*
          ~ Safety Analysis Report (FSAR), vendor. manual, technical specification, regulatory
points to indicate the source or basis for key technical information such as the Final
            commitments, etc. The Region One Procedure Working Group report considered the
~ Safety Analysis Report (FSAR), vendor. manual, technical specification, regulatory
,            basis document a strength, inspector's conversations with many plant personnel
commitments, etc. The Region One Procedure Working Group report considered the
;            indicated that they had high expectations from this document.
basis document a strength, inspector's conversations with many plant personnel
                                    _
,
indicated that they had high expectations from this document.
;
_
4~
4~
' The inspector reviewed numerous basis documents during the course of this
*
'
'
        * ' The inspector reviewed numerous basis documents during the course of this
inspection. While the basis document concept generally appears to be a strength,
            inspection. While the basis document concept generally appears to be a strength,
l
l           the inspector noted numerous basis documents to be incomplete. The documents
the inspector noted numerous basis documents to be incomplete. The documents
l.           were essentially the procedure with one or two basis blocks added in a pro forma
l.
j'           matter. Documents referenced in both the procedure and basis document were not
were essentially the procedure with one or two basis blocks added in a pro forma
i            further identified in the basis document as to where the referenced material actually
j'
.            applied. This appears to be's weakness in the practical usage of basis documents.
matter. Documents referenced in both the procedure and basis document were not
further identified in the basis document as to where the referenced material actually
i
applied. This appears to be's weakness in the practical usage of basis documents.
.
1
1
The licensee does not, however,' use the basis document as a procedure for plant
*
*
            The licensee does not, however,' use the basis document as a procedure for plant
operations.
            operations.
I
I
j       7e ^The inspector did a review of some Unit 3 operations procedures with a Unit 3 staff
j
j           engineer. Some minor technical (Hecrepancies were observed,' but were not
^The inspector did a review of some Unit 3 operations procedures with a Unit 3 staff
l           considered by the inspector to be' safety significant. In some cases, the operations
7e
j         . engineer had difficulty in determining the source for specific information in certain
j
j             procedures. For instance, the calculation for one instrument setpoint was only
engineer. Some minor technical (Hecrepancies were observed,' but were not
i-           available in the desk drawer of an l&C engineer; and the source of the setpoint was
l
j             not in the basis document. This was an example of one of several instances of
considered by the inspector to be' safety significant. In some cases, the operations
j
. engineer had difficulty in determining the source for specific information in certain
j
procedures. For instance, the calculation for one instrument setpoint was only
i-
available in the desk drawer of an l&C engineer; and the source of the setpoint was
j
not in the basis document. This was an example of one of several instances of
apparent configuration management control. However the configuration
-
-
              apparent configuration management control. However the configuration
i
i            management problem has already been identified to the licensee and is being
management problem has already been identified to the licensee and is being
              addressed generically by the licensee.
addressed generically by the licensee.
        *    As noted in previous NRC inspections, design basis discrepancies have been
As noted in previous NRC inspections, design basis discrepancies have been
              identified at all three Millstone units. It is possible that some procedures may not
*
              conform to the FSAR and other procedures may conform to FSAR conditions which
identified at all three Millstone units. It is possible that some procedures may not
              are contrary to the actual design basis. As a result of an NRC 10 CFR 50.54(f)
conform to the FSAR and other procedures may conform to FSAR conditions which
              letter, the licensee is currently performing an extensive design basis review which in
are contrary to the actual design basis. As a result of an NRC 10 CFR 50.54(f)
              turn will be independently verified. In a letter from the licensee dated July 22,
letter, the licensee is currently performing an extensive design basis review which in
            '1996, the licensee stated, in part, the following: "...As we believe was
turn will be independently verified. In a letter from the licensee dated July 22,
              communicated [to the NRC in a meeting conducted on April 30,1996], there was
'1996, the licensee stated, in part, the following: "...As we believe was
              no commitment to complete the PUP as a conditio 1 of restarting any of the
communicated [to the NRC in a meeting conducted on April 30,1996], there was
              [ Millstone] units. As part of the Operational Readiness Plan for Millstone unit No. 3,
no commitment to complete the PUP as a conditio 1 of restarting any of the
              findings resulting from the 10 CFR 50.54(f) related work will be reviewed to
[ Millstone] units. As part of the Operational Readiness Plan for Millstone unit No. 3,
              determine if any procedure modifications are required prior to restarting the unit.
findings resulting from the 10 CFR 50.54(f) related work will be reviewed to
              This will be done independent of procedure upgrades completed via the PUP..."
determine if any procedure modifications are required prior to restarting the unit.
              The licensee's corrective action plan for any required " procedure modifications" will
This will be done independent of procedure upgrades completed via the PUP..."
              be assessed in the future as part of the NRC restart assessment plan,
The licensee's corrective action plan for any required " procedure modifications" will
        *    The inspector observed that Unit 3 Operations Department had established a 67
be assessed in the future as part of the NRC restart assessment plan,
              page handbook in order to implement the DC procedures for the PUP process. This
The inspector observed that Unit 3 Operations Department had established a 67
              appeared to be an uncontrolled, unapproved and unofficial procedure. The licensee
*
page handbook in order to implement the DC procedures for the PUP process. This
appeared to be an uncontrolled, unapproved and unofficial procedure. The licensee


.
                                                                                                1
.
.
                                                  27
1
                                                                                                1
.
          stated at the conclusion of the onsite inspection that this handbook would be made
27
          into an officially controlled procedure. By telephone on February 26,1997, the
stated at the conclusion of the onsite inspection that this handbook would be made
          inspector was informed that the operations handbook had been deleted and only the
into an officially controlled procedure. By telephone on February 26,1997, the
                                                                                                !
inspector was informed that the operations handbook had been deleted and only the
          DC procedures were being used by the Operations Department as guidance for the
DC procedures were being used by the Operations Department as guidance for the
          PUP process.                                                                         .
PUP process.
                                                                                                l
.
          From January 13 through January 30,1997, the licensee's Nuclear Oversight             l
From January 13 through January 30,1997, the licensee's Nuclear Oversight
          Group conducted an audit in the areas of document control and the maintenance of     l
Group conducted an audit in the areas of document control and the maintenance of
          quality records. This audit identified a site-wide breakdown in the control of       j
l
          procedures in that procedures in use had not been properly updated. The               l
quality records. This audit identified a site-wide breakdown in the control of
          operations handbook (now deleted) was an example of an uncontrolled procedure in     I
j
          use. Because of its magnitude, the adverse condition report (ACR) generated by
procedures in that procedures in use had not been properly updated. The
          this audit was initially recommended for classification as a Level "A" ACR.
operations handbook (now deleted) was an example of an uncontrolled procedure in
  c.     Conclusions
use. Because of its magnitude, the adverse condition report (ACR) generated by
                                                                                                l
this audit was initially recommended for classification as a Level "A" ACR.
  The procedure upgrade program meets regulatory requirements and has been effective in         j
c.
  standardizing procedure formats across the site. The technical adequacy of upgraded           !
Conclusions
  procedures, except for a small sample of Unit 3 operations procedures, was not a subject     I
l
  for this inspection. Because of the number of individuals involved in procedure upgrade
The procedure upgrade program meets regulatory requirements and has been effective in
  and long period of time to upgrade the procedures (5 years), the quality of procedures       l
j
  vary. A number of ACRs reviewed indicate technical problems with some procedures
standardizing procedure formats across the site. The technical adequacy of upgraded
  already upgraded. The licensee has committed as part of their 10 CFR 50.54(f) process
procedures, except for a small sample of Unit 3 operations procedures, was not a subject
  and their Configuration Management Prograin to ensure procedures will meet the applicable
for this inspection. Because of the number of individuals involved in procedure upgrade
                                                                                              ~
and long period of time to upgrade the procedures (5 years), the quality of procedures
  design bases. The licensee's basis documents, as implemented, did not appear to meet
vary. A number of ACRs reviewed indicate technical problems with some procedures
  the licensee's own expectations as an adequate foundation for future procedure reviewers
already upgraded. The licensee has committed as part of their 10 CFR 50.54(f) process
  to have an adoquate technical basis for the information contained in each procedure.
and their Configuration Management Prograin to ensure procedures will meet the applicable
  U3 O'           Quality Assurance in Operations
~
  07.1 General Comments (40500,92901)
design bases. The licensee's basis documents, as implemented, did not appear to meet
  The inspector reviewed station procedures, assessed planned program changes, and
the licensee's own expectations as an adequate foundation for future procedure reviewers
  discussed various quality assurance activities with representatives from the Nuclear Safety
to have an adoquate technical basis for the information contained in each procedure.
  & Oversight (NS&O) organization and Unit 3 licensing, engineering and operations
U3 O'
  departments. The following topics were generally reviewed and evaluated during the
Quality Assurance in Operations
  conduct of this inspection:
07.1 General Comments (40500,92901)
  *        corrective action program changes (Revision 4 to the station procedure, RP-4,
The inspector reviewed station procedures, assessed planned program changes, and
            addressing " Corrective Action", effective February 25,1997)
discussed various quality assurance activities with representatives from the Nuclear Safety
  *      job rcAation between the Unit 3 line departments and the NS&O organization
& Oversight (NS&O) organization and Unit 3 licensing, engineering and operations
    *       engineering assurance recovery activities, conducted by the NS&O organization, to
departments. The following topics were generally reviewed and evaluated during the
            include planning and preparation for an Integrated Assessment Plan imp!ementation
conduct of this inspection:
            and review of the proposed changes to the Design Basis Document Package
corrective action program changes (Revision 4 to the station procedure, RP-4,
            upgrade program
*
addressing " Corrective Action", effective February 25,1997)
job rcAation between the Unit 3 line departments and the NS&O organization
*
engineering assurance recovery activities, conducted by the NS&O organization, to
*
include planning and preparation for an Integrated Assessment Plan imp!ementation
and review of the proposed changes to the Design Basis Document Package
upgrade program


.
.
.
                                                                                                I
.
                                                    28
I
  *
28
            issuance of a " Millstone 3 Line/ Oversight Interface Agreement"
issuance of a " Millstone 3 Line/ Oversight Interface Agreement"
  +        implementation of and subsequent release from a Quality and Assessment Services
*
            (QAS) " Hold" of all work on safety-related eqaipment requiring the use of "non-QA"
implementation of and subsequent release from a Quality and Assessment Services
            parts                                                                               j
+
                                                                                                  l
(QAS) " Hold" of all work on safety-related eqaipment requiring the use of "non-QA"
  With the progress of the noted program revisions, recovery activities, and organizational
parts
                                                                                                '
j
  initiatives still ongoing, the impact and effectiveness of the changes have not yet provided i
With the progress of the noted program revisions, recovery activities, and organizational
  measurable results. As of the end of this inspection period, the inspector observed           l
'
  increased NS&O involvement in performance monitoring, interfacing analysis, and support       l
initiatives still ongoing, the impact and effectiveness of the changes have not yet provided
  of the Unit 3 rnanagement and line staffs. Such involvement has included "real time"
i
  evaluation and feedback on routine operational activities and nonroutine' events. NRC
measurable results. As of the end of this inspection period, the inspector observed
  assessment of NS&O effectiveness (including an expectation of demonstrable results of the     ,
increased NS&O involvement in performance monitoring, interfacing analysis, and support
  corrective action program improvements) and specific QAS activities (e.g., Hold 97-1,         l
of the Unit 3 rnanagement and line staffs. Such involvement has included "real time"
  Revision 1) will continue over the course of the next severalinspection periods; covenng
evaluation and feedback on routine operational activities and nonroutine' events. NRC
  the ongoing recovery, open item closure, and work associated with the startup planning for
assessment of NS&O effectiveness (including an expectation of demonstrable results of the
  the unit.                                                                                     i
,
                                                                                                l
corrective action program improvements) and specific QAS activities (e.g., Hold 97-1,
                                          U3.Il Maintenance                                     l
Revision 1) will continue over the course of the next severalinspection periods; covenng
  USM1             Conduct of Maintenance
the ongoing recovery, open item closure, and work associated with the startup planning for
                                                                                                !
the unit.
  M 1.1 General Comments                                                                       I
i
  a.       Insoection Scoce (62707/61726)
U3.Il Maintenance
  The inspector observed / reviewed all or portions of the following maintenance and
l
  surveillance activities to verify proper calibration of test instruments, use of approved. +
USM1
  procedures, performance of work by qualified personnel, and conformance to technical
Conduct of Maintenance
    specification (TS) limiting conditions for operation.
M 1.1 General Comments
    *        M3-96-15203,         Battery 301 A-1 Removal
I
    *       M3-96-25108,         Calibrate ITT Barton (SP 3481B01)
a.
    *       SP 3626.8,           " Control Building Air Conditioning Booster Pump,3SWP'P2A,
Insoection Scoce (62707/61726)
                                  Operational Readiness Test"
The inspector observed / reviewed all or portions of the following maintenance and
  The inspector found the work performed under these activities to be professional and
surveillance activities to verify proper calibration of test instruments, use of approved.
    thorough. All activities observed were performed with the work package or surveillance
+
    procedure present at the job site and personnel were noted to be closely following the
procedures, performance of work by qualified personnel, and conformance to technical
    procedures. Review of the surveillance procedures revealed that the requirements of the     '
specification (TS) limiting conditions for operation.
    applicable TS were appropriately incorporated into the implementing procedure,
M3-96-15203,
                                                                                                ,
Battery 301 A-1 Removal
*
M3-96-25108,
Calibrate ITT Barton (SP 3481B01)
*
SP 3626.8,
" Control Building Air Conditioning Booster Pump,3SWP'P2A,
*
Operational Readiness Test"
The inspector found the work performed under these activities to be professional and
thorough. All activities observed were performed with the work package or surveillance
procedure present at the job site and personnel were noted to be closely following the
procedures. Review of the surveillance procedures revealed that the requirements of the
'
applicable TS were appropriately incorporated into the implementing procedure,
,


                                      __                  _   _
_ _
  .
_
                                                    29
_
    M1.2 Fix-It-Now (FIN) Conduct of Maintenance
.
    a.     Inspection Scope (62707)
29
M1.2 Fix-It-Now (FIN) Conduct of Maintenance
a.
Inspection Scope (62707)
^
^
    The licensee has implemented a number of changes to the work control process including
The licensee has implemented a number of changes to the work control process including
    the development of a FIN multi-discipline work team approach to augment the way
the development of a FIN multi-discipline work team approach to augment the way
    maintenance is performed at the unit. This process is in addition to their normal work
maintenance is performed at the unit. This process is in addition to their normal work
    control process. The inspector reviewed the FIN maintenance procedure and monitored
control process. The inspector reviewed the FIN maintenance procedure and monitored
    work that was performed under the FIN process to assess its implementation.
work that was performed under the FIN process to assess its implementation.
<
b.
    b.     Observations and Findinas
Observations and Findinas
    As part of the Unit 3 recovery process, the licensee developed a FIN work process to
<
    reduce the time it takes to respond to operations department needs, and to perform work
As part of the Unit 3 recovery process, the licensee developed a FIN work process to
    more efficiently. In addition, a minor maintenance work process was developed to allow         ,
reduce the time it takes to respond to operations department needs, and to perform work
    qualified personnel to accomplish tasks in a more efficient manner. It was envisioned that
more efficiently. In addition, a minor maintenance work process was developed to allow
    these work processes would contribute to reducing the corrective maintenance backlog.
,
    These work processes were initiated in November 1996.-
qualified personnel to accomplish tasks in a more efficient manner. It was envisioned that
    Maintenance procedure MP 3705B, "Fix It Now Conduct of Maintenance," states that the
these work processes would contribute to reducing the corrective maintenance backlog.
    FIN work process shall not be implemented for work requiring: major plant modifications,
These work processes were initiated in November 1996.-
    lengthy tag clearances, special radiological work permits that cannot be dispositioned by
Maintenance procedure MP 3705B, "Fix It Now Conduct of Maintenance," states that the
    the health physics (HP) team member, or repairs involving welding on specified plant
FIN work process shall not be implemented for work requiring: major plant modifications,
    equipment. The minor maintenance procedure U3 WC 1.1, " Minor Maintenance Process           "
lengthy tag clearances, special radiological work permits that cannot be dispositioned by
    Controls," allows work to be performed without the generation of a work order if the work       i
the health physics (HP) team member, or repairs involving welding on specified plant
    is performed on non-QA equipment and the work doesn't impact plant operations or require
equipment. The minor maintenance procedure U3 WC 1.1, " Minor Maintenance Process
    special work control needs.
"
                                                                                                    ,
Controls," allows work to be performed without the generation of a work order if the work
                                                                                                    i
i
    The FIN team is comprised of mechanics, electricians, maintenance planners, and                 '
is performed on non-QA equipment and the work doesn't impact plant operations or require
    instrument and control (l&C) technicians. In addition, there is a representative from the HP   l
special work control needs.
    and operations department, and an assigned first line supervisor (FLS). The inspector
,
    reviewed the training records for each FIN team member and verified that they were trained     ,
i
    on the new procedure. In addition, team members appeared to be well qualified. At least         i
The FIN team is comprised of mechanics, electricians, maintenance planners, and
    one member of the team was qualified for each of the matrices job tasks.
'
    Each morning the FIN team members review all the trouble reports (TRs) that were
instrument and control (l&C) technicians. In addition, there is a representative from the HP
    generated the previous day and determine which items can be performed by the team and
and operations department, and an assigned first line supervisor (FLS). The inspector
    which need to go through the normal maintenance process. At the 6:45 a.m. morning
reviewed the training records for each FIN team member and verified that they were trained
    meeting, the FIN team FLS notifies the operations shift manager and the work planning
,
    organization of the selected work items to ensure that these departments are cognizant of
on the new procedure. In addition, team members appeared to be well qualified. At least
    all FIN planned maintenance activities.
i
    The inspector attended the FIN and the 6:45 a.m. morning meeting. In addition to the off-
one member of the team was qualified for each of the matrices job tasks.
    going and on-coming shift managers, individuals at the 6:45 a.m. morning meeting
Each morning the FIN team members review all the trouble reports (TRs) that were
    included: the Unit Director, the operations, maintenance, l&C, and engineering department
generated the previous day and determine which items can be performed by the team and
      managers, and representatives from work planning, chemistry, and HP. Each TR is
which need to go through the normal maintenance process. At the 6:45 a.m. morning
    discussed then assigned to either the FIN or work planning department. Any TR that
meeting, the FIN team FLS notifies the operations shift manager and the work planning
      potentially affects equipment operability is identified and an adverse condition report
organization of the selected work items to ensure that these departments are cognizant of
all FIN planned maintenance activities.
The inspector attended the FIN and the 6:45 a.m. morning meeting. In addition to the off-
going and on-coming shift managers, individuals at the 6:45 a.m. morning meeting
included: the Unit Director, the operations, maintenance, l&C, and engineering department
managers, and representatives from work planning, chemistry, and HP. Each TR is
discussed then assigned to either the FIN or work planning department. Any TR that
potentially affects equipment operability is identified and an adverse condition report
;
;


  .
                                                                                                    l
.
.
                                                                                                    l
l
                                                    30
.
    generated. The inspector noted that all work on the protected train was assigned to the
30
    work planning department.
generated. The inspector noted that all work on the protected train was assigned to the
    There have been approximately one hundred TRs generated each week during the month of
work planning department.
    January 1997. Of these, the FIN team completed approximately fifty-five percent. A
There have been approximately one hundred TRs generated each week during the month of
    review of the TR backlog, those over one week old, revealed that the number has been
January 1997. Of these, the FIN team completed approximately fifty-five percent. A
    declining. The inspector monitored selected activities and reviewed those work items that
review of the TR backlog, those over one week old, revealed that the number has been
    were performed by the FIN team for the month of January. A review of the work activities
declining. The inspector monitored selected activities and reviewed those work items that
    revealed that work orders had been generated for all safety-related work activities in
were performed by the FIN team for the month of January. A review of the work activities
    accordance with procedure U3 WC 1.1. As a result of the high number of TRs being
revealed that work orders had been generated for all safety-related work activities in
    generated and the minor maintenance work activities performed, the FIN team has been
accordance with procedure U3 WC 1.1. As a result of the high number of TRs being
    unable to work off any corrective maintenance backlog items.
generated and the minor maintenance work activities performed, the FIN team has been
    c.     Conclusions
unable to work off any corrective maintenance backlog items.
    The licensee is implementing the FIN work process in a conservative manner. Any work on
c.
    the protected train equipment is not being assigned to the FIN team. All monitored work
Conclusions
    activities performed by the FIN team was performed in accordance with the unit and
The licensee is implementing the FIN work process in a conservative manner. Any work on
    station procedures. FIN team members appeared to be well qualified. No safety concerns         ,
the protected train equipment is not being assigned to the FIN team. All monitored work
    were identified from the specific activities observed.
activities performed by the FIN team was performed in accordance with the unit and
    U3 M8           Miscellaneous Maintenance issues
station procedures. FIN team members appeared to be well qualified. No safety concerns
    M8.1 Plant Insoection-Tours (62707. 92902)
,
    The inspectors conducted inspection-tours of several areas of the plant during this
were identified from the specific activities observed.
    inspection period, observing work in progress and raising some questions regarding
U3 M8
    completed field installations. As appropriate, discussions were held with workers, field
Miscellaneous Maintenance issues
    supervisors, and support personnel (e.g., health physics technicians). While most field
M8.1 Plant Insoection-Tours (62707. 92902)
    observations and questions were resolved prior to completion of the inspection-tours, the
The inspectors conducted inspection-tours of several areas of the plant during this
    following issues required followup, as documented below:
inspection period, observing work in progress and raising some questions regarding
    *        snubber removal on a residual heat removal (RHS) line in the engineered safety
completed field installations. As appropriate, discussions were held with workers, field
            features building; authorized by plant design change record (PDCR) MP3-90-003.
supervisors, and support personnel (e.g., health physics technicians). While most field
            The inspector reviewed the applicable PDCR and design change notice DM3-P-154-
observations and questions were resolved prior to completion of the inspection-tours, the
            90, verifying proper re-analysis of the RHS piping system and control of the snubber
following issues required followup, as documented below:
            elimination list. Since design criteria discussed in ASME Code Case N-411 were
snubber removal on a residual heat removal (RHS) line in the engineered safety
            used in the pipe stress re-verification, the inspector reviewed the related discussion
*
            of seismic design response spectra, provided on NRC Regulatory Guides 1.60 and
features building; authorized by plant design change record (PDCR) MP3-90-003.
            1.61, in the final safety analysis report (FSAR); and confirmed NRC approval for the
The inspector reviewed the applicable PDCR and design change notice DM3-P-154-
            use of ASME Code Case N-411 at Unit 3.
90, verifying proper re-analysis of the RHS piping system and control of the snubber
    *        white " frothing" of oil observed in the site glass for the speed increaser on the "B"
elimination list. Since design criteria discussed in ASME Code Case N-411 were
            charging (CHS) pump, located in the auxiliary building.
used in the pipe stress re-verification, the inspector reviewed the related discussion
            The inspector discussed this observation with the responsible system engineer, who
of seismic design response spectra, provided on NRC Regulatory Guides 1.60 and
            confirmed that the subject " frothing" was likely due to the turbulence caused by the
1.61, in the final safety analysis report (FSAR); and confirmed NRC approval for the
use of ASME Code Case N-411 at Unit 3.
white " frothing" of oil observed in the site glass for the speed increaser on the "B"
*
charging (CHS) pump, located in the auxiliary building.
The inspector discussed this observation with the responsible system engineer, who
confirmed that the subject " frothing" was likely due to the turbulence caused by the


