ML18194A413: Difference between revisions
StriderTol (talk | contribs) (Created page by program invented by StriderTol) |
StriderTol (talk | contribs) (Created page by program invented by StriderTol) |
||
| Line 17: | Line 17: | ||
=Text= | =Text= | ||
{{#Wiki_filter:July 18, 2018 | |||
Mr. William F. Maguire, Site Vice President | |||
Entergy Operations, Inc. | |||
River Bend Station | |||
5485 U.S. Highway 61N | |||
St. Francisville, LA 70775 | |||
SUBJECT: RIVER BEND STATION - NRC BASELINE INSPECTION REPORT | |||
05000458/2018012 | |||
Dear Mr. Maguire: | |||
On July 16, 2018, the U.S. Nuclear Regulatory Commission (NRC) completed a baseline | |||
inspection at your River Bend Station, Unit 1. On May 31 and July 16, 2018, the NRC | |||
inspection team discussed the results of this inspection with you and other members of your | |||
staff. The results of this inspection are documented in the enclosed report. | |||
NRC inspectors documented five findings of very low safety significance (Green) in this report. | |||
Four of these findings involved violations of NRC requirements. Additionally, NRC inspectors | |||
documented two violations that were determined to be Severity Level IV under the traditional | |||
enforcement process. The NRC is treating these violations as non-cited violations (NCVs) | |||
consistent with Section 2.3.2.a of the NRC Enforcement Policy. | |||
If you contest the violations or significance of these NCVs, you should provide a response within | |||
30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear | |||
Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with | |||
copies to the Regional Administrator, Region IV; the Director, Office of Enforcement; and the | |||
NRC resident inspector at the River Bend Station. | |||
If you disagree with a cross-cutting aspect assignment in this report, you should provide a | |||
response within 30 days of the date of this inspection report, with the basis for your | |||
disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, | |||
Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; and the | |||
NRC resident inspector at the River Bend Station. | |||
W. Maguire 2 | |||
This letter, its enclosure, and your response (if any) will be made available for public inspection | |||
and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document | |||
Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for | |||
Withholding. | |||
Sincerely, | |||
/RA/ | |||
Jason W. Kozal, Chief | |||
Project Branch C | |||
Division of Reactor Projects | |||
Docket No. 50-458 | |||
License No. NPF-47 | |||
Enclosure: | |||
Inspection Report 05000458/2018012 | |||
w/ Attachment: Documents Reviewed | |||
U.S. NUCLEAR REGULATORY COMMISSION | |||
Inspection Report | |||
Docket Number: 05000458 | |||
License Number: NPF-47 | |||
Report Number: 05000458/2018012 | |||
Enterprise Identifier: I-2018-012-0015 | |||
Licensee: Entergy Operations, Inc. | |||
Facility: River Bend Station | |||
Location: Saint Francisville, Louisiana | |||
Inspection Dates: February 1, 2018 to July 16, 2018. | |||
Inspectors: J. Sowa, Senior Resident Inspector | |||
J. Drake, Senior Reactor Inspector | |||
C. Young, Senior Project Engineer | |||
M. OBanion, Resident Inspector (Acting) | |||
B. Parks, Resident Inspector | |||
Approved By: J. Kozal, Chief, Branch C | |||
Division of Reactor Projects | |||
Enclosure | |||
SUMMARY | |||
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees | |||
performance by conducting a baseline inspection at River Bend Station in accordance with the | |||
Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for | |||
overseeing the safe operation of commercial nuclear power reactors. Refer to | |||
https://www.nrc.gov/reactors/operating/oversight.html for more information. Findings and | |||
violations being considered in the NRCs assessment are summarized in the tables below. | |||
List of Findings and Violations | |||
Failure to Identify and Correct a Broken Feedwater Chemistry Probe | |||
Cornerstone Significance Cross-cutting Report | |||
Aspect Section | |||
Barrier Green None 71152 - | |||
Integrity NCV 05000458/2018012-02 Problem | |||
Closed Identification | |||
and | |||
Resolution | |||
Two examples of a self-revealed non-cited violation (NCV) of 10 CFR Part 50, Appendix B, | |||
Criterion XVI, Corrective Action, were identified for the licensees failure to identify that a | |||
broken chemistry probe in the feedwater system had the potential to cause an adverse impact | |||
on plant safety, and promptly implement appropriate measures to address that condition. | |||
Failure to Provide Adequate Procedures for Post-Scram Recovery | |||
Cornerstone Significance Cross-cutting Report | |||
Aspect Section | |||
Mitigating Green None 71111.18 - | |||
Systems NCV 05000458/2018012-06 Plant | |||
Closed Modifications | |||
The inspectors reviewed a self-revealed, non-cited violation of Technical Specification 5.4.1.a for | |||
the licensees failure to establish, implement and maintain a procedure required by Regulatory | |||
Guide 1.33, Revision 2, Appendix A, dated February 1978. Specifically, Procedure OSP-0053, | |||
Emergency and Transient Response Support Procedure, Revision 22, which is required by | |||
Regulatory Guide 1.33, inappropriately directed operations personnel to establish feedwater flow | |||
to the reactor pressure vessel using the main feedwater regulating valve as part of the post- | |||
scram actions. This resulted in the main feedwater regulating valves being operated outside | |||
their design limits. This resulted in catastrophic failure of the main feedwater regulating valve | |||
variseals and subsequent damage to multiple fuel assemblies. | |||
2 | |||
Failure to Develop an Adequate Operational Decision-Making Issue for Compensatory Measures | |||
Related to a Degraded Condition of the Feedwater System Sparger Nozzles | |||
Cornerstone Significance Cross-cutting Report Section | |||
Aspect | |||
Mitigating Green [H.9] - 71111.15 - | |||
Systems NCV 05000458/2018012-05 Human Operability | |||
Closed | |||
Procedures | Procedures | ||
Number Title Revision | Number Title Revision | ||
AOP-0001 Reactor Scram 37 | |||
AOP-0024 Thermal Hydraulic Stability Controls 30, 31, & 32 | |||
EN-NF-102 Corporate Fuel Reliability 6 | |||
EN-OP-104 Operability Determination Process 14 | |||
EN-OP-111 Operational Decision Making Issue Process 15 | |||
EN-OP-117 Operations Assessments 4 | |||
EOP-0001 Emergency Operating Procedure - RPV Control 28 | |||
GOP-0001 Plant Startup 99 | |||
GOP-0002 Power Decrease/Plant Shutdown 78 | |||
GOP-0003 Scram Recovery 31 | |||
GOP-0004 Single Loop Operation 25 | |||
OE-100 Operating Experience Program 1 | |||
R-PL-012 Corrective Action Program 1 | |||
STP-000-0001 Daily Operating Logs 082 | |||
Work Order | |||
52599498 | |||
71153Follow-up of Events and Notices of Enforcement Discretion | |||
EN-NF-102 Corporate Fuel Reliability | |||
- RPV Control | |||
52599498 | |||
Procedures | Procedures | ||
Number Title Revision EN-OP-115 Conduct of Operations | Number Title Revision | ||
EN-OP-115 Conduct of Operations 23 | |||
GOP-0004 Single Loop Operation 23 | |||
-RBS-) 2018-03149 2018-03953 | Condition Reports (CR-RBS-) | ||
2018-03149 2018-03953 | |||
A-3 | |||
ML18194A413 | |||
SUNSI Review: ADAMS: Non-Publicly Available Non-Sensitive Keyword: | |||
By: CHY/RDR Yes No Publicly Available Sensitive NRC-002 | |||
OFFICE SRI:DRP/C RI:DRP/C SPE:DRP/C ARI:DRP/C C:DRS/EB2 D:DRP | |||
NAME JSowa BParks CYoung MOBanion JDrake AVegel | |||
SIGNATURE /RA/ /RA/ /RA/ /RA/ /RA/ /RA/ | |||
DATE 6/22/2018 6/21/2018 6/21/2018 6/25/2018 7/10/2018 7/18/18 | |||
OFFICE BC:DRP/C | |||
NAME JKozal | |||
SIGNATURE /RA/ | |||
DATE 7/18/18 | |||
}} | }} | ||
Revision as of 20:14, 20 October 2019
| ML18194A413 | |
| Person / Time | |
|---|---|
| Site: | River Bend |
| Issue date: | 07/18/2018 |
| From: | Jason Kozal NRC/RGN-IV/DRP/RPB-C |
| To: | Maguire W Entergy Operations |
| Kozal J | |
| References | |
| IR 2018012 | |
| Download: ML18194A413 (32) | |
See also: IR 05000458/2018012
Text
July 18, 2018
Mr. William F. Maguire, Site Vice President
Entergy Operations, Inc.
River Bend Station
5485 U.S. Highway 61N
St. Francisville, LA 70775
SUBJECT: RIVER BEND STATION - NRC BASELINE INSPECTION REPORT
Dear Mr. Maguire:
On July 16, 2018, the U.S. Nuclear Regulatory Commission (NRC) completed a baseline
inspection at your River Bend Station, Unit 1. On May 31 and July 16, 2018, the NRC
inspection team discussed the results of this inspection with you and other members of your
staff. The results of this inspection are documented in the enclosed report.
NRC inspectors documented five findings of very low safety significance (Green) in this report.
Four of these findings involved violations of NRC requirements. Additionally, NRC inspectors
documented two violations that were determined to be Severity Level IV under the traditional
enforcement process. The NRC is treating these violations as non-cited violations (NCVs)
consistent with Section 2.3.2.a of the NRC Enforcement Policy.
If you contest the violations or significance of these NCVs, you should provide a response within
30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear
Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with
copies to the Regional Administrator, Region IV; the Director, Office of Enforcement; and the
NRC resident inspector at the River Bend Station.
If you disagree with a cross-cutting aspect assignment in this report, you should provide a
response within 30 days of the date of this inspection report, with the basis for your
disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk,
Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; and the
NRC resident inspector at the River Bend Station.
W. Maguire 2
This letter, its enclosure, and your response (if any) will be made available for public inspection
and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document
Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for
Withholding.
