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{{#Wiki_filter:RIGRITY1ACCELERATEDRIDSPROCESSING),REGULATORYINFORMATIONDISTRIBUTIONSYSTEM(RIDS)r'ESSIONNBR9511210113DOC~DATE'5/11/15NOTARIZEDNOFACIL:50-335St.LuciePlant,Unit1,FloridaPower&LightCo.50-389St.LuciePlant,Unit2,FloridaPower&LightCo.AUTH.NAMEAUTHORAFFILIATIONGOLDBERG,J.H.FloridaPower&'ightCo.RECIP.NAMERECIPIENTAFFILIATIONDocumentControlBranch(DocumentControlDesk)SUBJECT:ForwardsresponsetoNRCltrreviolationsnotedininsprepts50-335/95-15&50-389/95-15.Correctiveactions:MSISwasblocked&resetimmediatelyfollowingeventon950802.IDISTRIBUTIONCODE:IE01DCOPIESRECEIVED:LTRENCLSIZE:TITLE:General(50Dkt)-InspRept/NoticeofViolationResponseNOTESDOCKETN0500033505000389INTERNAL:RECIPIENTIDCODE/NAMEPD2-1PDACRSAEOD/SPD/RABDEDRONRR/DISP/PIPBNRR/DRPM/PECBOEDIRRGN2FILE01COPIESRECIPIENTLTTRENCLIDCODE/NAME11NORRIS,J2AEOD/DEIB1A'E.1FILECENTER1/'DRC8/HFB1NUDOCS-ABSTRACT1'GC/HDS31COPIESLTTRENCL11111111111111EXTERNAL:LITCOBRYCE,JHNRCPDR1111NOAC11iNOTETOALLRIDS"RECIPIEYTS:PLEASEHELPUSTOREDUCE4VASTE!CONTACTTHEDOCL'!iIEYTCO."iTROLDESK,ROOiiIPl-37(EXT.504-2083)TOELIiIINATEYOURNA!iIEFROiIDISTRIBUTIOY.LISTSFORDOCL'IiIEi'I'S5'OUDOi"I'L'LD!TOTALNUMBEROFCOPIESREQUIRED:LTTR19ENCL19  
{{#Wiki_filter:RIGRITY1ACCELERATED
RIDSPROCESSING),
REGULATORY
INFORMATION
DISTRIBUTION
SYSTEM(RIDS)r'ESSIONNBR9511210113
DOC~DATE'5/11/15
NOTARIZED
NOFACIL:50-335
St.LuciePlant,Unit1,FloridaPower&LightCo.50-389St.LuciePlant,Unit2,FloridaPower&LightCo.AUTH.NAMEAUTHORAFFILIATION
GOLDBERG,J.H.
FloridaPower&'ightCo.RECIP.NAME
RECIPIENT
AFFILIATION
DocumentControlBranch(Document
ControlDesk)SUBJECT:ForwardsresponsetoNRCltrreviolations
notedininsprepts50-335/95-15
&50-389/95-15.Corrective
actions:MSIS
wasblocked&resetimmediately
following
eventon950802.IDISTRIBUTION
CODE:IE01DCOPIESRECEIVED:LTR
ENCLSIZE:TITLE:General(50Dkt)-Insp
Rept/Notice
ofViolation
ResponseNOTESDOCKETN0500033505000389INTERNAL:
RECIPIENT
IDCODE/NAME
PD2-1PDACRSAEOD/SPD/RAB
DEDRONRR/DISP/PIPB
NRR/DRPM/PECB
OEDIRRGN2FILE01COPIESRECIPIENT
LTTRENCLIDCODE/NAME
11NORRIS,J2AEOD/DEIB
1A'E.1FILECENTER1/'DRC8/HFB1NUDOCS-ABSTRACT
1'GC/HDS31COPIESLTTRENCL11111111111111EXTERNAL:
LITCOBRYCE,JHNRCPDR1111NOAC11iNOTETOALLRIDS"RECIPIEYTS:
PLEASEHELPUSTOREDUCE4VASTE!CONTACTTHEDOCL'!iIEYT
CO."iTROL
DESK,ROOiiIPl-37(EXT.504-2083)TOELIiIINATEYOURNA!iIEFROiIDISTRIBUTIOY.