  .
  .
                                                    31
                                                                                                  ;
            meshing of gears in the CHS pump speed increaser. The inspector reviewed the
            results of the most recent chemical analysis performed on this pump and identified
            no adverse conditions or additional concerns.
                                                                                                  1
    *
            treatment of reactor plant sampling (SSR) tubing runs and flexible hose connections
            inside the containment building as ASME class 2 components, as discussed in the
            Unit 3 FSAR.
.
.
            The inspector reviewed the fabrication installation control drawings for the SSR
.
            piping and common header connections from the containment penetrations to the         i
31
            steam generator blowdown lir.es (i.e, a review of approximately 60 Stone &
meshing of gears in the CHS pump speed increaser. The inspector reviewed the
            Webster Engineering Corporation isometric drawings); and confirmed proper ASME       j
results of the most recent chemical analysis performed on this pump and identified
            Code classification of the subject sample lines.
no adverse conditions or additional concerns.
                                                                                                  1
treatment of reactor plant sampling (SSR) tubing runs and flexible hose connections
    *
*
            an unrestrained trolley assembly, located on a structural beam at the lower elevation j
inside the containment building as ASME class 2 components, as discussed in the
            (-24'6") of the containment building, in proximity to some safety-related trisodium   1
Unit 3 FSAR.
            phosphate baskets.
.
            Inspector followup of the status of this assembly revealed that the trolley had been
The inspector reviewed the fabrication installation control drawings for the SSR
            installed as a temporary component during the first refueling outage in 1987, but
piping and common header connections from the containment penetrations to the
            never removed. The licensee removed the unauthorized trolley and issued an
i
            adverse condition report (ACR) M3-97-0563, documenting the concern that current
steam generator blowdown lir.es (i.e, a review of approximately 60 Stone &
            procedural controls for " incomplete work" were not being followed. Subsequently
Webster Engineering Corporation isometric drawings); and confirmed proper ASME
            (note: after the conclusion of this inspection report period), the licensee issued
j
            another Condition Report (CR) M3-97-0850, documenting inadequate corrective
Code classification of the subject sample lines.
            action implementation relative to a licensee event report, LER 3-96-003, involving
1
            unauthorized temporary I-beams over safety-related equipment.
an unrestrained trolley assembly, located on a structural beam at the lower elevation
            CR M3-97-0850 also documented current licensee findings of heavy, unrestrained
j
            tools and chain falls located in proximity to safety-related equipment. Based upon
*
            the discovery of the unrestrained trolley assembly, as well as the more recent
(-24'6") of the containment building, in proximity to some safety-related trisodium
            licensee-identified issues of CR M3-97-0850, the inspector determined that
1
            additional licensee management attention to such " seismic II/l" concerns would be
phosphate baskets.
            prudent. The Significant items List (SIL) enclosed with the NRC Restart Assessment
Inspector followup of the status of this assembly revealed that the trolley had been
            Plan for Millstone Unit 3 documents an item for " Resident Emphasis: Seismic II/l".
installed as a temporary component during the first refueling outage in 1987, but
            This issue, with emphasis upon the new problems documented above, will be
never removed. The licensee removed the unauthorized trolley and issued an
            tracked as an inspector followup item (IFl 423/97-01-07) to evaluate both the
adverse condition report (ACR) M3-97-0563, documenting the concern that current
            timeliness and adequacy of further corrective measures in this area.
procedural controls for " incomplete work" were not being followed. Subsequently
    Overall, the plant inspection-tours revealed improvements in Unit 3 areas of housekeeping,
(note: after the conclusion of this inspection report period), the licensee issued
    material conditions, and work controls. With the exception of the problem with
another Condition Report (CR) M3-97-0850, documenting inadequate corrective
    unrestrained equipment, noted as an IFl above, the licensee provided adequate response to
action implementation relative to a licensee event report, LER 3-96-003, involving
    the inspector questions and field observations and demonstrated continued progress in the
unauthorized temporary I-beams over safety-related equipment.
    physical enhancements to the plant field conditions.
CR M3-97-0850 also documented current licensee findings of heavy, unrestrained
tools and chain falls located in proximity to safety-related equipment. Based upon
the discovery of the unrestrained trolley assembly, as well as the more recent
licensee-identified issues of CR M3-97-0850, the inspector determined that
additional licensee management attention to such " seismic II/l" concerns would be
prudent. The Significant items List (SIL) enclosed with the NRC Restart Assessment
Plan for Millstone Unit 3 documents an item for " Resident Emphasis: Seismic II/l".
This issue, with emphasis upon the new problems documented above, will be
tracked as an inspector followup item (IFl 423/97-01-07) to evaluate both the
timeliness and adequacy of further corrective measures in this area.
Overall, the plant inspection-tours revealed improvements in Unit 3 areas of housekeeping,
material conditions, and work controls. With the exception of the problem with
unrestrained equipment, noted as an IFl above, the licensee provided adequate response to
the inspector questions and field observations and demonstrated continued progress in the
physical enhancements to the plant field conditions.


-
-
.
.
                                                                                                '
'
                                                32
32
                                                                                                l
U3.lli Enaineerina
                                        U3.lli Enaineerina                                     l
U3 E8
  U3 E8         Miscellaneous Engineering issues
Miscellaneous Engineering issues
  E8.1   IOnen) Unresolved item 50-423/96-01-08: Slave Relav/Overlan Test Deficiencies
E8.1
  a.     Inspection Scope (92903)
IOnen) Unresolved item 50-423/96-01-08: Slave Relav/Overlan Test Deficiencies
  In 1993 the licensee identified slave relay and other testing deficiencies. As a result of
a.
  those findings, the unit director established an overlap testing task force to review the
Inspection Scope (92903)
  adequacy of overlap testing for the reactor trip and engineered safeguard systems circuitry.
In 1993 the licensee identified slave relay and other testing deficiencies. As a result of
  These reviews were completed in 1993 and the licensee later credited these reviews with
those findings, the unit director established an overlap testing task force to review the
  accomplishing the reviews requested in NRC Generic Letter 96-01, " Testing Of Safety-
adequacy of overlap testing for the reactor trip and engineered safeguard systems circuitry.
  Related Logic Circuits."
These reviews were completed in 1993 and the licensee later credited these reviews with
                                                                                                l
accomplishing the reviews requested in NRC Generic Letter 96-01, " Testing Of Safety-
  in 1996, the licensee performed a review of safety and non-safety related functions,' as '
Related Logic Circuits."
  described in the Final Safety Analysis Report (FSAR) and/or the Safety Evaluation Report
l
  (SER) to determine if the functions were properly tested. The scope of that review
in 1996, the licensee performed a review of safety and non-safety related functions,' as '
  included systems that were considered to be accident mitigating or risk significant as     '
described in the Final Safety Analysis Report (FSAR) and/or the Safety Evaluation Report
  defined in the Maintenance Rule (10 CFR 50.65).
(SER) to determine if the functions were properly tested. The scope of that review
  The inspector reviewed selected test procedures, elementary electrical and logic drawings,
included systems that were considered to be accident mitigating or risk significant as
  Open item Reports (OIRs), ACRs and other documents associated with the testing review
'
  efforts to assess the effectiveness of the reviews.
defined in the Maintenance Rule (10 CFR 50.65).
  b.     Observations and Findinas
The inspector reviewed selected test procedures, elementary electrical and logic drawings,
  The licensee task force reviews performed in 1993 identified procedural deficiencies,
Open item Reports (OIRs), ACRs and other documents associated with the testing review
  circuitry which required design changes, incorrect drawings and FSAR errors. Three LERs
efforts to assess the effectiveness of the reviews.
  were issued as a result of technical specification violations that occurred due to testing
b.
  deficiencies (LERs 3-93-005,-010,-017). In each case the affected circuit performed
Observations and Findinas
  satisfactorily when tested. The followup reviews of the FSAR and SER performed in 1996
The licensee task force reviews performed in 1993 identified procedural deficiencies,
  identified a number of questions regarding testing adequacy and the licensee was
circuitry which required design changes, incorrect drawings and FSAR errors. Three LERs
  continuing to disposition the associated OIRs. The OIRs that had been dispositioned to
were issued as a result of technical specification violations that occurred due to testing
  date had not identified logic testing deficiencies of the types discussed in GL 96-01.
deficiencies (LERs 3-93-005,-010,-017). In each case the affected circuit performed
  The inspector performed an independent review of testing that was performed on reactor
satisfactorily when tested. The followup reviews of the FSAR and SER performed in 1996
  protection and engineered safety features logic circuits to assess the adequacy of the test
identified a number of questions regarding testing adequacy and the licensee was
  procedures. These reviews included the steam generator low level reactor trip and
continuing to disposition the associated OIRs. The OIRs that had been dispositioned to
  emergency feedwater pump start testing and portions of the emergency diesel generator
date had not identified logic testing deficiencies of the types discussed in GL 96-01.
  start, load shed and load sequencing testing. The inspector also reviewed several OIRs to
The inspector performed an independent review of testing that was performed on reactor
  assess the significance of the issues and the adequacy of the licensee resolutions.
protection and engineered safety features logic circuits to assess the adequacy of the test
  The inspector's review of the steam generator low level channel testing included the
procedures. These reviews included the steam generator low level reactor trip and
  following procedures:
emergency feedwater pump start testing and portions of the emergency diesel generator
    *      SP 3444A01 (Rev. 04) - Steam Generator Water Level Channel Calibration
start, load shed and load sequencing testing. The inspector also reviewed several OIRs to
    *       SP 3443A21 (Rev.10) - Protection Set Cabinet i Operational Test
assess the significance of the issues and the adequacy of the licensee resolutions.
The inspector's review of the steam generator low level channel testing included the
following procedures:
SP 3444A01 (Rev. 04) - Steam Generator Water Level Channel Calibration
*
SP 3443A21 (Rev.10) - Protection Set Cabinet i Operational Test
*


      _ _ . _ _ . _ _ _ _ _ _ . _ _ _ _ . _ _ . _ . _ _ _ _                                                         . . _ _ . . _ _ _ . . .
_ _ . _ _ . _ _ _ _ _ _ . _ _ _ _ . _ _ . _ . _ _ _ _
                                                                                                                                                I
. . _ _ .
                                                                                                                                                i
. _ _ _ . . .
i
e
e
;.
;.
;
;
4
4
.                                                                                 33
l
I   '                  *              SP 3446B11_(Rev. 09) - Train A Solid State Protection System Operational Test
33
;                     ~ The review included testing of the circuitry from the steam generator level transmitters to
.
i                       the output devices, the reactor trip breakers and the auxiliary feedwater pump controls.
I
                        The test procedures were thorough and no problems were identified, in addition to the
SP 3446B11_(Rev. 09) - Train A Solid State Protection System Operational Test
:                        testing of the automatic reactor trip, the inspector also reviewed the testing of the manual
*
'
;
~ The review included testing of the circuitry from the steam generator level transmitters to
i
the output devices, the reactor trip breakers and the auxiliary feedwater pump controls.
The test procedures were thorough and no problems were identified, in addition to the
testing of the automatic reactor trip, the inspector also reviewed the testing of the manual
:
i
reactor trip push buttons that is performed in'accordance with test SP 3446F331, "SSPS
}
Refueling Tests". The inspector found_that the manual push buttons were properly tested
_
and ensured they would each independently open the reactor trip breakers on either the
: shunt trip or undervoltage trip mechanism.
The inspector also reviewed test procedures and selected drawings associated.with the
*
i
emergency diesel generator starting, load shedding and load sequencing functions. The -
j
following procedures were included in this review:
*
- SP 3646.A.1 (Rev.12) - Emergency. Diesel Generator A Operability Test- -
')
)'
;
SP 3646A.5. (Rev. 05) - Offsite Power Transfer Operability Test
-*
i
i
                        reactor trip push buttons that is performed in'accordance with test SP 3446F331, "SSPS
SP 3646A.8 (Rev.14).- Slave Relay Testing' Train A
}                        Refueling Tests". The inspector found_that the manual push buttons were properly tested
j
_                        and ensured they would each independently open the reactor trip breakers on either the
                        : shunt trip or undervoltage trip mechanism.
*
*
                        The inspector also reviewed test procedures and selected drawings associated.with the
[
i                        emergency diesel generator starting, load shedding and load sequencing functions. The -
SP 3646A.12 (Rev. 07) - Emergency Diesel Generator A Lockout Test -
j                        following procedures were included in this review:
*
)'                      *            - SP 3646.A.1 (Rev.12) - Emergency. Diesel Generator A Operability Test- -                              ')
-
;                      -*             SP 3646A.5. (Rev. 05) - Offsite Power Transfer Operability Test
SP 3646A.15 (Rev.11) - Train A Loss of Power Test
i                        *            SP 3646A.8 (Rev.14).- Slave Relay Testing' Train A                                                     j
I
[  '
                          *            SP 3646A.12 (Rev. 07) - Emergency Diesel Generator A Lockout Test -                          -
                                                                                                                                                l
1
1
'
*
~
~
                          *            SP 3646A.15 (Rev.11) - Train A Loss of Power Test                                                     I
SP 3646A'.17 (Rev. 09)- Train A ESF With LOP Test
                          *             SP 3646A'.17 (Rev. 09)- Train A ESF With LOP Test
*
* .
SP 3646A.19 (Rev. 03) - SIS Transfer of DG From Test to Standby
*
*-
SP 3646A.21 (Rev. 05) - DG Auto Start on ESF Signal
j
*
*
SP 3448E51 (Rev. 01) - Diesel Sequencer Train' A Actuation Timer Test
j
SP 31447MA (Rev. 01)- MP3 Bus 34C Loss of Power Channel Calibration
'
*
Although this review did not include 100% of the circuitry, the inspector identified the
d
following testing issues:
During the loss of power testing, the EDG receives a start signal from relay 27Y2 in
*
the bus undervoltage logic circuit. A set of contacts from a different relay in the
]
undervoltage logic feeds a loss of power signal to the emergency generator loading
.
sequencer (EGLS) resulting in an additional EDG start signal. The existing test
]
procedures were not adequate to properly verify the operation of the parallel
;
signals.
,
The bus undervoltage relays provide trip signals to the emergency bus tie breaker
j
*
and the feeder breaker from the reserve station' service transformer (RSST). The tie
<
breaker trip circuit contains _three parallel trip circuits and the testing does not verify
j
each path. The RSST breaker trip was not included in any of the surveillance test
j
procedures.
1
1
The EDG starting control has two circuits that are designed such that a start signal
*
*
*.
to either circuit will result in the opening of both air start solenoid valves even if one
                          *-            SP 3646A.19 (Rev. 03) - SIS Transfer of DG From Test to Standby
or more circuit component failures may have occurred. The current testing'does not
                          *            SP 3646A.21 (Rev. 05) - DG Auto Start on ESF Signal                                                    j
independently test the redundancy designed into the circuits.
                          *            SP 3448E51 (Rev. 01) - Diesel Sequencer Train' A Actuation Timer Test                                  j
J
                          *            SP 31447MA (Rev. 01)- MP3 Bus 34C Loss of Power Channel Calibration                                    '
                          Although this review did not include 100% of the circuitry, the inspector identified the                            d
                          following testing issues:
                          *              During the loss of power testing, the EDG receives a start signal from relay 27Y2 in                  l
                                        the bus undervoltage logic circuit. A set of contacts from a different relay in the
                                                                                                                                                ]
                                        undervoltage logic feeds a loss of power signal to the emergency generator loading                    .
                                        sequencer (EGLS) resulting in an additional EDG start signal. The existing test                      ]
                                        procedures were not adequate to properly verify the operation of the parallel                        ;
                                        signals.
                                        ,
                          *              The bus undervoltage relays provide trip signals to the emergency bus tie breaker                    j
                                        and the feeder breaker from the reserve station' service transformer (RSST). The tie                  <
                                        breaker trip circuit contains _three parallel trip circuits and the testing does not verify            j
                                        each path. The RSST breaker trip was not included in any of the surveillance test                      j
                                        procedures.                                                                                          1
                                                                                                                                              1
                          *              The EDG starting control has two circuits that are designed such that a start signal
                                        to either circuit will result in the opening of both air start solenoid valves even if one
                                        or more circuit component failures may have occurred. The current testing'does not
                                        independently test the redundancy designed into the circuits.
                                                                                                                                              J


                . - _ _ _ . _ . . _ _ . . .                             _             . - _ . _ _,         _ . _ . _ . _ . _ - . _   _ _ _ - . . _ _ _ . . _.
. - _ _ _ . _ . . _ _ . . .
                                                                                                                                                                    :
_
                                                                                                                                                                    .
. -
        . .
_ . _ _,
                                                                                                      34
_ . _ . _ . _ . _ - . _
_ _ _ - . . _ _ _ . . _.
:
. .
.
34
;
;
j                                       *            Procedure SP 3646A17 contains notes that state:
j
                                                      "If possible, the SW pump not tested in lead during SP 3646A.15 should be lead."
Procedure SP 3646A17 contains notes that state:
                            '
*
      -
-
                                                                                                                                                                    t
'
!                                                     "The CCP pump not tested in SP 3646A.15 should be tested here: the other must.                               4
"If possible, the SW pump not tested in lead during SP 3646A.15 should be lead."
!                                                     be in " PULL-TO-LOCK.""
t
                                                                                                                                                                    '
!
:                                                    - "The CHS pump not tested in SP 3646A.15 should be tested here; the other pump
"The CCP pump not tested in SP 3646A.15 should be tested here: the other must.
                                                      must be in " PULL-TO-LOCK.""
4
                                                                                                                                                                    ,
!
                                                      These notes are intended to ensure that all of the equipment is tested either in SP                           :
be in " PULL-TO-LOCK.""
                                                      3646A15 or SP 3646A17.' These notes are worded as to provide
:
                                                      recommendations, rather than requirements, and as such may not ensure that the                                 1
- "The CHS pump not tested in SP 3646A.15 should be tested here; the other pump
                                                      standby and swing pumps get tested as required by technical specifications.
'
  ' ' "
must be in " PULL-TO-LOCK.""
                                      ~ Based on these findings th'e' inspector questioned the adequacy of the previous overlap ' -
,
          +                           -testing. reviews that were credited with ensuring that test procedures are adequate to
These notes are intended to ensure that all of the equipment is tested either in SP
                                                                                                                                                                    *
:
                                        ensure the technical specification test requirements are met. As a result, the licensee
3646A15 or SP 3646A17.' These notes are worded as to provide
              A:                       developed an action plan to address this concern. . The' planned actions included: . _ ..e
recommendations, rather than requirements, and as such may not ensure that the
                                      -*            A review for overlap test issues of several circuits by comparing electrical
1
                            '
standby and swing pumps get tested as required by technical specifications.
                                                      schematic drawings and logic drawings against plant surveillance test pro:edures to
' ' "
                                                      ensure that all portions of the logic circuitry, including the parallel logic, interlocks,
~ Based on these findings th'e' inspector questioned the adequacy of the previous overlap ' -
                                                      bypasses and inhibit circuits, are adequately covered in the surveillance procedures                         "
+
                                                      to fulfill the TS requirements. These reviews were to include the loss of power
-testing. reviews that were credited with ensuring that test procedures are adequate to
                                                      schemes (undervoltage and degraded voltage), one ESF actuation system, and one                                 4
*
                                                      reactor trip instrumentation functional unit.
ensure the technical specification test requirements are met. As a result, the licensee
                                        *            The revision of the surveillance testing for the loss of power initiation logic to                             '
A:
                                                      adequately verify parallel logic.
developed an action plan to address this concern. . The' planned actions included: . _ ..e
                                        *            The performance of a root cause analysis to determine the cause of missed contacts
A review for overlap test issues of several circuits by comparing electrical
                                                      to determine if the failure was a generic issue that applied to the overall effort of
- *
                                                    - the overlap task force. Based on the findings of the root cause analysis any
schematic drawings and logic drawings against plant surveillance test pro:edures to
                                                      additional corrective actions would be determined.
'
                                      - Subsequent licensee reviews identified additional testing deficiencies. The licensee
ensure that all portions of the logic circuitry, including the parallel logic, interlocks,
                                        performed a self-assessment of the Unit 3 response to Generic Letter 96-01 and concluded
bypasses and inhibit circuits, are adequately covered in the surveillance procedures
                                        that the response did not meet the requirements of the letter. This was based on the
"
                                        above specific findings where actuation' contacts were not tested, a lack of auditable
to fulfill the TS requirements. These reviews were to include the loss of power
                                        documentation and a difference in philosophy between the 1993 overlap task force and the
schemes (undervoltage and degraded voltage), one ESF actuation system, and one
                                        requirements of the Generic Letter. This issue was documented in ACR M3-97-0529 and
4
                                        additional corrective actions were being developed by the licensee at the end of this
reactor trip instrumentation functional unit.
                                        inspection period.
The revision of the surveillance testing for the loss of power initiation logic to
                                                                                            ,
'
  k-,-     - - + ,               c-           ,s.w-           -             ,-,e - .- ,                 , - ~                 -       y- c
*
                                                                                                                                                                y
adequately verify parallel logic.
The performance of a root cause analysis to determine the cause of missed contacts
*
to determine if the failure was a generic issue that applied to the overall effort of
- the overlap task force. Based on the findings of the root cause analysis any
additional corrective actions would be determined.
- Subsequent licensee reviews identified additional testing deficiencies. The licensee
performed a self-assessment of the Unit 3 response to Generic Letter 96-01 and concluded
that the response did not meet the requirements of the letter. This was based on the
above specific findings where actuation' contacts were not tested, a lack of auditable
documentation and a difference in philosophy between the 1993 overlap task force and the
requirements of the Generic Letter. This issue was documented in ACR M3-97-0529 and
additional corrective actions were being developed by the licensee at the end of this
inspection period.
,
k-,-
- - + ,
c-
,s.w-
-
,-,e
- .- ,
, - ~
-
y-
c
y


                                                  - . _ . . . _ _ . - _       _ _ _ . _ _
- . _ . . . _ _ . - _
    ,
_ _ _ . _ _
                                                                                                                  !
,
  ..                                                                                                             !
!
                                                                        35                                       ;
..
              c.     Conclusion                                                                                 ,
35
                                                                                                                  I
c.
  ": - ' ~ The inspector found that the licensee had expended significant resources in the past to~             i
Conclusion
              review the logic testing and had identified and corrected numerous deficiencies. The test'         l
,
              procedures reviewed were generally thorough. However, as discussed above, some test               -
":
              deficiencies continued to exist. The failure to ensure all contacts are operable could result      ,
- ' ~ The inspector found that the licensee had expended significant resources in the past to~
              in significant undetected problems. For example, if the emergency bus tie and feeder              1
i
              breakers failed to trip on an undervoltage signal, the EDG output circuit breaker would be
review the logic testing and had identified and corrected numerous deficiencies. The test'
              prevented from closing to' energize the bus to power necessary safety equipment. The
procedures reviewed were generally thorough. However, as discussed above, some test
              inspector also noted that a more thorough self-assessment would have been appropriate            ,
              prior to the licensee submission of a response to GL 96-01.
                                                                                                                ]
                                                                        . .                                      !
              This item remains open pending NRC review of additional licensee corrective actions, and          )
              the assessment'of the significance of any additional findings and the results of additional        l
              tes:ing that is performed.                                                                        i
                                                                                                                  .
              E8.2 (Closed - Part of SIL ltem 67) ACR M3-96-0621: Potential For Overloadina Station
                      Blackout (SBO) Diesel
                                                                                                                  l
              a.      Insoection Scope (92903)
              This ACR identified a concern that the station blackout (SBO) diesel generator could be
              overloaded if a safety injection or containment depressurization signal occurred while the
        -
              SBO diesel was supplying power to an emergency bus.                                      -    ~
              b.      Observations and Findinas
-
-
          . In the event of a loss of all ac power,-the SBO dieselis manually started in accordance .a       Y
deficiencies continued to exist. The failure to ensure all contacts are operable could result
              with procedure ECA O.0, " Loss of All'AC Power." Prior to energizing the bus from the
,
              SBO diesel, the procedure directs the operators to place the control switches for large           )
in significant undetected problems. For example, if the emergency bus tie and feeder
              loads in the pull-to-lock position. This action blocks the automatic start of the loads.           !
1
              Following the energization of the bus, the operator then manually starts loads needed to '-       !
breakers failed to trip on an undervoltage signal, the EDG output circuit breaker would be
              cope with the station blackout condition,                                                         i
prevented from closing to' energize the bus to power necessary safety equipment. The
              c.     Conclusions
inspector also noted that a more thorough self-assessment would have been appropriate
              - The inspector reviewed the associated ACR, procedure and elementary electrical drawings           )
,
                and concluded that the licensee had appropriately reviewed and dispositioned this ACR.           l
prior to the licensee submission of a response to GL 96-01.
              This item is closed, (representing partial closure of SIL ltem 67).
]
                                                                                                            _
.
.
This item remains open pending NRC review of additional licensee corrective actions, and
)
the assessment'of the significance of any additional findings and the results of additional
tes:ing that is performed.
i
.
E8.2 (Closed - Part of SIL ltem 67) ACR M3-96-0621: Potential For Overloadina Station
Blackout (SBO) Diesel
a.
Insoection Scope (92903)
This ACR identified a concern that the station blackout (SBO) diesel generator could be
overloaded if a safety injection or containment depressurization signal occurred while the
-
SBO diesel was supplying power to an emergency bus.
-
~
b.
Observations and Findinas
-
. In the event of a loss of all ac power,-the SBO dieselis manually started in accordance .a
Y
with procedure ECA O.0, " Loss of All'AC Power." Prior to energizing the bus from the
SBO diesel, the procedure directs the operators to place the control switches for large
)
loads in the pull-to-lock position. This action blocks the automatic start of the loads.
Following the energization of the bus, the operator then manually starts loads needed to '-
cope with the station blackout condition,
i
c.
Conclusions
- The inspector reviewed the associated ACR, procedure and elementary electrical drawings
)
and concluded that the licensee had appropriately reviewed and dispositioned this ACR.
This item is closed, (representing partial closure of SIL ltem 67).