Sincerely,
/RA/
Jason W. Kozal, Chief
Project Branch C
Division of Reactor Projects
Docket No. 50-458
License No. NPF-47
Enclosure:
Inspection Report 05000458/2018012
w/ Attachment: Documents Reviewed
U.S. NUCLEAR REGULATORY COMMISSION
Inspection Report
Docket Number: 05000458
License Number: NPF-47
Report Number: 05000458/2018012
Enterprise Identifier: I-2018-012-0015
Licensee: Entergy Operations, Inc.
Facility: River Bend Station
Location: Saint Francisville, Louisiana
Inspection Dates: February 1, 2018 to July 16, 2018.
Inspectors: J. Sowa, Senior Resident Inspector
J. Drake, Senior Reactor Inspector
C. Young, Senior Project Engineer
M. OBanion, Resident Inspector (Acting)
B. Parks, Resident Inspector
Approved By: J. Kozal, Chief, Branch C
Division of Reactor Projects
Enclosure
SUMMARY
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees
performance by conducting a baseline inspection at River Bend Station in accordance with the
Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for
overseeing the safe operation of commercial nuclear power reactors. Refer to
https://www.nrc.gov/reactors/operating/oversight.html for more information. Findings and
violations being considered in the NRCs assessment are summarized in the tables below.
List of Findings and Violations
Failure to Identify and Correct a Broken Feedwater Chemistry Probe
Cornerstone Significance Cross-cutting Report
Aspect Section
Barrier Green None 71152 -
Integrity NCV 05000458/2018012-02 Problem
Closed Identification
and
Resolution
Two examples of a self-revealed non-cited violation (NCV) of 10 CFR Part 50, Appendix B,
Criterion XVI, Corrective Action, were identified for the licensees failure to identify that a
broken chemistry probe in the feedwater system had the potential to cause an adverse impact
on plant safety, and promptly implement appropriate measures to address that condition.
Failure to Provide Adequate Procedures for Post-Scram Recovery
Cornerstone Significance Cross-cutting Report
Aspect Section
Mitigating Green None 71111.18 -
Systems NCV 05000458/2018012-06 Plant
Closed Modifications
The inspectors reviewed a self-revealed, non-cited violation of Technical Specification 5.4.1.a for
the licensees failure to establish, implement and maintain a procedure required by Regulatory
Guide 1.33, Revision 2, Appendix A, dated February 1978. Specifically, Procedure OSP-0053,
Emergency and Transient Response Support Procedure, Revision 22, which is required by
Regulatory Guide 1.33, inappropriately directed operations personnel to establish feedwater flow
to the reactor pressure vessel using the main feedwater regulating valve as part of the post-
scram actions. This resulted in the main feedwater regulating valves being operated outside
their design limits. This resulted in catastrophic failure of the main feedwater regulating valve
variseals and subsequent damage to multiple fuel assemblies.
2
Failure to Develop an Adequate Operational Decision-Making Issue for Compensatory Measures
Related to a Degraded Condition of the Feedwater System Sparger Nozzles
Cornerstone Significance Cross-cutting Report Section
Aspect
Mitigating Green [H.9] - 71111.15 -
Systems NCV 05000458/2018012-05 Human Operability
Closed Performance, Determinations
Training and
Functionality
Assessment
The inspectors identified a Green non-cited violation of 10 CFR Part 50, Appendix B, Criterion V,
Instructions, Procedures, and Drawings, for the failure to develop an adequate Operational
Decision-Making Issue (ODMI) document per Procedure EN-OP-111, Operational Decision-
Making Issue Process. Specifically, the licensee failed to develop an ODMI that provided
adequate guidance to the operators for safely operating the plant with degraded feedwater
sparger nozzles.
Failure to Establish Procedural Guidance for Determining Core Flow During Unanticipated
Single Loop Operations
Cornerstone Significance Cross-cutting Report
Aspect Section
Initiating Green [P.3] - 71153 -
Events NCV 05000458/2018012-03 Problem Follow-up of
Closed Identification Events and
and Notices of
Resolution, Enforcement
Resolution Discretion
The inspectors reviewed a self-revealed, non-cited violation of 10 CFR Part 50 Appendix B,
Criterion V, Instructions, Procedures, and Drawings, for the licensees failure to establish
appropriate instructions in the abnormal operating procedure for thermal hydraulic instabilities.
Specifically, the procedural step for determining core flow when in single loop operations at low
power did not provide appropriate instructions to operators. As a result, station personnel could
not conclusively determine core flow and inserted a manual reactor scram.
Failure to Perform 10 CFR 50.59 Evaluation for Main Feedwater System Sparger Nozzle
Damage
Cornerstone Significance Cross-cutting Report
Aspect Section
None SL-IV None 71111.18 -
NCV 05000458/2018012-07 Plant
Closed Modifications
The inspectors identified a Severity Level IV non-cited violation of 10 CFR 50.59, Changes,
Tests, and Experiments, for the licensees failure to provide a written safety evaluation for the
determination that operation with compensatory measures for damaged feedwater sparger
nozzles did not require a license amendment pursuant to 10 CFR 50.90, Application for
amendment of license, construction permit, or early site permit. Specifically, the licensee failed
to recognize that compensatory measures prohibiting operation in single loop conditions
required technical specification changes, and as such required prior NRC approval.
3
Failure to Conduct Adequate Transient Snap Shot Assessment Following Recirculation Pump
Trip
Cornerstone Significance Cross-cutting Report
Aspect Section
Initiating Green None 71152 -
Events FIN 05000458/2018012-01 Problem
Closed Identification
and
Resolution
The inspectors identified a finding for the licensees failure to adequately validate simulator
response during a transient snap shot assessment following an unexpected trip of reactor
recirculation pump A on December 19, 2012.
Failure to Submit a Licensee Event Report for a Manual Scram
Cornerstone Significance Cross-cutting Report
Aspect Section
None SL-IV None 71153 -
NCV 05000458/2018012-04 Follow-up of
Closed Events and
Notices of
Enforcement
Discretion
The inspectors identified a Severity Level IV non-cited violation of 10 CFR 50.73, Licensee
Event Report System, for the licensees failure to submit a required licensee event report (LER).
Specifically, on February 1, 2018, after an unexpected trip of the recirculation pump B, the
licensee initiated a manual scram of the reactor that was not part of a preplanned sequence and
failed to submit an LER within 60 days.
4
INSPECTION SCOPES
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in
effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with
their attached revision histories are located on the public website at http://www.nrc.gov/reading-
rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared
complete when the IP requirements most appropriate to the inspection activity were met
consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection
Program - Operations Phase. The inspectors reviewed selected procedures and records,
observed activities, and interviewed personnel to assess licensee performance and compliance
with Commission rules and regulations, license conditions, site procedures, and standards.
REACTOR SAFETY
71111.15Operability Determinations and Functionality Assessments (1 Sample)
The inspectors evaluated the following operability determinations and functionality
assessments:
(1) Review of Operational Decision-Making Issue (ODMI) associated with damaged
feedwater sparger on February 8, 2018
71111.18Plant Modifications (2 Samples)
The inspectors evaluated the following temporary or permanent modifications:
(1) OSP-0053, Emergency And Transient Response Support Procedure, following
decision to control reactor vessel level with main feedwater regulating valves during
post-scram operations
(2) Review of plant operation following modification to feedwater sparger nozzles 7 and 8
OTHER ACTIVITIES - BASELINE
71152Problem Identification and Resolution
Annual Follow-up of Selected Issues (3 Samples)
The inspectors reviewed the licensees implementation of its corrective action program
related to the following issues:
(1) Review of 1) simulator modelling of core parameters during a recirculation pump trip at
low power and 2) licensed operator training associated with single loop operations at low
power
(2) Actions to address a broken isokinetic chemistry sampling probe in the feedwater
system
(3) Actions to address fuel failures caused by debris material in the reactor vessel
5
71153Follow-up of Events and Notices of Enforcement Discretion
Personnel Performance (1 Sample)
(1) The inspectors evaluated operator response to the unexpected trip of the reactor
recirculation pump B on February 1, 2018.
INSPECTION RESULTS
Failure to Identify and Correct a Broken Feedwater System Chemistry Probe
Cornerstone Significance Cross-cutting Report
Aspect Section
Barrier Green None 71152 -
Integrity NCV 05000458/2018012-02 Problem
Closed Identification
and
Resolution
Two examples of a self-revealed Green finding and associated NCV of 10 CFR Part 50,
Appendix B, Criterion XVI, were identified for the licensees failure to identify that a broken
chemistry probe in the feedwater system had the potential to cause an adverse impact on
plant safety, and promptly implement appropriate measures to address that condition.
Description:
In 1999, the licensee initiated Condition Report CR-RBS-1999-1011 to document that an
isokinetic chemistry sample probe was found to be missing from its installed location in the
feedwater system, having broken off in the system. Following unsuccessful attempts to
locate and remove the missing probe, the licensee performed evaluation ER-99-0539 to
evaluate the potential impact of the missing probe on the continued operation and function of
feedwater system components. This evaluation concluded that the missing probe remaining
in the system would not present any hazard to any feedwater system components, and would
have no adverse effect on continued operation. This conclusion was based, in part, on a
calculation showing that feedwater flow would not have enough energy to levitate the probe
past a 20-foot vertical riser portion of the system, and therefore would not have the potential
to enter a feedwater sparger in the reactor vessel downstream of the vertical riser. Another
calculation showed that the impact energy of the loose probe on any feedwater components
would be negligible.
In March 2004, the NRC issued Information Notice (IN) 2004-06, Loss of Feedwater
Isokinetic Sampling Probes at Dresden Units 2 and 3 (ADAMS Accession No.
ML040711214). The IN discussed that broken probes had been discovered at five other
stations from 1990 to 2001, and further described the conditions discovered at Dresden
Nuclear Power Station (Dresden), Units 2 and 3. In 2003, three holes in a feedwater sparger
at Dresden Unit 2 were discovered, along with the missing feedwater probe in the sparger,
which had apparently caused the damage. Two probes were discovered to be in a feedwater
sparger in Dresden Unit 3, with no damage to the sparger having occurred yet. These
conditions demonstrated that not only could the probes be transported to the feedwater
spargers in the reactor vessel, but that they could potentially damage the spargers. The
licensees evaluation of this operating experience concluded that, since the broken probe at
River Bend had been replaced with a probe of a design not susceptible to the same failure,
no further action was needed. The licensee failed to address the potential impacts of the
adverse condition of the broken probe that remained loose in the feedwater system.