LISTSFORDOCL'IiIEi'I'S
5'OUDOi"I'L'LD!TOTALNUMBEROFCOPIESREQUIRED:
LTTR19ENCL19  
40'  
40'  
0FloridaPowerLLightCompany,P.O.Box14000,JunoBeach,FL334080420NOV15$995L-95-30610CFR2.201U.S.NuclearRegulatoryCommissionAttn:DocumentControlDeskWashington,D.C.20555Re:St.LucieUnits1and2DocketNos.50-335and50-389ReplytoNoticeofViolationInsectionReort95-15FloridaPowerandLightCompany(FPL)hasreviewedthesubjectinspectionreportandpursuantto10CFR2.201theresponsetothenoticeofviolationisattached.Verytrulyyours,J.H.GoldbergPresident-NuclearDivisionJHG/DAS/EJBAttachmentcc:StewartD.Ebneter,RegionalAdministrator,USNRCRegionIISeniorResidentInspector,USNRC,St.LuciePlant95ii210i13'it5iii5PDRADOCK050003359PDRanFPLGroupcompany  
0FloridaPowerLLightCompany,P.O.Box14000,JunoBeach,FL334080420NOV15$995L-95-30610CFR2.201U.S.NuclearRegulatory
FPLRESPONSETOINSPECTIONREPORT95-15SUMMARYNRCInspectionReport50-335/389/95-15consideredSt.LuciePlantperformanceduringthesix(6)weekperiodfromJuly30,1995throughSeptember16,1995.Theviolationsbelowoccurredduringarelativelyshortperiodoftime,asdescribedintheinspectionreport,andseveralofthecorrectiveactionswereinstitutedfollowingananalysisoftheevents,collectively.Thecorrectivestepstoavoidfurtherviolationswereinsomecasesdeterminedtobegenericfollowingthisanalysis,andarethereforerepeatedinanumberoftheresponses.TheInspectionReportidentifiedseven(7)violationswhicharelistedbelow.ViolationA:FailuretoFollowProceduresandBlockMSISActuationViolationB:FailuretoFollowProceduresDuringRCPSealRestagingViolationC:FailuretoFollowProcedureandDocumentAbnormalValvePositionintheValve,SwitchDeviationlogViolationD:FailuretoFollowProceduresduringAlignmentofShutdownCoolingSystemViolationE:FailuretoFollowProcedureandDocumentaDeficiencyonContainmentSprayValveSurveillanceTestProcedureViolationF:FailuretoInitialMaintenanceProcedureStepsasWorkwasCompletedViolationG:FailuretoFollowProceduresDuringVentingofECCSSystemResultedinContainmentSpraydownAdditionally,bothFloridaPowerandLight(FPL)andtheNRCevaluatedplanteventstoidentifycommonunderlyingthemes.FPLpresentedasummaryofeventstotheNRConAugust29,1995.Weaknessesidentifiedinthissummaryincludedprocedurecontentanduse,aswellasmanagementoversightofeguipmentperformance.FPL'sPlantoImprovetheOperationalPerformanceatSt.LuciewasdevelopedasaresultoftheAugust29,1995,meetingandsubmittedtotheNRConSeptember15,1995.Todate,FPLhascompletedtheactivitiesaccordingtotheimprovementplanschedule.  
Commission
S=.LucieUnits1and2DocketNos.50-335and50-389ReplytoNoticeofViolationInsectionReort95-15VIOLATIONA:TechnicalSpecification6.8.1.arequiresthatwrittenproceduresbeestablished,implemented,andmaintainedcoveringtheactivitiesrecommendedinAppendixAofRegulatoryGuide1.33,Rev.2,February1978.AppendixA,paragraph1.dincludesadministrativeproceduresforproceduraladherence.ProcedureQI5-PR/PSL-1,Rev.62,"Preparation,Revision,Review/ApprovalofProcedures,"Section5.13.2,statesthatallproceduresshallbestrictlyadheredto.OP1-0030127,Rev68,"ReactorPlantCooldown-HotStandbytoColdShutdown,"required,inpart,thatoperatorsblockMainSteamIsolationSystem(MSIS)actuationwhenblockpermissiveannunciationswerereceived.ONOP1-0030131,Rev60,"PlantAnnunciatorSummary,"requiredthat,uponvalidreceiptofannunciatorsQ-18andQ-20,operatorsimmediatelyblockchannelsAandB,respectively.Contrarytotheabove,onAugust2,1995,duringacooldownofSt.LucieUnit1,validblock.permissiveannunciatorswerereceived,however,operatorsfailedtoestablishtherequiredMSISblocks,resultinginAandBchannelMSISactuations.RESPONSEA:REASONFORVIOLATIONTherootcauseofthisviolationwascognitivepersonnelerroronthepartofautilitylicensedoperatorwhofailedtoblocktheactuationofthemainsteamisolationsignal(MSIS)inaccordancewiththerequirementsoftheapprovedplantoperatingprocedure.2.CORRECTIVESTEPSTAKENANDTHERESULTSACHIEVEDA.Themainsteamisolationsignal(MSIS)wasblockedandresetimmediatelyfollowingtheeventonAugust2,1995.  