o
o
.
.
                                                                                                    l
l
                                                                                                    '
'
                                                36
36
                                          IV Plant Support                                         :
IV Plant Support
                                    Millstone Units 1,2, and 3
Millstone Units 1,2, and 3
  R1             Radiological Protection and Chemistry Controls
R1
  a.     Inspection Scope (83750)                                                                 l
Radiological Protection and Chemistry Controls
                                                                                                    l
a.
                                                                                                    i
Inspection Scope (83750)
  The inspector reviewed the licensee's radiation protection programs established at each           l
i
  unit and for the site. A review of specific work performed, the programs for maintaining
The inspector reviewed the licensee's radiation protection programs established at each
  occupational radiation exposures as low as is reasonably achievable, and tours of the
unit and for the site. A review of specific work performed, the programs for maintaining
  various radiologically controlled areas (RCAs) were conducted by the inspector.
occupational radiation exposures as low as is reasonably achievable, and tours of the
  b.     Observations and Findinas                                                                 l
various radiologically controlled areas (RCAs) were conducted by the inspector.
  Unit 1                                                                                           i
b.
                                                                                                    i
Observations and Findinas
  The inspector toured portions of the reactor and liquid radwaste buildings as part of the         j
Unit 1
  inspection at Unit 1. The inspector noted a significant decrease in the number and size of       I
i
  posted contaminated areas in the unit, which was described to the inspector as part of.the
i
  unit's clean-up policy. The inspector noted that while some work was being performed in
The inspector toured portions of the reactor and liquid radwaste buildings as part of the
  the reactor building at the time of this inspection, significant radiological work, especially in
j
  the drywell and on the refueling floor had yet to commence. The inspector also toured the
inspection at Unit 1. The inspector noted a significant decrease in the number and size of
  Xenon / krypton building, which houses some of the off-gas treatment systems and delay
posted contaminated areas in the unit, which was described to the inspector as part of.the
  tanks. This structure and its component systems had undergone a significant
unit's clean-up policy. The inspector noted that while some work was being performed in
  refurbishment during 1996. Two areas within the structure were appropriately posted and
the reactor building at the time of this inspection, significant radiological work, especially in
  controlled as high radiation areas. The upper level of the structure housed two glycol
the drywell and on the refueling floor had yet to commence. The inspector also toured the
  chiller systems, one of which was still under refurbishment.
Xenon / krypton building, which houses some of the off-gas treatment systems and delay
                                                                                                    1
tanks. This structure and its component systems had undergone a significant
  For 1997, the licensee had established a goal of not more than 399 person-rem. This goal         '
refurbishment during 1996. Two areas within the structure were appropriately posted and
  is based on completing significant work and having the unit ready for restart of operations
controlled as high radiation areas. The upper level of the structure housed two glycol
  during 1997. As described in a previous NRC Inspection Report (50-245/96-09), the unit
chiller systems, one of which was still under refurbishment.
  has significantly increased the number of personnel assigned to perform work planning and
For 1997, the licensee had established a goal of not more than 399 person-rem. This goal
  ALARA functions. Seven persons within the Radiation Protection Department are now
'
  assigned to ALARA, and two technicians are on loan as work week managers. Each of the
is based on completing significant work and having the unit ready for restart of operations
  ALARA personnel have been assigned specific work packages and/or work areas for
during 1997. As described in a previous NRC Inspection Report (50-245/96-09), the unit
  planning purposes, and are responsibla for coordination with engineering and the work
has significantly increased the number of personnel assigned to perform work planning and
  groups to ensure proper ALARA controls are incorporated into the work packages.
ALARA functions. Seven persons within the Radiation Protection Department are now
  Additionally, an ALARA Committee has been established, which includes all department
assigned to ALARA, and two technicians are on loan as work week managers. Each of the
  managers.
ALARA personnel have been assigned specific work packages and/or work areas for
  On January 15,1997, the licensec identified, through its Adverse Condition Reporting
planning purposes, and are responsibla for coordination with engineering and the work
  (ACR) process (ACR # M1-97-0094) that fan HVE-14, which exhausts portions of the
groups to ensure proper ALARA controls are incorporated into the work packages.
  Radwaste Storage Building, was potentially an unmonitored release pathway, as the fan
Additionally, an ALARA Committee has been established, which includes all department
  was not connected to the main plant stack, and no radiological effluent monitoring
managers.
  equipment was located with this fan. The inspector discussed this ACR with a licensee
On January 15,1997, the licensec identified, through its Adverse Condition Reporting
  representative during this inspection, and reviewed a reportability evaluation performed bt
(ACR) process (ACR # M1-97-0094) that fan HVE-14, which exhausts portions of the
  the site Engineering Department which analyzed the significance of this ACR. The
Radwaste Storage Building, was potentially an unmonitored release pathway, as the fan
  inspector determined that the reportability determination was invalid in that the evaluation
was not connected to the main plant stack, and no radiological effluent monitoring
equipment was located with this fan. The inspector discussed this ACR with a licensee
representative during this inspection, and reviewed a reportability evaluation performed bt
the site Engineering Department which analyzed the significance of this ACR. The
inspector determined that the reportability determination was invalid in that the evaluation


~
~
                                                                                                    1
1
                                                                                                    1
4
4
                                                    37
37
  erroneously addressed a building that was different from the Radwaste Storage Building.
erroneously addressed a building that was different from the Radwaste Storage Building.
  Subsequent to this finding, the licensee wrote another ACR (ACR # M1-97-0282) to
Subsequent to this finding, the licensee wrote another ACR (ACR # M1-97-0282) to
  document this error, and subsequently determined that a notification to the NRC was
document this error, and subsequently determined that a notification to the NRC was
  required, which was made on February 6,1997. Failure to monitor effluents released to
required, which was made on February 6,1997. Failure to monitor effluents released to
  the environment from the Radwaste Storage Building to demonstrate compliance with
the environment from the Radwaste Storage Building to demonstrate compliance with
  applicable regulatory limits, including 10 CFR 20.1301, is a violation of 10 CFR 20.1302.
applicable regulatory limits, including 10 CFR 20.1301, is a violation of 10 CFR 20.1302.
  (VIO 245/97-01-08)
(VIO 245/97-01-08)
  Unit 2
Unit 2
  The inspector toured various portions of the Unit 2 RCA, including the Auxiliary and
The inspector toured various portions of the Unit 2 RCA, including the Auxiliary and
                                                                                                    I
Containment Buildings, as part of this inspection. In general, all areas were determined to
  Containment Buildings, as part of this inspection. In general, all areas were determined to
be in compliance with NRC requirements for radiological postings and control of radioactive
  be in compliance with NRC requirements for radiological postings and control of radioactive
material. On February 5,1997, the inspector observed the removal and subsequent
  material. On February 5,1997, the inspector observed the removal and subsequent
transfer of two highly radioactive pieces of debris previously found in the reactor vessel. A
  transfer of two highly radioactive pieces of debris previously found in the reactor vessel. A
metal nut and a tie wrap, each reading in excess of 10 Roentgens per hour on contact,
  metal nut and a tie wrap, each reading in excess of 10 Roentgens per hour on contact,
were removed from a storage bucket that was being kept in the refueling cavity,
  were removed from a storage bucket that was being kept in the refueling cavity,
transferred to a lead pig, and moved from the Containment Building, through the Auxiliary
  transferred to a lead pig, and moved from the Containment Building, through the Auxiliary
Building and outside the unit to a designated storage area. The inspector observed the pre-
    Building and outside the unit to a designated storage area. The inspector observed the pre-
job briefing, which included a discussion of engineering controls for the minimization of
  job briefing, which included a discussion of engineering controls for the minimization of
personnel exposure, and the conduct of all work until the shield pig with the objects was
    personnel exposure, and the conduct of all work until the shield pig with the objects was
removed from the unit. This activity also involved significant coordination between the
    removed from the unit. This activity also involved significant coordination between the
unit operations department, the health physics department, the site security organization
    unit operations department, the health physics department, the site security organization
"
                                                                                                  "
and the self-directed work group. Due to the careful planning process used, total exposure
    and the self-directed work group. Due to the careful planning process used, total exposure
for this work was less than 25 millirem.
    for this work was less than 25 millirem.
For 1997, the unit established a goal of not more than 182 person-rem. Since the last
    For 1997, the unit established a goal of not more than 182 person-rem. Since the last
specialist inspection (50-336/96-09), the unit had flooded up the refueling cavity and
    specialist inspection (50-336/96-09), the unit had flooded up the refueling cavity and
successfully off-loaded the reactor fuel to the spent fuel pool. Significant strides in
    successfully off-loaded the reactor fuel to the spent fuel pool. Significant strides in
improving the unit ALARA program have also been made. ALARA coordinators have been
    improving the unit ALARA program have also been made. ALARA coordinators have been
identified in each of the major work departments within the unit, and the Unit ALARA
    identified in each of the major work departments within the unit, and the Unit ALARA
coordinator was in the process of developing a training program for them. A unit ALARA
    coordinator was in the process of developing a training program for them. A unit ALARA
program procedure was also drafted, however, it was not issued at the time of this
    program procedure was also drafted, however, it was not issued at the time of this
inspection. Discussions with the ALARA coordinator, Health Physics Manager and Unit
    inspection. Discussions with the ALARA coordinator, Health Physics Manager and Unit
Directr,r indicated the intent to establish an ALARA Committee, to include the major
    Directr,r indicated the intent to establish an ALARA Committee, to include the major
depa:tment heads and their ALARA coordinators.
    depa:tment heads and their ALARA coordinators.
The inspector interviewed the health physics manager, and reviewed the documentation
    The inspector interviewed the health physics manager, and reviewed the documentation
associated with three ACRs (M2-97-0086, M2-97-0091 and M2-97-0142) written to
    associated with three ACRs (M2-97-0086, M2-97-0091 and M2-97-0142) written to                   ;
identify improper entries to the RCA which occurred during a ten day period in January
    identify improper entries to the RCA which occurred during a ten day period in January
1997. In two of the instances, workers entered the RCA without having signed in on a
    1997. In two of the instances, workers entered the RCA without having signed in on a
RWP, and without having on an electronic docimeter, as directed by the unit radiation
    RWP, and without having on an electronic docimeter, as directed by the unit radiation
protection staff. In the third instance, a fire watch entered the unit with an electronic
    protection staff. In the third instance, a fire watch entered the unit with an electronic
dosimeter that had not been properly turned on. When discovered through self-checking,
    dosimeter that had not been properly turned on. When discovered through self-checking,
the fire watch remained in the RCA with the non-functioning electronic dosimeter unti!
    the fire watch remained in the RCA with the non-functioning electronic dosimeter unti!         l
completion of the fire watch round. Procedure RPM 5.22 requires radiation workers to
    completion of the fire watch round. Procedure RPM 5.22 requires radiation workers to           l
comply with written instructions, including RWPs, from the radiation protection staff.
    comply with written instructions, including RWPs, from the radiation protection staff.         I
Although the safety significance of each of these events is individ ally low, as each worker
                                                                                                    '
'
    Although the safety significance of each of these events is individ ally low, as each worker
.


                                                                                                    l
1
                                                                                                    1
i
                                                                                                    i
e
e                                                                                                   i
i
                                                38
38
  was wearing a thermoluminescent dosimeter (TLD) which is utilized to determine dose of
was wearing a thermoluminescent dosimeter (TLD) which is utilized to determine dose of
  record, the number of events in such a short duration are of concern. Additionally, the fire
record, the number of events in such a short duration are of concern. Additionally, the fire
  watch event may highlight a problem with the training given and the perception of the             ;
watch event may highlight a problem with the training given and the perception of the
  workers performing this task relative to other plant requirements, such as radiological           j
workers performing this task relative to other plant requirements, such as radiological
  safety. Both of these issues were discussed by the inspector with the unit Health Physics
j
  Manager and Unit Director, and with the station Vice President - Work Services. Short-             )
safety. Both of these issues were discussed by the inspector with the unit Health Physics
  term corrective actions taken by the licensee included posting a health physics technician       !
Manager and Unit Director, and with the station Vice President - Work Services. Short-
  at the main RCA entrance to ensure that personnel entering the RCA were wearing a
)
  functional electronic dosimeter. Long-term corrective actions were not identified, however,
term corrective actions taken by the licensee included posting a health physics technician
  at the time of this inspection. Failure to adhere to the licensee's radiation protection
at the main RCA entrance to ensure that personnel entering the RCA were wearing a
  program, specifically procedure RPM 5.22,is a violation of 10 CFR 20.1101. (VIO                   !
functional electronic dosimeter. Long-term corrective actions were not identified, however,
  336/97-01-09)
at the time of this inspection. Failure to adhere to the licensee's radiation protection
  Unit 3
program, specifically procedure RPM 5.22,is a violation of 10 CFR 20.1101. (VIO
                                                                                                    l
336/97-01-09)
  The inspector toured various portions of the Unit 3 RCA, including the containment and
Unit 3
  auxiliary buildings. Since the last specialist inspection (50-423/96-07) a significant             !
The inspector toured various portions of the Unit 3 RCA, including the containment and
  reduction in the number of leaking valves was observed, based on the reduced number of
auxiliary buildings. Since the last specialist inspection (50-423/96-07) a significant
  catch containments observed. The unit continues te have very low dose rates in most         ,,
reduction in the number of leaking valves was observed, based on the reduced number of
                                                                                                    i
catch containments observed. The unit continues te have very low dose rates in most
  areas, and significant portions of the Containment rematri accessible as clean areas.             I
i
  The inspector reviewed the licensee's ALARA program, including the 1997 ALARA goal of
,,
  not more than 170 person-rem. The unit focus in ALARA has been to improve the work             -
areas, and significant portions of the Containment rematri accessible as clean areas.
  order process, to include having RWP and ALARA control information included in the work
The inspector reviewed the licensee's ALARA program, including the 1997 ALARA goal of
  orders, in addition, the licensee has begun to include detailed maps and pictures of areas
not more than 170 person-rem. The unit focus in ALARA has been to improve the work
  and systems to be worked in the work order package. This is the result of a significant
order process, to include having RWP and ALARA control information included in the work
  campaign completed in 1996 by the unit radiation protection staff to photograph over
-
  30,000 components in the RCA.
orders, in addition, the licensee has begun to include detailed maps and pictures of areas
  Site Health Physics
and systems to be worked in the work order package. This is the result of a significant
  The site health physics group is responsible for providing calibration and dosimetry
campaign completed in 1996 by the unit radiation protection staff to photograph over
  services, health physics engineering and health physics support to the units and to other
30,000 components in the RCA.
  site-wide organizations. As part of this inspection, a review of certain activities was           i
Site Health Physics
  coni:cted by the inspector.                                                                       l
The site health physics group is responsible for providing calibration and dosimetry
  The self-directed work group includes six health physics technicians whose primary focus
services, health physics engineering and health physics support to the units and to other
  is to support the activities of the Waste Services Department. As previously noted in the
site-wide organizations. As part of this inspection, a review of certain activities was
  discussion on Unit 2, above, this group was involved in the transfer of two highly activated
i
  pieces of material from the Unit 2 vessel to a storage location outside the unit. In addition,
coni:cted by the inspector.
  the inspector also reviewed the performance of this group during a recently completed
l
  waste transfer evolution.
The self-directed work group includes six health physics technicians whose primary focus
  As part of the Liquid Radwaste Remediation Project at Unit 1, waste concentrates spilled
is to support the activities of the Waste Services Department. As previously noted in the
  inside the "A" Concentrator cubicle were removed in 1996. In addition to being                   i
discussion on Unit 2, above, this group was involved in the transfer of two highly activated
  radioactive, this material also contained asbestos, and thus required specialized engineering
pieces of material from the Unit 2 vessel to a storage location outside the unit. In addition,
  controls for handling, as required by the Occupational Safety and Health Administration
the inspector also reviewed the performance of this group during a recently completed
  (OSHA). On January 24,1997, ten barrels of this material, each containing several
waste transfer evolution.
As part of the Liquid Radwaste Remediation Project at Unit 1, waste concentrates spilled
inside the "A" Concentrator cubicle were removed in 1996. In addition to being
i
radioactive, this material also contained asbestos, and thus required specialized engineering
controls for handling, as required by the Occupational Safety and Health Administration
(OSHA). On January 24,1997, ten barrels of this material, each containing several


7 V
7
  e
V
                                                                                                I
e
                                                    39
39
    plastic-wrapped bags of the waste, were transferred to a processing liner, which ultimately l
plastic-wrapped bags of the waste, were transferred to a processing liner, which ultimately
    was to be solidified and buried as low-level radioactive waste. Due to OSHA requirements,
was to be solidified and buried as low-level radioactive waste. Due to OSHA requirements,
                                                                                                l
this transfer was conducted inside a tent-like structure erected around the liner by a team
    this transfer was conducted inside a tent-like structure erected around the liner by a team '
'
    of five specially trained contractors. Because of the OSHA requirements, the health
of five specially trained contractors. Because of the OSHA requirements, the health
    physics technicians from the self-directed work group could not enter the tent once work
physics technicians from the self-directed work group could not enter the tent once work
                                                                                                l
began. Based upon interviews conducted by the inspector with all members of the
    began. Based upon interviews conducted by the inspector with all members of the             j
j
    contractor work team, the contractor industrial hygienist, and the self directed work group ;
contractor work team, the contractor industrial hygienist, and the self directed work group
    technicians, and a review of documentation associated with this activity (RWP, ALARA
technicians, and a review of documentation associated with this activity (RWP, ALARA
                                                                                                l
review, pre-job briefing package, post-job review) the inspector determined that the work
    review, pre-job briefing package, post-job review) the inspector determined that the work   i
i
    was appropriately controlled in accordance with NRC regulations. While all five contractors l
was appropriately controlled in accordance with NRC regulations. While all five contractors
    were contaminated on their person and/or clothing upon completion of the work, this was     '
were contaminated on their person and/or clothing upon completion of the work, this was
    not the result of a breakdown of radiological controls. None of the contaminations resulted ,
'
    in a significant radiological exposure.                                                     '
not the result of a breakdown of radiological controls. None of the contaminations resulted
    c.       Conclusions                                                                       I
,
                                                                                                l
in a significant radiological exposure.
    Unit 1
'
    Noticeable reductions in the amount of contaminated spaces within the unit were
c.
    observed. ALARA planning and staffing of the ALARA group have significantly improved,
Conclusions
    however, the effectiveness of this cannot be determined until more radiologically
Unit 1
    significant work commences. One violation of NRC requirement involving an unmonitored
Noticeable reductions in the amount of contaminated spaces within the unit were
    release path was identified.
observed. ALARA planning and staffing of the ALARA group have significantly improved,
    Unit 2
however, the effectiveness of this cannot be determined until more radiologically
    Good work planning and control was observed for the transfer of highly irradiated materials j
significant work commences. One violation of NRC requirement involving an unmonitored
    from the reactor vessel. Significant changes in the planning and control of radiological , ;
release path was identified.
    work is under development. A violation of NRC requirements involving poor radiological
Unit 2
    worker practices was identified. While short-term corrective actions were implemented by
Good work planning and control was observed for the transfer of highly irradiated materials
    the licensee at the time of this inspection, long-term actions had not yet been identified.
j
      Unit 3
from the reactor vessel. Significant changes in the planning and control of radiological ,
    Contamination control improvements, especially the reduction in the number and need for
work is under development. A violation of NRC requirements involving poor radiological
    catch containments, was observed during tours of the RCA. Incorporation of RWP and
worker practices was identified. While short-term corrective actions were implemented by
    ALARA information into the work orders was an improvement, although the effectiveness
the licensee at the time of this inspection, long-term actions had not yet been identified.
      of this will have to be evaluated once significant radiological work resumes.
Unit 3
      Site Health Physics
Contamination control improvements, especially the reduction in the number and need for
      Appropriate support to Unit 2 was observed during the transfer of highly irradiated
catch containments, was observed during tours of the RCA. Incorporation of RWP and
      material. Appropriate work controls were implemented during the transfer of asbestos
ALARA information into the work orders was an improvement, although the effectiveness
      contaminated concentrates wastes.
of this will have to be evaluated once significant radiological work resumes.
Site Health Physics
Appropriate support to Unit 2 was observed during the transfer of highly irradiated
material. Appropriate work controls were implemented during the transfer of asbestos
contaminated concentrates wastes.


  $
$
                                                  40
40
    R8             Miscellaneous Radiological Protection and Chemistry Issues
R8
    A recent discovery of a licensee operating their facility in a manner contrary to the Updated
Miscellaneous Radiological Protection and Chemistry Issues
    Final Safety Analysis Report (UFSAR) description highlighted the need for a special focused
A recent discovery of a licensee operating their facility in a manner contrary to the Updated
    review that compares plant practices, procedures and/or parameters to the UFSAR
Final Safety Analysis Report (UFSAR) description highlighted the need for a special focused
    descriptions.
review that compares plant practices, procedures and/or parameters to the UFSAR
    While performing the inspections discussed in this report, the inspector reviewed the
descriptions.
    applicable portions of the UFSAR that related to the areas inspected. The inspector
While performing the inspections discussed in this report, the inspector reviewed the
    verified that the UFSAR wording was consistent with the observed plant practices,
applicable portions of the UFSAR that related to the areas inspected. The inspector
    procedures and/or parameters, except in the area of the management organization and
verified that the UFSAR wording was consistent with the observed plant practices,
    responsibilities for radiation protection. Section 12.5 of the Unit 1 UFSAR and Section
procedures and/or parameters, except in the area of the management organization and
    11.2.3 of the Unit 2 UFSAR make reference to Section 12.5.1 of the Unit 3 UFSAR for a
responsibilities for radiation protection. Section 12.5 of the Unit 1 UFSAR and Section
    full description of the health physics organization and reporting functions. This description
11.2.3 of the Unit 2 UFSAR make reference to Section 12.5.1 of the Unit 3 UFSAR for a
    no longer is accurate due to the restructuring and unitization of the Radiation Protection
full description of the health physics organization and reporting functions. This description
    Program. The Work Services organization recognized the need to update the Unit 3 UFSAR
no longer is accurate due to the restructuring and unitization of the Radiation Protection
    to reflect the management changes and identified it to the Site Licensing Director by
Program. The Work Services organization recognized the need to update the Unit 3 UFSAR
    memorandum, dated November 29,1996.
to reflect the management changes and identified it to the Site Licensing Director by
                                      V. Manaaement Meetinas
memorandum, dated November 29,1996.
    X1             Exit Meeting Summary
V. Manaaement Meetinas
    The inspectors presented the inspection results to members of licensee management at the
X1
    conclusion of the inspectian. The licensee acknowledged the findings presented.
Exit Meeting Summary
    X1.2 Final Safety Analysis Report Review
The inspectors presented the inspection results to members of licensee management at the
    A recent discovery of a licensee operating their facility in a manner contrary to the final
conclusion of the inspectian. The licensee acknowledged the findings presented.
    safety analysis report (FSAR) description highlighted the need for additional verification
X1.2 Final Safety Analysis Report Review
    that licensees were complying with FSAR commitments. All reactor inspections will
A recent discovery of a licensee operating their facility in a manner contrary to the final
    provide additional attention to FSAR commitments and their incorporation into plant
safety analysis report (FSAR) description highlighted the need for additional verification
    practices, procedures and parameters.
that licensees were complying with FSAR commitments. All reactor inspections will
    While performing the inspections which are discussed in this report the inspectors
provide additional attention to FSAR commitments and their incorporation into plant
    reviewed the applicable portions of the FSAR that related to the areas inspected.
practices, procedures and parameters.
    inconsistencies were noted between the wording of the FSAR and the plant practices,
While performing the inspections which are discussed in this report the inspectors
    procedures and/or parameters observed by the inspectors, as documented in Sections
reviewed the applicable portions of the FSAR that related to the areas inspected.
    U3.E8.1 and R8.
inconsistencies were noted between the wording of the FSAR and the plant practices,
procedures and/or parameters observed by the inspectors, as documented in Sections
U3.E8.1 and R8.
<
<


    , _ _-__ _   __             . . - _.       .-.~. _ - --     ._         ..       _ _ _ .     - - _ _ . _
, _ _-__
  b
_
__
. . -
_.
.-.~. _ - --
._
..
_ _ _ .
- - _ _ . _
b
f
f
                                                          41
41
                                        INSPECTION PROCEDURES USED
INSPECTION PROCEDURES USED
;
;
            IP 37550:
~
~
IP 37550:
                      Engineering
Engineering
,            IP 37551: Onsite Engineering
IP 37551:
Onsite Engineering
,
1
1
            IP 40500: Licensee Self-Assessments Related to Safety issues inspections
IP 40500:
                                                                                                                ]
Licensee Self-Assessments Related to Safety issues inspections
:           IP 61726: Surveillance Observations                                                               I
]
i                                                                                                               l
:
            IP 62707: Maintenance Observations
IP 61726:
Surveillance Observations
i
l
IP 62707:
Maintenance Observations
1'
1'
                                                                                                                l
l
            IP 71707: Plant Operations
IP 71707:
            IP 71750: Plant Support Activities                                                                 j
Plant Operations
                                                                                                                l
IP 71750:
            IP 83750: Occupational Radiation Exposure                                                         '
Plant Support Activities
;            IP 92700: Onsite follow-up of Written reports of Nonroutine Events at Power Reactor .,
j
IP 83750:
Occupational Radiation Exposure
'
IP 92700:
Onsite follow-up of Written reports of Nonroutine Events at Power Reactor .,
;
Facilities
,
,
                      Facilities
i
                                                                                                                i
IP 92901:
            IP 92901: Follow-up Operations
Follow-up Operations
            IP 92902: Follow-up Maintenance                                                                   l
IP 92902:
            IP 92903: Follow-up Engineering
Follow-up Maintenance
                                                                                                                .
IP 92903:
                                                                                                                .
Follow-up Engineering
.
.