6
In 2011, the licensee documented an evaluation of a similar condition that had been
discovered at Brunswick Steam Electric Plant, Unit 2, where a feedwater sample probe was
discovered inside a feedwater sparger. The licensees evaluation of this operating
experience concluded that the current design (i.e. the probe that replaced the previous
broken probe) was not susceptible to this kind of failure. The licensee again failed to address
the impact of the previous broken probe that remained in the system, given that its potential
to be transported into a feedwater sparger in the reactor vessel had been shown.
In January 2018, the licensee discovered damage in the form of two holes in feedwater
sparger nozzles in the reactor vessel, with the broken probe protruding from one of the holes
in the direction of the other. The broken probe remaining in the feedwater system resulted in
potential adverse impacts on the reactor vessel wall due to impingement of feedwater flow
through the holes in the damaged sparger, as well as potential adverse impacts on the
integrity of fuel cladding due to the introduction of foreign material (pieces of the feedwater
sparger and chemistry probe) in the reactor vessel.
Corrective Actions: The broken probe was removed from the system. The licensee
performed evaluations to identify plant operational limitations to ensure that adverse impacts
to reactor pressure vessel wall integrity from additional holes in a feedwater sparger are
minimized. The licensee also issued an action to perform a review of historical loose parts
evaluations to add to tracking mechanisms and ensure adequacy of previous evaluations.
Corrective Action Reference: CR-RBS-2018-0294, CR-RBS-2018-0613, and
Performance Assessment:
Performance Deficiency: The licensees failure on two occasions to identify a broken
chemistry probe in the feedwater system had the potential to cause an adverse impact on
plant safety and to promptly implement appropriate measures to address that condition was a
performance deficiency.
Screening: The inspectors determined the performance deficiency was more than minor
because it was associated with the Cladding Performance, as well as the RCS Equipment
and Barrier Performance, attributes of the Barrier Integrity Cornerstone, and adversely
impacted the cornerstone objective to provide reasonable assurance that physical design
barriers (fuel cladding, reactor coolant system, and containment) protect the public from
radionuclide releases caused by accidents or events. Specifically, the unaddressed condition
of the broken probe remaining in the feedwater system resulted in damage to the feedwater
sparger, which resulted in thermal stresses to the reactor pressure vessel due to feedwater
impingement on the inner reactor pressure vessel wall, as well as the introduction of foreign
material inside the reactor vessel having the potential to result in damaged fuel. The licensee
performed an evaluation to determine what plant operational limitations were necessary in
order to ensure that additional thermal stresses on the reactor pressure vessel inner wall
remained below a threshold that would challenge the structural integrity of the vessel.
Significance: In accordance with Inspection Manual Chapter 0609, Appendix A, Section 5.0,
RCS boundary issues other than pressurized thermal shock are evaluated under the Initiating
Events Cornerstone. Using Inspection Manual Chapter 0609, Appendix A, The Significance
Determination Process for Findings At-Power, Exhibit 1, Initiating Events Screening
Questions, the finding was screened, as a potential loss of coolant accident (LOCA) initiator,
as having very low safety significance (Green) because, after a reasonable assessment of
7
degradation, the finding could not result in exceeding the RCS leak rate for a small LOCA and
could not have likely affected other systems used to mitigate a LOCA.
Cross-cutting Aspect: A cross-cutting aspect of P.5, Operating Experience, was determined
to be applicable to the performance deficiencies; however, no cross-cutting aspect was
assigned since the performance deficiencies occurred in 2004 and 2011, and are not
indicative of current licensee performance.
Enforcement:
Violation: Title 10 CFR Part 50, Appendix B, Criterion XVI, requires, in part, that measures
shall be established to assure that conditions adverse to quality, such as failures,
malfunctions, deficiencies, deviations, defective material and equipment, and
nonconformances are promptly identified and corrected. Contrary to the above, from
June 2004 to January 2018, the licensee failed to establish measures to assure that a
condition adverse to quality was promptly identified and corrected. Specifically, the licensee
failed to identify and correct a condition involving a broken sampling probe inside the
feedwater system. The uncorrected condition resulted in damage to a feedwater sparger,
with the potential to impact the available margin for integrity of the reactor vessel.
Disposition: This violation is being treated as a non-cited violation, consistent with
Section 2.3.2.a of the Enforcement Policy.
Failure to Provide Adequate Procedures for Post-Scram Recovery
Cornerstone Significance Cross-cutting Report
Aspect Section
Mitigating Green None 71111.18 -
Systems NCV 05000458/2018012-06 Plant
Closed Modifications
The inspectors reviewed a self-revealing, non-cited violation of Technical Specification 5.4.1.a
for the licensees failure to establish, implement and maintain a procedure required by
Regulatory Guide 1.33, Revision 2, Appendix A, dated February 1978. Specifically,
Procedure OSP-0053, Emergency and Transient Response Support Procedure,
Revision 22, which is required by Regulatory Guide 1.33, inappropriately directed operations
personnel to establish feedwater flow to the reactor pressure vessel using the main feedwater
regulating valve (MFRV) as part of the post-scram actions. This resulted in the MFRVs being
operated outside their design limits. This resulted in catastrophic failure of the MFRV
variseals and subsequent damage to multiple fuel assemblies.
Description:
In January 2015, the licensee revised Procedure OSP-0053, Emergency And Transient
Response Support Procedure, to use one of the three MFRVs to control reactor water level
following a scram event, and not use C33-LVF002, Start-Up FRV, which is designed to be
used for this application. This resulted in proceduralizing the use of a MFRV in circumstances
below the minimum controllable flow for the MFRV of 209,000 lbs/hr that the Main FRV
Copes Vulcan sizing datasheet provides as the a minimum controllable flow condition. As a
result of this change to the procedure to use a MFRV, the valves cycled numerous times in
the process of controlling level at low flow post-scram when feedwater flow demand was
below the MFRV minimum controllable flow volume. This repeated cycling of the valve led to
excessive open/close cycling of the MFRVs and caused the catastrophic failure of the
variseals.
8
As a result, foreign material parts of the variseal were introduced into the core. It is
suspected that this material resulted in six nuclear fuel cladding failures caused by debris
fretting.
Corrective Actions: The licensee revised Procedure OSP-0053, Emergency and Transient
Response Support Procedure, to control reactor vessel level post scram using a startup
feedwater regulating valve and modified the design of the MFRV variseal.
Corrective Action Reference: CR-RBS-2016-00893
Performance Assessment:
Performance Deficiency: The failure to establish adequate procedural guidance for operation
of the main feedwater system was a performance deficiency.
Screening: The performance deficiency was more than minor, and therefore a finding,
because it was associated with the procedure quality attribute of the Mitigating Systems
Cornerstone and adversely affected the cornerstone objective to ensure the availability,
reliability, and capability of systems that respond to initiating events to prevent undesirable
consequences. Specifically, Procedure OSP-0053, Emergency and Transient Response
Support Procedure, Revision 22, inappropriately directed operations personnel to establish
feedwater flow to the reactor pressure vessel using the MFRV as part of the post-scram
actions. This resulted in the MFRVs being operated outside their design limits.
Significance: The inspectors screened the finding in accordance with Inspection Manual
Chapter 0609, Appendix A, The Significance Determination Process for (SDP) for Findings
At-Power. Using Inspection Manual Chapter 0609, Appendix A, Exhibit 2, Mitigating
Systems Screening Questions, the inspectors determined this finding was of very low safety
significance (Green) because the finding: (1) was not a deficiency affecting the design or
qualification of a mitigating structure, system, or component, and did not result in a loss of
operability or functionality; (2) did not represent a loss of system and/or function; (3) did not
represent an actual loss of function of at least a single train for longer than its technical
specification allowed outage time, or two separate safety systems out-of-service for longer
than their technical specification allowed outage time; and (4) did not represent an actual loss
of function of one or more nontechnical specification trains of equipment designated as high
safety-significant in accordance with the licensees maintenance rule program.
Cross-cutting Aspect: No cross-cutting aspect was assigned since the performance
deficiency occurred in January 2015 and is not indicative of current licensee performance.
Enforcement:
Violation: Technical Specification 5.4.1.a requires in part, that written procedures shall be
established, implemented, and maintained covering the applicable procedures recommended
in Regulatory Guide 1.33, Revision 2, Appendix A, dated February 1978. Regulatory
Guide 1.33, Appendix A, Section 6.u., identifies procedures for responding to a reactor trip as
required procedures. Procedure OSP-0053, Attachment 16, Post Scram
Feedwater/Condensate Manipulations Below 5% Reactor Power, was a procedure
established by the licensee for responding to a reactor trip.
Contrary to the above, from January 30, 2015, until April 13, 2017, the licensee failed to
maintain adequate written procedures for responding to a reactor trip. Specifically,
Procedure OSP-0053 inappropriately directed operations personnel to establish feedwater
9
flow to the reactor pressure vessel using the MFRV as part of the post-scram actions. The
MFRV operator characteristics are not designed to operate at the low flow conditions
immediately following a reactor scram from high power. As a result, the MFRV variseals
degraded and resulted in damage to multiple fuel assemblies. Subsequent to the event, the
licensee changed the procedure, directing operations personnel to utilize one of the startup
feedwater regulating valves.
Disposition: This violation is being treated as an non-cited violation consistent with
Section 2.3.2.a of the NRC Enforcement Policy.
Failure to Develop an Adequate Operational Decision-Making Issue for Compensatory
Measures Related to a Degraded Condition of the Feedwater System Sparger Nozzles
Cornerstone Significance Cross-cutting Report Section
Aspect
Mitigating Green [H.9] - 71111.15 -
Systems NCV 05000458/2018012-05 Human Operability
Closed Performance, Determinations
Training and
Functionality
Assessments
The inspectors identified a Green non-cited violation of 10 CFR Part 50, Appendix B,
Criterion V, Instructions, Procedures, and Drawings, for the failure to develop an adequate
operational decision-making issue (ODMI) document per Procedure EN-OP-111, Operational
Decision-Making Issue Process. Specifically, the licensee failed to develop an ODMI that
provided adequate guidance to the operators for safely operating the plant with degraded
feedwater sparger nozzles.