Attn:DocumentControlDeskWashington,
St.LucieUnits1and2DocketNos.50-335and50-389ReplytoNoticeofViolationInsectionReort95-153.CORRECTXVESTEPSTOAVOXDFURTHERVXOLATXONSA.Thelicensedoperatorwhowasinvolvedintheeventwascounseledontheneedtofollowproceduresandreceiveddisciplineinaccordancewithplant'policy.B.AllOperationsNuclearPlantSupervisors(NPS)heldmeetingswiththeircrewssubsequenttothiseventtoreiterateFPL'sgoalforerrorfreeperformance.C.Thiseventwillbeincorporatedintolicensedoperatorrequalificationtrainingtoemphasizeproceduralcompliance,propercommunicationamongtheControlRoom'team,andtheimportanceofsupervision-inthecontrolroommaintaininganoverallawareness,ofactivities.ThisactionwillbecompletebyJanuary1,1996.D.St.LuciePlantadoptedverbatimcomplianceastheonlyacceptablemeansofprocedurecompliance.ThisrequirementhasbeenincorporatedintoplantQualityInstructionQI5-PR/PSL-1,"Preparation,Revision,Review/ApprovalofProcedures'~"4.FullcompliancewasachievedonAugust2,1995withthecompletionofitem2above.  
D.C.20555Re:St.LucieUnits1and2DocketNos.50-335and50-389ReplytoNoticeofViolation
InsectionReort95-15FloridaPowerandLightCompany(FPL)hasreviewedthesubjectinspection
reportandpursuantto10CFR2.201theresponsetothenoticeofviolation
isattached.
Verytrulyyours,J.H.GoldbergPresident
-NuclearDivisionJHG/DAS/EJB
Attachment
cc:StewartD.Ebneter,RegionalAdministrator,
USNRCRegionIISeniorResidentInspector,
USNRC,St.LuciePlant95ii210i13
'it5iii5PDRADOCK050003359PDRanFPLGroupcompany  
FPLRESPONSETOINSPECTION
REPORT95-15SUMMARYNRCInspection
Report50-335/389/95-15
considered
St.LuciePlantperformance
duringthesix(6)weekperiodfromJuly30,1995throughSeptember
16,1995.Theviolations
belowoccurredduringarelatively
shortperiodoftime,asdescribed
intheinspection
report,andseveralofthecorrective
actionswereinstituted
following
ananalysisoftheevents,collectively.
Thecorrective
stepstoavoidfurtherviolations
wereinsomecasesdetermined
tobegenericfollowing
thisanalysis,
andaretherefore
repeatedinanumberoftheresponses.
TheInspection
Reportidentified
seven(7)violations
whicharelistedbelow.Violation
A:FailuretoFollowProcedures
andBlockMSISActuation
Violation
B:FailuretoFollowProcedures
DuringRCPSealRestaging
Violation
C:FailuretoFollowProcedure
andDocumentAbnormalValvePositionintheValve,SwitchDeviation
logViolation
D:FailuretoFollowProcedures
duringAlignment
ofShutdownCoolingSystemViolation
E:FailuretoFollowProcedure
andDocumentaDeficiency
onContainment
SprayValveSurveillance
TestProcedure
Violation
F:FailuretoInitialMaintenance
Procedure
StepsasWorkwasCompleted
Violation
G:FailuretoFollowProcedures
DuringVentingofECCSSystemResultedinContainment
Spraydown
Additionally,
bothFloridaPowerandLight(FPL)andtheNRCevaluated
planteventstoidentifycommonunderlying
themes.FPLpresented
asummaryofeventstotheNRConAugust29,1995.Weaknesses
identified
inthissummaryincludedprocedure
contentanduse,aswellasmanagement
oversight
ofeguipment
performance.
FPL'sPlantoImprovetheOperational
Performance
atSt.Luciewasdeveloped
asaresultoftheAugust29,1995,meetingandsubmitted
totheNRConSeptember
15,1995.Todate,FPLhascompleted
theactivities
according
totheimprovement
planschedule.  
S=.LucieUnits1and2DocketNos.50-335and50-389ReplytoNoticeofViolation
InsectionReort95-15VIOLATION
A:Technical
Specification
6.8.1.arequiresthatwrittenprocedures
beestablished,
implemented,
andmaintained
coveringtheactivities
recommended
inAppendixAofRegulatory
Guide1.33,Rev.2,February1978.AppendixA,paragraph
1.dincludesadministrative
procedures
forprocedural
adherence.
Procedure
QI5-PR/PSL-1,
Rev.62,"Preparation,
Revision,
Review/Approval
ofProcedures,"
Section5.13.2,statesthatallprocedures
shallbestrictlyadheredto.OP1-0030127,
Rev68,"ReactorPlantCooldown-HotStandbytoColdShutdown,"
required,
inpart,thatoperators
blockMainSteamIsolation
System(MSIS)actuation
whenblockpermissive
annunciations
werereceived.