            ,-             ..       ..                     ~. -     -.       --     .   ,.   -
,-
                                                                                                    !
..
                                                                                                    I
..
  v                                                                                                  i
~. -
                                                                                                    i
-.
                                                                                                    1
--
                                                  42
.
                                                                                                    )
,.
                              ITEMS OPENED, CLOSED, AND DISCUSSED
-
    Opened
v
    URI 50-245/97 01-01         U 1.02.1 Spent Fuel Pool Cleanliness                             I
i
    URI 50-245/97-01-02         U 1.03.1 Operations Procedure Adequacy                           1
i
    URI 50 245,336,423/         U 1.05.1 Inaccurate Personal Qualification Statements
1
                  97-01-03
42
    URI 50-245/97-01-04         U 1.E1.1 Resolution of A-46 Program Outliers
ITEMS OPENED, CLOSED, AND DISCUSSED
    URI 50-245/97-01-05 -       U1.E2.2   Low Flow Operation of Containment isolation Check         i
Opened
                                          Valve 1-CU-29                                             l
URI 50-245/97 01-01
    NCV                         U2.08.2   Failure to Enter TS Action for inoperable Nis
U 1.02.1
    IFl 50-423/97-01-06         U3.01.1   Interpretation of TS Language and LCO Actions
Spent Fuel Pool Cleanliness
    IFl 50-423/97-01-07         U3.M 8.1 Seismic 11/1 Concerns
I
    VIO 50-245/97-01-08         R1       Failure to Monitor Gaseous Effluents from the           i
URI 50-245/97-01-02
                                          Radwaste Storage Building
U 1.03.1
    VIO 50-336/97-01-09         R1       Entering RCA w/o Electronic Dosimeter or Signing
Operations Procedure Adequacy
                                          RWP
1
    Closed
URI 50 245,336,423/
    LER 50-245/96-03             U 1.E1.1
U 1.05.1
    LER 50-336/96-15             U2.02.2
Inaccurate Personal Qualification Statements
    VIO 50-336/94-17-10         U2.08.1   Operation Outside Systtim Design Parameters               i
97-01-03
                                                                                                    '
URI 50-245/97-01-04
    URI 50-336/96-04-09         U 2.M8.1 Troubleshooting Controls
U 1.E1.1
    URI 50-336/96-06-06         U2.M8.2 High Pressure Safety injection Check Valve Backflow
Resolution of A-46 Program Outliers
                                          Testing                                                   j
URI 50-245/97-01-05 -
U1.E2.2
Low Flow Operation of Containment isolation Check
i
Valve 1-CU-29
l
NCV
U2.08.2
Failure to Enter TS Action for inoperable Nis
IFl 50-423/97-01-06
U3.01.1
Interpretation of TS Language and LCO Actions
IFl 50-423/97-01-07
U3.M 8.1
Seismic 11/1 Concerns
VIO 50-245/97-01-08
R1
Failure to Monitor Gaseous Effluents from the
i
Radwaste Storage Building
VIO 50-336/97-01-09
R1
Entering RCA w/o Electronic Dosimeter or Signing
RWP
Closed
LER 50-245/96-03
U 1.E1.1
LER 50-336/96-15
U2.02.2
VIO 50-336/94-17-10
U2.08.1
Operation Outside Systtim Design Parameters
'
URI 50-336/96-04-09
U 2.M8.1
Troubleshooting Controls
URI 50-336/96-06-06
U2.M8.2 High Pressure Safety injection Check Valve Backflow
Testing
j
URI 50 336/95-07-06
U2.E8.1,
Condensate Storage Tank Siphon Break
-
-
    URI 50 336/95-07-06          U2.E8.1, Condensate Storage Tank Siphon Break                  -
-
    URI 50-336/95-11-03         U2.E8.2   10 CFR 21 Reportability Review
URI 50-336/95-11-03
    Discussed
U2.E8.2
                                                                                                    l
10 CFR 21 Reportability Review
    VIO 50-245/95-42-01         U 1.08.1 Failure to Prevent Work Which had the Potential for       !
Discussed
                                          Draining the Reactor Vessel
VIO 50-245/95-42-01
    URI 50-336/96-01-04         U2.02.2   Loss of DC Bus Event
U 1.08.1
    URI 50-423/96-01-08         U3.E8.1   Slave Relay / Overlap Test Deficiencies
Failure to Prevent Work Which had the Potential for
    Sianificant items List
Draining the Reactor Vessel
                                                                                                    i
URI 50-336/96-01-04
    Unit 3 SIL #67         Partial Closure
U2.02.2
                                                                                                    ,
Loss of DC Bus Event
URI 50-423/96-01-08
U3.E8.1
Slave Relay / Overlap Test Deficiencies
Sianificant items List
i
Unit 3 SIL #67
Partial Closure
,


                                                                                .- . - . - .
,
,
  ,
.- . - . - .
  '
,
                                                                                            i
'
                                              43
i
                                    LIST OF ACRONYMS USED
43
    ACR(s)   adverse condition report (s)
LIST OF ACRONYMS USED
    AISC     American Institute of Steel Construction
ACR(s)
    ALARA     as low as reasonably achievable
adverse condition report (s)
    ANSI /ANS American National Standards Institute /American Nuclear
AISC
    ASME     American Society of Mechanical Engineers
American Institute of Steel Construction
    CCP       reactor plant component cooling
ALARA
    CES/NTE   component engineering services / nondestructive test engineering
as low as reasonably achievable
    CFR       Code of Federal Regulations
ANSI /ANS
    CHS       charging system
American National Standards Institute /American Nuclear
    CR(s)     condition report (s)
ASME
    DCN       design change notice
American Society of Mechanical Engineers
    DG       diesel generator
CCP
    EDG       emergency diesel generator
reactor plant component cooling
    EGLS     emergency generator loading sequence
CES/NTE
    ESAS     engineered safeguards actuation system                                       i
component engineering services / nondestructive test engineering
    ESF       engineered safety feature
CFR
    FIN       Fix-It-Now
Code of Federal Regulations
    FLS       first line supervisor
CHS
    FME       foreign material exclusion                                                   i
charging system
    GIP (s)   generic implementation procedure (s)
CR(s)
    GL       Generic Letter                                                               l
condition report (s)
    gpm       gallons per minute                                                           l
DCN
    HELB     high energy line break
design change notice
    HPSI     high pressure safety injection
DG
    ICAVP     Independent Corrective Action Verification Program
diesel generator
    IFl       inspector follow item
EDG
    IR(s)     inspection Reports (s)
emergency diesel generator
    LCO       limiting condition for operation
EGLS
    LER(s)   licensee event report (s)
emergency generator loading sequence
    M&TE     material & test equipment
ESAS
    NDT       nil ductility transition
engineered safeguards actuation system
    NRC       Nuclear Regulatory Commission
i
      NRR     Nuchar Reactor Regulation
ESF
      NSIC     Nut.,ar Safety Information Center
engineered safety feature
      NS&O     nuclear safety and oversight
FIN
      NUREG   Nuclear Regulation
Fix-It-Now
    .OCA       Office of. Congressional Affairs
FLS
      OIR(s)   open item report (s)
first line supervisor
      OJT     on the job training
FME
    . OSHA     Occupational Safety & Health Administration
foreign material exclusion
      PAO     Public Affairs Office
GIP (s)
      PDCR     plant design change record                                                   '
generic implementation procedure (s)
      PDR     Public Document Room
GL
      PiR(s)   plant information report (s)
Generic Letter
      PUP     procedure upgrade program
gpm
      QA       quality assurance
gallons per minute
HELB
high energy line break
HPSI
high pressure safety injection
ICAVP
Independent Corrective Action Verification Program
IFl
inspector follow item
IR(s)
inspection Reports (s)
LCO
limiting condition for operation
LER(s)
licensee event report (s)
M&TE
material & test equipment
NDT
nil ductility transition
NRC
Nuclear Regulatory Commission
NRR
Nuchar Reactor Regulation
NSIC
Nut.,ar Safety Information Center
NS&O
nuclear safety and oversight
NUREG
Nuclear Regulation
.OCA
Office of. Congressional Affairs
OIR(s)
open item report (s)
OJT
on the job training
. OSHA
Occupational Safety & Health Administration
PAO
Public Affairs Office
PDCR
plant design change record
'
PDR
Public Document Room
PiR(s)
plant information report (s)
PUP
procedure upgrade program
QA
quality assurance


        . ._ _       _     ..     . . .           ~ . . -         . - _ . .             .. . . . - . _.
.
      d
._
_
_
..
. . .
~ . .
-
. - _ . .
..
.
. . - .
_.
d
. o
. o
    e
e
                                                                                                            '
'
                                                          44                                                 ,
44
i             QAS   - Quality and Assessment Services
,
              OPTR     quadrant power ti!! ratio
i
              RBCCW   reactor building closed cooling water
QAS
              RCA     radiologically controlled area
- Quality and Assessment Services
              RFO     refueling outage
OPTR
;              RHS     residual heat removal
quadrant power ti!! ratio
;             RI       Region I
RBCCW
^                                                                                                             i
reactor building closed cooling water
              RPS     reaction protection system
RCA
              RSST     reserve station service transformer                                                 !
radiologically controlled area
RFO
refueling outage
RHS
residual heat removal
;
RI
Region I
;
i
^
RPS
reaction protection system
RSST
reserve station service transformer
RWCU
reactor water cleanup
*
*
              RWCU    reactor water cleanup
RWP(s)
              RWP(s)   radiation work permit (s)
radiation work permit (s)
              SBO     station blackout
SBO
'
station blackout
              SER(s)   safety evaluation report (s)
SER(s)
              SPO     Special Projects Office                                                             :
safety evaluation report (s)
,             SQUG     seismic qualification utility group
'
SPO
Special Projects Office
,
SQUG
seismic qualification utility group
"-
"-
              SSER     supplementel safety evaluation report
SSER
;              SSR     reactor plant samples
supplementel safety evaluation report
SSR
reactor plant samples
;
i
i
TBSCCW
turbine building secondary closed cooling water
'
'
              TBSCCW  turbine building secondary closed cooling water                                      l
TLD(s)
              TLD(s)   thermoluminescent dosimeter (s)
thermoluminescent dosimeter (s)
i             TR(s)   trouble report (s)
i
              TS(s)   technical specification (s)
TR(s)
:             UFSAR   updated final safety analysis report
trouble report (s)
              USl     unresolved safety issue
TS(s)
,
technical specification (s)
              VIO      violation
:
l             WC       work control
UFSAR
                                                                                                              I
updated final safety analysis report
4                                                                                                             i
USl
r
unresolved safety issue
VIO
violation
,
l
WC
work control
I
i
4
r
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                                                                                                            I
-
                                -    .~   . _ . .                           , . , . . - -
.~
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Latest revision as of 17:08, 11 December 2024

Insp Repts 50-245/97-01,50-336/97-01 & 50-423/97-01 on 970101-0310.Violations Noted.Major Areas Inspected:Maint, Engineering & Plant Support
ML20140C564
Person / Time
Site: Millstone  Dominion icon.png
Issue date: 04/11/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20140C552 List:
References
50-245-97-01, 50-245-97-1, 50-336-97-01, 50-336-97-1, 50-423-97-01, 50-423-97-1, NUDOCS 9704170127
Download: ML20140C564 (50)


See also: IR 05000245/1997001

Text

.

--

.

.

-

._. _-- -

.

.

,

l

'.

U.S. NUCLEAR REGULATORY COMMISSION

REGION I

Docket Nos.:

50-245

50-336

50-423

1

l

Report Nos.:

97-01

97-01

97-01

,

License Nos.:

DPR-21

DPR-65

NPF-49

i

Licensee:

Northeast Nuclear Energy Company

.

P. O. Box 128

i

Waterford, CT 06385

.

Facility:

Millstone Nuclear Power Station, Units 1,2, and 3

Inspection at:

Waterford, CT

i

Dates:

January 1,1997 - March 10,1997

inspectors:

T. A. Easlick, Senior Resident inspector Unit 1

D. P. Beaulieu, Senior Resident inspector, Unit 2

I

A. C. Cerne, Senior Resident inspector, Unit 3

j

A. L. Burritt, Resident inspector, Unit 1

2

R. J. Arrighi, Resident inspector, Unit 3

'

L. L. Scholl, Reactor Engineer, Region l

N. J. Blumberg, Project Engineer, Region i

R. J. Urban, Project Engineer, Region I

3

,

'

J. T. Furia, Senior Radiation Specialist, Region I, DRS

a

J. E. Carrasco, Reactor Engineer, Region I, DRS

i

Approved by:

Jacque P. Durr, Chief

Inspection Branch

Special Projects Office, NRR

I

1

7

9704170127 970411

PDR

ADOCK 05000245

Q

PDR

f

e

_. -

_ _ .

- -_

_ . - . . _ _ __

___

.___

_

,

,1

,

TABLE OF CONTENTS

EX EC UTIVE S U M M AR Y . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . ii

.

4'

'

U1.1 Operations

.................................................. 1

U101

Cond uct of O perations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

U102

Operational Status of. Facilities and Equipment . . . . . . . . . .

1

,

...

U103

Operations Procedures and Documentation

3

,

................

U105

Operator Training Qualification . . . . . . . . . . . . . . . . . . . . . . . . . 3

U108

Miscellaneous Operations issues . . . . . . . . . . . . . . . . . . . . . . . . 5

1

i

U 1.ll M ainte na n c e . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 6

U1 M2

Maintenance and Material Condition of Facilities and

Equipment

6

.......................................

'

U 1.lli Enginee ring . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 7

'

U1 E1

Conduct of Engineering

7

..............................

U1 E2

Engineering Support of Facilities and Equipment . . . . . . . . . . . . . 9

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U1 E8

Miscellaneous Engineering issues . . . . . . . . . . . . . . . . . . . . . . 11

S2.1 Operations

12

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U2 01

Conduct of Operations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 12

U2 O2

Operational Status of Facilities and Equipment . . . . . . . . . . . . . 12

)

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U2 08

Miscellaneous Operations issues . . . . . . . . . . . . . . . . . . . . . . . 14

U 2.ll M ainte n a n c e . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 16

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U2 M8

Miscellaneous Maintenance issues

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U 2.lli Engine e ring . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17

U2 E8

Miscellaneous Engineering issues . . . . . . . . . . . . . . . . . . . . . . 17

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U3.1 Operations

20

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U3 01

Conduct of Operations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 20

U~s 03

Operations Procedures and Documentation

23

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U3 07

Quality Assurance in Operations . . . . . . . . . . . . . . . . . . . . . . . 26

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U 3.11 M ain te n a n c e . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 27

U3 M1

Conduct of Maintenance

27

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U3 M8

Miscellaneous Maintenance issues

29

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U 3.Ill Engine e ring . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 31

U3 E8

Miscellaneous Engineering issues . . . . . . . . . . . . . . . . . . . . . . 31

IV Plant Support

35

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R1

Radiological Protection and Chemistry Controls

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R8

Miscellaneous Radiological Protection and Chemistry issues

39

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V. M anage ment M eetings . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 39

X1

Exit Meeting Summary . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 39

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EXECUTIVE SUMMARY L

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Millstone Nuclear Power Station'

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Combined inspection 245/97-01; 336/97-01; 423/97-01

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Operations

  • .

Numerous inaccurate Personal Qualification Statements (Form 398) were identified

'

at all four Connecticut plants following NRC questions on two recent adverse

condition reports. Approximately two thirds of the Personal Qualification

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Statements submitted for recent license applicants were inaccurate. These

applications resulted in the conduct of NRC license examinations and the issuance -

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of licenses. In a significant number of cases, the licenses were issued without the.

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candidates fully completing the licensee's training and qualification program, and in

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a few cases the reactivity manipulations, specifically required by 10 CFR 55, were

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also not complete. This issue is unresolved for'each Millstone unit pending the

completion of the licensee investigation, resolution of allidentified deficiencies and

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implementation of programmatic corrective actions. (Section U1.05.1)

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The degraded conditions found in the Unit 1 spent fuel pool are representative of a

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icng standing disregard for foreign material exclusion (FME) during the conduct of

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refuelmg fioor activities. Past low standards for FME control allowed the

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accumulation of a large amount of debris, which could potentially have a significant

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-impact on the fuel assemblies stored in the pool. Once the recovery organization

!

became aware of the extent of the problem, by reviewing video tapes, the

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inspectors noted a good response, including clear direction as to what needed to be

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8

done in the short term. Based on this information, the acceptability of the degraded

conditions in the spent fuel pool will be unresolved pending NRC review of the

,

issues. (Section U1.02.1)

1

At Unit 1, the licensee failed to evaluate and address a violation concerning the

  • -

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failure to prevent work which had the potential for draining the reactor vessel during

refueling. Further, the licensee failed to provide a comprehensive closure package -

of a quality consistent =with the process committed to in December 1996. The

' manner in which this issue was addressed provides evidence of the licensees ability

to perform effective reviews and to implement appropriate corrective' actions. As a

result of the inspector's concerns with the quality of the completion packages, the

licensee withdrew the NRC completion package schedule. A revised schedule was

still in developmcat at the end of the inspection period. (Section U1.08.1)

Although the Unit 2 backlog of 798 adverse condition reports (ACRs) that are

greater than 120 days old indicates that timeliness for completing corrective actions

remains a concern, the reduction in the backlog of older ACRs from 940 to 798

since the last inspection period is a positive trend which reflects the licensee's

increased level of effort in this area. Timeliness and effectiveness of corrective

actions are areas '... which the licensee must demonstrate sustained improved

performance. (Section U2.02.1)-

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A Unit 2 licensee event report discussed that while recovering from a loss of a

direct current (dc) bus, an operator failed to enter an action statement when three

channels of wide range nuclear instrumentation were rendered inoperable. This was

characterized as a non-cited violation. The primary concern associated with this

event was the fact that there was minimal procedural guidance provided to

operators to recover the loss of a de bus. The licensee is in the process of

preparing 12 abnormal operating procedures for recovering various de buses and

distribution panels. This concern is being tracked by an unresolved item. (Section

U2.02.2)

In addition to the physical plant design controls, a longstanding NRC concern at Unit

2 is that operating procedures do not reflect the Final Safety Analysis Report

(FSAR), and an NRC open item has existed since 1993 to address this concern.

This inspection report closes the old open item npqt because adequate corrective

actions have been taken, but because this concern is being addressed and tracked

by more recent items. The issue includes an evaluation of the procedure change

process, as well as the design control process, to ensure future operation is

conducted in accordance with the FSAR. (Section U2.08.1)

The procedure upgrade program has been effective in standardizing procedure

formats across the site. Because of the number of individuals involved in the

procedure upgrades and the long period of time to complete the task, the quality of

procedures vary substantially. As an adjunct to the Demand For Information

process [10 CFR 50.54(f)], which incorporates a verification of the design and

licensing bases, procedure accuracy will be verified. (Section U3 03)

The licensee's root cause investigation and corrective action plan for control of high

energy line break (HELB) doors were determined to be good. However, the

requirement to label the required HELB doors with a minimum number of turns to

ensure proper latching should have been included in the adverse condition report

corrective action plan if it was deemed necessary to prevent recurrence. (Section

U3.01.2)

Good' contingency planning and appropriate consideration of the applicable standard

and regulations were in evidence for both planned operational evolutions and

emergent shutdown conditions. Where necessary to improve shutdown risk

margins, temporary modifications or special system lineup were considered and well

controlled. The licensee development of a standardized approach for disseminating

operations policy for interpreting the language and action statement applicability of

the Unit 3 technical specifications appeared warranted. The examples noted during

this period will be reviewed further as an inspector follow item. (Section U3.01.1)

Maintenance

At Unit 1, the preparation and conduct of work associated with the entry and video

survey of the reactor water cleanup (RWCU) demineralizer room were well

controlled. The inspector noted that good radiological practices were used.

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The material condition in the room was acceptable and no deficiencies were

identified. (Section U1.M2.1)

Maintenance and surveillance activities were performed professionally and

thoroughly. All observed maintenance activities were performed with the work

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package or surveillance procedure present at the job site and personnel were noted

to be closely following the procedures. Review of the surveillance procedures

revealed that the requirements of the applicable technical specifications were

'

appropriately incorporated into the implementing procedure. (Section U3.M1.1)

The licensee developed a Fix-It-Now (FIN) multi-discipline work team approach to

augment the way maintenance is performed at the unit. This process is in addition

to the normal work control process. The FIN work process is being implemented in

a conservative manner. Any work required on protected train equipment was not

being assigned to the FIN team. All monitored work activities performed by the FIN

team were performed in accordance with the unit and station procedures. FIN team

members appeared to be well qualified. (Section U3.M1.1)

Plant inspection-tourt revealed improvements in the Unit 3 areas of housekeeping,

material conditions, and work controls. Field observations raised no new

unresolved safety issues, but did highlight the need for additional management

attention to a previously identified concern regarding the control of temporary

equipment with the potential to adversely impact safety-related components. This

" Seismic II/l" issue will be tracked as an inspector follow item and will receive

further evaluation as a "significant item" in the NRC Restart Assessment Plan.

