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| issue date = 04/04/1977
| issue date = 04/04/1977
| title = LER 1977-016-00 for St. Lucie Unit 1, Low Steam Generator Pressure Trips Received on Channel a RPS and Channel a MSIS
| title = LER 1977-016-00 for St. Lucie Unit 1, Low Steam Generator Pressure Trips Received on Channel a RPS and Channel a MSIS
| author name = Schmidt A D
| author name = Schmidt A
| author affiliation = Florida Power & Light Co
| author affiliation = Florida Power & Light Co
| addressee name = Moseley N C
| addressee name = Moseley N
| addressee affiliation = NRC/IE, NRC/RGN-II
| addressee affiliation = NRC/IE, NRC/RGN-II
| docket = 05000335
| docket = 05000335
Line 17: Line 17:


=Text=
=Text=
{{#Wiki_filter:NRV'FORM J5<2.7G)U.S.NUCLEAR REGULATORV Co SSION DOC~T NUMBER'SO~BM NRC DISTRIBUTION FoR PART 50 DOCKET MATERIAL FILE NUMBER INCIDENT REPORT TO:.Mr.Norman C.Moseley Florida Power 6 Light Company Miami, Florida A~D~Schmidt.DATE OF DOCUMENT 4/4/77 DATE RECEIVED 4/18/77 ETTER CRRIGINAL Ocopv ONOTORIZED PRONCLASSIFIED I PLANT NAME:)~!ISt.Lucie Unit No.1 RJL DESCRIPTION Ltr, trans the following:
{{#Wiki_filter:DOC~T NUMBER NRV'FORM
PROP (1-P)INPUT FORM NUMBER OF COPIES RECEIVED ENCLOSURE sE<~~(2-P)<m@@BSI Ig Jiff hHBf..NOTE: IF PERSONNEL EXPOSURE IS INVOLVED SEND DIRECTLY TO KREGER/J, COLLINS Licensee Event Report (RO 50-335/77-16) on 3/5/77 concerning low steam gener'ator pressure trips being received on channel A RPS and channel A MSIS~~~~~~BRANCH CHIEF: 8 3 CYS FOR ACTION LICo ASST,: W CYS'CRS CYS S!%&INC S FOR ACTION/INFORMATION R iC~nrt NT EG RIL NRC PDR M6cE 2 MIPC SCHROEDER/IPPOLITO HOUSTON NOVAK/CHECK GRIMES CASE BUTLER HANAUER TEDESCO/MACCARY EISENHUT BAER SHAO VOLLMER/BUNCH KREGER/J COLLINS INTERNAL D R I BUTION IST LPDR0 TZC0 N E NAL DISTRIBUTION CONTROL NUMBER NRC FORM 196 (2 7GI PPJo go+5'f 4~Ivy 4 yg FLORIOA POWER&LIGHT COMPANY April 4, 1977-Px-77-PQ$
<2.7G)
j;Mr.Norman C.Moseley, Director, Region Office of Inspection and Enforcement U.S.Nuclear Regulatory Commission 230 Peachtree Street, N.W., Suite 1217 Atlanta, Georgia 30303
J5                                  U.S. NUCLEAR REGULATORV Co     SSION
                                                                                                  'SO~BM FILE NUMBER NRC DISTRIBUTION FoR PART 50 DOCKET MATERIAL                               INCIDENT REPORT TO: .                                                                                           DATE OF DOCUMENT Florida   Power 6   Light   Company               4/4/77 Miami, Florida Mr. Norman C. Moseley                        A~ D~ Schmidt.
DATE RECEIVED 4/18/77 ETTER                     ONOTORIZED         PROP                   INPUT FORM           NUMBER OF COPIES RECEIVED CRRIGINAL Ocopv PRONCLASSIFIED ENCLOSURE sE<~~
DESCRIPTION Ltr, trans          the following:                             Licensee Event Report (RO 50-335/77-16) on 3/5/77 concerning low steam gener'ator pressure trips being received on channel A RPS and channel A MSIS ~ ~ ~ ~ ~ ~
                                                                                      <m@@BSI I
PLANT NAME:                                          (1-P)        (2-P)
  )    ~
ISt. Lucie Unit            No. 1 Ig Jiff hHBf..
RJL                                                            NOTE:    IF PERSONNEL EXPOSURE IS INVOLVED SEND DIRECTLY TO KREGER/J, COLLINS FOR ACTION/INFORMATION BRANCH CHIEF:                     R iC~nrt 8 3 CYS FOR ACTION LICo ASST,:
W CYS'CRS CYS S!%&INC S NT INTERNAL D IST R I BUTION EG RIL NRC PDR M6cE               2 MIPC SCHROEDER/IPPOLITO HOUSTON NOVAK/CHECK GRIMES CASE BUTLER HANAUER TEDESCO/MACCARY EISENHUT BAER SHAO VOLLMER/BUNCH KREGER/J         COLLINS E   NAL DISTRIBUTION                                       CONTROL NUMBER LPDR0 TZC0 N
PPJo  go+ 5'f NRC FORM 196 (2 7GI


