ENS 45619: Difference between revisions

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| event date = 01/11/2010 10:55 EST
| event date = 01/11/2010 10:55 EST
| last update date = 01/11/2010
| last update date = 01/11/2010
| title = Manual Reactor Trip Initiated Due To High Steam Generator Level
| title = Manual Reactor Trip Initiated Due to High Steam Generator Level
| event text = At 1055 on 1/11/2010, Turkey Point Unit 4 was manually tripped on high steam generator level. Steam generator level was high due to plant response to a turbine runback. The runback was manually initiated by stopping the 4A Steam Generator Feed Pump from the Control Room due to mechanical seal failure.
| event text = At 1055 on 1/11/2010, Turkey Point Unit 4 was manually tripped on high steam generator level. Steam generator level was high due to plant response to a turbine runback. The runback was manually initiated by stopping the 4A Steam Generator Feed Pump from the Control Room due to mechanical seal failure.
At the time of the trip, reactor power was 30%. Auxiliary Feedwater was not required since Steam Generator levels were maintained above the low level actuation setpoint.
At the time of the trip, reactor power was 30%. Auxiliary Feedwater was not required since Steam Generator levels were maintained above the low level actuation setpoint.

Latest revision as of 21:10, 1 March 2018

ENS 45619 +/-
Where
Turkey Point NextEra Energy icon.png
Florida (NRC Region 2)
Reporting
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation

10 CFR 50.72(b)(3)(iv)(A), System Actuation
Time - Person (Reporting Time:+-3.02 h-0.126 days <br />-0.018 weeks <br />-0.00414 months <br />)
Opened: Jim Speicher
12:54 Jan 11, 2010
NRC Officer: Howie Crouch
Last Updated: Jan 11, 2010
45619 - NRC Website
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