ONOP1-0030131,
Rev60,"PlantAnnunciator
Summary,"
requiredthat,uponvalidreceiptofannunciators
Q-18andQ-20,operators
immediately
blockchannelsAandB,respectively.
Contrarytotheabove,onAugust2,1995,duringacooldownofSt.LucieUnit1,validblock.permissive
annunciators
werereceived,
however,operators
failedtoestablish
therequiredMSISblocks,resulting
inAandBchannelMSISactuations.
RESPONSEA:REASONFORVIOLATION
Therootcauseofthisviolation
wascognitive
personnel
erroronthepartofautilitylicensedoperatorwhofailedtoblocktheactuation
ofthemainsteamisolation
signal(MSIS)inaccordance
withtherequirements
oftheapprovedplantoperating
procedure.
2.CORRECTIVE
STEPSTAKENANDTHERESULTSACHIEVEDA.Themainsteamisolation
signal(MSIS)wasblockedandresetimmediately
following
theeventonAugust2,1995.  
St.LucieUnits1and2DocketNos.50-335and50-389ReplytoNoticeofViolation
InsectionReort95-153.CORRECTXVE
STEPSTOAVOXDFURTHERVXOLATXONS
A.Thelicensedoperatorwhowasinvolvedintheeventwascounseled
ontheneedtofollowprocedures
andreceiveddiscipline
inaccordance
withplant'policy.
B.AllOperations
NuclearPlantSupervisors
(NPS)heldmeetingswiththeircrewssubsequent
tothiseventtoreiterate
FPL'sgoalforerrorfreeperformance.
C.Thiseventwillbeincorporated
intolicensedoperatorrequalification
trainingtoemphasize
procedural
compliance,
propercommunication
amongtheControlRoom'team,andtheimportance
ofsupervision
-inthecontrolroommaintaining
anoverallawareness,
ofactivities.
ThisactionwillbecompletebyJanuary1,1996.D.St.LuciePlantadoptedverbatimcompliance
astheonlyacceptable
meansofprocedure
compliance.
Thisrequirement
hasbeenincorporated
intoplantQualityInstruction
QI5-PR/PSL-1,
"Preparation,
Revision,
Review/Approval
ofProcedures'~
"4.Fullcompliance
wasachievedonAugust2,1995withthecompletion
ofitem2above.  
   
   
St.LucieUnits1and2DocketNos.50-335and50-389ReplytoNoticeofViolationInsectionReort95-15VIOLATIONB:TechnicalSpecification6.8.1.arequiresthatwrittenproceduresbeestablished,implemented,andmaintainedcoveringtheactivitiesrecommendedinAppendixAofRegulatoryGuide1.33,Rev.2,February1978.AppendixA,paragraph1..dincludesadministrativeproceduresforproceduraladherence.ProcedureQI5-PR/PSL-1,Rev.62,"Preparation,Revision,Review/ApprovalofProcedures,"Section5.13.2,statesthatallproceduresshallbestrictlyadheredto.Contrarytotheabove,procedureswerenotadheredtostrictlyinthefollowingexamples:OP1-0120020,Rev.72,"FillingandVentingtheRCS,"precaution4.2,requiredthatReactorCoolantSystem(RCS)venting,describedintheprocedure,notbeattemptedifRCStemperaturewasabove200'F.OnAugust2,1995,ReactorCoolantPump(RCP)sealventing,performedinanattempttocorrectsealpackageleakageinthe1A2RCPinaccordancewithAppendixEofthesubjectprocedure,wasperformedwhileRCStemperaturewasapproximately370'F.Asaresult,designtemperaturesofRCPsealcomponentswereapproachedorexceeded.2.OP1-0120020,Rev.72,"FillingandVentingtheRCS,"AppendixE,"RestagingReactorCoolantPumpSeals,"requiredtheuseofRCPsealinjectionwhilerestagingwasattempted.OnAugust2,1995,restagingofthe1A2RCPsealpackagewasattemptedwithoutsealinjectionalignedtothesealpackage.Asaresult,designtemperaturesofRCPsealcomponentswereapproachedorexceeded.RESPONSEB:REASONFORVIOLATIONTherootcauseofthisviolationwascognitivepersonnelerroronthepartofautilitylicensedoperatorwhofailedtofollowanapprovedplantprocedurewhileperformingarestagingevolutiononaReactorCoolant'Pump(RCP)sealpackage.TheoperatordidnotstrictlyadheretotheconditionscontainedintheprocedurewhichrequiredthatRCStemperaturebenogreaterthan200'F,andthatsealinjectionbeinservice.  
