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| issue date = 11/09/2012
| issue date = 11/09/2012
| title = PNO-lll-12-015A (Update) Palisades Shutdown Due to Leakage from the Main Steam System
| title = PNO-lll-12-015A (Update) Palisades Shutdown Due to Leakage from the Main Steam System
| author name = Giessner J B, Taylor T P
| author name = Giessner J, Taylor T
| author affiliation = NRC/RGN-III
| author affiliation = NRC/RGN-III
| addressee name =  
| addressee name =  
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=Text=
=Text=
{{#Wiki_filter:PRELIMINARY NOTIFICATION - REGION III November 9, 2012 PRELIMINARY NOTIFICATION OF EVENT OR UNUSUAL OCCURRENCE
{{#Wiki_filter:PRELIMINARY NOTIFICATION - REGION III November 9, 2012 PRELIMINARY NOTIFICATION OF EVENT OR UNUSUAL OCCURRENCE - PNO-III-12-015A This preliminary notification constitutes EARLY notice of events of POSSIBLE safety or public interest or significance. Some of the information may not yet be fully verified or evaluated by the Region III staff.
- PNO-III-12-015A  
Facility                                               Licensee Emergency Classification Palisades Nuclear Plant                               __ Notification of Unusual Event Entergy Nuclear Operations, Inc.                       __ Alert Covert, Michigan                                       __ Site Area Emergency Docket: 05000255                                       __ General Emergency License: DPR-20                                         X Not Applicable
 
This preliminary notification constitutes EARLY not ice of events of POSSIBLE safety or public interest or significance. Some of the information may not yet be fully verified or evaluated by the Region III staff.  
 
Facility       Licensee Emergency Classification Palisades Nuclear Plant   __ Notification of Unusual Event Entergy Nuclear Operations, Inc. __ Alert Covert, Michigan     __ Site Area Emergency Docket: 05000255     __ General Emergency License: DPR-20     X Not Applicable  


==SUBJECT:==
==SUBJECT:==
UPDATE - PALISADES SHUTDOWN DUE TO LEAKAGE FROM THE MAIN STEAM SYSTEM This Preliminary Notification updates information discussed in PNO-III-12-015, which discussed the Palisades plant shutdown on November 4, 2012. The shutdown was required because of a small, un-isolable through-wall steam leak on a drain valve on the piping for an atmospheric dump valve on the 'B' steam generator secondary side. Because the leak was un-isolable, the  
UPDATE - PALISADES SHUTDOWN DUE TO LEAKAGE FROM THE MAIN STEAM SYSTEM This Preliminary Notification updates information discussed in PNO-III-12-015, which discussed the Palisades plant shutdown on November 4, 2012. The shutdown was required because of a small, un-isolable through-wall steam leak on a drain valve on the piping for an atmospheric dump valve on the B steam generator secondary side. Because the leak was un-isolable, the B steam generator had to be declared inoperable and Technical Specifications required the plant to be shut down within 6 hours.
'B' steam generator had to be declared inoperable and Technical Specifications required the plant to be shut down within 6 hours.  
While the plant was shut down November 4 - 7, 2012, the licensee replaced the steam piping drain valve that had the through-wall steam leak.
 
During this plant shutdown, the licensee also replaced a service water valve that had a pinhole, through-wall leak. NRC inspectors and the licensee had been monitoring the leak, which was identified by NRC inspectors on September 20, 2012, during a routine tour in the auxiliary building. The leak on the service water valve did not require a plant shutdown; did not interfere with the systems ability to perform its function; was not impacting other plant equipment; was not radioactive; and was not a threat to public health and safety. The service water valve pinhole, through-wall leak was previously discussed in PNO-III-12-012.
While the plant was shut down November 4 - 7, 2012, the licensee replaced the steam piping drain valve that had the through-wall steam leak.  
NRC inspectors monitored the repair and testing activities that were conducted for replacing the steam piping drain valve and the service water valve to verify that the repairs were adequate.
 
The testing that was conducted after the valves were replaced confirmed that there was no leakage from either valve.
During this plant shutdown, the licensee also replaced a service water valve that had a pinhole, through-wall leak. NRC inspectors and the licensee had been monitoring the leak, which was identified by NRC inspectors on September 20, 2012, during a routine tour in the auxiliary building. The leak on the service water valve did not require a plant shutdown; did not interfere  
 
with the system's ability to perform its function; was not impacting other plant equipment; was not radioactive; and was not a threat to public health and safety. The service water valve pinhole, through-wall leak was previously discussed in PNO-III-12-012.  
 