Description:
During a reactor startup on February 1, 2018, reactor recirculation pump B unexpectedly
tripped during an attempted upshift to fast speed. As a result, the plant was operating with
recirculation pump A in fast speed and recirculation pump B not running. Prior to this startup,
during an outage that was being conducted to replace failed fuel assemblies, damage to
feedwater sparger nozzles was identified.
Example 1: The evaluation of the damaged feedwater sparger nozzles 7 and 8 on
sparger N4C identified that the damaged sections of the feedwater sparger nozzles had the
potential to adversely affect the vessel cladding by allowing relatively colder water to directly
flow into the relatively hotter vessel wall, thus inducing thermal fatigue. All components of the
reactor coolant system (RCS) are designed to withstand effects of cyclic loads due to system
pressure and temperature changes. These loads are introduced by startup (heatup) and
shutdown (cooldown) operations, power transients, and reactor trips. Limits are established
for pressure and temperature changes during RCS heatup and cooldown, such that plant
systems remain within the design assumptions and the stress limits for cyclic operation.
Limits on RCS pressure, temperature, heatup rate, and cooldown rate define allowable
operating regions and operating cycles to prevent nonductile failure of system components.
Because operation with the sparger nozzle damage was outside the limits originally analyzed,
the licensee requested General Electric-Hitachi (GEH) to provide an operability analysis of
the degraded condition. GEH Report 004N6557, Revision 0, dated January 26, 2018,
Operability Assessment of the River Bend Station Feedwater Sparger Assembly in the
January 2018 As-found Condition, stated, in part, this evaluation does not account for Final
10
Feedwater Temperature Reduction (FFWTR), Feedwater Heater Out-of-Service (FWH OOS)
conditions, nor Single Loop Operation (SLO) operating conditions. Based on this analysis,
the licensees engineering department concluded that the recommended classification of this
condition was OPERABLE-COMP MEAS (operable with compensatory measures), with the
degraded/nonconforming condition being the holes in the feedwater sparger nozzles. Based
on the results of this analysis, one of the operational restrictions/limitations stipulated in the
licensees ODMI was that, RBS will not operate in Single Loop Operation (SLO).
The ODMI developed by the licensee included two trigger points:
Trigger Point 1:
An unexpected operational state below approximately 85 percent power in which the vessel
wall-to-feedwater delta-T stabilizes at less than or equal to 154 degrees Fahrenheit (F), as
detected by periodic monitoring during normal operations, OR due to a transient as defined
above.
Trigger Point 2:
An unexpected operational state in which the vessel wall-to-feedwater delta-T stabilizes at
greater than 154 degrees F, as detected by periodic monitoring during normal operations, OR
due to a transient as defined above.
The ODMI failed to provide adequate guidance to the operators if they found themselves in
any of the conditions that GEH had listed as not being evaluated for continued operation with
the degraded condition. When reactor recirculation pump B failed to shift to fast speed at
9:46 a.m., the operators logged entry into Procedure GOP-004, Single Loop Operations.
The plant was in single loop operating conditions, and remained there until 10:57 a.m. when
the Mode switch was placed in shutdown. The ODMI failed to provide adequate guidance on
the actions required if the plant entered any of the conditions that were not evaluated for the
degraded sparger condition. In addition, the Just In Time Training given to the operators
prior to taking the watch to commence power operations with the degraded condition did not
address these issues either. As a result, rather than take prompt actions to place the plant in
a known safe condition upon entry into single loop operations, the control room supervisor
requested that GEH be contacted to determine if it was acceptable to remain in single loop
operations.
Example 2: The evaluation of the damaged feedwater sparger nozzles 7 and 8 on
sparger N4C identified that the damaged sections of the feedwater sparger nozzles had the
potential to adversely affect the B narrow range level instrument. The damage on feedwater
sparger N4C created unexpected feedwater flow paths in the reactor vessel during plant
operation that had the potential to adversely affect the "B" variable leg reactor water level
instruments. There were two potential impacts of this condition on indicated level from
narrow range level instruments that tap off of the B variable leg. Flow from the holes in the
feedwater sparger nozzle elbows could flow across the variable leg nozzle opening at AZ
200 degrees (B Leg), lowering the pressure on the variable leg side of the differential
pressure measurements, or the flow from the sparger nozzle damage could directly impact
the B variable leg, increasing the pressure on the variable leg side of the differential pressure
measurements.
11
The narrow range RPV level instrumentation supports two reactor water level trips: low level
(Level 3) and high level (Level 8). During a transient or accident event where the RPV water
level is changing, the trip signal from the B narrow range instrument could be affected.
Based on the GE report, during a transient or accident event where the RPV water level is
increasing, the high level (Level 8) trips (RPS trip and Feedwater Pump trip) in the affected
channel may occur later than the trips in the unaffected channels. This may delay the overall
Level 8 trips. For the Level 8 RPS trip, the margin between the calculated nominal trip
setpoint and the technical specification allowable value is 0.77 inches. For the Level 3 RPS
trip, the margin between the calculated nominal trip setpoint and the technical specification
allowable value is 0.67 inches. An operability determination of the narrow range level
instruments was performed under CR-RBS-2018-00633 CA-01.
The ODMI developed by the licensee included two trigger points:
Trigger Point 1:
Action: Refer to applicable SRs as specified by STP-000-0001, Att. 9.2
Step 30 in STP-000-0001 not within 4 inches
Step 71 in STP-000-0001 not within 6 inches
Notify the Duty Manager and the Ops Duty Manager
Trigger Point 2:
The magnitude of the B channel deviation is 1.5 inches in either direction from the average
of the A, C and D channel average + 1.1 inches.
Notify the Duty Manager and the Engineering Duty Manager.
The ODMI implemented by the licensee allowed level indication deviation in the affected
channel for the B21-LTN080 instruments to be monitored to ensure it remained within the
allowable margin to ensure the technical specification trip limit is not exceeded. It stated in
part that, If the deviation exceeds a change of 1.5 inches from historical deviation of
1.1 inches above the average of the A, C, and D channels in either an increasing or
decreasing direction, then condition will be evaluated by engineering. The monitored trigger
point of +1.5 inches will provide adequate margin for both the Level 3 and Level 8 trips.
However, if a 1.5-inch bias in the low direction would have been reached, two Technical
Specification (TS) Allowable Values could have been exceeded (by 0.5 inches for TS
Table 3.3.5.2-1, Function 2, Reactor Core Isolation Cooling System Instrumentation, and by
0.49 inches for TS Table 3.3.5.2-1, Function 5, Reactor Protection System Instrumentation).
The 1.5-inch bias in the low direction would have rendered the instrument inoperable based
on 10 CFR 50.36(c)(2)(i), which states, Limiting conditions for operation are the lowest
functional capability or performance levels of equipment required for safe operation of the
facility. Since the limiting conditions for operations (LCOs) include Allowable Values (e.g.,
LCO 3.3.5.2 includes Table 3.3.5.2-1 which has Allowable Values for Functions 2 and 5), the
Allowable Values are understood to be the lowest functional capability or performance levels
of equipment required for safe operation of the facility.
The licensees technical specifications provide the following guidance: Surveillance
Requirement 3.0.1, Failure to meet a Surveillance, whether such failure is experienced
during the performance of the Surveillance or between performances of the Surveillance,
shall be failure to meet the LCO.
12
1.1 Definitions: A CHANNEL CALIBRATION shall be the adjustment, as necessary, of the
channel output such that it responds within the necessary range and accuracy to known
values of the parameter that the channel monitors
In addition, the TS Bases state, SR 3.0.1 through SR 3.0.4 establish the general
requirements applicable to all Specifications and apply at all times, unless otherwise stated.
The OPERABILITY of the RPS (Reactor Protection System) is dependent on the
OPERABILITY of the individual instrumentation channel Functions specified in
Table 3.3.1.1-1. Each Function must have a required number of OPERABLE channels [2 per
RPS trip system for the vessel level function] per RPS trip system, with their setpoints within
the specified Allowable Value, where appropriate. The actual setpoint is calibrated consistent
with applicable setpoint methodology assumptions. Each channel must also respond within
its assumed response time. Allowable Values are specified for each RPS Function specified
in the Table. Nominal trip setpoints are specified in the setpoint calculations. The nominal
setpoints are selected to ensure that the actual setpoints do not exceed the Allowable Value
between successive channel calibrations. Operation with a trip setpoint less conservative
than the nominal trip setpoint, but within its Allowable Value, is acceptable. A channel is
inoperable if its actual trip setpoint is not within its required Allowable Value.
Process effects impact the establishment of the appropriate Nominal Trip Setpoint, which is
determined by addressing all instrument channel uncertainties (including biases) and
offsetting them from the Analytical Limit. The currently licensed Allowable Values are fixed
within the technical specification tables. Nominal Trip Setpoints are established on the basis
of a calculation that identifies all known uncertainties between the Analytical Limit and the
Nominal Trip Setpoint. If a new, unaccounted-for process effect bias in the nonconservative
direction is discovered, this effect needs to be reflected in the calculation of a new Nominal
Trip Setpoint and a corresponding new Allowable Value. However, in this case, the licensee
did not elect to pursue a license amendment or other process to change its currently licensed
Allowable Value, nor did it ask for a temporary enforcement discretion. Therefore, with the
new (unaccounted for) postulated process effect present, this has the effect of making the
existing Nominal Trip Setpoint (calibrated value) offset in the nonconservative direction by the
amount of the new postulated process effect (i.e., up to 1.5 inches), which reduces the margin
between the actual trip setpoint and the existing licensed Allowable Value.
Therefore, to meet the River Bend technical specification requirement that a channel be
considered inoperable if its actual trip setpoint is not within its required Allowable Value
without changing the currently licensed Allowable Value, only approximately a 1/2-inch of the
1.5 inches of new postulated process effect can be accommodated between the existing
calibrated setpoint and the (existing) licensed Allowable Value. Thus, the direction to notify
engineering only if the Rx vessel level indication bias had reached a value of 1.5 inches in
either direction was inadequate direction for the operating staff in order to ensure that the
instruments remained operable.
