ENS 45791: Difference between revisions

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| event date = 03/25/2010 15:40 EDT
| event date = 03/25/2010 15:40 EDT
| last update date = 04/23/2010
| last update date = 04/23/2010
| title = High Head Safety Injection Inoperable Due To Voids Identified In Piping
| title = High Head Safety Injection Inoperable Due to Voids Identified in Piping
| event text = At 1540 on 3/25/2010, engineering identified a gas void in the Unit 4 B Cold Leg High Head Safety Injection (HHSI) pipe which exceeded the station's allowable gas accumulation acceptance criteria. This condition rendered the cold leg injection flow path inoperable and required entry into Technical Specification 3.0.3 at 1540. The void was immediately vented and Technical Specification 3.0.3 was exited at 1750.
| event text = At 1540 on 3/25/2010, engineering identified a gas void in the Unit 4 B Cold Leg High Head Safety Injection (HHSI) pipe which exceeded the station's allowable gas accumulation acceptance criteria. This condition rendered the cold leg injection flow path inoperable and required entry into Technical Specification 3.0.3 at 1540. The void was immediately vented and Technical Specification 3.0.3 was exited at 1750.
The licensee notified the NRC Resident Inspector.
The licensee notified the NRC Resident Inspector.

Latest revision as of 21:09, 1 March 2018

ENS 45791 +/-
Where
Turkey Point NextEra Energy icon.png
Florida (NRC Region 2)
Reporting
10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
Time - Person (Reporting Time:+0.63 h0.0263 days <br />0.00375 weeks <br />8.62974e-4 months <br />)
Opened: Roger Montgomery
20:18 Mar 25, 2010
NRC Officer: Pete Snyder
Last Updated: Apr 23, 2010
45791 - NRC Website
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