==Dear Mr.Moseley:==
4 ~
REPORTABLE OCCURRENCE 335-77-16 ST.LUCIE UNIT 1 DATE OF OCCURRENCE:
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MARCH 5, 1977 STEAM GENERATOR PRESSURE TRANSMITTER The attached Licensee Event Report is being submitted in accordance with Technical Specification 6.9 to provide 30-day notification of the subject occurrence.
 
Very truly yours, D.c it Vice President Power Resources MAS/cpc Attachment cc: Robert Lowenstein, Esquire Director, Office of Inspection and Enforcement (30)Director, Office of Management Information and Program Control (3)>7mb'dA Y$I PEOPLE...SERVING PEOPLE  
FLORIOA POWER & LIGHT COMPANY April    4, 1977
~-.e.~>~P'I P CONTROL 8LOCK LICENSEE EVENT REPORT~(PLEASE PRINT ALL RECIUIREO INFORMATION)
                                                          -Px-77-PQ$ j; Mr. Norman C. Moseley,  Director, Region Office of Inspection and Enforcement U. S. Nuclear Regulatory Commission 230 Peachtree Street, N. W., Suite 1217 Atlanta, Georgia 30303
UCENSEE NAME 01 F L S L S 1 0.7 89 14 15 REPORT AEPOAT CATEGORY TYPE SOURCE I001]coN'T~~L L 7 8 57 58 59 60 EVENT DESCRIPTION Qg Durin Power 0 eration UCENSE EVENT~UCENSE NUMSER TYPE TYPE 0-0 0 0 0 0-0 0 A 1 1 1 1 L0OO3~I 25 26 30 31 32 OOCKET NUh18EA EVENT OATE REPORT OATE 0 5 0-0 3 3 5 0 3 0 5 7 7 0 3 1 6 7 7 61 68 69 74 75 , 8O low steam enerator'essure tri s were received on channel A 89 t003j RPS and channel A MSIS.Action was taken in accordance with Technical S ecifications 7 89~4..1 ion 2.and..2.1 action'.The affected channel A tri s were 8O 80 7 8 9 Qog 7 8 9 Jog 80 d o service in 1.25 hours.This was the fourth occurrence of an ino erable RPS 80 FAS channe.The revious occurrences were re orted as LER's 335-76-5 loss of 7 8 9 PAME SYSTEM CAUSE COMPONENT COOE COOE, COMPONENT COOE SUPPUER I007I~TA~E x x x x x x z 7 8 9 10 11 12 17 43 CAUSE OESCRIPTION I008 The fuse rotectin the DC ower su 1 for z 9 9 9 a7 N 48 steam enerator channel A ressure trans-80 7 8 9 Q~I mitter PT-8013A failed.The ower su 1 and'nstrument loo were checked for other 80 7 8 9 roblems and none were found.The fuse was re laced and the channel A tri 80 set oint was OTHER STATUS NA'7 89 LOSS OR OAMAGE TO FACIUTY TYPE OESCAIPTICN z 7 89 10 PUSLICITY 7 89 7 89 FACiUTY STATUS.1 POWER 0~g 0~O 7 8 9 10 12 13 FOAM OF ACTIVITY COATENT RELEASEO OF RELEASE AhIOUNT OF ACTIVITY KRI NA 7 8 9 10 11 PERSONNEL EXPOSURES NUMSER TYPE OFSCAIPTION Q~~]~(~0 z 7 8 9 11 12 13 PERS'ONNEL
 
!N JURIES OESCAIPTION
==Dear Mr. Moseley:==
~~4 0 0 0 7 8 9 11 12 PROBABLE CONSEQUENCES Qg METHOO OF OISCOVEAY OISCOVEAY OESCAIPTION A NA 44 45 46 LOCATION OF RELEASE NA 44 45 NA NA NA NA NA 8O 80 80 60 80 80~80 AOOITIONAL FACTORS Q~g See a e two for continuation of Event Descri tion and Cause Description.
 
