ENS 55513
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ENS Event | |
---|---|
07:00 Oct 9, 2021 | |
Title | Auxiliary Feedwater System AUTO-STARTED on Feedwater Isolation Signal |
Event Description | At 0300 EDT, with Unit 3 in Mode 3 at 0 percent power, an actuation of the Auxiliary Feedwater System occurred when steam generator water level rose to 80 percent causing a Feedwater Isolation signal, which tripped the last remaining Steam Generator Feed Pump during plant cooldown. The Auxiliary Feedwater System automatically started as designed when the feedwater isolation signal was received.
This event is being reported pursuant to 10 CFR 50.72(b)(3)(iv)(A). The NRC Resident Inspector has been notified. The cause of the high steam generator level is under investigation. |
Where | |
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Turkey Point Florida (NRC Region 2) | |
Reporting | |
10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
Time - Person (Reporting Time:+0.45 h0.0188 days <br />0.00268 weeks <br />6.1641e-4 months <br />) | |
Opened: | Ryan Frank 07:27 Oct 9, 2021 |
NRC Officer: | Howie Crouch |
Last Updated: | Oct 9, 2021 |
55513 - NRC Website
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Unit 3 | |
---|---|
Reactor critical | Not Critical |
Scram | No |
Before | Hot Standby (0 %) |
After | Hot Standby (0 %) |
WEEKMONTHYEARENS 568132023-10-25T01:59:00025 October 2023 01:59:00
[Table view]10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip ENS 567552023-09-22T22:19:00022 September 2023 22:19:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip ENS 566582023-08-04T17:20:0004 August 2023 17:20:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip ENS 555132021-10-09T07:00:0009 October 2021 07:00:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Auxiliary Feedwater System AUTO-STARTED on Feedwater Isolation Signal ENS 540722019-05-18T15:08:00018 May 2019 15:08:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due Grid Disturbance ENS 529602017-09-10T22:55:00010 September 2017 22:55:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip on Lowering Steam Generator Water Level ENS 526232017-03-18T15:07:00018 March 2017 15:07:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident, 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Reactor Trip and Loss of Ability for Unit 4 to Supply Power to Unit 3 ENS 510652015-05-12T08:30:00012 May 2015 08:30:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Trip Due to Main Generator Differential Trip ENS 506452014-11-30T18:54:00030 November 2014 18:54:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Auxiliary Feedwater Actuation Due to Planned Reactor Trip ENS 503542014-08-11T14:20:00011 August 2014 14:20:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip on Loss of Instrument Air Followed by Safety Injection ENS 500542014-04-23T17:02:00023 April 2014 17:02:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Specified System Actuation During Rod Testing ENS 489482013-04-19T21:20:00019 April 2013 21:20:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unusual Event Due to Loss of Offsite Power Greater than 15 Minutes ENS 488212013-03-13T15:20:00013 March 2013 15:20:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Afw Actuation Due to Trip of 3B Feedwater Pump ENS 487642013-02-18T06:31:00018 February 2013 06:31:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to High Seal Leakoff on Reactor Coolant Pump 3A ENS 487442013-02-12T03:36:00012 February 2013 03:36:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Turbine Trip on Loss of Condenser Vacuum ENS 464192010-11-15T11:03:00015 November 2010 11:03:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Loss of a Circulating Water Pump with Another Pump Out of Service for Maintenance ENS 462742010-09-23T21:14:00023 September 2010 21:14:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Trip Due to Inadvertent Energization Generator Trip ENS 462652010-09-22T00:17:00022 September 2010 00:17:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip ENS 462462010-09-09T19:34:0009 September 2010 19:34:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip During Startup Due to a Control Bank Step Counter Failure ENS 462352010-09-08T17:45:0008 September 2010 17:45:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip During Maintenance on a Reactor Protection System Relay ENS 456192010-01-11T15:55:00011 January 2010 15:55:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Initiated Due to High Steam Generator Level ENS 455222009-11-27T04:40:00027 November 2009 04:40:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Two Shutdown Bank Rods Were Dropped from Fully Withdrawn Position ENS 440092008-02-26T18:09:00026 February 2008 18:09:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Units 3 and 4 Tripped Due to Grid Fluctuations ENS 423992006-03-08T20:53:0008 March 2006 20:53:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Valid Actuation of Emergency Diesel Generators ENS 421372005-11-11T20:02:00011 November 2005 20:02:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip During Startup Following Failure of Rod Control Power Cabinet ENS 421042005-11-01T03:27:0001 November 2005 03:27:00 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unusual Event Declaration: Loss of Offsite Power Due to Loss of Startup Transformer ENS 420562005-10-15T11:02:00015 October 2005 11:02:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Auxiliary Feedwater Actuation on a Manual Reactor Trip ENS 418002005-06-27T07:16:00027 June 2005 07:16:00 10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release, 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Declaration of an Unusual Event Due Transformer Fire >10 Minutes ENS 415112005-03-22T08:47:00022 March 2005 08:47:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Manually Tripped Following Loss of Main Feed Pump ENS 412982004-12-29T03:46:00029 December 2004 03:46:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Generator Exciter Cooling Water Leak ENS 412322004-11-30T13:50:00030 November 2004 13:50:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specification Required Shutdown Due to Dropped Control Rod ENS 412292004-11-29T05:09:00029 November 2004 05:09:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specifications Required Shutdown Due to Dropped Control Rod ENS 407522004-05-14T21:29:00014 May 2004 21:29:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Scram Due to Lowering Steam Generator Level 2023-09-22T22:19:00 | |
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