(U3.M8.1 )

Engineering

A review was performed at Unit 1 of the licensee's progress in resolution of the

Unresolved Safety issue (USI) A-46 outliers documented in the Licensee Event

Report (LER)96-003, Rev. 2. These deficiencies involved inadequate anchorage of

the emergency diesel generator day tank and the turbine building secondary closed

cooling water air coolers. The regulatory requirements for reportability were met

and the corrective action prescribed in the LER were adequate in general, based on

the detailed walkdown of the A-46 modifications, the inspector concluded that the

licensee performed a substantial number of field modifications to accommodate the

seismic loading on mechanical and electrical equipment identified in the USl A-46

scope and documented in LER 96-003; this LER is closed. The followup of the

licensee's commitments to resolve the A-46 program outliers prior to startup for

cycle 16 operation and the assessment of the implication of this event on the

operation of Unit 1 will be unresolved pending further NRC review. (Section

U 1.E1.1 )

The corrective actions taken by the Unit 1 Cnmponent Engineering

Services / Nondestructive Test Engineering (CES/NTE) concerning the use of test

equipment was acceptable. The corrective actions appeared to be broad-based. A

majority of the short term corrective actions were complete, and the long term

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corrective actions were being tracked for closure., The significance of the UT

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instruments being past their calibration due dates was minimal because they were

. subsequently found to be within tolerance. (Section U1.E2.1)

The NRC is concerned about the operation of the new containment isolation check

a

valve 1-CU-29 at Unit 1, which is operating with lower than expected flow rates

during this extended shutdown. While the use of non-intrusive check valve testing

has verified that the check valve is backseated, this is a short term indication. The

long term effects of the low flow operation have yet to be determined. This issue is

unresolved pending the NRC review of the licensee's final determination of the

operability of the valve prior to plant startup. (Section U1.E2.2)

The inspectors found that overlap test reviews performed in 1993 were not

adequate. The licensee failed to identify this deficiency and improperly concluded

that the 1993 reviews accomplished the actions requested by NRC Generic Letter 96-01, " Testing Of Safety-Related Logic Circuits." (Section U3.E8.1)

t

Plant Support

The licensee has demonstrated a significant increase in management attention

towards work control and maintaining occupational exposures as low as is

reasonably achievable. However, two of the licensee's activities were determined

not to be in compliance with NRC regulations. The Unit 1 violation involves a long-

standing situation (since initial plant start-up), concerning an unmonitored release

pathway in the ventilation system for the radwaste storage building. The violation

at Unit 2 involves a failure to adhere to the licensee's radiation protection program

concerning proper use of electronic dosimeters. (Section R1)

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Report Details

Summarv of Plant Status

Unit 1 remained in an extended outage for the duration of the inspection period. The

licensee continues to implement configuration management program activities, engineering

reviews, and docketed correspondence assessments to verify compliance with the

established design and licensing basis of the unit. The successful completion of these

activities is required by NRC order prior to restart of the unit. During this period, the

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licensee implemented a major revision to the corrective action procedure. The goal was to

simplify the process, and at the same time make it more responsive towards restart and

needed organizational improvements. Under the new process, " condition reports" have

replaced " adverse condition reports" to capture both the regulatory defined adverse

condition, as well as other conditions that do not meet managements expectations.

The licensee has recently made two changes to the organizational structure at Unit 1. A

project management group was established to facilitate the implementation of plant

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modifications prior to startup. Additionally, a restart manager was selected to oversee

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completion of the Operational Readiness Plan, which will be used to identify and control

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the actions necessary to achieve and maintain improved performance. The restart manager

will also be responsible for the review of corrective action completion packages, which will

provide objective evidence of corrective action completion. Section U1.08.1 & U1.E8.1 of

this report provides an assessment of the licensee's progress in the area of completion

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package development. The effectiveness of these changes, as well as the new corrective

action program, will be assessed as part of future NRC inspections.

U1.1 Operations

U101

Conduct of Operations

01.1 General Comments (71707)

Using Inspection Procedure 71707, the inspectors conducted frequent reviews of ongoing

plant operations. The inspectors reviewed operability determinations, availability

determinations, and witnessed the conduct of management review team discussions

regarding the disposition and closure of condition reports (CRs). During a routine tour of

the Unit 1 intake structure, the inspector found the material condition of systems and

components to be adequate. The licensee initiated a material condition improvement

project in the Spring of 1996. The inspector observed some material improvement work

on-going. Specific events and noteworthy observations are detailed in the sections below.

U102

Operational Status of Facilities and Equipment

O 2.1 Soent Fuel Pool Cleanliness

a.

Inspection Scope (71707)

NRC inspection report 245/96-08, dated December 3,1996, discussed the continued

identification of discrepant conditions in the spent fuel pool, indicating a need to accelerate

the evaluation portion of the spent fuel pool cleanup / recovery plan. At that time, the

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-inspectors concluded that all discrepant conditions warrant identification and evaluation in

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the short term to ensure the collective impact of these issues were addressed. On January

10,1997, the inspectors reviewed a video tape surveillance of the spent fuel pool

conducted on January 3, using an under water camera. The video tapes were reviewed to

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evaluate the conditions in the spent fuel pool including the fuel storage racks and stored

fuel bundles.

b.

Observations and Findinas

As discussed in NRC report 245/96-08, the earlier video tapes identified improperly seated

)

fuel bundles. In light of the recent video surveys, the licensee determined that the

improperly seated bundles were caused by one of three conditions: 1) There are 55 fuel

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bundles elevated as a result of their channel fasteners being caught on the spent fue!

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racks; 2) 14 fuel bundles are elevated due to unknown reasons, although it is suspected

)

that debris is in the fuel rack preventing proper seating; 3) One additional fuel bundle was

resting on a 1/4 inch metal tube (suspected to be a boron tube from a control rod blade

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segment) that is lying on the floor liner and bends upward into the bottom of the fuel

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storage cell. An evaluation was performed to address all relevant issues including: the

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effect of a bundle drop on the fuel bundle itself, the fuel rack, and spent fuel pool liner;

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seismic response of the fuel racks; the criticality margin; fuel assembly cooling; and water

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shielding. The licensee concluded that the storage racks that contained elevated fuel

assemblies were operable, but were not full qualified, since the fuel assemblies were not

fully seated. In response to this concern, procedural controls were put in place to ensure

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that no fuel assemblies are transferred within the spent fuel pool until all fuel is fully

.

seated.

The video tapes also revealed a significant amount of debris on the fuel bundles, fuel

{

racks, and the floor of the fuel pool. The debris included rope, cable, boron tubes, a broom

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head, filter hoses, nuts, and unidentifiable objects. In addition, the bottom of the fuel pool

was covered by a layer of sediment. Additionally, the viden ^) view identified that the

velocity limiter portion cf '.our control rod blade assemblies vere stored vertically on top of

one another without support. The velocity limiter sections were located on the spent fuel

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pool floor in the space between a spent fuel rack and the control rod blade storage rack.

An engineering evaluation of the velocity limiter storage configuration concluded that the

structural integrity of the spent fuel rack, the control rod blade storage rack, and the pool

liner would be maintained in the event of an impact caused by the velocity limiters falling

over.

A dent was identified in the spent fuel pool floor liner from an impact of an unknown

object. The dent was approximately 4 inches in diameter and was relatively uniform and

smooth, with no obvious nicks or gouges. A final operability determination and safety

evaluation concluded that there were no operability or safety issues, and that the dent did

not challenge the leak tightness or structural integrity of the fuel pool.

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A previously known condition concerning the storage of a damaged, irradiated fuel

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assemble stored in a " damaged fuel container," was roviewed to consider the collective

impact of this issue and the other fuel pool discrepan:les. The fuel assemble was

damaged in 1974, placed in a storage container in 1976, and moved to its current location

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in 1989. The licensee performed a safety evaluation, as part of an operability

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determination, that addressed the storage configuration of the damaged fuel container and

its location in the control rod storage rack. Similar to the unseated bundles, criticality,

<

seismic response, water shielding, and decay heat removal were evaluated. Based on that

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evaluation, the licensee concluded that the storage configuration is safe and does not

constitute an unreviewed safety question. In addition, a procedural restriction was placed

in procedure EN 1067, Supplemental Procedure for Inventory and Control of Special

Nuclear Material, to prevent storing fuelin locations adjacent to the damaged fuel

assembly. This was required since the criticality margin for storage of fuel assemblies in

adjacent rack locations has not been fully evaluated and full qualification has not been

verified,

c.

Conclusions

The inspectors concluded that the degraded conditions in the spent fuel pool are

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representative of a long standing lack of concern for fore:gn material exclusion (FME)

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during the conduct of refueling floor activities. Past low standards for FME control allowed

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the accumulation of a large amount of debris, which could potentially have a significant

4

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impact en the fuel assemblies stored in the pool. Once the recovery organization became

aware of the extent of the problem, by reviewing the video tapes, the inspectors noted a

,

good resoonse, including clear direction as to what needed to be done in the short term.

,

The appropriate operability determinations and safety evaluations were prepared, and

adverse condition reports were initiated to document the findings.

In a letter to the NRC dated February 21,1997, the licensee documented the current

conditions in the spent fuel pool and their future plans for correcting the adverse

, conditions. Prior to core reload all unseated fuel assemblies will be properly seated and all

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new and reload fuel bundles will be visually inspected from below to check for foreign -

material before placement in the core. The licensee committed to cleaning up the pool,

including removal of debris and various used components, prior to Refueling Outage 16.

Based on this information, the acceptability of the degraded conditions in the spent fuel

_

pool will be unresolved (URI 245/97-01-01) pending NRC review of the issues and the

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completion of the licensee's root cause analysis.

U103

Operations Procedures and Documentation

03.1 Operations Procedures

During May and June,1996, two Unit 1 Operations department staff engineers performed

a self assessment of the Procedure Upgrade Program (PUP) for Unit 1 Operations

procedures. The Unit 1 operations self-assessment contained a significant number of

negative findings concerning the Unit 1 PUP process for the Operations Department and for

the quality of the upgraded procedures produced. The inspector discussed this assessment

with one of the staff engineers and the Unit 1 Operations Manager. Although the

assessment applied to Unit 1 only, the Unit 1 Operations Manager stated that he would

share the self assessment results with other Unit 1 Departments and with the operations

managers of the other Millstone units. The licensee's resolution of the problems identified

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in the Unit 1 self assessment are unresolved (URI 97-01-02) pending the NRC's review of

the associated corrective actions.

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U105

Operator Training Qualification

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05.1 Inaccuracies in Personal Qualification Statements Certifications

)

a.

Inspection Scope

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Two adverse condition reports (ACRs) were initiated to address operator license training -

related deficiencies. The ACRs document the failure of license candidates to complete all

classes, on the job training (OJT), and on shift watch standing time, along with the failure

to comply with procedures resulting in weaknesses in the systematic approach to training.

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The issues were identified as a result of preliminary findings and insights gained from an

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independent root cause investigation to address poor candidate performance during a

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recent Millstone Unit 1 initial license examination. The inspectors reviewed the short term

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actions taken in response to these two ACRs. The reviews focused on the accuracy of

Personal Qualification Statements (Form 398) submitted to the NRC staff as an application

for an operators license. The Form 398 contains assertions by the applicant, the training

coordinator and senior management representative on site, that among other things, the

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applicant completed the licensee's requirements to be a licensed operator.

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b.

Observations and Findinas

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During the review subsequent to the initiation of the ACRs, the licensee identified

numerous discrepancies which resulted in inaccurate Personal Qualification Statements

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(Form 398). In some cases, the errors resulted in candidates not meeting the licensee's.

minimum program requirements prior to signing of the 398 forms; however, the necessary

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training was completed prior to the license examination. In other cases, the candidates

were issued licenses without the program requirements being met. The discrepancies

include failure to complete the required on shift watchstanding time, OJT, and the required

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number of reactivity manipulations, in addition, several candidates failed to meet the

program prerequisites such as technical degree or additional experience requirements.

At Millstone Unit 1, the four most recent license classes were reviewed by the licensee, in

the two most recent classes,12 of 13 candidates submitted inaccurate 398 forms. In the

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two prior classes, only 1 of 9 candidate's 398 form was inaccurate. Most of the

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discrepancies involved the failure to complete required under-instruction watches, but also

included the failure to complete the required OJT. In the worst case, the candidate

completed little more than 3 of the required 13 weeks of OJT specified by the training

program description.

At Millstone Unit 2, a review of the two most recent license classes revealed 14 out of 16

candidates submitted inaccurate 398 forms. These discrepancies generally consisted of

insufficient hours of under-instruction watchstanding, but also included one case of

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insufficient reactivity manipulations and two cases in which OJT records appear to be lost.

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At Millstone Unit 3, the review of the most recent license class revealed 3 of 10 of the

candidates submitted inaccurate 398 forms. These discrepancies included one missed

under-instruction watch, one case of insufficient reactivity manipulations and the failure to

meet the program prerequisites, and one case in which OJT requirements were

accomplished after the assertion that all training program requirements were completed on

the 398 form.

At Connecticut Yankee, the review of the most recent license class revealed 10 out 12

candidates submitted inaccurate 398 forms. These discrepancies included insufficient

hours of under-instruction watchstanding, insufficient reactivity manipulations in two

cases, and program prerequisites not met in two cases. Additionally, OJT records were

lost or signed after the 398 was completed.

On March 3,1997, the licensee issued a letter to the NRC staff to discussing these issues.

Subsequently, the NRC staff issued a confirmatory action letter. The reviews are being

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expanded on Millstone Unit 3 and Connecticut Yankee. Millstone Unit 2 is still evaluating

if review scope expansion is warranted and Millstone Unit 1 is preparing a position that

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additional expansion is not necessary. The licensee has removed numerous individuals

from watchstanding duties and requested the withdrawal of two licenses. However, in the

case of Millstone Unit 2, some licensed operators removed frorn watchstanding duties have

been restored to an active status following the completion of missed requirements. The

licensee believes the majority of the discrepancies can be attributed to unclear

expectations on program requirements, the failure to maintain the programs currer t using

the systems approach to training, and poor record keeping practices. All of the fctors are

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the result of inadequate management oversight.

c.

Conclusion

The licensee identified numerous inaccurate Personal Qualification Statements (Form 398)

following NRC questions on two recent ACRs. Approximately two thirds of the Personal

Qualification Statements submitted for recent license applicants were inaccurate. These

applications resulted in the conduct of NRC license examinations and the issuance of

licensees. In a significant number of cases, the licenses were issued without the

candidates completing the licensee's training and qualification program, and in a few cases

the reactivity manipulations, specifically required by 10 CFR 55, were also not complete.

This issue is unresolved (URI 245,336,423/97-01-03) pending the completion of the

licensee's investigation, resolution of allidentified deficiencies and implementation of

programmatic corrective actions.

U108

Miscellaneous Operations issues (92700)

08.1 (Undate) Violation 50-245/95-42-01: Failure to Prevent Work Which Had the

Potential for Drainina the Reactor Vessel Durina Fuel Movements

This violation concerned the failure to prevent work which had the potential for draining

the reactor vessel while fuel removal was in progress. In addition, the licensee does not

have a formal process to ensure all applicable technical specifications are properly

implemented during refueling. Further, based on the inspector's review of the licensing

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bases for the current Technical Specification 3.5.F 7, it did not appear that the conditions

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. initially established and reviewed by the NRC were appropriately maintained during

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subsequent amendments.

The licensee developed a process for preparation of corrective action completion packages

and a schedule for providing them to the NRC, as a result of a previous NRC request. The

inspector reviewed the first corrective action completion package prepared to address the

three issues discussed above. The documentation package contained a root cause analysis

-(RCA), license event report, and a violation response, which were developed to address the

3

issues. However, these documents were not consistent with each other and generally did

not address the cited violation. The identified causes and many of the corrective actions,

address maintenance and planning issues that led to the unplanned draining of a small

amount of reactor water during maintenance on a recirculation discharge valve. The RCA

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appears to have been performed prior to the licensee's acknowledgment of the technical

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specification compliance issue. The majority of the corrective actions specified, involve

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improvements to the shutdown risk program; however, the inspector determined that these

actions would not preclude a recurrence of the technical specification non-compliance.

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The violation response discussed the development of mode change checklists and

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enhanced logs; however, these actions, which may address technical specification

'

compliance, were not implemented by the end of the inspection period.

The licensee did not address the adequacy of Technical Specification 3.5.F.7, nor verify

that the conditions initially established and reviewed by the NRC were appropriately

maintained during subsequent amendments. The license event report was submitted 3

months after the event without a detailed reason for the delay and no corrective actions

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were specified for the late reporting.

2

This item will remain open pending resolution of this item. The licensee failed to

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appropriately evaluate and address these issues for more than a year since the event.

!

Further, the licensee failed to provide a closure package consistent with the process

committed to in December 1996. The manner in which this issue was addressed provides

evidence of the licensees ability to perform effective reviews and to implement appropriate

corrective actions. As a result of the inspector's concerns with the quality of the

completion packages, the licensee withdrew the NRC completion package schedule. A

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revised schedule was stillin development at the end of the inspection period.

U1.ll Maintenance

U1 M2

Maintenance and Material Condition of Facilities and Equipment

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M2.1 RWCU Demineralizer Room Material Condition

a.

insoection Scope (71750)

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The inspector observed activities associated with the entry into, and video survey of, the

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reactor water cleanup (RWCU) demineralizer room. The purpose of the entry was to

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determine the material condition of the infrequently accessed room. A remote controlled

robot was used, which supported both a video camera and radiation detection equipment.

.

.

7

b.

Observations and Findinas

The health physics (HP) department was well prepared for this activity since preparations

'

and staging were completed the day before. This allowed potential problems to be

identified and corrected prior to the start of work. In particular, it was identified in

advance that the robot would need to be lifted into the room through the access in the

wall, and preparations were made to account for this. Positive control over personnel

access, was observed with only people that were needed for the activity permitted in the

area. The workers' awareness of radiological hazards was evident. HP supervision and

the system engineer provided oversight of this activity. The video survey indicated that

the room was in good condition and the structural integrity of the piping and three

'

domineralizer tanks was intact. There was no indication of any system leakage and

radiation levels in the general area were normal.

c.

Conclusions

Based on the above review, the inspector determined that the preparation and conduct of

work associated with the entry and video survey of the RWCU demineralizer room was

well controlled. The inspector noted that good radiological practices were used. The

material condition in the room was acceptable and no deficiencies were identified.

U1.Ill Enaineerina

U1 E1

Conduct of Engineering

E1.1

Unresolved Safety issue USl A-46 " Seismic Qualification of Eauipment in Operatina

Plants."

a.

Insoection Scope (37550)

The scope of this inspection was to review the licensee's progress in resolving the outliers

identified during the implementation of the Unresolved Safety issue (USI) A-46 " Seismic

Qualification of Equipment in Operating Plants."

b.

Observations

The inspector reviewed the Licensee Event Report (LER)96-003, Rev. 2 that documented

deficiencies involving inadequate anchorage of the emergency diesel generator (EDG) day

tank and the turbine building secondary closed cooling water (TBSCCW) air coolers.

Backaround

in December 1980, The NRC staff initiated an Unresolved Safety issue, (USI) A-46,

" Seismic Qualification of Equipment in Operating Plants," related to seismic adequacy of

mechanical and electrical equipment in older nuclear plants. After technical research by

the Seismic Qualification Utility Group (SQUG) and the NRC regarding this issue, the NRC

.,__ _

_

_

- _ _

.-

.

_ . _ . _

_

. _ _ _ . . .

. _

_

.re i

,

.

'

7

b.

Observations and Findinas

i

The health physics (HP) department was well prepared for this activity since preparations

and staging were completed the day before. This allowed potential problems to be

identified and corrected prior to the start of work. In particular, it was identified in

"

advance that the robot would need to be lifted into the room through the access in the

wall, and preparations were made to account for this. Positive control over personnel-

,

access, was observed with only people that were needed for the activity permitted in the

j

]

area. The workers' awareness of radiological hazards was evident. HP supervision and

'

the system engineer provided oversight of this activity. The video survey indicated that

l

the room was in good condition and the structural integrity of the piping and three

,

l

demineralizer tanks was intact. There was no indication of any system leakage and

l

radiation levels in the general area were normal.

c.

Conclusions

t.

Based on the above review, the inspector determined that the preparation and conduct of

j

work associated with the entry and video survey of the RWCU demineralizer room was

well controlled. -The inspector noted that good radiological practices were used. - The

material condition in the room was acceptable and no deficiencies were identified.

,

I

U1.Ill Enaineerina

'

I

U1 El

Conduct of Engineering

E1.1

Unresolved Safety issue USI A-46 " Seismic Qualification of Eauioment in Ooeratina

,

Plants."

I

a.

Inspection Scope (37550)

l

The scope of this inspection was to review the licensee's progress in resolving the outliers

identified during the implementation of the Unresolved Safety issue (USl) A-46 " Seismic

i

Qualification of Equipment in Operating Plants."

b.

Observations

The inspector reviewed the Licensee Event Report (LER)96-003, Rev. 2 that documented

deficiencies involving inadequate anchorage of the emergency diesel generator (EDG) day

tank and the turbine building secondary closed cooling water (TBSCCW) air coolers,

i

Beckaround

in December 1980, The NRC staff initiated an Unresolved Safety issue, (USI) A-46,

" Seismic Qualification of Equipment in Operating Plants," related to seismic adequacy of

mechanical and electrical equipment in older nuclear plants. After technical research by

the Seismic Qualification Utility. Group (SQUG) and the NRC regarding this issue, the NRC

.

-

. .

_

.

.

. - _ . .

.

-

-

. -

- - -

.

1

8

4

>

published a detailed approach for resolving USl A-46, in Generic Letter 87-02, "Verif!:ation

of Seismic Adequacy of Mechanical and Electrical Equipment in Operating Reactors, USl A-

-

4 6. "

The Generic Letter procedure set forth an approach for verifying seismic adequacy of

i

equipment using earthquake experience data supplemented by test results and analyses, as

,

necessary. Licensees subject to USl A-46 were encouraged to participate in the generic

'

'

program to accomplish seismic verification of equipment. As a result, SQUG developed the

" Generic Implementation Procedure (GIP) for seismic verification of Nuclear Plant

equipment."

l

USl A-46 Proaram at MS1

At Millstone Unit 1, the USl A-46 program was conducted to address the concerns

expressed in GL 87-02 regarding the seismic adequacy of safety related electrical and

d

mechanical equipment. The resolution of the seismic adequacy issue appeared to be

conducted in accordance with the SOUG approach, using the generic implementation plan

(GlP) as approved by the NRC in Supplemental Safety Evaluation Report (SSER) No.2.

I

Supplement 1 to GL 87-02, transmitted May 22,1992 includes SSER-2 which reviews the

l

GIP, requires the licensee to identify within 120 days a schedule for implementation and

'

any anticipated deviation from the GIP methods. The inspector verified that the licensee

met this requirement by reviewing the licensee's letter dated September 21,1992. In this

letter the licensee identified a schedule for MS1, which stated that the submittal of the

final report will take place six months after refueling outage 15, which is stillin progress.

The inspector noted that the implementation of the USI A-46 review program has resulted

'in the identification of outlier conditions which challenged the operability of the plant

,

components. These outliers were reported in an LER. The LER described the proposed

corrective action, which includes resolution of all outlier conditions prior to start up from

Refueling Outage (RFO) 15.

The LER selected for this inspection addresses operability concerns involving inadequate

anchorage of the EDG day tank and the TBSCCW air coolers. These operability concerns

were properly documented as LER,96-003, Rev. 2. The inspector reviewed the LER 96-

003, to ensure that regulatory requirements for reportability were met. The licensee has

properly identified this design deficiency as a USl A-46 program outlier, and has properly

characterized it as being reportable in accordance with 10 CFR 50.72 and 10 CFR 50.73.

The inspector found the LER's event described in a chronological sequence and the

prescribed corrective action appeared to be appropriate.

Conclusion

in terms of reportability, the proper characterizations were given to the outliers of the USl

A-46 program. The licensee prepared the LERs documenting these outliers in accordance

with established regulatory requirements. Based on these inspection results, LER 50-

.

245/96-003 is closed. The followup of the licensee's commitments to resolve the A-46

program outliers prior to startup for cycle 16 operation and the assessment of the

,

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_ __ _ _

._

.

9

,

implication of this event on the operation of Unit 1.will be unresolved pending further.NRC.

.

. review (URI 50-245/97-01-04)

Review of the Corrective Action for the EDG Day Tank

,

Since the EDG system is an emergency ac power system and the EDG day tank is a safety

,

related component, the inspector focused his review on the licensee's corrective action

- package. In the package, the Design Change Notice (DCN) designed and installed the

seismic restraint that consists of a box frame around the tank supported by the block

wall's structural reinforcements.

f

The design modification package was found to be complete, and the frame was designed

l

in accordance with the American Institute of Steel Construction (AISC) Manual for Steel

Construction, 9th Edition. However, key design parameters in the calculation were not

properly referenced making it difficult for an independent auditor to determine whether or

l

l

not these parameters are correct. These key design parameters questioned by the

inspector included acceleration values, friction values between the day tank and the

concrete base pad; the calculated reaction of the block wall; and the shear capacity of the

block wall. All the inspector's questions and observations were properly resolved by thea

.

licensee.

d

1

Conclusion

.

The inspector determined that,the modification package was complete and the frame

properly designed.

Walkdown of the Modifications

The inspector and the licensee design engineer walked down the modifications for the EDG

day tank and the TBSCCW air coolers, with the following details.