,7 89 80 7 89 NAME M.A.Scho man PHONEI 305/552-3779 80 CPO IISI 6IIT LICENSEE EVENT REPORT REPORTABLE OCCURRENCE 335-77-16 PAGE TWO EVENT DESCRIPTION (Continued) power caused by loose electrical connections), 335-76-17 (ESFAS setpoint drift), and 335-76-26 (loss of power due to 1C inverter failure).This occurrence was not related to the previous occurrences.
REPORTABLE OCCURRENCE 335-77-16 ST. LUCIE UNIT 1 DATE OF OCCURRENCE: MARCH 5, 1977 STEAM GENERATOR PRESSURE TRANSMITTER The attached Licensee Event Report is being submitted in accordance with Technical Specification 6.9 to provide 30-day notification of the subject occurrence.
Very truly yours, D. c it Vice President Power Resources MAS/cpc Attachment cc:   Robert Lowenstein, Esquire Director, Office of Inspection and Enforcement   (30)
Director, Office of Management Information and Program Control (3)
                                                              > 7mb'dA Y$
I PEOPLE... SERVING PEOPLE
 
      ~-.e. ~> ~
P'I P
 
LICENSEE EVENT REPORT CONTROL 8LOCK
                                                                                                                    ~
(PLEASE PRINT ALL RECIUIREO INFORMATION)
UCENSEE                                                                                           UCENSE                EVENT  ~
NAME                                       UCENSE NUMSER                                        TYPE                  TYPE 01       F     L     S   L       S   1         0   0   0       0   0   0   0   0         0         A   1   1   1     1     L0OO3~I
.7      89
                    ~
14    15                                                  25     26                     30     31     32 REPORT      AEPOAT CATEGORY          TYPE    SOURCE                OOCKET NUh18EA                             EVENT OATE                       REPORT OATE I001] coN'T                        ~L          L      0     5   0     0       3   3     5         0   3   0   5   7   7       0   3   1   6     7       7 7    8          57      58          59      60      61                                     68   69                         74     75                     ,     8O EVENT DESCRIPTION Qg Durin 89 Power 0        eration        low steam         enerator 'essure               tri s     were received on channel A 8O t003j RPS and             channel A MSIS.               Action     was   taken in accordance with Technical                         S ecifications 7 89                                                                                                                                                                   80
  ~4 7 8 9
                .     .1           ion 2.         and     .   .2.1     action'           . The   affected channel           A   tri s   were 80 Qog                     d   o   service in 1.25 hours. This was the fourth occurrence of an ino erable RPS 7    8 9                                                                                                                                                              80 Jog                FAS   channe . The revious occurrences were re orted as LER's 335-76-5 loss of 7   8 9                                                                       PAME                                                                                   80 SYSTEM       CAUSE                                             COMPONENT COOE         COOE,               COMPONENT COOE                 SUPPUER I007I   ~TA             ~E               x x x x x x                           z             z    9    9    9              N 7 8 9       10           11           12                           17         43                               a7          48 CAUSE OESCRIPTION I008       The     fuse       rotectin the             DC     ower su       1   for   steam       enerator channel             A   ressure trans-7   8 9                                                                                                                                                             80 7
Q~ I8 9 mitter       PT-8013A           failed.       The     ower su         1   and'nstrument loo were checked for other 80 7     89 roblems and none were found.                           The fuse was         re laced and the channel                   A tri     set oint       was FACiUTY 8O METHOO OF STATUS             .1 POWER                   OTHER STATUS            OISCOVEAY                          OISCOVEAY OESCAIPTION 0~g             0           ~O                                 NA                      A                                      NA 7     8       9             10               12   13                           44      45        46                                                                80 FOAM OF ACTIVITY       COATENT RELEASEO       OF RELEASE               AhIOUNT OF ACTIVITY                                                   LOCATION OF RELEASE KRI                                                           NA                                                                NA 7     8       9                 10       11                                       44        45 PERSONNEL EXPOSURES NUMSER           TYPE         OFSCAIPTION 7
Q~~]
8 9
          ~(~0           11 z
12       13 NA 80 PERS'ONNEL !NJURIES OESCAIPTION
~~4       0     0     0                                                                 NA 7 8 9                   11   12                                                                                                                                       60 PROBABLE CONSEQUENCES Qg                                                                                       NA
'7    89                                                                                                                                                                80 LOSS OR OAMAGE TO FACIUTY TYPE      OESCAIPTICN z                                                                            NA 7    89            10                                                                                                                                                  80 PUSLICITY NA 7    89                                                                                                                                                              ~ 80 AOOITIONAL FACTORS Q~ g See           a e two         for continuation of               Event Descri           tion   and Cause       Description.
,7   89                                                                                                                                                               80 7     89                                                                                                                                                             80 NAME       M. A. Scho           man                                                               305/552-3779 PHONEI CPO   IISI 6IIT
 