St.LucieUnits1and2DocketNos.50-335and50-389ReplytoNoticeofViolation
InsectionReort95-15VIOLATION
B:Technical
Specification
6.8.1.arequiresthatwrittenprocedures
beestablished,
implemented,
andmaintained
coveringtheactivities
recommended
inAppendixAofRegulatory
Guide1.33,Rev.2,February1978.AppendixA,paragraph
1..dincludesadministrative
procedures
forprocedural
adherence.
Procedure
QI5-PR/PSL-1,
Rev.62,"Preparation,
Revision,
Review/Approval
ofProcedures,"
Section5.13.2,statesthatallprocedures
shallbestrictlyadheredto.Contrarytotheabove,procedures
werenotadheredtostrictlyinthefollowing
examples:
OP1-0120020,
Rev.72,"FillingandVentingtheRCS,"precaution
4.2,requiredthatReactorCoolantSystem(RCS)venting,described
intheprocedure,
notbeattempted
ifRCStemperature
wasabove200'F.OnAugust2,1995,ReactorCoolantPump(RCP)sealventing,performed
inanattempttocorrectsealpackageleakageinthe1A2RCPinaccordance
withAppendixEofthesubjectprocedure,
wasperformed
whileRCStemperature
wasapproximately
370'F.Asaresult,designtemperatures
ofRCPsealcomponents
wereapproached
orexceeded.
2.OP1-0120020,
Rev.72,"FillingandVentingtheRCS,"AppendixE,"Restaging
ReactorCoolantPumpSeals,"requiredtheuseofRCPsealinjection
whilerestaging
wasattempted.
OnAugust2,1995,restaging
ofthe1A2RCPsealpackagewasattempted
withoutsealinjection
alignedtothesealpackage.Asaresult,designtemperatures
ofRCPsealcomponents
wereapproached
orexceeded.
RESPONSEB:REASONFORVIOLATION
Therootcauseofthisviolation
wascognitive
personnel
erroronthepartofautilitylicensedoperatorwhofailedtofollowanapprovedplantprocedure
whileperforming
arestaging
evolution
onaReactorCoolant'Pump(RCP)sealpackage.Theoperatordidnotstrictlyadheretotheconditions
contained
intheprocedure
whichrequiredthatRCStemperature
benogreaterthan200'F,andthatsealinjection
beinservice.  
0  
0  
St.LucieUnits1and2DocketNos.50-335and50-389Reply'oNoticeofViolationInsectionReort95-152.CORRECTXVESTEPSTAKENANDTHERESULTSACHIEVEDA.TheRCP'estagingevolutionwasdiscontinued,andOperationscooledanddepressurizedtheReactorCoolantSystem(RCS)inaccordancewithapprovedplantproceduretolowerRCPsealtemperaturestowithintheacceptablerange.The1A2RCPwassecured.B.Thedamaged1A2RCPsealpackagewasreplacedpriortoreturningUnit1tooperation.3.CORRECTIVESTEPSTOAVOIDFURTHERVXOLATXONSA.Thelicensedoperatorinvolvedinthiseventwasdisciplinedinaccordancewithplantpolicy.B.TheprocedureappendixwhichwasusedforperformingtherestagingoftheRCPswasdeletedandisnolongeravailableforuse.C.PlantmanagementperformedanassessmentofthedecisionmakingprocessthatledtotherestagingoftheRCPsealundertheexistingplantconditions.Basedonthisassessment,Plantpolicy105,"PlantOperationBeyondtheEnvelopeofApprovedPlantOperatingProcedures",wasrevisedtorequireatechnicalreviewofprocedureswhicharebeingimplementedforthefirsttimeorforwhichplantconditionsaredifferentfromthosedescribedintheproceduresD.AllOperationsNuclearPlantSupervisors(NPS)heldmeetingswiththeircrewssubsequenttothiseventtoreiterateFPL'sgoalforerrorfreeperformance.E.St.LuciePlantadoptedverbatimcomplianceastheonlyacceptablemeansofprocedurecompliance.ThisrequirementhasbeenincorporatedintoplantQualityInstructionQI5-PR/PSL-1,"Preparation,Revision,Review/ApprovalofProcedures."4.FullcompliancewasachievedonAugust2,1995withthecompletionofitem2A,above.  