Corrective Actions: The licensee corrected the condition by revising the ODMI to include
adequate operator guidance and trigger points.
Corrective Action Reference: CR-RBS-2018-03148
13
Performance Assessment:
Performance Deficiency: The failure to establish ODMI guidance per Procedure EN-OP-111
to address the compensatory measures implemented to maintain operability of the plant with
degraded feedwater sparger nozzles was a performance deficiency.
Screening: For Example 1, the performance deficiency was more than minor, and therefore a
finding, because it was associated with the equipment reliability attribute of the Mitigating
Systems Cornerstone and adversely affected the cornerstone objective to ensure the
availability, reliability, and capability of systems that respond to initiating events to prevent
undesirable consequences. Specifically, the licensee failed to provide adequate guidance to
the operators for actions required if the plant inadvertently entered any of the unanalyzed
conditions for continued operation with the degraded sparger. For Example 2, the
performance deficiency was more than minor, and therefore a finding, because if left
uncorrected it would have the potential to lead to a more significant safety concern.
Specifically, the use of less conservative calculated values than the Allowable Values stated
in the facility TS as a basis for establishing a threshold for operability of TS equipment could
result in the inappropriate evaluation of actual degraded conditions that impact the ability of
components to perform their required safety functions.
Significance: The inspectors screened the finding in accordance with Inspection Manual
Chapter 0609, Appendix A, The Significance Determination Process for (SDP) for Findings
At-Power. Using Inspection Manual Chapter 0609, Appendix A, Exhibit 1, Initiating Events
Screening Questions, the inspectors determined this finding was of very low safety
significance (Green) because for Example 1, the finding would not result in exceeding the
RCS leak rate for a small LOCA and could not have likely affected other systems used to
mitigate a LOCA. For Example 2, it was not a design/qualification deficiency, did not
represent a loss of system safety function, did not result in a loss of function of a single train
for greater than its TS-allowable outage time, did not result in a loss of function of nonsafety-
related risk-significant equipment and was not risk significant due to external events. In
addition, no actual deviation of the B narrow range level instrument was observed during
plant startup on February 9, 2018.
Cross-cutting Aspect: This finding had a cross-cutting aspect of human performance, change
management H.3: Leaders use a systematic process for evaluating and implementing
change so that nuclear safety remains the overriding priority. Specifically, the licensee did
not use a systematic process to develop and verify the adequacy of the ODMIs associated
with the compensatory measures implemented for the degraded sparger.
Enforcement:
Violation: Title 10 CFR Part 50, Appendix B, Criterion V, requires in part that, activities
affecting quality shall be prescribed by documented instructions, procedures, or drawings, of
a type appropriate to the circumstances. Licensee Procedure EN-OP-111, Operational
Decision-Making Issue (ODMI) Process, Revision 16, an Appendix B quality-related
procedure, provides instructions for developing guidance for plant operation with
compensatory measures in place to maintain plant system operable with degraded
conditions. Procedure EN-OP-111, step 5.2.4, states that Operational Decision-Making
Considerations should ensure that a course of action is selected based upon a critical
consideration of risks and potential consequences, as well as a thorough understanding of
alternate solutions. The final decision should be a deliberate act, providing clear direction,
trigger points, contingencies, and abort criteria. The Action Plans should provide clear
14
guidance in each ODMI which delineate actions to be taken when conditions escalate
unexpectedly, conditions are outside the scope of the ODMI analysis, or actions are not able
to be implemented. Actions that contain recommendations to "consider or evaluate" in
response to triggers should be avoided. When such actions are used, a definite period to
finish the evaluation or consideration should be provided.
Contrary to the above, prior to February 1, 2018, the licensee failed to ensure that the ODMIs
provided a course of action based upon a critical consideration of risks and potential
consequences, as well as a thorough understanding of alternate solutions; and that the final
decision was a deliberate act providing clear direction, trigger points, contingencies, and abort
criteria. Specifically, the licensee failed to develop adequate guidance for the operators to
maintain safe operation of the plant with compensatory measures in place for degraded
feedwater sparger nozzles. The action plans failed to provide clear guidance in each ODMI
to delineate actions to be taken when conditions escalate unexpectedly; instead, the actions
specified directed the operators to consult with offsite contractors regarding the acceptability
of allowing the plant to remain in operation with given conditions.
Disposition: This violation is being treated as a non-cited violation, consistent with
Section 2.3.2.a of the NRC Enforcement Policy.
Failure to Establish Procedural Guidance for Determining Core Flow During Unanticipated
Single Loop Operations
Cornerstone Significance Cross-cutting Report
Aspect Section
Initiating Green [P.3] - 71153 -
Events NCV 05000458/2018012-03 Problem Follow-up of
Closed Identification Events and
and Notices of
Resolution, Enforcement
Resolution Discretion
The inspectors reviewed a self-revealed, non-cited violation of 10 CFR Part 50, Appendix B,
Criterion V, Instructions, Procedures and Drawings, for the licensees failure to establish
appropriate instructions in the abnormal operating procedure for thermal hydraulic
instabilities. Specifically, the procedural step for determining core flow when in single loop
operations at low power did not provide appropriate instructions to operators. As a result,
station personnel could not conclusively determine core flow and inserted a manual reactor
Description:
On February 1, 2018, with the unit in Mode 1 at approximately 27 percent power, reactor
recirculation pump B unexpectedly tripped during an upshift in the speed of the pump. As a
result, the reactor was in a single loop configuration with the recirculation pump A running in
fast speed and the recirculation pump B not running. Operators entered Abnormal Operating
Procedure AOP-0024, Thermal Hydraulic Instability Controls, Revision 30, as a result of the
unplanned entry into single loop operations. Step 5.8 of this procedure directed operators to
determine core flow and enter the General Operating Procedure GOP-004, for single loop
operations. Step 5.8 also instructed operators to determine core flow using process computer
point B33NA01V when in a configuration with one recirculation pump in fast speed and one
recirculation pump off. Control room operators observed the value of this data point as
13.9 Mlbm/hr. The operators concluded that this value was not valid since the indicated flow
15
was much lower than expected with one recirculation pump running in fast speed. The
operators then observed a value of 27.3 Mlbm/hr core flow using the ERIS data point for
B33NA01V. This value appeared to be a valid number based on the single loop operation
power/flow map contained in AOP-0024, Attachment 2. Normal data points are displayed in
ERIS with a white text, but control room operators observed the ERIS data point displayed in
a magenta color. Additionally, the word suspect appeared adjacent to the data point for
core flow. Control room operators contacted information technology personnel and attempted
to understand the magenta color and suspect information associated with the core flow data
point. Concurrently, operators attempted to validate core flow using alternate means but
were unsuccessful as the alternate indications did not provide accurate core flow readings at
low reactor power when in a single loop configuration. After approximately one hour spent
seeking to understand the unfamiliar indication associated with B33NA01V, control room
operators conducted a brief and made the decision to shut down the unit due to the
uncertainties associated with the core flow data point. Following plant shutdown and
subsequent troubleshooting and investigation, licensee personnel concluded that the
magenta text and suspect note associated with ERIS B33NA01V was an expected system
response. Below approximately 40 percent core flow, the plant process computer shifts the
calculation method from the primary means of calculating core flow using the sum of jet pump
flows to an alternate process that uses core plate differential pressure. As a result of shifting
to the alternate calculation of core flow, data point ERIS B33NA01V was programmed to turn
magenta in color and display suspect to alert operators that the method of calculating core
flow had changed.
The inspectors reviewed Condition Report CR-RBS-2012-07759. This condition report was
generated by operations department personnel on December 19, 2012, and identified that
ERIS point B33NA01V indicated suspect and was not available for use. The condition
report also stated that this data point was needed for determining core flow when the plant
configuration consisted of one recirculation pump running in fast speed and another
recirculation pump was off. The inspectors confirmed that this condition report was generated
during a single loop plant configuration that was the result of an unanticipated reactor
recirculation pump A trip on December 19, 2012. The condition report corrective actions
explained the reason for the suspect reading of ERIS point B33NA01V. No corrective
actions were generated to address AOP-0024, which directs licensed operators to validate
core flow in single loop operations. Additionally, no corrective actions were generated to
validate plant simulator response to unanticipated single loop operations.
Corrective Actions: After this information was disseminated to licensed operators, the
licensee implemented procedural changes to AOP-0024 that provided amplifying information
regarding B33NA01V validated core flow. Specifically, the licensee revised the procedure on
February 7, 2018, in order to 1) direct operators to determine core flow using ERIS data point
B33NA01V during single loop operations when core flow is below 40 percent and 2) provide
clear guidance regarding expected system response of the process computer data points
during abnormal flow configurations.
Corrective Action Reference: CR-RBS-2018-00776
Performance Assessment:
Performance Deficiency: The failure to establish appropriate guidance to determine core flow
during single loop operations in quality-related abnormal operating procedure AOP-0024,
Thermal Hydraulic Instability Controls, Revision 30, was a performance deficiency.
16
Screening: The performance deficiency was more than minor, and therefore a finding,
because it was associated with the procedure quality attribute of the Initiating Events
Cornerstone and adversely affected the cornerstone objective to limit the likelihood of events
that upset plant stability. Specifically, the failure to understand core flow data indicated by
plant process computer point B33NA01V and ERIS data point B33NA01V resulted in
confusion and the ultimate decision to insert a manual reactor scram.
Significance: The inspectors screened the finding in accordance with Inspection Manual
Chapter 0609, Appendix A, The Significance Determination Process for (SDP) for Findings
At-Power. Using Inspection Manual Chapter 0609, Appendix A, Exhibit 1, Initiating Events
Screening Questions, the inspectors determined this finding is of very low safety significance
(Green) because the finding did not cause a reactor trip and the loss of mitigation equipment
relied upon to transition the plant from the onset of the trip to a stable shutdown condition.
Cross-cutting Aspect: This finding has a cross-cutting aspect in the area of problem
identification and resolution, resolution, because the licensee failed to take effective
corrective actions to address issues in a timely manner commensurate with their safety
significance. Specifically, the station failed to implement procedure changes to AOP-0024
after discovering similar confusing indications associated with B33NA01V on
December 19, 2012.