LICENSEE EVENT REPORT REPORTABLE OCCURRENCE 335-77-16 PAGE TWO EVENT DESCRIPTION (Continued) power caused by loose electrical connections), 335-76-17 (ESFAS setpoint drift),
and 335-76-26 (loss of power due to 1C inverter failure). This occurrence was not related to the previous occurrences.
(335-77-16).
(335-77-16).
CAUSE DESCRIPTION (Continued)
CAUSE DESCRIPTION (Continued)
Verified.
Verified.
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Latest revision as of 03:30, 3 February 2020

LER 1977-016-00 for St. Lucie Unit 1, Low Steam Generator Pressure Trips Received on Channel a RPS and Channel a MSIS
ML18110A891
Person / Time
Site: Saint Lucie NextEra Energy icon.png
Issue date: 04/04/1977
From: Schmidt A
Florida Power & Light Co
To: Moseley N
NRC/IE, NRC/RGN-II
References
PRN-LI-77-98 LER 1977-016-00
Download: ML18110A891 (7)


Text

DOC~T NUMBER NRV'FORM

<2.7G)

J5 U.S. NUCLEAR REGULATORV Co SSION

'SO~BM FILE NUMBER NRC DISTRIBUTION FoR PART 50 DOCKET MATERIAL INCIDENT REPORT TO: . DATE OF DOCUMENT Florida Power 6 Light Company 4/4/77 Miami, Florida Mr. Norman C. Moseley A~ D~ Schmidt.

DATE RECEIVED 4/18/77 ETTER ONOTORIZED PROP INPUT FORM NUMBER OF COPIES RECEIVED CRRIGINAL Ocopv PRONCLASSIFIED ENCLOSURE sE<~~

DESCRIPTION Ltr, trans the following: Licensee Event Report (RO 50-335/77-16) on 3/5/77 concerning low steam gener'ator pressure trips being received on channel A RPS and channel A MSIS ~ ~ ~ ~ ~ ~

<m@@BSI I

PLANT NAME: (1-P) (2-P)

) ~

ISt. Lucie Unit No. 1 Ig Jiff hHBf..

RJL NOTE: IF PERSONNEL EXPOSURE IS INVOLVED SEND DIRECTLY TO KREGER/J, COLLINS FOR ACTION/INFORMATION BRANCH CHIEF: R iC~nrt 8 3 CYS FOR ACTION LICo ASST,:

W CYS'CRS CYS S!%&INC S NT INTERNAL D IST R I BUTION EG RIL NRC PDR M6cE 2 MIPC SCHROEDER/IPPOLITO HOUSTON NOVAK/CHECK GRIMES CASE BUTLER HANAUER TEDESCO/MACCARY EISENHUT BAER SHAO VOLLMER/BUNCH KREGER/J COLLINS E NAL DISTRIBUTION CONTROL NUMBER LPDR0 TZC0 N

PPJo go+ 5'f NRC FORM 196 (2 7GI

4 ~

Ivy 4 yg

FLORIOA POWER & LIGHT COMPANY April 4, 1977

-Px-77-PQ$ j; Mr. Norman C. Moseley, Director, Region Office of Inspection and Enforcement U. S. Nuclear Regulatory Commission 230 Peachtree Street, N. W., Suite 1217 Atlanta, Georgia 30303

Dear Mr. Moseley:

REPORTABLE OCCURRENCE 335-77-16 ST. LUCIE UNIT 1 DATE OF OCCURRENCE: MARCH 5, 1977 STEAM GENERATOR PRESSURE TRANSMITTER The attached Licensee Event Report is being submitted in accordance with Technical Specification 6.9 to provide 30-day notification of the subject occurrence.