St.LucieUnits1and2DocketNos.50-335and50-389Reply'oNoticeofViolation
St.LucieUnits1and2DocketNos.50-335and50-389ReplytoNoticeofViolationInsectionReort95-15VIOLATIONC:TechnicalSpecification6.8.1.arequiresthatwrittenproceduresbeestablished,implemented,andmaintainedcoveringtheactivitiesrecommendedinAppendixAofRegulatoryGuide1.33,Rev.2,February1978.AppendixA,paragraph1.dincludesadministrativeproceduresforproceduraladherence.ProcedureQI5-PR/PSL-1,Rev.62,"Preparation,Revision,Review/ApprovalofProcedures,"Section5.13',statesthatallproceduresshallbestrictlyadheredto.AP1-0010123,Rev99,"AdministrativeControlsofValves,Locks,andSwitches,"step8.1.6,required,inpart,thatallvalvepositiondeviationsbedocumentedintheValveSwitchDeviationLog.Contrarytotheabove,onoraboutAugust1,1995,HCV-25-1through7wererepositionedandleftintheclosedpositionwithouttherequiredentriesbeingmadeintheValveSwitchDeviationLog.TheValves'ositionscomplicatedalossofRCSinventory.RESPONSEC:REASONFORVIOLATIONTherootcauseofthisviolationwascognitivepersonnelerroronthepartofutilitylicensedoperatorswhodidnotproperlydocumenttheclosedstatusofthesubjectvalvesintheValveSwitchDeviationLog,asrequiredbytheapprovedplantprocedure.2.CORRECTIVESTEPSTAKENANDTHERESULTSACHIEVEDTheSafeguardsPumpRoomSumpIsolationvalves,HCV25-1throughHCV25-7,wererealignedtotheopenpositionimmediatelyfollowingthelossofRCSinventoryeventonAugust10,1995,whenControlRoomoperatorsdiscoveredtheclosedstatusofthevalves.  
InsectionReort95-152.CORRECTXVE
St.LucieUnits1and2DocketNos.50-335and50-389ReplytoNoticeofViolationInsectionReort95-153.CORRECTXVESTEPSTOAVOXDFURTHERVXOLATXONSA.AllOperationsNuclearPlantSupervisors(NPS)heldmeetingswiththeircrewssubsequenttothiseventtoreiterateFPL'sgoalforerrorfreeperformance.B.C.D.Theplanthasadoptedverbatimcomplianceastheonlyacceptablemeansofprocedurecompliance.ThisrequirementhasbeenincorporatedintoplantQualityInstructionQI5-PR/PSL-1,"Preparation,Revision,Review/ApprovalofProcedures."ManagementisconductingadailyreviewofControlRoomchronologicallogstoreinforcetheexpectationfordetailandcompleteness.IPlantadministrativeprocedureshavebeenrevisedtoprovideforincreasedreviewsbyplantstaffofthelogscontrollingvalverepositioning.FullcompliancewasachievedonAugust10,1995,withthecompletionofitem2above.  
STEPSTAKENANDTHERESULTSACHIEVEDA.TheRCP'estaging
evolution
wasdiscontinued,
andOperations
cooledanddepressurized
theReactorCoolantSystem(RCS)inaccordance
withapprovedplantprocedure
tolowerRCPsealtemperatures
towithintheacceptable
range.The1A2RCPwassecured.B.Thedamaged1A2RCPsealpackagewasreplacedpriortoreturning
Unit1tooperation.
3.CORRECTIVE
STEPSTOAVOIDFURTHERVXOLATXONS
A.Thelicensedoperatorinvolvedinthiseventwasdisciplined
inaccordance
withplantpolicy.B.Theprocedure
appendixwhichwasusedforperforming
therestaging
oftheRCPswasdeletedandisnolongeravailable
foruse.C.Plantmanagement
performed
anassessment
ofthedecisionmakingprocessthatledtotherestaging
oftheRCPsealundertheexistingplantconditions.
Basedonthisassessment,
Plantpolicy105,"PlantOperation
BeyondtheEnvelopeofApprovedPlantOperating
Procedures",
wasrevisedtorequireatechnical
reviewofprocedures
whicharebeingimplemented
forthefirsttimeorforwhichplantconditions
aredifferent
fromthosedescribed
intheprocedures
D.AllOperations
NuclearPlantSupervisors
(NPS)heldmeetingswiththeircrewssubsequent
tothiseventtoreiterate
FPL'sgoalforerrorfreeperformance.
E.St.LuciePlantadoptedverbatimcompliance
astheonlyacceptable
meansofprocedure
compliance.
Thisrequirement
hasbeenincorporated
intoplantQualityInstruction
QI5-PR/PSL-1,
"Preparation,
Revision,
Review/Approval
ofProcedures."
4.Fullcompliance
wasachievedonAugust2,1995withthecompletion
ofitem2A,above.  
St.LucieUnits1and2DocketNos.50-335and50-389ReplytoNoticeofViolation
InsectionReort95-15VIOLATION
C:Technical
Specification
6.8.1.arequiresthatwrittenprocedures
beestablished,
implemented,
andmaintained
coveringtheactivities
recommended
inAppendixAofRegulatory
Guide1.33,Rev.2,February1978.AppendixA,paragraph
1.dincludesadministrative
procedures
forprocedural
adherence.