With regard to the EDG day tank, the general area was inspected and the framing to

distribute the tank's load appeared to be structurally sound. The tank was inspected and it

was noted that the impact on the block wall (T-27B) was minimal and limited to shear in

the plane of the block wall. The inspector also noted that these block walls had been

previously upgraded in response to NRC Bulletin 80-11. Outside the EDG day tank along

the hallways the inspector noted that proper seismic bracing and anchorage was evident

on the following:

Several modifications to vital electrical equipment (switchgear, load centers and

motor control centers) were installed.

Modification to vital batteries consisted of shim material which was installed to

address A-46 outlier conditions.

Modifications to prevent seismic interaction between lighting fixtures and vital

equipment were installed.

--

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i

10

)

. At the turbine building, elevation 14'-6" the inspector noted that the TBSCCW air

. coolers identified in the USl A-46 program scope were modified to accommodate

-

seismic bracing and anchorage. in the EDG room, more air coolers and other

i

components (air-start tanks, motor control center, and control panel) were

j

seismically anchored or braced to address USl A-46 outliers.

Conclusion

Based on the detailed walkdown of the A-46 modifications, the inspector concluded that

the licensee has performed a substantial number of field modifications to accommodate the

seismic loading on mechanical and electrical equipment identified in the USl A 46 scope.

U1 E2

Engineering Support of Facilities and Equipment

'

E2.1

Adverse Condition Report (ACR) Review

i

a.

Inspection Scope (37550)

i

1

The inspector reviewed an ACR issued on August 16,1996, to assess whether appropriate

)

'

corrective actions were identified and implemented to prevent recurrence of the adverse

condition. The ACR (M1-96-0427) reviewed by the inspector concerned Component

l

Engineering Services / Nondestructive Test Engineering (CES/NTE) ultrasonic test (UT)

instruments that had exceeded their calibration due dates.

]

b.

Observations and Findinos

Six CES/NTE UT instruments were found to have exceeded their yearly calibration due

dates, with four of them having been possibly used during examinations at Unit 1. As

"

' stated on the ACR,'the person who previously handled the CES/NTE material and test

equipment (M&TE) program no longer workea for the company, and none of the job

functions were replaced or reassigned. As a result, there was no ownership of the

CES/NTE M&TE program.

The six instruments in question were sent offsite to a vendor for calibration. All six were

found to be within tolerance when they were received. Additionally, before and after each

examination was performed, the instruments were calibrated in accordance with procedure

NU-UT-1, using a step wedge or calibration blocx The missed yearly calibrations are

j

performed to verify instrument operability only, and do not represent a quality related

i

calibration. In other words, the calibrations done during examinations might be sufficient

to preclude sending these instruments offsite for yearly calibrations. Since these yearly

calibrations are not required by the ASME Code, the licensee will determine whether to

suspend them.

The inspector reviewed Quality Assurance Audit Package A-60607, " Measuring & Test

i

Equipment," an audit that was conducted from August 26,1996 through September 18,

1996. This audit evaluated the key elements and processes of the M&TE program and

determined that the program at Millstone and Connecticut Yankee was ineffective in

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1

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l

11

fulfilling its mission and did not fully comply with 10 CFR 50 Appendix B criteria. in

- < .

response to this audit, ACR M1-96-0614 was written to address the adverse condition.'

1

i

i

To address the ACRs and audit report, CES/NTE developed a corrective action plan and

dedicated an individual to implement the plan and take ownership of the CES/NTE M&TE

program. Additionally, the licensee ensured that all CES/NTE quality related equipment

currently being used at Millstone and Connecticut Yankee was in calibration.

c.

Conclusion

The inspector concluded that the corrective actions taken by CES/NTE associated with the

ACRs and the QA audit was acceptable. The corrective actions appeared to be broad-

based. A majority of the short term corrective actions were complete, and the long term

corrective actions were being tracked for closure. The safety significance of the UT

j

instruments being past their calibration due dates was minimal because they were

subsequently found to be within tolerance.

E2.2 Containment isolation Check Valve.1-CU-29

a.

Inspection Scope (37551)

'

The inspector reviewed adverse condition report (ACR) 96-0539, which documents an

issue concerning the design specifications of the new containment isolation check valve 1-

1

CU-29. The valve was replaced with a smaller size valve for better flow characteristics,

and to allow testing and maintenance during this outage.

]

b.

Observations and Findinas

i

!

The replacement valve was a specially designed 6" check valve with a 4.5" disc. The disc

'

size was selected based on two flow conditions other than normal operations: 1) shutdown

flow conditions occurring approximately 10% of the time (70 days per operating cycle)

with a minimum system flow of 300 gpm; 2) and startup flow condition, occurring about

1

0.2% of the time with a system flow rate of 100-200 gpm. Due to the current extended

outage, it is not known if the shutdown flow rate will affect the valve. In fact, the RWCU

system is unable to produce the 300 gpm used in selecting the disc size due to the flow

restriction created by the pressure control valve 1-CU-10. During the followup of this

issue, the inspector noted that the actual system flow rate is approximately 190-200 gpm

using the auxiliary cleanup pump, it is not known what effects, if any, will be created by

i

operating the valve at these lower flow rates for this extended period.

In a effort to determine if the valve disc was fluttering or banging into the backseat due to

the low flow conditions, the licensee employed Liberty Technologies to perform non-

intrusive check valve testing. Liberty Technologies performed both acoustic and magnetic

testing on CU-29. Their report stated that the test results provide positive indication of full

opening during the flow initiation test. Acoustic data recorded during steady state flow

indicated no anomalous behavior (such as excessive trim wear or rattling). The report also

'

noted that due to large valve body signal strength from the magnetic sensors during the

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12

valve opening and steady state tests were insufficient to provide useful results. However, .

they determined the acoustic data was a sufficient basis for the conclusions documented.

-

A member of the engineering staff informed the inspector that ACR 96-0539 was currently

open and under review. Engineering needs to determine a method for ascertaining the

actual impact of the lower flow operation on the valve. Localleak rate testing is being

considered as a possible method to determine if any valve degradation has occurred,

c.

Conclusions

The NRC is concerned about the operation of CU-29 with lower than expected flow rates

during this extended shutdown. While the use of non-intrusive check valve testing has

verified that the check valve is backseated, this is a short term indication. The long term

effects of the lower flow operation have yet to be determined. This issue is unresolved

-(URI 245/97-01-05) pending the NRC review of the licensee's finial determination of the

operability of the valve prior to plant startup.

U1 E8

Miscellaneous Engineering issues

E8.1

Closecut Documentation Packaae Review

The inspector reviewed the contents of a corrective action documentation package for NRC

unresolved item 96-04-07 (safety relief valve electric lift modification). The inspector

noted that the package included a draft licensee response to an NRC request for additional

information associated with the license amendment. Per previous arrangements the

licensee documentation packages were to be complete and contain only approved

documents. The package was returned to the licensee and no inspection was performed at

this time.

.

.

13

Report Details

Summary of Unit 2 Status

Unit 2 entered the inspection period with the core off-loaded. The unit was initially shut

down on February 20,1996, to address containment sump screen concerns and has

remained shut down to address an NRC Demand for Information [10 CFR 50.54(f)] letter

requiring an assertion by the licensee that future operations are conducted in accordance

with the regulations, the license, and the Final Safety Analysis Report.

U2.1 Operations

U201

Conduct of Operations

01.1 General Comments (71707)

Using Inspection Procedure 71707, the inspectors conducted frequent reviews of ongoing

plant operations to ensure that licensee's controls were effective in achieving continued

safe operation of the faciiity while shut down. The inspectors observed that proper control

room staffing was maintained, access to the control room was properly controlled, and

operator behavior was commensurate with the plant configuration and plant activities in

progress. In general, the conduct of operations was professional and safety-conscious.

Operations Management has recently placed greater attention on improving performance

associated with operator response to control room alarms with a focus on communications

and use of alarm response procedures. The NRC has noted the improvements in this area,

i

particularly regarding control room operators communicating to the unit supervisors what

alarms were received and ensuring a mutual understanding of why the alarm was received.

The licensee discovery of potential discrepancies in the personal qualification statements

(NRC Form 398) of certain Unit 2 licensed operators has been assessed for immediate

impact and determined to require further evaluation. This is considered an unresolved

,

issue as described in Section U1.05.1 of this inspection report.

The inspector toured the Unit 2 intake structure and found the material condition of

systems and components to be acceptable, in the Spring of 1996, the licensee instituted a

corrective action plan to address material deficiencies. A number of items have been

corrected, which has improved the material condition of the intake structure.

U2 O2

Operational Status of Facilities and Equipment

02.1 Adverse Condition Report Backloa

a.

Insocction Scope

The NRC evaluated the timeliness in which the licensee completed corrective actions

associated with Unit 2 adverse condition reports (ACRs).

.

.

14

b.

Observetions and Findinas

Timeliness for completion of corrective actions has been a longstanding concern at

'

Millstone. Having an ACR backlog in itself is not a reflection of poor performance because

as the threshold for writing ACRs decreases, the ACR backlog willincrease accordingly.

The concern is the number of ACRs that are not closed in a timely manner. To help

provide the NRC some sense of the licensee's progress in addressing the timeliness

concern, the licensee was asked to provide the number of ACRs having outstanding

corrective actions that are greater than 120 days old. Although the NRC does not consider

120 days a level of excellence nor is it acceptable when addressing immediate safety

concerns, it does provide some understanding of licensee management effectiveness in

addressing the corrective action timeliness issue.

Several months ago, the NRC raised a concern that the licensee's ACR database did not

allow them to determine the number of ACRs having outstanding corrective actions. The

1

licensee's previous understanding, as documented in NRC Inspection Report (IR) 50-

336/96-09, was that the ACR data entries had been corrected to provide reliable ACR

'

backlog numbers. However, additional licensee reviews of the ACR database indicate that

the number of ACRs greater than 120 days old as of December 31',1997, was 940 ACRs,

i

no_t 732 ACRs as stated in IR 50-336/96-09. The increase of 208 ACRS is based on a

licensee review of previously closed ACRs that they decided to reopen based on

incomplete closure documentation. At the end of the current inspection period (February

24,1997), there were 798 ACRs greater than 120 days old that have not been closed.

DEPARTMENT

ACRs OLDER

THAN 120 DAYS

Operations

56

Design Engineering

211

Technical Support (System Engineering)

254

Work Planning

28

Maintenance

55

_

l&C

42

Safety / Licensing

25

Other

127

TOTAL

798

c.

Conclusion

Although the backlog of 798 adverse condition reports (ACRs) that are greater than 120

days old indicates that timeliness for completing corrective actions continues to be a

,

>

15

concern, the reduction in this backlog of older ACRs from 940 to 798 since the last.

inspection period is a positive trend which reflects the licensee's increased level of effort in

this area. As discussed in NRC Inspection Report 50-336/96-04, timeliness and

effectiveness of corrective actions is an area in which the licensee must demonstrate

sustained improved performance.

U2 08

Miscellaneous Operations issues (92700)

08.1 (Closed) Violation 50-336/94-17-10: O_peration Outside System Desian Parameters

a.

inspection Scope

The sc-ope of this inspection included a review of Violation 50-336/94-17-10.

b.

Observations and Findinas

This violation involved the failure to correctly translate design basis temperature limits of

the service water (SW) and reactor building closed cooling water (RBCCW) 2ystems into

operating procedures. As a result, on May 24,1993, a reactor trip occurred when the SW

and RBCCW system temperature limits were exceeded during a main condenser thermal

j

backwashing evolution. This violation was previously reviewed in NRC Inspection Report

50-336/96-05 which concluded that the violation could not be closed because although

'

the specific procedures regarding thermal backweshing were adequately aabemd, the

corrective actions were too narrow in that they failed to address the possibility eat other

plant procedures did not insure operation was in accordance with the plant's oesign basis.

c.

Conclusion

Violation 50-336/94-17-10, which resulted from a 1993 unresolved item, reflects that the

failure to operate the plant in accordance with the design basis had been a longstanding

NRC concern. The licensee failure to address this type of concern eventually culminated in

their current extended shutdown and 10 CFR 50.54(f) effort which is intended to ensure

i

the plant is designed and operated in accordance with the licensing and design basis.

There are several outstanding violations including Escalated Enforcement items 50-336/96-

'

06-05 & 96-08-06 which also address plant operation that is inconsistent with the

licensing basis. Therefore, Violation 50-336/94-17-10 is being closed nql because

adequate corrective actions have been taken but because this concern is being addressed

and tracked by more recent items.

'

08.2 (Closed) LER 50-336/96-15, (Open) Unresolved item 50-336/96-01-04: Failure to

Enter Action Statement Reaardina the Number of Operable Nuclear instrument

Channels

a.

inspection Scooe

The scope of this inspection included a review of Licensee Event Report 50-336/96-15.

.

.

16

b.

Observations and Findinas

On March 12,1996, while the unit was shut down, the "B" train vital de bus was

inadvertently deenergized due to operator error. The resultant loss of various vital and non

vital power supplies overflowed the reactor building closed cooling water surge tank

through a failed open make-up valve, and challenged the operators to recover from this

complex event. The event was complicated by the fact that there was minimal procedural

guidance for operators to use to recover the bus. One train of shutdown cooling remained

in operation throughout the event and normal power was restored within four hours.

During the recovery, operators were required by procedure to deenergize bus VA-40, a

vital 120 Volt ac instrument panel which supplies channel "D" of the reactor protection

system (RPS). Operators were aware that a loss of RPS channel "D" would cause the

channel "D" wide range nuclear instrument to be inoperable. Prior to the loss of the "B"

train vital de bus, in an unrelated situation, channel "B" and "C" wide range nuclear

instruments had been declared inoperable. The action statement for Technical Specification (TS) 3.3.1.1 is applicable when less than two channels of wide range nuclear

instruments are operable. The action statement requires the immediate verification of

shutdown margin and at least once every 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> thereafter. The operators did not

~ recognize the need to erter the TS 3.3.1.1 limiting condition for operation when bus VA .

40 was deenergized.

LER 50-336/96-15 stated that a contributing cause for failing to enter the TS 3.3.1.1

action statement was that the shift was occupied with the restoration of the deenergized

dc bus and was considering the effects of deenergizing loads on plant operatico. The

licensee's corrective actions included training of operators to not only consider the effects

of their actions on plani operations, but they must also assess TS requirements, in

addition, operating procedures were changed to remind operators to determine if TSs are

affected when deenergizing an electrical bus.

c.

Conclusion

The failure of operators to enter the action statement for TS 3.3.1.1 when three channels

of wide range nuclear instrumentation were inoperable is considered a violation. This

licensee-identified and corrected violation is being treated as a Non-Cited Violation,

consistent with Section Vll.B.1 of the NRC Enforcement Policy. The primary concern

associated with tnis event was the fact that there was minimal procedural guidance

provided to operators to recover the loss of de bus. The licensee is in the process of

preparing 12 abnormal operating procedures for recovering various dc buses and

distribution panels. This concern is being tracked by Unresolved Item 50-336/96-01-04.

I

,

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17

U2.ll Maintenance

i

U2 M8

Miscellaneous Maintenance issues (92903)

M8.1 (Closed) Unresolved item 50-336/96-04-09: Troubleshootina Controls

'

i

a,

lnspection Scope

'

in April 1996, the NRC resident inspectors identified programmatic concerns regarding the

U

conduct of troubleshooting. The concerns centered around the practice of performing

" troubleshooting" under the guise of " investigating" to avoid implementing the

administrative requirements for the performance of troubleshooting that are contained in

procedure WC-1, " Work Control Process." This issue was unresolved pending licensee

changes to WC-1.

b.

Observations and Findinas

in July 1996, the licensee issued Attachment 5.2 to procedure WC-1. This attachment

provides guidelines to be used in conjunction with a work order when a formal

.

troubleshooting plan is not required by Attachment 5 of WC-1.

'

The inspector reviewed the instructions contained in WC-1 and reviewed several work

I

orders that performed troubleshooting since the issuance of the change to WC-1.

c.

Conclusions

The inspector found that Attachment 5.2 of WC-1 contains appropriate directions to

ensure that all troubleshooting work is documented, supervision is consulted prior to

.

performing repair or replacement of components and retest requirements are determined

following the completion of the troubleshooting. No problems were identified during the

review of the troubleshooting work orders. This item is closed.

I

M8.2 (Closed) Unresolved item 50-336/96-06-06: Hioh Pressure Safety Iniectiori Check

Valve Backflow Testino

a.

Insoection Scope (92903)

The inspectors identified that the licensee had unnecessarily relaxed the frequency of

backflow testing of high pressure safety injection system (HPSI) pump discharge check

valves. The licensee agreed to revise the surveillance procedure to perform quarterly

backflow testing. This issue was unresolved pending NRC review of the planned

procedure changes,

b.

Observations and Findinas

The licensee revised procedure SP 21136, " Safety injection and Containment Spray

System Valves Operational Readiness Test," to include quarterly backflow testing of the

HPSI pump discharge check valves.

,

. --

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18

i

c.

Conclusions

'

The NRC concluded that the licensee had appropriately resolved the check valve testing

concern in Revision 10 of procedure SP 21136 and the associated data forms. This item is

closed.

U2.lll Enaineerina

'

U2 E8

Miscellaneous Engineering issues

i

E8.1 LClosed) Unresolved item 50-336/95-07-06: Condensate Storaae Tank Siohon Break

a.

Inspection Scope (92903)

On February 10,1995, the licensee discovered that the condensate storage tank (CST)

level had dropped to approximately 30% due to a heat exchanger tube leak. At the time of

the event the plant was defueled and no minimum tank volume was require by the plant.

technical specifications. During an investigation of the inadvertent loss of CST inventory

the licensee discovered that a siphon break (a 1/2 inch hole) in the tank recirculation piping

was missing. This issue was unresolved pending further review of how the plant design

change process missed the removal of the siphon break,

b.

Observations and Findinas

Plant information Report (PIR) 2-95-174 documented the licensee's investigation of the

missing siphon break. The licensee's review concluded that the section of piping, in which

the siphon break was located, may have been removed and replaced during a modification

performed in 1992 to install a CST nitrogen blanketing system. The modification included

the addition of a stiffener beam on the internal tank wall that required the recirculation loop

suction piping to be modified to provide clearance for the beam.

The interference problem between the stiffener and the recirculation piping was not

identified during the initial modification design. When the problem was identified a design

change notice (DCN) was processed to provide details on how to modify the piping.

However, the drawing provided with this DCN did not depict the existence of the siphon

break hole.

The work description in the work order that modified the piping was to " fabricate and

installinternal piping to the CST per drawing #25203-13006 Sheet 44". Although only

the section of piping at the elevation of the stiffener beam was affected, the work order

did not preclude the replacement of the section of piping that contained the siphon break

hole, nor did the drawing provide the details necessary to drill the hole in the event the

piping was replaced.

The cause of the event appears to be inadequate attention to detail during the preparation

of the DCN and the associated drawing since other drawings (the system piping and

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instrumentation drawing and the original piping isometric drawing) showed the existence of

a siphon break hole.

The licensee briefed the design engineering staff on this event and the need to pay

particular attention to less obvious design attributes such as siphon breakers when

developing design changes. Also, since the time of this event, the licensee has

implemented programmatic improvements to the design control process to improve the

effectiveness of the process.

The inspector noted that the plant technical specifications require the maintenance of a

minimum volume of 150,000 gallons of water in the CST when in modes 1,2 or 3 and the

volume is verified every 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. These requirements reduce the possibility of a

significant, undetected loss of CST inventory when the plant is in operation.

c.

Conclusion

l

The inspector concluded that the licensee had taken appropriate actions to resolve this

issue. However, the inspector noted that the licensee evaluation could have been more

thorough in that the investigator did not review the associated work order until questioned

by the inspector. A review of the work order was necessary to determine if the event may

have been a result of poor work controls, which has been a problem in the past at this site.

This item is closed.

E8.2 LClosed) Unresolved item 50-336/95-11-03: 10 CFR 21 Reportability Review

a.

Inspection Scone (92903)

Following the licensee identification of several design problems that affected replacement

components of the engineered safeguards actuation system (ESAS) cabinets, the NRC

inspectors questioned if the findings had been reviewed for reportability under the

requirements of 10 CFR 21, " Reporting of Defects and Noncompliance." At the time of

the inspection in 1995, no formal review had been initiated and the issue was unresolved

pending further actions to be taken by NU, and NRC review of the licensee actions.

b.

Observations and Findinas

in June 1995, the licensee performed an assessment of the design problems experienced

with the ESAS system during the previous two refueling outages. The assessment

identified four significant design problems that were related to defects in the components

provided by the vendor. The four problems were assessed for reportability in engineering

evaluation M2-EV-97-0004, Revision 0, " Evaluation of URI 95-11-03, Reportability of

ESAS Design Deficiencies."

Three of the four issues had been reported to the NRC in Licensee Event Reports (LERs)

94-12-00, 95-18-00 and 95-21-00. The issue associated with LER 94-12-00 had also

been reported by the vendor ~(Eaton Corporation) in accordance 10 CFR 21. The fourth

issue was documented in ACR 00506 and the licensee had determined that the issue was

not reportable.

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The engineering evaluation notea that problems reported in an LER did not require

additional reporting in accordance with 10 CFR 21. The bases for an LER fulfilling the

{

licensee's reporting obligations under 10 CFR 21 is contained in 10 CFR 21.2(c).

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The inspector also noted in discussions with the licensee that the components that were

'the subject of LERs95-018 and 95-021 were designs that were unique to Millstone Unit 2.

c.

Conclusion

The inspector reviewed the licensee evaluation, LERs and ACR and found that the licensee

appropriately evaluated and reported the failures to the NRC. This item is closed.

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Reoort Details

Summary of Unit 3 Status

Unit 3 remained in cold shutdown (mode 5) status throughout the inspection period. The

licensee continued its implementation of the Millstone Unit 3 Recovery Plan and the

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configuration management program activities in support of the milestones leading to the

readiness for the unit restart. In accordance with commitments made to the NRC with

regard to corrective action progress and documentation of the completed work items, the

licensee provided the first set of corrective action completion packages for NRC review.

To date, the presentation of such packages to the NRC has been timely,. relative to the

scheduled workload. This documentation has also provided evidence of progress in the

resolution of open NRC inspection items, as well as an indication of the licensee efforts to

demonstrate corrective action program effectiveness. NRC review of the available closure

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packages will continue as an ongoing process, with the individual technical issues

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discussed, as appropriate, in the following report sections and in future NRC inspection

reports.

On January 22,1997, the appointment of Mr. M. H. Brothers, then the Unit 3 Director, to

the position of Vice President-Millstone Unit 3, was announced, in this new position, Mr.

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Brothers fills the role of Recovery Officer for the unit. On January 28,1997, Mr. Brothers

announced the appointment of Mr. G. D. Hicks, who had been serving on the Carolina

Power & Light Recovery Team for Unit 3, to the position of Unit 3 Director, in an acting

capacity. Both of these managerial changes became effective on February 3,1997. The

inspector noted that Mr. Hicks' qualifications to assume the Unit 3 Director position had

been reviewed by both the licensing department and the Nuclear Safety & Oversight

organization. -The inspector also reviewed section 6.3.1 of the unit technical specifications

and American National Standard, ANSI N18.1-1971, regarding " Plant Managers" and -

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identified no qualification concerns or other questions regarding these licensee

management changes.

U3.1 ODer8tions

U3 01

Conduct of Operations

01.1 General Comments (71707)

Using inspection Procedure 71707, the inspectors conducted frequent reviews of ongoing

plant operations. During a walkdown of the Unit 3 intake structure, the inspector observed

large scale painting and materialimprovement work in progress. Various degrees of work

activity have been on-going in the intake structure since the licensee instituted a material

condition improvement project in the Spring of 1996. The inspector noted that adverse

condition report M3-97-0370, dated February 1,1997, was written to report that station

air and instrument air supply piping in the intake structure was in poor extemal condition.

The licensee is planning to replace or paint the piping. In general, the conduct of

operations was professional and safety-conscious; specific events and noteworthy

i

observations are detailed in the sections below.

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< Over the course of this inspection, the inspectors witnessed and/or reviewed a number of

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,. operational activities, and noted the following observations and assessments of operations

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performance:

Good contingency planning (e.g., preparation for field flashing the "B" emergency _

f

diesel generator during the Battery 2 outage) was in evidence.