Enforcement:
Violation: Title 10 CFR Part 50, Appendix B, Criterion V, requires in part that, activities
affecting quality shall be prescribed by documented instructions, procedures, or drawings, of
a type appropriate to the circumstances.
Contrary to the above, prior to February 7, 2018, the licensee failed to provide a procedure of
a type appropriate to the circumstances for an activity affecting quality. Specifically,
AOP-0024, Thermal Hydraulic Stability Controls, a quality-related procedure, was not
appropriate to the circumstances. AOP-0024 did not provide accurate and adequate
instruction to operators to determine core flow during single loop operations. The licensee
restored compliance by revising AOP-0024 to include accurate and adequate guidance to
determine core flow during unanticipated single loop operations.
Disposition: This violation is being treated as an non-cited violation consistent with
Section 2.3.2.a of the NRC Enforcement Policy.
Failure to Perform 10 CFR 50.59 Evaluation for Main Feedwater System Sparger Nozzle
Damage
Cornerstone Significance Cross-cutting Report
Aspect Section
None SL-IV None 71111.18 -
NCV 05000458/2018012-07 Plant
Closed Modifications
The inspectors identified a Severity Level IV NCV of 10 CFR 50.59, Changes, Tests, and
Experiments, for the licensees failure to provide a written safety evaluation for the
determination that operation with compensatory measures for damaged feedwater sparger
nozzles did not require a license amendment pursuant to 10 CFR 50.90, Application for
amendment of license, construction permit, or early site permit. Specifically, the licensee
17
failed to recognize that compensatory measures prohibiting operation in single loop
conditions were technical specification changes, and as such required prior NRC approval.
Description:
During an outage that was conducted to replace failed fuel assemblies in January 2018,
damage to feedwater sparger nozzles was identified. The evaluation of the damaged
feedwater sparger nozzles #7 and #8 on sparger N4C identified that the damaged sections of
the feedwater sparger nozzles had the potential to adversely affect the vessel cladding by
allowing relatively colder water to directly flow into the relatively hotter vessel wall, thus
inducing thermal fatigue. All components of the RCS are designed to withstand effects of
cyclic loads due to system pressure and temperature changes. These loads are introduced
by startup (heatup) and shutdown (cooldown) operations, power transients, and reactor trips.
Limits are established for pressure and temperature changes during RCS heatup and
cooldown, such that plant systems remain within the design assumptions and the stress limits
for cyclic operation. Limits on RCS pressure, temperature, heatup rate, and cooldown rate
define allowable operating regions and operating cycles to prevent nonductile failure of
system components. Because operation with the sparger nozzle damage was outside the
limits originally analyzed, the licensee requested General Electric-Hitachi (GEH) to provide an
operability analysis of the degraded condition. GEH Report #004N6557 Revision 0, dated
January 26, 2018, Operability Assessment of the River Bend Station Feedwater Sparger
Assembly in the January 2018 As-found Condition, stated in part, this evaluation does not
account for Final Feedwater Temperature Reduction (FFWTR), Feedwater Heater Out-of-
Service (FWH OOS) conditions, nor Single Loop Operation (SLO) operating conditions.
Based on this analysis, the licensees engineering department concluded that the
recommended classification of this condition was OPERABLE-COMP MEAS (operable with
compensatory measures), with the degraded/nonconforming condition being the holes in the
feedwater sparger nozzles. One of the operational restrictions/limitations was that, RBS will
not operate in Single Loop Operation (SLO). These compensatory measures directly
affected Technical Specification (TS) 3.4.1, Recirculation Loops Operating. The TS limiting
condition for operation (LCO) B, One recirculation loop shall be in operation, which is
applicable when operating in Modes 1 and 2, had the following limitations:
1. THERMAL POWER 77.6% rated thermal power (RTP);
2. Total core flow within limits;
3. LCO 3.2.1,"AVERAGE PLANAR LINEAR HEAT GENERATION RATE (APLHGR),"
single loop operation limits specified in the Core Operating Limits Reports (COLR);
4. LCO 3.2.2,"MINIMUM CRITICAL POWER RATIO (MCPR)," single loop operation
limits specified in the COLR; and
5. LCO 3.3.1.1, "Reactor Protection System (RPS) Instrumentation," Function 2.b
(Average Power Range Monitors Flow Biased Simulated Thermal Power- High), Allowable
Value for single loop operation as specified in the COLR.
The licensees compensatory measures established a more restrictive LCO whereby Single
Loop Operations are limited by more restrictive criteria than those stated in the existing LCO.
Specifically, the licensees compensatory measures stated that the station would not operate
in Single Loop Operation.
NRC Administrative Letter 98-10: Dispositioning of Technical Specifications That Are
Insufficient To Assure Plant Safety, dated December 29, 1988, provides the following
guidance:
18
Title 10 of the Code of Federal Regulations, Section 50.36, Technical Specifications
requires that each TS limiting condition for operation (LCO) specify, at a minimum, the lowest
functional capability or performance level of equipment required for the safe operation of the
facility.
IMC0326 states, in part: Additionally, if a compensatory measure involves a temporary facility
or procedure change, 10 CFR 50.59 should be applied to the temporary change with the
intent to determine whether the temporary change/compensatory measure itself (not the
degraded or nonconforming condition) impacts other aspects of the facility or procedures
described in the UFSAR. In considering whether a temporary facility or procedure change
impacts other aspects of the facility, a licensee should apply 10 CFR 50.59, paying particular
attention to ancillary aspects of the temporary change that result from actions taken to directly
compensate for the degraded condition. Whenever degraded or nonconforming conditions
are discovered, 10 CFR Part 50, Appendix B, requires prompt corrective action to correct or
resolve the condition.
In summary, the discovery of an improper or inadequate TS value or required action is
considered a degraded or nonconforming condition as defined in IMC0326. Imposing
administrative controls in response to an improper or inadequate TS is considered an
acceptable short-term corrective action. The NRC staff expects that, following the imposition
of administrative controls, an amendment to the TS, with appropriate justification and
schedule, will be submitted in a timely fashion. Once any amendment correcting the TS is
approved, the licensee must update the final safety analysis report, as necessary, to comply
with 10 CFR 50.71(e).
Because the licensee did not perform a 50.59 screening for the compensatory measures
associated with the restricted operating conditions, the licensee failed to recognize that the
TSs were now non-conservative and that NRC approval was required.
Corrective Actions: The licensee documented the violation in the corrective action program
and created actions to review 50.59 screening requirements.
Corrective Action Reference: CR-RBS-2018-03147
Performance Assessment:
Performance Deficiency: The failure to perform a written safety evaluation for the effect of
compensatory measures implemented due to degraded feedwater sparger nozzles was a
performance deficiency.
Screening: The performance deficiency was evaluated in accordance with the traditional
enforcement process because it impacted the ability of the NRC to perform its regulatory
oversight function.
Significance: Using example 6.1.d.2 from the NRC Enforcement Policy, the violation was
determined to be a Severity Level IV violation.
Cross-cutting Aspect: Because the violation was dispositioned using the traditional
enforcement process, no cross cutting aspect was assigned.
19
Enforcement:
Violation: Title 10 CFR 50.59(d)(1) requires, in part, that the licensee shall maintain records
of changes in the facility, of changes in procedures, and of tests and experiments as
described in the updated final safety analysis report (UFSAR). These records must include a
written evaluation which provides a basis for the determination that the change, test, or
experiment does not require a license amendment.
Contrary to the above, since January 29, 2018, the licensee failed to maintain records of a
change to the facility, as described in the UFSAR, that include a written evaluation which
provides a basis for the determination that the change did not require a license amendment.
Specifically, the licensee made changes pursuant to 10 CFR 50.59(c) to the plant as
described in the UFSAR and did not provide a written evaluation for the determination that
compensatory measures prohibiting operation in single loop condition were technical
specification changes, and as such required prior NRC approval.
Disposition: This violation is being treated as an non-cited violation consistent with
Section 2.3.2.a of the NRC Enforcement Policy.
Failure to Conduct Adequate Transient Snap Shot Assessment Following Recirculation Pump
Trip
Cornerstone Significance Cross-cutting Report
Aspect Section
Initiating Events Green None 71152 -
FIN 05000458/2018012-01 Problem
Closed Identification
and
Resolution
The inspectors identified a Green finding for the licensees failure to adequately validate
simulator response during a transient snap shot assessment following an unexpected trip of
reactor recirculation pump A on December 19, 2012.
Description:
On December 19, 2012, with the plant operating at 100 percent power, reactor recirculation
pump A unexpectedly tripped off. As a result, the plant configuration consisted of one
recirculation pump running in fast speed and the other recirculation pump secured. During
this single loop configuration, station personnel identified that emergency response
information system (ERIS) point B33NA01V indicated suspect and was not available for
use. The station documented this condition in Condition Report CR-RBS-2012-07759.
On February 1, 2018, with the unit in Mode 1 at approximately 27 percent power, reactor
recirculation pump B unexpectedly tripped during an upshift in the speed of the pump. As a
result, the reactor was in a single loop configuration with the recirculation pump A running in
fast speed and the recirculation pump B not running. Operators entered abnormal operating
procedure AOP-0024, Thermal Hydraulic Instability Controls, Revision 30, as a result of the
unplanned entry into single loop operations. Step 5.8 of this procedure directed operators to
determine core flow and enter general operating procedure GOP-004, Single Loop
Operations. Step 5.8 also instructed operators to determine core flow using process
computer point B33NA01V (which can be observed in both ERIS and the plant process
computer) when in a configuration with one recirculation pump in fast speed and one
20
recirculation pump off. Control room operators observed the value of this data point as
13.9 million pounds mass per hour (Mlbm/hr) of flow through the reactor core. The operators
concluded that this value was not valid since the indicated flow was much lower than
expected with one recirculation pump running in fast speed. The operators then observed a
value of 27.3Mlbm/hr core flow using the ERIS data point for B33NA01V. This value
appeared to be a valid number based on the single loop operation power/flow map contained
in AOP-0024, Attachment 2. Normal data points on ERIS are displayed with a white text, but
control room operators observed the ERIS data point displayed in a magenta color.
Additionally, the word suspect appeared adjacent to the data point for core flow. Control
room operators contacted information technology personnel and attempted to understand the
magenta color and suspect information associated with the core flow data point.
