ENS 53052: Difference between revisions

From kanterella
Jump to navigation Jump to search
(Created page by program invented by StriderTol)
 
(Created page by program invented by StriderTol)
 
Line 16: Line 16:
| event date = 11/03/2017 20:22 EDT
| event date = 11/03/2017 20:22 EDT
| last update date = 11/06/2017
| last update date = 11/06/2017
| title = Indian Point Unit 3 Reactor Trip On Low Steam Generator Level
| title = Indian Point Unit 3 Reactor Trip on Low Steam Generator Level
| event text = On November 3rd, 2017 at 2022 EDT, the Indian Point Unit 3 Reactor Protection system automatically actuated at 100 percent power. Annunciator first out indication was from 33 SG [Steam Generator] Low Level. This automatic reactor trip is reportable to the NRC under 10 CFR 50.72(b)(2)(iv)(B). All control rods fully inserted on the reactor trip. All safety systems responded as expected. The Auxiliary Feedwater System actuated as expected. Offsite power and plant electrical lineups are normal. All plant equipment responded normally to the unit trip. No primary or secondary code safeties lifted during the trip.
| event text = On November 3rd, 2017 at 2022 EDT, the Indian Point Unit 3 Reactor Protection system automatically actuated at 100 percent power. Annunciator first out indication was from 33 SG [Steam Generator] Low Level. This automatic reactor trip is reportable to the NRC under 10 CFR 50.72(b)(2)(iv)(B). All control rods fully inserted on the reactor trip. All safety systems responded as expected. The Auxiliary Feedwater System actuated as expected. Offsite power and plant electrical lineups are normal. All plant equipment responded normally to the unit trip. No primary or secondary code safeties lifted during the trip.
The Auxiliary Feedwater System actuated following the automatic trip as expected. This is reportable under 10 CFR 50.72(b)(3)(iv)(A). The Emergency Diesel Generators did not start as offsite power remained available and stable. The Unit remains on offsite power and all electrical loads are stable. Unit 3 is in Hot Standby at normal operating temperature and pressure with decay heat removal using auxiliary feedwater to the steam generators and normal heat removal through the condenser via the high pressure steam dumps. Unit 2 was unaffected and remains at 100 percent power.
The Auxiliary Feedwater System actuated following the automatic trip as expected. This is reportable under 10 CFR 50.72(b)(3)(iv)(A). The Emergency Diesel Generators did not start as offsite power remained available and stable. The Unit remains on offsite power and all electrical loads are stable. Unit 3 is in Hot Standby at normal operating temperature and pressure with decay heat removal using auxiliary feedwater to the steam generators and normal heat removal through the condenser via the high pressure steam dumps. Unit 2 was unaffected and remains at 100 percent power.

Latest revision as of 21:41, 1 March 2018

ENS 53052 +/-
Where
Indian Point Entergy icon.png
New York (NRC Region 1)
Reporting
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation

10 CFR 50.72(b)(3)(iv)(A), System Actuation
Time - Person (Reporting Time:+-3.23 h-0.135 days <br />-0.0192 weeks <br />-0.00442 months <br />)
Opened: Ovidio Ramirez
21:08 Nov 3, 2017
NRC Officer: Jeff Herrera
Last Updated: Nov 6, 2017
53052 - NRC Website
Loading map...