Very truly yours, D. c it Vice President Power Resources MAS/cpc Attachment cc: Robert Lowenstein, Esquire Director, Office of Inspection and Enforcement (30)

Director, Office of Management Information and Program Control (3)

> 7mb'dA Y$

I PEOPLE... SERVING PEOPLE

~-.e. ~> ~

P'I P

LICENSEE EVENT REPORT CONTROL 8LOCK

~

(PLEASE PRINT ALL RECIUIREO INFORMATION)

UCENSEE UCENSE EVENT ~

NAME UCENSE NUMSER TYPE TYPE 01 F L S L S 1 0 0 0 0 0 0 0 0 0 A 1 1 1 1 L0OO3~I

.7 89

~

14 15 25 26 30 31 32 REPORT AEPOAT CATEGORY TYPE SOURCE OOCKET NUh18EA EVENT OATE REPORT OATE I001] coN'T ~L L 0 5 0 0 3 3 5 0 3 0 5 7 7 0 3 1 6 7 7 7 8 57 58 59 60 61 68 69 74 75 , 8O EVENT DESCRIPTION Qg Durin 89 Power 0 eration low steam enerator 'essure tri s were received on channel A 8O t003j RPS and channel A MSIS. Action was taken in accordance with Technical S ecifications 7 89 80

~4 7 8 9

. .1 ion 2. and . .2.1 action' . The affected channel A tri s were 80 Qog d o service in 1.25 hours2.893519e-4 days <br />0.00694 hours <br />4.133598e-5 weeks <br />9.5125e-6 months <br />. This was the fourth occurrence of an ino erable RPS 7 8 9 80 Jog FAS channe . The revious occurrences were re orted as LER's 335-76-5 loss of 7 8 9 PAME 80 SYSTEM CAUSE COMPONENT COOE COOE, COMPONENT COOE SUPPUER I007I ~TA ~E x x x x x x z z 9 9 9 N 7 8 9 10 11 12 17 43 a7 48 CAUSE OESCRIPTION I008 The fuse rotectin the DC ower su 1 for steam enerator channel A ressure trans-7 8 9 80 7

Q~ I8 9 mitter PT-8013A failed. The ower su 1 and'nstrument loo were checked for other 80 7 89 roblems and none were found. The fuse was re laced and the channel A tri set oint was FACiUTY 8O METHOO OF STATUS .1 POWER OTHER STATUS OISCOVEAY OISCOVEAY OESCAIPTION 0~g 0 ~O NA A NA 7 8 9 10 12 13 44 45 46 80 FOAM OF ACTIVITY COATENT RELEASEO OF RELEASE AhIOUNT OF ACTIVITY LOCATION OF RELEASE KRI NA NA 7 8 9 10 11 44 45 PERSONNEL EXPOSURES NUMSER TYPE OFSCAIPTION 7

Q~~]

8 9

~(~0 11 z

12 13 NA 80 PERS'ONNEL !NJURIES OESCAIPTION

~~4 0 0 0 NA 7 8 9 11 12 60 PROBABLE CONSEQUENCES Qg NA

'7 89 80 LOSS OR OAMAGE TO FACIUTY TYPE OESCAIPTICN z NA 7 89 10 80 PUSLICITY NA 7 89 ~ 80 AOOITIONAL FACTORS Q~ g See a e two for continuation of Event Descri tion and Cause Description.

,7 89 80 7 89 80 NAME M. A. Scho man 305/552-3779 PHONEI CPO IISI 6IIT

LICENSEE EVENT REPORT REPORTABLE OCCURRENCE 335-77-16 PAGE TWO EVENT DESCRIPTION (Continued) power caused by loose electrical connections), 335-76-17 (ESFAS setpoint drift),

and 335-76-26 (loss of power due to 1C inverter failure). This occurrence was not related to the previous occurrences.

(335-77-16).

CAUSE DESCRIPTION (Continued)

Verified.

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