Concurrently, operators attempted to validate core flow using alternate means but were
unsuccessful, as the alternate indications did not provide accurate core flow readings at low
reactor power when in a single loop configuration. After approximately one hour spent
seeking to understand the unfamiliar indication associated with B33NA01V, control room
operators conducted a brief and made the decision to shut down the unit due to the
uncertainties associated with the core flow data point. Following plant shutdown and
subsequent troubleshooting and investigation, licensee personnel concluded that the
magenta text and suspect note associated with ERIS B33NA01V was an expected system
response. Below approximately 40 percent core flow, the plant process computer shifts the
calculation method from the primary means of calculating core flow using the sum of jet pump
flows to an alternate process that uses core plate differential pressure. As a result of shifting
to the alternate calculation of core flow, data point ERIS B33NA01V was programmed to turn
magenta in color and display suspect to alert operators that the method of calculating core
flow had changed. After this information was disseminated to licensed operators, the
licensee implemented procedural changes to AOP-0024 that provided amplifying information
regarding B33NA01V validated core flow. Specifically, the licensee revised the procedure on
February 7, 2018, in order to provide clear guidance regarding expected system response of
the process computer data points during abnormal flow configurations.
The inspectors compared the actual plant response to the simulator response for the trip of a
recirculation pump while at low power. The actual conditions in the main control room during
the event on February 1, 2018, resulted in ERIS point B33NA01V indicating the correct flow
(27.3Mlbm/hr), but the data point turned magenta in color and displayed the warning label
suspect. This was later determined by information technology personnel to be the correct
response and data display, and was the result of the core flow calculation methodology
swapping from the primary method (jet pump flow) to the alternate method (core plate
differential pressure).
In the simulator, the inspectors determined that ERIS point B33NA01V provided erratic
indications of core flow following a simulated trip of the recirculation pump B from an initial
condition of approximately 25 percent. The indicated flow varied, and ultimately stabilized at
approximately 10Mlbm/hr, which is less than half of the expected indication. Additionally,
B33NA01V did not change to a magenta color, and it did not display the word suspect. The
inspectors determined that ERIS B33NA01V was programmed to calculate core flow using
the sum of jet pump flows at all power levels. As a result, the displayed value was inaccurate
below 40 percent core flow, and the data point was not programmed to turn magenta or
indicate suspect since no swap to a backup means of calculation below 40 percent core
flow was modelled.
21
The inspectors reviewed procedure EN-OP-117, Operations Assessments, Version 4,
Section 5.4, which states that transient snap-shot assessments are performed whenever a
plant transient occurs. A plant transient is defined in section 5.4[2] as including any turbine
generator power change in excess of 10 percent of rated power in less than one minute other
than a momentary spike due to a grid disturbance or a manually initiated runback. The
inspectors concluded that the recirculation pump A trip on December 19, 2012, met the
definition of a transient. EN-OP-117, Attachment 9.2, Transient Snap Shot Assessment
Documentation Form, Objective 7, discusses the training preparation aspect of the
assessment. Specifically, the transient snap-shot assessment is performed in order to
validate that the simulator accurately represented the plant characteristics of the transient.
The licensee provided a Post-Event Simulator Test report that was run on February 14, 2013.
The report concluded that the simulator response matched the parameters observed in the
plant. The inspectors determined that although the snap-shot assessment was performed,
station personnel did not validate that ERIS B33NA01V (validated core flow) provided
operators with the same indications seen by operators in the plant during a recirculation
pump trip.
The inspectors determined that no condition report or simulator deficiency report was
generated to document the discrepancy between the plant and the simulator for displaying
ERIS B33NA01V. The simulator ERIS B33NA01V core flow indication did not display the
correct value for core flow and also did not indicate suspect or turn magenta. The
inspectors reviewed training documentation to determine why this discrepancy was not
observed during continuing simulator training scenarios. The inspectors concluded that this
discrepancy was not documented because the station did not conduct training on abnormal
single loop operations during low power operations. The inspectors reviewed industry
standards and guidelines for simulator training and determined that the station is required to
periodically conduct training on abnormal events that occur during low power operations.
Corrective Actions: The station documented the core flow indication simulator deficiency in a
deficiency report and generated actions to incorporate the discrepancy into future licensed
operator training sessions.
Corrective Action Reference: CR-RBS-2018-03145
Performance Assessment:
Performance Deficiency: The licensees failure to validate core flow in the simulator during a
transient snap shot assessment following the trip of the reactor recirculation pump A on
December 19, 2012, was a performance deficiency.
Screening: The performance deficiency was more than minor, and therefore a finding,
because it was associated with the human performance attribute of the Initiating Events
Cornerstone and adversely affected the cornerstone objective to limit the likelihood of events
that upset plant stability and challenge critical safety functions during shutdown as well as
power operations. Specifically, the failure to validate simulator fidelity following a plant
transient prevented the licensee from identifying simulator model discrepancies when
determining core flow during low power, single loop operations.
22
Significance: The inspectors screened the finding in accordance with Inspection Manual
Chapter 0609, Appendix A, The Significance Determination Process for Findings At-Power.
The finding was determined to be of very low safety significance (Green) because the finding
did not contribute to both the likelihood of a reactor trip and the likelihood that mitigating
equipment would not be available.
Cross-cutting Aspect: No cross cutting aspect was assigned because the performance
deficiency is not indicative of current licensee performance.
Enforcement: Inspectors did not identify a violation of regulatory requirements associated
with this finding.
Failure to Submit a Licensee Event Report for a Manual Scram
Cornerstone Significance Cross-cutting Report
Aspect Section
None SLIV None 71153 -
NCV 05000458/2018012-04 Follow-up of
Closed Events and
Notices of
Enforcement
Discretion
The inspectors identified a Severity Level IV non-cited violation of 10 CFR 50.73, Licensee
Event Report System, for the licensees failure to submit a required licensee event report
(LER). Specifically, on February 1, 2018, after an unexpected trip of the recirculation pump
B, the licensee initiated a manual scram of the reactor that was not part of a preplanned
sequence and failed to submit an LER within 60 days.
Description: At approximately 9:46 a.m. on February 1, 2018, with the unit operating at
approximately 27 percent power, the recirculation pump B unexpectedly tripped during an
attempted transfer from slow to fast speed. The licensee promptly entered AOP-0024,
Thermal Hydraulic Instability, and GOP-0004, Single Loop Operation. Note 5.8 of AOP-
0024 and Precaution 3.6 of GOP-0004 instruct the licensee to use process computer point
B33NA01V to determine core flow while in single loop operation. The plant process computer
(PPC) and emergency response information system (ERIS) readouts showed conflicting
indications for this computer point, with the PPC showing approximately 13,900 Mlbm/hr of
flow and ERIS showing approximately 26,000 Mlbm/hr of flow.
Step 5.1 of AOP-0024 instructs the licensee to determine where on the power-to-flow map the
plant is operating. If the plant is operating in the restricted region, the procedure states to exit
that region by lowering power or raising flow. If the plant is operating in the exclusion region,
the procedure states to verify that a scram has occurred. The indicated PPC value for core
flow put the plant in an unanalyzed region of the power-to-flow map, with less flow than the
minimum amount of flow that defines any region, including the exclusion region. The
indicated ERIS value put the plant in the restricted region, just above the boundary that
delineates the restricted region from the monitoring region.
The licensee initially believed the ERIS value to be the correct value; however, this value was
accompanied by a magenta suspect note on the ERIS screen, which caused the licensee to
question its validity. In an effort to determine the true value of core flow, the licensee
performed a manual calculation using other known inputs. The licensee performed this
calculation incorrectly and wrongly corroborated the PPC value as the correct value. Given
the inability to establish that the plant was operating in any allowed region of the power-to-
23
flow map, the licensee made the decision to manually actuate the reactor protection system
(RPS) by taking the reactor mode switch to shutdown.
During the investigation after the scram, the licensee determined that the ERIS value was, in
fact, a valid indication of core flow at the time of the event. Operators had not been
adequately trained on the meaning of the magenta suspect indication, and were therefore
unable to determine the implications of the indications on the validity of the data point.
Pursuant to the requirements of 10 CFR 50.72(b)(3)(iv), the licensee reported the scram
event to the NRC at 1:23 p.m. as an event that resulted in an actuation of the RPS. On
March 23, 2018, the licensee retracted the report on the grounds that the actuation was part
of a pre-planned sequence during testing or reactor operation. The inspectors concluded that
this retraction was inappropriate and that the event was reportable for the reasons provided
below.
The inspectors reviewed NUREG-1022, Event Report Guidelines 10 CFR 50.72 and 50.73,
revision 3, which provides the following guidance: Actuations that need not be reported are
those initiated for reasons other than to mitigate the consequences of an event (e.g., at the
discretion of the licensee as part of a preplanned procedure). In the case of the February 1,
2018, River Bend scram event, the inspectors determined that the manual RPS actuation was
initiated in order to mitigate the consequences (i.e., uncertainty as to the condition of the plant
with respect to core flow and power-to-flow considerations) of an event (i.e., the unexpected
loss of a reactor recirculation pump).
NUREG-1022 also provides an example of a reportable manual scram that was event driven
and not part of a preplanned sequence during testing or reactor operation:
At a BWR, both recirculation pumps tripped as a result of a breaker problem. This
placed the plant in a condition in which BWRs are typically scrammed to avoid
potential power/flow oscillations. At this plant, for this condition, a written off-normal
procedure required the plant operations staff to scram the reactor. The plant staff
performed a reactor scram, which was uncomplicated. This event is reportable as a
manual RPS actuation. Even though the reactor scram was in response to an existing
written procedure, this event does not involve a preplanned sequence because the
loss of recirculation pumps and the resultant off-normal procedure entry were event
driven, not preplanned. Both an ENS notification and an LER are required. In this
case, the licensee initially retracted the ENS notification, believing that the event was
not reportable. After staff review and further discussion, it was agreed that the event
is reportable for the reasons discussed above.