Procedure
QI5-PR/PSL-1,
Rev.62,"Preparation,
Revision,
Review/Approval
ofProcedures,"
Section5.13',statesthatallprocedures
shallbestrictlyadheredto.AP1-0010123,
Rev99,"Administrative
ControlsofValves,Locks,andSwitches,"
step8.1.6,required,
inpart,thatallvalvepositiondeviations
bedocumented
intheValveSwitchDeviation
Log.Contrarytotheabove,onoraboutAugust1,1995,HCV-25-1through7wererepositioned
andleftintheclosedpositionwithouttherequiredentriesbeingmadeintheValveSwitchDeviation
Log.TheValves'ositions
complicated
alossofRCSinventory.
RESPONSEC:REASONFORVIOLATION
Therootcauseofthisviolation
wascognitive
personnel
erroronthepartofutilitylicensedoperators
whodidnotproperlydocumenttheclosedstatusofthesubjectvalvesintheValveSwitchDeviation
Log,asrequiredbytheapprovedplantprocedure.
2.CORRECTIVE
STEPSTAKENANDTHERESULTSACHIEVEDTheSafeguards
PumpRoomSumpIsolation
valves,HCV25-1throughHCV25-7,wererealigned
totheopenpositionimmediately
following
thelossofRCSinventory
eventonAugust10,1995,whenControlRoomoperators
discovered
theclosedstatusofthevalves.  
St.LucieUnits1and2DocketNos.50-335and50-389ReplytoNoticeofViolation
InsectionReort95-153.CORRECTXVE
STEPSTOAVOXDFURTHERVXOLATXONS
A.AllOperations
NuclearPlantSupervisors
(NPS)heldmeetingswiththeircrewssubsequent
tothiseventtoreiterate
FPL'sgoalforerrorfreeperformance.
B.C.D.Theplanthasadoptedverbatimcompliance
astheonlyacceptable
meansofprocedure
compliance.
Thisrequirement
hasbeenincorporated
intoplantQualityInstruction
QI5-PR/PSL-1,
"Preparation,
Revision,
Review/Approval
ofProcedures."
Management
isconducting
adailyreviewofControlRoomchronological
logstoreinforce
theexpectation
fordetailandcompleteness.
IPlantadministrative
procedures
havebeenrevisedtoprovideforincreased
reviewsbyplantstaffofthelogscontrolling
valverepositioning.
Fullcompliance
wasachievedonAugust10,1995,withthecompletion
ofitem2above.  
   
   
St.LucieUnits1and2DocketNos.50-335and50-389ReplytoNoticeofViolationInsectionReort95-15VIOLATIOND:TechnicalSpecification6.8.1.arequiresthatwrittenproceduresbeestablished,implemented,andmaintainedcoveringtheactivitiesrecommendedinAppendixAofRegulatoryGuide1.33,Rev.2,February1978.AppendixA,paragraph1.dincludesadministrativeproceduresforproceduraladherence.ProcedureQI5-PR/PSL-1,Rev.62,"Preparation,Revision,Review/ApprovalofProcedures,"Section5'3.2,statesthatallproceduresshallbestrictlyadheredto.OP1-0410022,Rev22,"ShutdownCooling,"step8.3.7,requiredthatV3652,theBShutdownCooling(SDC)hotlegsuctionisolationvalve,belockedopenwhileplacingtheBSDCloopinservice.Contrarytotheabove,onAugust29,acontrolroomoperatorfailedtoplaceV3652inalockedopenconditionwhileplacingtheBSDCloopinservice.Asaresult,the1BLowPressureSafetyInjectionPumpwasoperatedwithitssuctionlineisolated.RESPONSED:REASONFORVIOLATIONTherootcauseofthisviolationwascognitivepersonnelerroronthepartofautilitylicensedoperatorwhofailedtoproperlyverifythealignmentoftheshutdowncooling(SDC)systemflowpathinaccordancewiththeapprovedplantprocedure,priortostartingthe1BLowPressureSafetyInjection(LPSI)Pump.Thisresultedinthefailuretoopenthe1BLPSIPumpsuctionisolationvalve.2.CORRECTIVESTEPSTAKENANDTHERESULTSACHIEVEDA.TheControlRoomoperatorsnotedtheerrorinvalvealignmentandtheLPSIpumpwassecuredapproximately5minutesafterbeingstarted.Asubsequentinspectiondeterminedthatnodamagehadoccurredduringtheshortperiodofpumpoperation.B.ThesystemwasrealignedinaccordancewiththeapprovedprocedureandtheLPSIpumpwasrestarted.SubsequentoperationoftheLPSIpumpwassatisfactory.C.AnASMESectionXIcoderunwasperformedsatisfactorilyonthe1BLPSIPumpandasubsequentEngineeringassessmentconcludedthatpumpoperabilityhadnotbeenadverselyaffected.  