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Appropriate regulatory provisions (e.g', a technical specification [TS] " bases"

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change to allow operation of the safety injection pumps in mode 5 to fill an

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accumulator) were considered and dispositioned to address emergent operational

conditions.

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Consideration of how the incore flux mapping results affect the quadrant power tilt

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ratio (OPTR) was found to be consistent with both the TS definition for QPTR and

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the Westinghouse position statement on " core tilt".

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Evaluation of the calibration provisions for the range and accuracy of digital

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instrumentation utilized in the performance of operational surveillances was

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determined to meet the NRC guidance discussed.in NUREG-1482.

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Reductions in the range of reactor coolant system operating temperatures (i.e., T-

avg) to maintain margins relative to nil ductility transition (NDT) considerations were

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implemented consistent with both TS 3.4.10 and ASME Code requirements.

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The implementation of temporary modifications (e.g., a bypass-jumper for cross-

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tying trains in the auxiliary feedwater system flow paths) was determined to be

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conservative in providing additional heat sinks (i.e., two steam generators) for

mshutdown risk considerations.

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The licensee discovery of potential discrepancies in the personal qualification-

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statements (NRC Form 398) of certain Unit 3 licensed operators has been assessed

for immediate impact and determined to require further evaluation. (NOTE: See

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unresolved item associated with similar Unit 1 activities - Section U1.05.1 of this

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inspection report)

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Additionally, during control room inspections and reviews of TS limiting condition for

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operability (LCO) action statements, the inspector raised a question regarding the

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applicability of actions for single system / train inoperability when more than one system or

train is determined to be inoperable. Examples where the need for interpretation of the

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LCO actions might be appropriate for multiple system or component unavailability were

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identified in TS 3.7.7 and 3.7.1.2. The inspector also noted recent correspondence (i.e., a

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memorandum dated January 17,1997) from the Unit 3 licensing staff providing a

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clarification of TS terminology, e.g., how to interpret "at least once per 7 days". The

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inspector determined that the licensee needed to further develop its approach to

4'

promulgating such interpretive guidance. While no TS violations or technical concerns

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were evident in the areas of TS compliance questioned by the inspector, a standardized

method for disseminating Unit 3 policy in the interpretation of TS language and LCO

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actions appears prudent. The inspector discussed this issue with cognizant licensee

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personnel and intends to review this matter further as an inspector followup item. (IFl

423/97-01-06)

01.2 Control of Hiah Enerav Line Break (HELB) Doors

a.

Insoection Scooe (71707)

On several occasions during this inspection period the licensee identified that HELB doors

were open or not fully latched. These conditions were reported in accordance with 10 CFR 50.72 as a condition that could have prevented a safety system from functioning as

required. The inspector reviewed the licensee's corrective actions to assess the

effectiveness of the licensee's root cause determination and whether appropriate corrective

actions were identified and implemented to prevent recurrence of the adverse condition.

b.

Observations and Findinas

,

On January 10,1997, the licensee reported that the HELB door to the "A" train 4160 volt

switchgear room was open. The door had been opened to facilitate battery 301 A-1

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replacement. Within the next few days, four additional occurrences of an open or

improperly latched HELB door were identified, including one by the resident inspector. All

the doors had a HELB sign affixed on both sides of the door.

As a result of these incidents, a level "B" adverse condition report (ACR) was gererated

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and an event review team assembled. As an immediate corrective action, a work stand

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down was held within all departments and licensee management briefed employees on the

control of plant doors. During the next several days, several other ACRs regarding HELB

issues were generated; including doors not being appropriately labeled in the field or on

prints.

The licensee's root cause investigation detarmined that the cause of the events was a

failure to develop and implement a HELB door control program, which resulted in a lack of

understanding of the HELB requirements associated with the plant design basis. Corrective

actions included: develop a door control program, insert a door control training module in

general employee training, and simplify and label all HELB doors. Although not specifically

stated in the corrective action plan, the licensee indicated that door labels would specify

the number of turns required to latch the doors.

As part of the investigation, the licensee concluded that the HELB door issue was not a

reportable condition with the plant in modes 5 or 6. Final Safety Analysis Report, Section

3.6.1 states that a high energy system is a fluid system that operates during normal plant

operating conditions. Normal plant conditions are defined as startup, operation at power,

hot standby, or reactor cooldown to cold shutdown conditions. Therefore, those

conditions that were identified while in mode 5 were retracted. However, the licensee

concluded that the status of HELB doors should be considered in the shutdown risk

program since a rupture of the hot water heating line in the service building could result in

the loss of safety-related equipment located in the switchgear room, independent of the

plant mode.

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The inspector toured the plant and verified that HELB doors 'nere properly latched.

Applicable HELB doors were labeled to indicated the required number of turns to properly

latch the door. The inspector also verified that a training module was being developed for

inclusion in the general employee training. The other corrective actions are scheduled to

be complete prior to the unit entering mode 4.

c.

Conclusion

The licensee's root cause investigation and corrective action plan for control of HELB doors

were determined to be good. However, the requirement to label the required HELB doors

with a minimum number of turns to ensure prope- U.ching should have been included in

the ACR corrective action plan if it was deemed necessary to prevent recurrence.

U3 03

Operations Proceduies and Documentation

a.

Inspection Scope

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The purpose of this inspection was to determine the adequacy of the procedure upgrade

program (PUP) as it applies to Unit 3. The licensee started the PUP in 1992 to standardize

procedure format for all units on the site and to improve the technical adequacy of all

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procedures. The process was a third iteration of previous procedure improvement

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programs which were started in the late 1980's. This inspection was performed from

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August 1996 through February 24,1997.

The onsite inspection included interviews with the site PUP group, Unit 3 procedure

coordinators and procedure writers, station oversight group, station quality assurance, and

Unit 1 operations personnel. Documents reviewed included, but were not limited to,

document control (DC) procedures: DC-1, " Administration of Millstone Procedures and

Forms"; DC-2, " Developing and Revising Millstone Procedures and Forms"; DC-3,

" Verification and Validation of Millstone Procedures and Forms"; and a sample uf Unit 3

procedures which had already been upgraded. in addition, the inspector reviewed the

Millstone Unit 3 PUP self assessment of their Operations Department (conducted March-

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May,1996); Millstone Unit 1 PUP self assessment of their Operations Department

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(conducted May-June,1996); Station oversight audit conducted during September 1996;

and various procedure related adverse condition reports (ACRs).

Although the focus of this inspection was Unit 3, the Unit 1 self assessment was reviewed

and discussed with Unit 1 personnel who performed the assessment and the Unit 1

Operations Manager. The inspector considered its potential applicability to Unit 3.

b.

Observations and Findinas

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At the start of this inspection, there was a station wide Procedure Upgrade Group to

provide overall control of the program. This group developed and maintaineci the station

DC procedures for control of the program, the overall status of upgraded procedures,

coordinators for each Millstone Unit, and the hiring of contractors, as necessary, to write

the procedures. The actual upgrade of procedures was the responsibility of each

department within each unit. Since the licensee's reorganization in October 1996, the

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station PUP group has been decentralized. The group now controls the station

administrative procedures including the PUP DC procedures. It has no control of the

production of upgraded procedures. Despite the changes in PUP control, the quality and

quantity of upgraded procedures has depended on the individual technical departments in

each unit.

A review of the program as it applies to Unit 3 noted the following:

The program has been effective in standardizing procedure formats. The document

control procedures are lengthy and cumbersome to use, but appear to be

comprehensive. The quality of the upgraded procedures appears to depend on the

producers of the procedures and the adequacy of the performance verification and

validation (V&V) process rather than on any apparent process deficiency.

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The V&V process can be by table top review, procedure walkdowns, or by

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procedure performance. All three methods are used, but the table top review by a

technical peer is the most common form of validation for Operations and

Maintenance Department procedures. Instrument & Control procedure technicians

stated that when possible their V&V process consisted of procedure walkdowns. -

In general, management involvement in the upgrade process seems to be minimal.

Some department managers have more involvement than others. There is heavy

reliance on the procedure coordinators for each department. For example, the Unit

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3 operations manager authorized his procedure coordinator to act on his behalf for

procedure review and approval.

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The inspector noted that during the five years that the PUP has been in place, there

had been no Quality Assurance (QA) audits of the program itself. Unit 3 Operations

Department had performed a self assessment of the PUP process in May 1996, but

this assessment was fairly limited. As a result of this NRC inspection, the licensee

performed two further assessments of the PUP program as it relates to Unit 3.

An assessment of the verification and validation process by Nuclear Oversight for

Unit 3 was performed in September 1996. This assessment noted some

weaknesses and problems in the V&V process. Another assessment was performed

on the PUP program for Units 1,2 and 3, November 13-16,1996, by the Region

One Procedere Working Group. This group is composed of persons from other NRC

Region i nuclear utilities. This assessment also noted strengths and weaknesses.

Both assessments noted deficiencies in the PUP program but did not conclude that

the program was seriously flawed.

On February 19,1997, the licensee forwarded to the inspector three recent QA

audits and fourteen quality control surveillance activities performed in the last

quarter of 1996 and the first quarter of 1997. These audits and surveillance

indicated that procedures are routinely reviewed as part of that activity and, where

appropriate, procedure deficiencies are identified. Also forwarded were recent

adverse condition reports identifying procedure problems.

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As part of the PUP, the licensee developed the procedure basis document. The

Intent'of this document was to duplicate the procedure and to add blocks at certain

points to indicate the source or basis for key technical information such as the Final

~ Safety Analysis Report (FSAR), vendor. manual, technical specification, regulatory

commitments, etc. The Region One Procedure Working Group report considered the

basis document a strength, inspector's conversations with many plant personnel

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indicated that they had high expectations from this document.

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' The inspector reviewed numerous basis documents during the course of this

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inspection. While the basis document concept generally appears to be a strength,

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the inspector noted numerous basis documents to be incomplete. The documents

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were essentially the procedure with one or two basis blocks added in a pro forma

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matter. Documents referenced in both the procedure and basis document were not

further identified in the basis document as to where the referenced material actually

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applied. This appears to be's weakness in the practical usage of basis documents.

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The licensee does not, however,' use the basis document as a procedure for plant

operations.

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^The inspector did a review of some Unit 3 operations procedures with a Unit 3 staff

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engineer. Some minor technical (Hecrepancies were observed,' but were not

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considered by the inspector to be' safety significant. In some cases, the operations

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. engineer had difficulty in determining the source for specific information in certain

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procedures. For instance, the calculation for one instrument setpoint was only

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available in the desk drawer of an l&C engineer; and the source of the setpoint was

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not in the basis document. This was an example of one of several instances of

apparent configuration management control. However the configuration

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management problem has already been identified to the licensee and is being

addressed generically by the licensee.

As noted in previous NRC inspections, design basis discrepancies have been

identified at all three Millstone units. It is possible that some procedures may not

conform to the FSAR and other procedures may conform to FSAR conditions which

are contrary to the actual design basis. As a result of an NRC 10 CFR 50.54(f)

letter, the licensee is currently performing an extensive design basis review which in

turn will be independently verified. In a letter from the licensee dated July 22,

'1996, the licensee stated, in part, the following: "...As we believe was

communicated [to the NRC in a meeting conducted on April 30,1996], there was

no commitment to complete the PUP as a conditio 1 of restarting any of the

[ Millstone] units. As part of the Operational Readiness Plan for Millstone unit No. 3,

findings resulting from the 10 CFR 50.54(f) related work will be reviewed to

determine if any procedure modifications are required prior to restarting the unit.

This will be done independent of procedure upgrades completed via the PUP..."

The licensee's corrective action plan for any required " procedure modifications" will

be assessed in the future as part of the NRC restart assessment plan,

The inspector observed that Unit 3 Operations Department had established a 67

page handbook in order to implement the DC procedures for the PUP process. This

appeared to be an uncontrolled, unapproved and unofficial procedure. The licensee

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stated at the conclusion of the onsite inspection that this handbook would be made

into an officially controlled procedure. By telephone on February 26,1997, the

inspector was informed that the operations handbook had been deleted and only the

DC procedures were being used by the Operations Department as guidance for the

PUP process.

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From January 13 through January 30,1997, the licensee's Nuclear Oversight

Group conducted an audit in the areas of document control and the maintenance of

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quality records. This audit identified a site-wide breakdown in the control of

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procedures in that procedures in use had not been properly updated. The

operations handbook (now deleted) was an example of an uncontrolled procedure in

use. Because of its magnitude, the adverse condition report (ACR) generated by

this audit was initially recommended for classification as a Level "A" ACR.

c.

Conclusions

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The procedure upgrade program meets regulatory requirements and has been effective in

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standardizing procedure formats across the site. The technical adequacy of upgraded

procedures, except for a small sample of Unit 3 operations procedures, was not a subject

for this inspection. Because of the number of individuals involved in procedure upgrade

and long period of time to upgrade the procedures (5 years), the quality of procedures

vary. A number of ACRs reviewed indicate technical problems with some procedures

already upgraded. The licensee has committed as part of their 10 CFR 50.54(f) process

and their Configuration Management Prograin to ensure procedures will meet the applicable

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design bases. The licensee's basis documents, as implemented, did not appear to meet

the licensee's own expectations as an adequate foundation for future procedure reviewers

to have an adoquate technical basis for the information contained in each procedure.

U3 O'

Quality Assurance in Operations

07.1 General Comments (40500,92901)

The inspector reviewed station procedures, assessed planned program changes, and

discussed various quality assurance activities with representatives from the Nuclear Safety

& Oversight (NS&O) organization and Unit 3 licensing, engineering and operations

departments. The following topics were generally reviewed and evaluated during the

conduct of this inspection:

corrective action program changes (Revision 4 to the station procedure, RP-4,

addressing " Corrective Action", effective February 25,1997)

job rcAation between the Unit 3 line departments and the NS&O organization

engineering assurance recovery activities, conducted by the NS&O organization, to

include planning and preparation for an Integrated Assessment Plan imp!ementation

and review of the proposed changes to the Design Basis Document Package

upgrade program

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issuance of a " Millstone 3 Line/ Oversight Interface Agreement"

implementation of and subsequent release from a Quality and Assessment Services

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(QAS) " Hold" of all work on safety-related eqaipment requiring the use of "non-QA"

parts

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With the progress of the noted program revisions, recovery activities, and organizational

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initiatives still ongoing, the impact and effectiveness of the changes have not yet provided

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measurable results. As of the end of this inspection period, the inspector observed

increased NS&O involvement in performance monitoring, interfacing analysis, and support

of the Unit 3 rnanagement and line staffs. Such involvement has included "real time"

evaluation and feedback on routine operational activities and nonroutine' events. NRC

assessment of NS&O effectiveness (including an expectation of demonstrable results of the

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corrective action program improvements) and specific QAS activities (e.g., Hold 97-1,

Revision 1) will continue over the course of the next severalinspection periods; covenng

the ongoing recovery, open item closure, and work associated with the startup planning for

the unit.

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U3.Il Maintenance

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USM1

Conduct of Maintenance

M 1.1 General Comments

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a.

Insoection Scoce (62707/61726)

The inspector observed / reviewed all or portions of the following maintenance and

surveillance activities to verify proper calibration of test instruments, use of approved.

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procedures, performance of work by qualified personnel, and conformance to technical

specification (TS) limiting conditions for operation.

M3-96-15203,

Battery 301 A-1 Removal

M3-96-25108,

Calibrate ITT Barton (SP 3481B01)

SP 3626.8,

" Control Building Air Conditioning Booster Pump,3SWP'P2A,

Operational Readiness Test"

The inspector found the work performed under these activities to be professional and

thorough. All activities observed were performed with the work package or surveillance

procedure present at the job site and personnel were noted to be closely following the

procedures. Review of the surveillance procedures revealed that the requirements of the

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applicable TS were appropriately incorporated into the implementing procedure,

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M1.2 Fix-It-Now (FIN) Conduct of Maintenance

a.

Inspection Scope (62707)

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The licensee has implemented a number of changes to the work control process including

the development of a FIN multi-discipline work team approach to augment the way

maintenance is performed at the unit. This process is in addition to their normal work

control process. The inspector reviewed the FIN maintenance procedure and monitored

work that was performed under the FIN process to assess its implementation.

b.

Observations and Findinas

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As part of the Unit 3 recovery process, the licensee developed a FIN work process to

reduce the time it takes to respond to operations department needs, and to perform work

more efficiently. In addition, a minor maintenance work process was developed to allow

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qualified personnel to accomplish tasks in a more efficient manner. It was envisioned that

these work processes would contribute to reducing the corrective maintenance backlog.

These work processes were initiated in November 1996.-

Maintenance procedure MP 3705B, "Fix It Now Conduct of Maintenance," states that the

FIN work process shall not be implemented for work requiring: major plant modifications,

lengthy tag clearances, special radiological work permits that cannot be dispositioned by

the health physics (HP) team member, or repairs involving welding on specified plant

equipment. The minor maintenance procedure U3 WC 1.1, " Minor Maintenance Process

"

Controls," allows work to be performed without the generation of a work order if the work

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is performed on non-QA equipment and the work doesn't impact plant operations or require

special work control needs.

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The FIN team is comprised of mechanics, electricians, maintenance planners, and

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instrument and control (l&C) technicians. In addition, there is a representative from the HP

and operations department, and an assigned first line supervisor (FLS). The inspector

reviewed the training records for each FIN team member and verified that they were trained

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on the new procedure. In addition, team members appeared to be well qualified. At least

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one member of the team was qualified for each of the matrices job tasks.

Each morning the FIN team members review all the trouble reports (TRs) that were

generated the previous day and determine which items can be performed by the team and

which need to go through the normal maintenance process. At the 6:45 a.m. morning

meeting, the FIN team FLS notifies the operations shift manager and the work planning

organization of the selected work items to ensure that these departments are cognizant of

all FIN planned maintenance activities.

The inspector attended the FIN and the 6:45 a.m. morning meeting. In addition to the off-

going and on-coming shift managers, individuals at the 6:45 a.m. morning meeting

included: the Unit Director, the operations, maintenance, l&C, and engineering department

managers, and representatives from work planning, chemistry, and HP. Each TR is

discussed then assigned to either the FIN or work planning department. Any TR that

potentially affects equipment operability is identified and an adverse condition report

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generated. The inspector noted that all work on the protected train was assigned to the

work planning department.

There have been approximately one hundred TRs generated each week during the month of

January 1997. Of these, the FIN team completed approximately fifty-five percent. A

review of the TR backlog, those over one week old, revealed that the number has been

declining. The inspector monitored selected activities and reviewed those work items that

were performed by the FIN team for the month of January. A review of the work activities

revealed that work orders had been generated for all safety-related work activities in

accordance with procedure U3 WC 1.1. As a result of the high number of TRs being

generated and the minor maintenance work activities performed, the FIN team has been

unable to work off any corrective maintenance backlog items.

c.

Conclusions

The licensee is implementing the FIN work process in a conservative manner. Any work on

the protected train equipment is not being assigned to the FIN team. All monitored work

activities performed by the FIN team was performed in accordance with the unit and

station procedures. FIN team members appeared to be well qualified. No safety concerns

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were identified from the specific activities observed.

U3 M8

Miscellaneous Maintenance issues

M8.1 Plant Insoection-Tours (62707. 92902)

The inspectors conducted inspection-tours of several areas of the plant during this

inspection period, observing work in progress and raising some questions regarding

completed field installations. As appropriate, discussions were held with workers, field

supervisors, and support personnel (e.g., health physics technicians). While most field

observations and questions were resolved prior to completion of the inspection-tours, the

following issues required followup, as documented below:

snubber removal on a residual heat removal (RHS) line in the engineered safety

features building; authorized by plant design change record (PDCR) MP3-90-003.

The inspector reviewed the applicable PDCR and design change notice DM3-P-154-

90, verifying proper re-analysis of the RHS piping system and control of the snubber

elimination list. Since design criteria discussed in ASME Code Case N-411 were

used in the pipe stress re-verification, the inspector reviewed the related discussion

of seismic design response spectra, provided on NRC Regulatory Guides 1.60 and

1.61, in the final safety analysis report (FSAR); and confirmed NRC approval for the

use of ASME Code Case N-411 at Unit 3.

white " frothing" of oil observed in the site glass for the speed increaser on the "B"

charging (CHS) pump, located in the auxiliary building.

The inspector discussed this observation with the responsible system engineer, who

confirmed that the subject " frothing" was likely due to the turbulence caused by the

.

.

31

meshing of gears in the CHS pump speed increaser. The inspector reviewed the

results of the most recent chemical analysis performed on this pump and identified

no adverse conditions or additional concerns.

treatment of reactor plant sampling (SSR) tubing runs and flexible hose connections

inside the containment building as ASME class 2 components, as discussed in the

Unit 3 FSAR.

.

The inspector reviewed the fabrication installation control drawings for the SSR

piping and common header connections from the containment penetrations to the

i

steam generator blowdown lir.es (i.e, a review of approximately 60 Stone &

Webster Engineering Corporation isometric drawings); and confirmed proper ASME

j

Code classification of the subject sample lines.

1

an unrestrained trolley assembly, located on a structural beam at the lower elevation

j

(-24'6") of the containment building, in proximity to some safety-related trisodium

1

phosphate baskets.

Inspector followup of the status of this assembly revealed that the trolley had been

installed as a temporary component during the first refueling outage in 1987, but

never removed. The licensee removed the unauthorized trolley and issued an

adverse condition report (ACR) M3-97-0563, documenting the concern that current

procedural controls for " incomplete work" were not being followed. Subsequently

(note: after the conclusion of this inspection report period), the licensee issued

another Condition Report (CR) M3-97-0850, documenting inadequate corrective

action implementation relative to a licensee event report, LER 3-96-003, involving

unauthorized temporary I-beams over safety-related equipment.

CR M3-97-0850 also documented current licensee findings of heavy, unrestrained

tools and chain falls located in proximity to safety-related equipment. Based upon

the discovery of the unrestrained trolley assembly, as well as the more recent

licensee-identified issues of CR M3-97-0850, the inspector determined that

additional licensee management attention to such " seismic II/l" concerns would be

prudent. The Significant items List (SIL) enclosed with the NRC Restart Assessment

Plan for Millstone Unit 3 documents an item for " Resident Emphasis: Seismic II/l".

This issue, with emphasis upon the new problems documented above, will be

tracked as an inspector followup item (IFl 423/97-01-07) to evaluate both the

timeliness and adequacy of further corrective measures in this area.

Overall, the plant inspection-tours revealed improvements in Unit 3 areas of housekeeping,

material conditions, and work controls. With the exception of the problem with

unrestrained equipment, noted as an IFl above, the licensee provided adequate response to

the inspector questions and field observations and demonstrated continued progress in the

physical enhancements to the plant field conditions.

-

.

'

32

U3.lli Enaineerina

U3 E8

Miscellaneous Engineering issues

E8.1

IOnen) Unresolved item 50-423/96-01-08: Slave Relav/Overlan Test Deficiencies

a.

Inspection Scope (92903)

In 1993 the licensee identified slave relay and other testing deficiencies. As a result of

those findings, the unit director established an overlap testing task force to review the

adequacy of overlap testing for the reactor trip and engineered safeguard systems circuitry.

These reviews were completed in 1993 and the licensee later credited these reviews with

accomplishing the reviews requested in NRC Generic Letter 96-01, " Testing Of Safety-

Related Logic Circuits."

l

in 1996, the licensee performed a review of safety and non-safety related functions,' as '

described in the Final Safety Analysis Report (FSAR) and/or the Safety Evaluation Report

(SER) to determine if the functions were properly tested. The scope of that review

included systems that were considered to be accident mitigating or risk significant as

'

defined in the Maintenance Rule (10 CFR 50.65).

The inspector reviewed selected test procedures, elementary electrical and logic drawings,

Open item Reports (OIRs), ACRs and other documents associated with the testing review

efforts to assess the effectiveness of the reviews.

b.

Observations and Findinas

The licensee task force reviews performed in 1993 identified procedural deficiencies,

circuitry which required design changes, incorrect drawings and FSAR errors. Three LERs

were issued as a result of technical specification violations that occurred due to testing

deficiencies (LERs 3-93-005,-010,-017). In each case the affected circuit performed

satisfactorily when tested. The followup reviews of the FSAR and SER performed in 1996

identified a number of questions regarding testing adequacy and the licensee was

continuing to disposition the associated OIRs. The OIRs that had been dispositioned to

date had not identified logic testing deficiencies of the types discussed in GL 96-01.