As with the scram in the above example, the scram that occurred at River Bend Station was
not part of a preplanned sequence during testing or reactor operation, but was instead an
event driven response to a series of unplanned and unexpected adverse occurrences in the
plant. These occurrences included: a trip of the recirculation pump B, entry into an abnormal
operating procedure for thermal hydraulic instability, an inability to determine core flow and
location on the power-to-flow map in accordance with that procedure, a realization that the
PPC indication of core flow put the plant outside of any allowed operating region of the
power-to-flow map, an incorrect manual calculation that wrongly corroborated the accuracy of
the PPC indication, and the presence of a poorly understood suspect indication that
appeared to undermine the validity of the ERIS flow indication. These adverse occurrences
generated uncertainty as to the status of reactor safety. The subsequent decision to perform
24
a manual reactor scram was consistent with general instruction provided in EN-OP-115,
Conduct of Operations, which states: do not hesitate to reduce power or perform an
immediate reactor shutdown when reactor safety is uncertain. As with the scram in the
above example, the February 1, 2018, River Bend scram also involved entry into an off-
normal procedure due to an unexpected plant equipment malfunction that resulted in the
potential for the plant to be in an undesired condition with respect to power-to-flow
considerations.
The senior resident inspector was present in the control room during the events and was able
to confirm that the shutdown was event driven rather than preplanned. At 10:55 a.m., the
control room briefed that because PPC and ERIS showed conflicting indications of core flow
with ERIS indicating suspect, the mode switch was going to be placed in shutdown. At
10:57 a.m., roughly two minutes after the brief was completed, the reactor operator
scrammed the reactor, and the following station log entry was made: MCR [main control
room] announces placing plant in shut down due to inability to regulate recirculation flow. If
the reactor shutdown had been preplanned, it would not have proceeded at this accelerated
pace. Rather, the licensee would have worked through the relevant steps of the applicable
shutdown procedure, GOP-0004, Single Loop Operation, scramming the reactor only after
those steps had been completed and signed for. Upon review of the copy of GOP-0004 that
was in use by the operators on February 1, 2018, the inspectors noted that no steps of
Attachment 3, Shutdown from Single Loop Operation, were marked as completed, and the
attachment was not signed off as being initiated or completed. The deviation from normal
practice was appropriate because the scram was not being initiated as part of a preplanned
sequence. It was instead being initiated in response to the unanticipated emergence of a
safety concern.
Corrective Actions: The licensee documented the violation in the corrective action program
and generated corrective actions to review reportability requirements.
Corrective Action Reference(s): CR-RBS-2018-03953
Performance Assessment:
Performance Deficiency: The failure to submit a required licensee event report was a
performance deficiency.
Screening: The performance deficiency was evaluated in accordance with the reactor
oversight process and was determined to be minor because it could not be reasonably
viewed as a precursor to a significant event, would not have the potential to lead to a more
significant safety concern, does not relate to a performance indicator that would have caused
the performance indicator to exceed a threshold, and did not adversely affect a cornerstone
objective. The performance deficiency was evaluated in accordance with the traditional
enforcement process because it impacted the ability of the NRC to perform its regulatory
oversight function.
Significance: Using example 6.9.d.9 from the NRC Enforcement Policy, the violation was
determined to be a Severity Level IV violation.
Cross-cutting Aspect: Because the violation was dispositioned using the traditional
enforcement process, no cross-cutting aspect was assigned.
25
Enforcement:
Violation: 10 CFR 50.73(a)(1) requires, in part, that the licensee shall submit a Licensee
Event Report (LER) for any event of the type described in this paragraph within 60 days after
the discovery of the event. 10 CFR 50.73(a)(2)(iv)(A) requires, in part, that the licensee shall
report any event or condition that resulted in manual actuation of the reactor protection
system (RPS) except when the actuation resulted from and was part of a pre-planned
sequence during testing or reactor operation. Contrary to the above, on April 2, 2018, the
licensee failed to submit an LER within 60 days after the discovery of an event or condition
that resulted in manual actuation of the RPS that did not result from and that was not a part of
a pre-planned sequence during testing or reactor operation. Specifically, the licensee failed
to submit an LER within 60 days of a manual reactor scram that occurred on February 1,
2018.
Disposition: Because this SLIV violation was neither repetitive nor willful, and because it was
entered into the licensees corrective action program as Condition Report
CR-RBS-2018-03953, it is being treated as a non-cited violation consistent with
Section 2.3.2.a of the NRC Enforcement Policy.
EXIT MEETINGS AND DEBRIEFS
The inspectors verified no proprietary information was retained or documented in this report.
On May 31, 2018, and on July 16, 2018, the inspectors presented the inspection results to
Mr. W. Maguire, Site Vice President, and other members of the licensee staff.
26
DOCUMENTS REVIEWED
71111.15Operability Determinations and Functionality Assessments
Procedures
Number Title Revision
EN-OE-100 Operating Experience Program 12 & 13
STP-051-4206 (RPS Bypassed) RPS/RHR Reactor Vessel Level-Low, 305
Level 3, High, Level 8, Channel Calibration and Logic
System Functional Test (B21-N680B, B21-N683B, B21-
N080B)
STP-051-4227 ECCS/RCIC Actuation Ads Trip System B Reactor 20
Vessel Water Level Low, Level 3/High, Level 8 Channel
Calibration, and Logic System Functional Test (B21-
N095B, B21-N695B, B21-N693B)
STP-501-4202 FWS/MAIN Turbine Trip System - Reactor Vessel Water 15
Level - High Level 8, Channel Calibration and LSFT
(C33-N004B, C33-K624B, C33-R606B, C33-K650-3)
G13.18.6.1.B21 Reactor Vessel Water Level - Low, Level 3 Trip Function 3
G13.18.6.1.B21*003 Reactor Vessel Water Level - Low, Level 3 Trip Function 3
G13.18.6.1.B21*010 Reactor Vessel Water Level - Low, Level 8 Narrow 0, 1, 2, & 3
Range
MCP-IC-501-4202 FWS/FEED Pump Trip System (MSO) - Reactor Vessel 0
Water Level - High Level 8, Loop Calibration (C33-
LTN006B, C33-ESN606B)
71111.18Plant Modifications
Condition Reports (CR-RBS-)
CR-RBS-2014-05194 CR-RBS-2014-06685 CR-RBS-2014-06691 CR-RBS-2015-03253
CR-RBS-2015-03983 CR-RBS-2015-04065 CR-RBS-2015-04117 CR-RBS-2015-08476
CR-RBS-2015-08515 CR-RBS-2016-00791 CR-RBS-2016-00893 CR-RBS-2016-00893
CR-RBS-2016-04351 CR-RBS-2016-04353 CR-RBS-2017-02828 OE-NOE-2004-00008
OE-NOE-2004-00084
Engineering Changes
Number Title Revision
EC-75588 Accept As-Is Evaluation for Remainder of Cycle 20: Sparger 0 & 1
N4C Nozzles 7 and 8 Damaged
Attachment
Procedures
Number Title Revision
OSP-0053 Emergency and Transient Response Support Procedure 20-25
STP-000-0001 Daily Operating Logs 082
DBR-0035279 GEH Comment Resolution Form 0
4221.110-000- Operability Assessment of the River Bend Station 0
043 Feedwater Sparger Assembly in the January 2018 As-
Found Condition
71152 - Problem Identification and Resolution
Condition Reports (CR-RBS-)
CR-RBS-2018-00358 CR-RBS-2018-00613 CR-RBS-2018-00633 CR-RBS-2018-00733
CR-RBS-2018-00895 CR-RBS-2018-00294 OE-NOE-2004-00008 OE-NOE-2004-00084
Engineering Changes
Number Title Revision
EC-75663 Loose Parts Evaluation for Material Lost From 0
Feedwater Spargers Identified During PO-18-01
Foreign Material FME LPA-000
Miscellaneous Documents
Number Title Revision/Date
OSRC Meeting 2018-0001 Minutes
OSRC Meeting 2018-0002 Minutes
Action Item OE33308-20110507-A2-RBS-001
CNR RBS PO-18-01-01 Foreign Material Customer Notification Report 0
ECH-NE-17-00039 River Bend MOC-20a Fuel Inspection Plan 0
NEDC-31336P-A General Electric Instrument Setpoint 0
Methodology
NEDE-21821-A Boiling Water Reactor Feedwater 0
Nozzle/Sparger Final Report
NEI 96-07 Guidelines for 10 CFR 50.59 Implementation 1
OE33308-20110507 Sampling Probe Found in Feedwater Sparger August 17, 2011
A-2
Miscellaneous Documents
Number Title Revision/Date
PO 18-01 BOP Foreign Material Inspection Report
RBS-ER-99-0539 Engineering Response Associated with Loose 0
Part in the Feedwater System
Procedures
Number Title Revision
AOP-0024 Thermal Hydraulic Stability Controls 30, 31, & 32
EN-NF-102 Corporate Fuel Reliability 6
EN-OP-104 Operability Determination Process 14
EN-OP-111 Operational Decision Making Issue Process 15
EN-OP-117 Operations Assessments 4
EOP-0001 Emergency Operating Procedure - RPV Control 28
GOP-0001 Plant Startup 99
GOP-0002 Power Decrease/Plant Shutdown 78
GOP-0003 Scram Recovery 31
GOP-0004 Single Loop Operation 25
OE-100 Operating Experience Program 1
R-PL-012 Corrective Action Program 1
STP-000-0001 Daily Operating Logs 082
71153Follow-up of Events and Notices of Enforcement Discretion
Procedures
Number Title Revision
EN-OP-115 Conduct of Operations 23
GOP-0004 Single Loop Operation 23
Condition Reports (CR-RBS-)
2018-03149 2018-03953
A-3
SUNSI Review: ADAMS: Non-Publicly Available Non-Sensitive Keyword:
By: CHY/RDR Yes No Publicly Available Sensitive NRC-002
OFFICE SRI:DRP/C RI:DRP/C SPE:DRP/C ARI:DRP/C C:DRS/EB2 D:DRP
NAME JSowa BParks CYoung MOBanion JDrake AVegel
SIGNATURE /RA/ /RA/ /RA/ /RA/ /RA/ /RA/
DATE 6/22/2018 6/21/2018 6/21/2018 6/25/2018 7/10/2018 7/18/18
OFFICE BC:DRP/C
NAME JKozal
SIGNATURE /RA/
DATE 7/18/18