NRC inspectors monitored the repair and testing activities that were conducted for replacing the steam piping drain valve and the service water valve to verify that the repairs were adequate. The testing that was conducted after the valves were replaced confirmed that there was no leakage from either valve.
 
On November 7, 2012, the Palisades plant resumed operation after the repairs were completed.
On November 7, 2012, the Palisades plant resumed operation after the repairs were completed.
The reactor was made critical at 1:52 a.m. (EST) and the main generator was synchronized to the grid at 1:09 p.m. (EST).  
The reactor was made critical at 1:52 a.m. (EST) and the main generator was synchronized to the grid at 1:09 p.m. (EST).
 
The State of Michigan has been notified.
The State of Michigan has been notified.  
 
2  The information in this preliminary notification is current as of 0900 a.m. (EST) on November 9, 2012. This information has been reviewed with plant management.
 
ADAMS Accession Number:  ML 12314A271


Contacts: John B. Giessner     Thomas Taylor 630-829-9619       269-764-8971 John.Giessner@nrc.gov     Thomas.Taylor@nrc.gov}}
The information in this preliminary notification is current as of 0900 a.m. (EST) on November 9, 2012. This information has been reviewed with plant management.
ADAMS Accession Number: ML12314A271 Contacts:     John B. Giessner                                       Thomas Taylor 630-829-9619                                           269-764-8971 John.Giessner@nrc.gov                                   Thomas.Taylor@nrc.gov 2}}

Latest revision as of 21:15, 11 November 2019

PNO-lll-12-015A (Update) Palisades Shutdown Due to Leakage from the Main Steam System
ML12314A271
Person / Time
Site: Palisades Entergy icon.png
Issue date: 11/09/2012
From: Jack Giessner, Thomas Taylor
NRC/RGN-III
To:
References
PNO-lll-12-015A
Download: ML12314A271 (2)


Text

PRELIMINARY NOTIFICATION - REGION III November 9, 2012 PRELIMINARY NOTIFICATION OF EVENT OR UNUSUAL OCCURRENCE - PNO-III-12-015A This preliminary notification constitutes EARLY notice of events of POSSIBLE safety or public interest or significance. Some of the information may not yet be fully verified or evaluated by the Region III staff.

Facility Licensee Emergency Classification Palisades Nuclear Plant __ Notification of Unusual Event Entergy Nuclear Operations, Inc. __ Alert Covert, Michigan __ Site Area Emergency Docket: 05000255 __ General Emergency License: DPR-20 X Not Applicable

SUBJECT:

UPDATE - PALISADES SHUTDOWN DUE TO LEAKAGE FROM THE MAIN STEAM SYSTEM This Preliminary Notification updates information discussed in PNO-III-12-015, which discussed the Palisades plant shutdown on November 4, 2012. The shutdown was required because of a small, un-isolable through-wall steam leak on a drain valve on the piping for an atmospheric dump valve on the B steam generator secondary side. Because the leak was un-isolable, the B steam generator had to be declared inoperable and Technical Specifications required the plant to be shut down within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />.

While the plant was shut down November 4 - 7, 2012, the licensee replaced the steam piping drain valve that had the through-wall steam leak.

During this plant shutdown, the licensee also replaced a service water valve that had a pinhole, through-wall leak. NRC inspectors and the licensee had been monitoring the leak, which was identified by NRC inspectors on September 20, 2012, during a routine tour in the auxiliary building. The leak on the service water valve did not require a plant shutdown; did not interfere with the systems ability to perform its function; was not impacting other plant equipment; was not radioactive; and was not a threat to public health and safety. The service water valve pinhole, through-wall leak was previously discussed in PNO-III-12-012.

NRC inspectors monitored the repair and testing activities that were conducted for replacing the steam piping drain valve and the service water valve to verify that the repairs were adequate.

The testing that was conducted after the valves were replaced confirmed that there was no leakage from either valve.

On November 7, 2012, the Palisades plant resumed operation after the repairs were completed.

The reactor was made critical at 1:52 a.m. (EST) and the main generator was synchronized to the grid at 1:09 p.m. (EST).

The State of Michigan has been notified.

The information in this preliminary notification is current as of 0900 a.m. (EST) on November 9, 2012. This information has been reviewed with plant management.

ADAMS Accession Number: ML12314A271 Contacts: John B. Giessner Thomas Taylor 630-829-9619 269-764-8971 John.Giessner@nrc.gov Thomas.Taylor@nrc.gov 2