The inspector performed an independent review of testing that was performed on reactor

protection and engineered safety features logic circuits to assess the adequacy of the test

procedures. These reviews included the steam generator low level reactor trip and

emergency feedwater pump start testing and portions of the emergency diesel generator

start, load shed and load sequencing testing. The inspector also reviewed several OIRs to

assess the significance of the issues and the adequacy of the licensee resolutions.

The inspector's review of the steam generator low level channel testing included the

following procedures:

SP 3444A01 (Rev. 04) - Steam Generator Water Level Channel Calibration

SP 3443A21 (Rev.10) - Protection Set Cabinet i Operational Test

_ _ . _ _ . _ _ _ _ _ _ . _ _ _ _ . _ _ . _ . _ _ _ _

. . _ _ .

. _ _ _ . . .

i

e

.

4

l

33

.

I

SP 3446B11_(Rev. 09) - Train A Solid State Protection System Operational Test

'

~ The review included testing of the circuitry from the steam generator level transmitters to

i

the output devices, the reactor trip breakers and the auxiliary feedwater pump controls.

The test procedures were thorough and no problems were identified, in addition to the

testing of the automatic reactor trip, the inspector also reviewed the testing of the manual

i

reactor trip push buttons that is performed in'accordance with test SP 3446F331, "SSPS

}

Refueling Tests". The inspector found_that the manual push buttons were properly tested

_

and ensured they would each independently open the reactor trip breakers on either the

shunt trip or undervoltage trip mechanism.

The inspector also reviewed test procedures and selected drawings associated.with the

i

emergency diesel generator starting, load shedding and load sequencing functions. The -

j

following procedures were included in this review:

- SP 3646.A.1 (Rev.12) - Emergency. Diesel Generator A Operability Test- -

')

)'

SP 3646A.5. (Rev. 05) - Offsite Power Transfer Operability Test

-*

i

SP 3646A.8 (Rev.14).- Slave Relay Testing' Train A

j

[

SP 3646A.12 (Rev. 07) - Emergency Diesel Generator A Lockout Test -

-

SP 3646A.15 (Rev.11) - Train A Loss of Power Test

I

1

'

~

SP 3646A'.17 (Rev. 09)- Train A ESF With LOP Test

  • .

SP 3646A.19 (Rev. 03) - SIS Transfer of DG From Test to Standby

  • -

SP 3646A.21 (Rev. 05) - DG Auto Start on ESF Signal

j

SP 3448E51 (Rev. 01) - Diesel Sequencer Train' A Actuation Timer Test

j

SP 31447MA (Rev. 01)- MP3 Bus 34C Loss of Power Channel Calibration

'

Although this review did not include 100% of the circuitry, the inspector identified the

d

following testing issues:

During the loss of power testing, the EDG receives a start signal from relay 27Y2 in

the bus undervoltage logic circuit. A set of contacts from a different relay in the

]

undervoltage logic feeds a loss of power signal to the emergency generator loading

.

sequencer (EGLS) resulting in an additional EDG start signal. The existing test

]

procedures were not adequate to properly verify the operation of the parallel

signals.

,

The bus undervoltage relays provide trip signals to the emergency bus tie breaker

j

and the feeder breaker from the reserve station' service transformer (RSST). The tie

<

breaker trip circuit contains _three parallel trip circuits and the testing does not verify

j

each path. The RSST breaker trip was not included in any of the surveillance test

j

procedures.

1

1

The EDG starting control has two circuits that are designed such that a start signal

to either circuit will result in the opening of both air start solenoid valves even if one

or more circuit component failures may have occurred. The current testing'does not

independently test the redundancy designed into the circuits.

J

. - _ _ _ . _ . . _ _ . . .

_

. -

_ . _ _,

_ . _ . _ . _ . _ - . _

_ _ _ - . . _ _ _ . . _.

. .

.

34

j

Procedure SP 3646A17 contains notes that state:

-

'

"If possible, the SW pump not tested in lead during SP 3646A.15 should be lead."

t

!

"The CCP pump not tested in SP 3646A.15 should be tested here: the other must.

4

!

be in " PULL-TO-LOCK.""

- "The CHS pump not tested in SP 3646A.15 should be tested here; the other pump

'

must be in " PULL-TO-LOCK.""

,

These notes are intended to ensure that all of the equipment is tested either in SP

3646A15 or SP 3646A17.' These notes are worded as to provide

recommendations, rather than requirements, and as such may not ensure that the

1

standby and swing pumps get tested as required by technical specifications.

' ' "

~ Based on these findings th'e' inspector questioned the adequacy of the previous overlap ' -

+

-testing. reviews that were credited with ensuring that test procedures are adequate to

ensure the technical specification test requirements are met. As a result, the licensee

A:

developed an action plan to address this concern. . The' planned actions included: . _ ..e

A review for overlap test issues of several circuits by comparing electrical

- *

schematic drawings and logic drawings against plant surveillance test pro:edures to

'

ensure that all portions of the logic circuitry, including the parallel logic, interlocks,

bypasses and inhibit circuits, are adequately covered in the surveillance procedures

"

to fulfill the TS requirements. These reviews were to include the loss of power

schemes (undervoltage and degraded voltage), one ESF actuation system, and one

4

reactor trip instrumentation functional unit.

The revision of the surveillance testing for the loss of power initiation logic to

'

adequately verify parallel logic.

The performance of a root cause analysis to determine the cause of missed contacts

to determine if the failure was a generic issue that applied to the overall effort of

- the overlap task force. Based on the findings of the root cause analysis any

additional corrective actions would be determined.

- Subsequent licensee reviews identified additional testing deficiencies. The licensee

performed a self-assessment of the Unit 3 response to Generic Letter 96-01 and concluded

that the response did not meet the requirements of the letter. This was based on the

above specific findings where actuation' contacts were not tested, a lack of auditable

documentation and a difference in philosophy between the 1993 overlap task force and the

requirements of the Generic Letter. This issue was documented in ACR M3-97-0529 and

additional corrective actions were being developed by the licensee at the end of this

inspection period.

,

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_ _ _ . _ _

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35

c.

Conclusion

,

":

- ' ~ The inspector found that the licensee had expended significant resources in the past to~

i

review the logic testing and had identified and corrected numerous deficiencies. The test'

procedures reviewed were generally thorough. However, as discussed above, some test

-

deficiencies continued to exist. The failure to ensure all contacts are operable could result

,

in significant undetected problems. For example, if the emergency bus tie and feeder

1

breakers failed to trip on an undervoltage signal, the EDG output circuit breaker would be

prevented from closing to' energize the bus to power necessary safety equipment. The

inspector also noted that a more thorough self-assessment would have been appropriate

,

prior to the licensee submission of a response to GL 96-01.

]

.

.

This item remains open pending NRC review of additional licensee corrective actions, and

)

the assessment'of the significance of any additional findings and the results of additional

tes:ing that is performed.

i

.

E8.2 (Closed - Part of SIL ltem 67) ACR M3-96-0621: Potential For Overloadina Station

Blackout (SBO) Diesel

a.

Insoection Scope (92903)

This ACR identified a concern that the station blackout (SBO) diesel generator could be

overloaded if a safety injection or containment depressurization signal occurred while the

-

SBO diesel was supplying power to an emergency bus.

-

~

b.

Observations and Findinas

-

. In the event of a loss of all ac power,-the SBO dieselis manually started in accordance .a

Y

with procedure ECA O.0, " Loss of All'AC Power." Prior to energizing the bus from the

SBO diesel, the procedure directs the operators to place the control switches for large

)

loads in the pull-to-lock position. This action blocks the automatic start of the loads.

Following the energization of the bus, the operator then manually starts loads needed to '-

cope with the station blackout condition,

i

c.

Conclusions

- The inspector reviewed the associated ACR, procedure and elementary electrical drawings

)

and concluded that the licensee had appropriately reviewed and dispositioned this ACR.

This item is closed, (representing partial closure of SIL ltem 67).

o

.

l

'

36

IV Plant Support

Millstone Units 1,2, and 3

R1

Radiological Protection and Chemistry Controls

a.

Inspection Scope (83750)

i

The inspector reviewed the licensee's radiation protection programs established at each

unit and for the site. A review of specific work performed, the programs for maintaining

occupational radiation exposures as low as is reasonably achievable, and tours of the

various radiologically controlled areas (RCAs) were conducted by the inspector.

b.

Observations and Findinas

Unit 1

i

i

The inspector toured portions of the reactor and liquid radwaste buildings as part of the

j

inspection at Unit 1. The inspector noted a significant decrease in the number and size of

posted contaminated areas in the unit, which was described to the inspector as part of.the

unit's clean-up policy. The inspector noted that while some work was being performed in

the reactor building at the time of this inspection, significant radiological work, especially in

the drywell and on the refueling floor had yet to commence. The inspector also toured the

Xenon / krypton building, which houses some of the off-gas treatment systems and delay

tanks. This structure and its component systems had undergone a significant

refurbishment during 1996. Two areas within the structure were appropriately posted and

controlled as high radiation areas. The upper level of the structure housed two glycol

chiller systems, one of which was still under refurbishment.

For 1997, the licensee had established a goal of not more than 399 person-rem. This goal

'

is based on completing significant work and having the unit ready for restart of operations

during 1997. As described in a previous NRC Inspection Report (50-245/96-09), the unit

has significantly increased the number of personnel assigned to perform work planning and

ALARA functions. Seven persons within the Radiation Protection Department are now

assigned to ALARA, and two technicians are on loan as work week managers. Each of the

ALARA personnel have been assigned specific work packages and/or work areas for

planning purposes, and are responsibla for coordination with engineering and the work

groups to ensure proper ALARA controls are incorporated into the work packages.

Additionally, an ALARA Committee has been established, which includes all department

managers.

On January 15,1997, the licensec identified, through its Adverse Condition Reporting

(ACR) process (ACR # M1-97-0094) that fan HVE-14, which exhausts portions of the

Radwaste Storage Building, was potentially an unmonitored release pathway, as the fan

was not connected to the main plant stack, and no radiological effluent monitoring

equipment was located with this fan. The inspector discussed this ACR with a licensee

representative during this inspection, and reviewed a reportability evaluation performed bt

the site Engineering Department which analyzed the significance of this ACR. The

inspector determined that the reportability determination was invalid in that the evaluation

~

1

4

37

erroneously addressed a building that was different from the Radwaste Storage Building.

Subsequent to this finding, the licensee wrote another ACR (ACR # M1-97-0282) to

document this error, and subsequently determined that a notification to the NRC was

required, which was made on February 6,1997. Failure to monitor effluents released to

the environment from the Radwaste Storage Building to demonstrate compliance with

applicable regulatory limits, including 10 CFR 20.1301, is a violation of 10 CFR 20.1302.

(VIO 245/97-01-08)

Unit 2

The inspector toured various portions of the Unit 2 RCA, including the Auxiliary and

Containment Buildings, as part of this inspection. In general, all areas were determined to

be in compliance with NRC requirements for radiological postings and control of radioactive

material. On February 5,1997, the inspector observed the removal and subsequent

transfer of two highly radioactive pieces of debris previously found in the reactor vessel. A

metal nut and a tie wrap, each reading in excess of 10 Roentgens per hour on contact,

were removed from a storage bucket that was being kept in the refueling cavity,

transferred to a lead pig, and moved from the Containment Building, through the Auxiliary

Building and outside the unit to a designated storage area. The inspector observed the pre-

job briefing, which included a discussion of engineering controls for the minimization of

personnel exposure, and the conduct of all work until the shield pig with the objects was

removed from the unit. This activity also involved significant coordination between the

unit operations department, the health physics department, the site security organization

"

and the self-directed work group. Due to the careful planning process used, total exposure

for this work was less than 25 millirem.

For 1997, the unit established a goal of not more than 182 person-rem. Since the last

specialist inspection (50-336/96-09), the unit had flooded up the refueling cavity and

successfully off-loaded the reactor fuel to the spent fuel pool. Significant strides in

improving the unit ALARA program have also been made. ALARA coordinators have been

identified in each of the major work departments within the unit, and the Unit ALARA

coordinator was in the process of developing a training program for them. A unit ALARA

program procedure was also drafted, however, it was not issued at the time of this

inspection. Discussions with the ALARA coordinator, Health Physics Manager and Unit

Directr,r indicated the intent to establish an ALARA Committee, to include the major

depa:tment heads and their ALARA coordinators.

The inspector interviewed the health physics manager, and reviewed the documentation

associated with three ACRs (M2-97-0086, M2-97-0091 and M2-97-0142) written to

identify improper entries to the RCA which occurred during a ten day period in January

1997. In two of the instances, workers entered the RCA without having signed in on a

RWP, and without having on an electronic docimeter, as directed by the unit radiation

protection staff. In the third instance, a fire watch entered the unit with an electronic

dosimeter that had not been properly turned on. When discovered through self-checking,

the fire watch remained in the RCA with the non-functioning electronic dosimeter unti!

completion of the fire watch round. Procedure RPM 5.22 requires radiation workers to

comply with written instructions, including RWPs, from the radiation protection staff.

Although the safety significance of each of these events is individ ally low, as each worker

'

.

1

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e

i

38

was wearing a thermoluminescent dosimeter (TLD) which is utilized to determine dose of

record, the number of events in such a short duration are of concern. Additionally, the fire

watch event may highlight a problem with the training given and the perception of the

workers performing this task relative to other plant requirements, such as radiological

j

safety. Both of these issues were discussed by the inspector with the unit Health Physics

Manager and Unit Director, and with the station Vice President - Work Services. Short-

)

term corrective actions taken by the licensee included posting a health physics technician

at the main RCA entrance to ensure that personnel entering the RCA were wearing a

functional electronic dosimeter. Long-term corrective actions were not identified, however,

at the time of this inspection. Failure to adhere to the licensee's radiation protection

program, specifically procedure RPM 5.22,is a violation of 10 CFR 20.1101. (VIO

336/97-01-09)

Unit 3

The inspector toured various portions of the Unit 3 RCA, including the containment and

auxiliary buildings. Since the last specialist inspection (50-423/96-07) a significant

reduction in the number of leaking valves was observed, based on the reduced number of

catch containments observed. The unit continues te have very low dose rates in most

i

,,

areas, and significant portions of the Containment rematri accessible as clean areas.

The inspector reviewed the licensee's ALARA program, including the 1997 ALARA goal of

not more than 170 person-rem. The unit focus in ALARA has been to improve the work

order process, to include having RWP and ALARA control information included in the work

-

orders, in addition, the licensee has begun to include detailed maps and pictures of areas

and systems to be worked in the work order package. This is the result of a significant

campaign completed in 1996 by the unit radiation protection staff to photograph over

30,000 components in the RCA.

Site Health Physics

The site health physics group is responsible for providing calibration and dosimetry

services, health physics engineering and health physics support to the units and to other

site-wide organizations. As part of this inspection, a review of certain activities was

i

coni:cted by the inspector.

l

The self-directed work group includes six health physics technicians whose primary focus

is to support the activities of the Waste Services Department. As previously noted in the

discussion on Unit 2, above, this group was involved in the transfer of two highly activated

pieces of material from the Unit 2 vessel to a storage location outside the unit. In addition,

the inspector also reviewed the performance of this group during a recently completed

waste transfer evolution.

As part of the Liquid Radwaste Remediation Project at Unit 1, waste concentrates spilled

inside the "A" Concentrator cubicle were removed in 1996. In addition to being

i

radioactive, this material also contained asbestos, and thus required specialized engineering

controls for handling, as required by the Occupational Safety and Health Administration

(OSHA). On January 24,1997, ten barrels of this material, each containing several

7

V

e

39

plastic-wrapped bags of the waste, were transferred to a processing liner, which ultimately

was to be solidified and buried as low-level radioactive waste. Due to OSHA requirements,

this transfer was conducted inside a tent-like structure erected around the liner by a team

'

of five specially trained contractors. Because of the OSHA requirements, the health

physics technicians from the self-directed work group could not enter the tent once work

began. Based upon interviews conducted by the inspector with all members of the

j

contractor work team, the contractor industrial hygienist, and the self directed work group

technicians, and a review of documentation associated with this activity (RWP, ALARA

review, pre-job briefing package, post-job review) the inspector determined that the work

i

was appropriately controlled in accordance with NRC regulations. While all five contractors

were contaminated on their person and/or clothing upon completion of the work, this was

'

not the result of a breakdown of radiological controls. None of the contaminations resulted

,

in a significant radiological exposure.

'

c.

Conclusions

Unit 1

Noticeable reductions in the amount of contaminated spaces within the unit were

observed. ALARA planning and staffing of the ALARA group have significantly improved,

however, the effectiveness of this cannot be determined until more radiologically

significant work commences. One violation of NRC requirement involving an unmonitored

release path was identified.

Unit 2

Good work planning and control was observed for the transfer of highly irradiated materials

j

from the reactor vessel. Significant changes in the planning and control of radiological ,

work is under development. A violation of NRC requirements involving poor radiological

worker practices was identified. While short-term corrective actions were implemented by

the licensee at the time of this inspection, long-term actions had not yet been identified.

Unit 3

Contamination control improvements, especially the reduction in the number and need for

catch containments, was observed during tours of the RCA. Incorporation of RWP and

ALARA information into the work orders was an improvement, although the effectiveness

of this will have to be evaluated once significant radiological work resumes.

Site Health Physics

Appropriate support to Unit 2 was observed during the transfer of highly irradiated

material. Appropriate work controls were implemented during the transfer of asbestos

contaminated concentrates wastes.

$

40

R8

Miscellaneous Radiological Protection and Chemistry Issues

A recent discovery of a licensee operating their facility in a manner contrary to the Updated

Final Safety Analysis Report (UFSAR) description highlighted the need for a special focused

review that compares plant practices, procedures and/or parameters to the UFSAR

descriptions.

While performing the inspections discussed in this report, the inspector reviewed the

applicable portions of the UFSAR that related to the areas inspected. The inspector

verified that the UFSAR wording was consistent with the observed plant practices,

procedures and/or parameters, except in the area of the management organization and

responsibilities for radiation protection. Section 12.5 of the Unit 1 UFSAR and Section

11.2.3 of the Unit 2 UFSAR make reference to Section 12.5.1 of the Unit 3 UFSAR for a

full description of the health physics organization and reporting functions. This description

no longer is accurate due to the restructuring and unitization of the Radiation Protection

Program. The Work Services organization recognized the need to update the Unit 3 UFSAR

to reflect the management changes and identified it to the Site Licensing Director by

memorandum, dated November 29,1996.

V. Manaaement Meetinas

X1

Exit Meeting Summary

The inspectors presented the inspection results to members of licensee management at the

conclusion of the inspectian. The licensee acknowledged the findings presented.

X1.2 Final Safety Analysis Report Review

A recent discovery of a licensee operating their facility in a manner contrary to the final

safety analysis report (FSAR) description highlighted the need for additional verification

that licensees were complying with FSAR commitments. All reactor inspections will

provide additional attention to FSAR commitments and their incorporation into plant

practices, procedures and parameters.

While performing the inspections which are discussed in this report the inspectors

reviewed the applicable portions of the FSAR that related to the areas inspected.

inconsistencies were noted between the wording of the FSAR and the plant practices,

procedures and/or parameters observed by the inspectors, as documented in Sections

U3.E8.1 and R8.

<

, _ _-__

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41

INSPECTION PROCEDURES USED

~

IP 37550:

Engineering

IP 37551:

Onsite Engineering

,

1

IP 40500:

Licensee Self-Assessments Related to Safety issues inspections

]

IP 61726:

Surveillance Observations

i

l

IP 62707:

Maintenance Observations

1'

l

IP 71707:

Plant Operations

IP 71750:

Plant Support Activities

j

IP 83750:

Occupational Radiation Exposure

'

IP 92700:

Onsite follow-up of Written reports of Nonroutine Events at Power Reactor .,

Facilities

,

i

IP 92901:

Follow-up Operations

IP 92902:

Follow-up Maintenance

IP 92903:

Follow-up Engineering

.

.

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42

ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

URI 50-245/97 01-01

U 1.02.1

Spent Fuel Pool Cleanliness

I

URI 50-245/97-01-02

U 1.03.1

Operations Procedure Adequacy

1

URI 50 245,336,423/

U 1.05.1

Inaccurate Personal Qualification Statements

97-01-03

URI 50-245/97-01-04

U 1.E1.1

Resolution of A-46 Program Outliers

URI 50-245/97-01-05 -

U1.E2.2

Low Flow Operation of Containment isolation Check

i

Valve 1-CU-29

l

NCV

U2.08.2

Failure to Enter TS Action for inoperable Nis

IFl 50-423/97-01-06

U3.01.1

Interpretation of TS Language and LCO Actions

IFl 50-423/97-01-07

U3.M 8.1

Seismic 11/1 Concerns

VIO 50-245/97-01-08

R1

Failure to Monitor Gaseous Effluents from the

i

Radwaste Storage Building

VIO 50-336/97-01-09

R1

Entering RCA w/o Electronic Dosimeter or Signing

RWP

Closed

LER 50-245/96-03

U 1.E1.1

LER 50-336/96-15

U2.02.2

VIO 50-336/94-17-10

U2.08.1

Operation Outside Systtim Design Parameters

'

URI 50-336/96-04-09

U 2.M8.1

Troubleshooting Controls

URI 50-336/96-06-06

U2.M8.2 High Pressure Safety injection Check Valve Backflow

Testing

j

URI 50 336/95-07-06

U2.E8.1,

Condensate Storage Tank Siphon Break

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URI 50-336/95-11-03

U2.E8.2

10 CFR 21 Reportability Review

Discussed

VIO 50-245/95-42-01

U 1.08.1

Failure to Prevent Work Which had the Potential for

Draining the Reactor Vessel

URI 50-336/96-01-04

U2.02.2

Loss of DC Bus Event

URI 50-423/96-01-08

U3.E8.1

Slave Relay / Overlap Test Deficiencies

Sianificant items List

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Unit 3 SIL #67

Partial Closure

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LIST OF ACRONYMS USED

ACR(s)

adverse condition report (s)

AISC

American Institute of Steel Construction

ALARA

as low as reasonably achievable

ANSI /ANS

American National Standards Institute /American Nuclear

ASME

American Society of Mechanical Engineers

CCP

reactor plant component cooling

CES/NTE

component engineering services / nondestructive test engineering

CFR

Code of Federal Regulations

CHS

charging system

CR(s)

condition report (s)

DCN

design change notice

DG

diesel generator

EDG

emergency diesel generator

EGLS

emergency generator loading sequence

ESAS

engineered safeguards actuation system

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ESF

engineered safety feature

FIN

Fix-It-Now

FLS

first line supervisor

FME

foreign material exclusion

GIP (s)

generic implementation procedure (s)

GL

Generic Letter

gpm

gallons per minute

HELB

high energy line break

HPSI

high pressure safety injection

ICAVP

Independent Corrective Action Verification Program

IFl

inspector follow item

IR(s)

inspection Reports (s)

LCO

limiting condition for operation

LER(s)

licensee event report (s)

M&TE

material & test equipment

NDT

nil ductility transition

NRC

Nuclear Regulatory Commission

NRR

Nuchar Reactor Regulation

NSIC

Nut.,ar Safety Information Center

NS&O

nuclear safety and oversight

NUREG

Nuclear Regulation

.OCA

Office of. Congressional Affairs

OIR(s)

open item report (s)

OJT

on the job training

. OSHA

Occupational Safety & Health Administration

PAO

Public Affairs Office

PDCR

plant design change record

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PDR

Public Document Room

PiR(s)

plant information report (s)

PUP

procedure upgrade program

QA

quality assurance

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QAS

- Quality and Assessment Services

OPTR

quadrant power ti!! ratio

RBCCW

reactor building closed cooling water

RCA

radiologically controlled area

RFO

refueling outage

RHS

residual heat removal

RI

Region I

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RPS

reaction protection system

RSST

reserve station service transformer

RWCU

reactor water cleanup

RWP(s)

radiation work permit (s)

SBO

station blackout

SER(s)

safety evaluation report (s)

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SPO

Special Projects Office

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SQUG

seismic qualification utility group

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SSER

supplementel safety evaluation report

SSR

reactor plant samples

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TBSCCW

turbine building secondary closed cooling water

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TLD(s)

thermoluminescent dosimeter (s)

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TR(s)

trouble report (s)

TS(s)

technical specification (s)

UFSAR

updated final safety analysis report

USl

unresolved safety issue

VIO

violation

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WC

work control

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