St.LucieUnits1and2DocketNos.50-335and50-389ReplytoNoticeofViolation
St.LucieUnits.1and2DocketNos.50-335and50-389ReplytoNoticeofViolationInsectionReort95-153.CORRECTIVESTEPSTOAVOIDFURTHERVIOLATIONSA.Thelicensedoperatorinvolvedinthiseventwasdisciplinedinaccordancewithplantpolicy.B.OperationsimplementedprocedurechangeswhichrequiretheuseofadedicatedprocedurereadertoassistintheimplementationofSDCrelatedevolutions.C.AllOperationsNuclearPlantSupervisors(NPS)heldmeetingswiththeircrewssubsequenttothiseventtoreiterateFPL'sgoalforerrorfreeperformance.D.Theplanthasadoptedverbatimcomplianceastheonlyacceptablemeansofprocedurecompliance.ThisrequirementhasbeenincorporatedintoplantQualityInstructionQI5-PR/PSL-1,"Preparation,Revision,Review/ApprovalofProcedures."E.Thiseventwillbeincludedintolicensedoperator,requalificationtraining.ThisactionwillbecompletedbyJanuary1,1996.4.FullcompliancewasachievedonAugust29,1995withthecompletionofitem2Aand2Babove.  
InsectionReort95-15VIOLATION
St.LucieUnits1and2DocketNos.50-335and50-389ReplytoNoticeofViolationInsectionReort95-15VIOLATIONE:TechnicalSpecification6.8.1.arequiresthatwrittenproceduresbeestablished,implemented,andmaintainedcoveringtheactivitiesrecommendedinAppendixAofRegulatoryGuide1.33,Rev.2,February1978.AppendixA,paragraph1.dincludesadministrativeproceduresforproceduraladherence.ProcedureQI5-PR/PSL-1,Rev.62,"Preparation,Revision,Review/ApprovalofProcedures,"Section5.13.2,statesthatallproceduresshallbestrictlyadheredto.QI16-PR/PSL-2,Rev.1,"St.LucieActionReport(STAR)Program,"requiredthatSTARsbeinitiatedforQualityAssuranceauditfindingsandindependenttechnicalreviewrecommendations'ontrarytotheabove,aSTARwasnotgeneratedwhenaQualityAssurancereviewofaninadvertentUnit1containmentspraydown,documentedininterofficecorrespondenceJQQ-95-143,identifiedthepracticeofprelubricatingFCV-07-1A,ContainmentSprayheaderAflowcontrolvalve,whenperformingvalvestroketimetesting.RESPONSEE:1.REASONFORVIOLATIONTherootcauseofthisviolationwascognitivepersonnelerroronthepartofutilityQualityAssurance(QA)personnel.QApersonnelwereintheprocessofconductinganindependentreviewfocusingonthecontributingfactorsassociatedwithaUnit1containmentspraydownevent.Thepracticeofpre-lubricatingContainmentSprayheaderflowcontrolvalveFCV-07-lApriortosurveillancetestingwasidentifiedduringthis.review,butwasnotdeterminedtobeacontributingfactortothisevent.RecommendationstocorrectthisdeficiencywerethereforenotcontainedintheresultingQAreport,norwasaSt.LucieActionRequest(STAR)generatedinatimelymanner.2.=CORRECTIVESTEPSTAKENANDTHERESULTSACHIEVEDA.ASt.LucieActionRequest(STAR951048)wasgeneratedonSeptember7,1995todocumentthedeficientpracticeofpre-lubricatingUnit1andUnit2containmentsprayflowcontrolvalvespriortosurveillancestroketimetesting.B.TemporarychangeswereissuedtoplantsurveillanceproceduresonSeptember2,1995toremovethepracticeof'pre-lubricatingvalvespriortosurveillancetesting.10  
D:Technical
St.LucieUnits1and2DocketNos.50-335and50-389ReplytoNoticeofViolationInsectionReort95-153.CORRECTIVESTEPSTOAVOIDFURTHERVIOLATIONSA.B.C.AmeetingwasheldonSeptember13,1995betweentheVicePresidentofNuclearAssuranceandallSt.LucieQualityAssuranceandQualityControlpersonnel.Duringthismeeting,clearexpectationswereprovidedregardingthethresholdforidentificationanddocumentationofdeficienciesbyQualitypersonnel.EOnOctober25,1995,asecondmeetingwasheldbetweenthesiteQualityManagerandSt.LucieQApersonnel.Duringthismeeting,therequirementsoftheQualityInstructionQI16-PR/PSL-2,"St.LucieActionReport(STAR)Program"werereviewed.TheresponsibilityofQApersonnelfortimelyidentificationanddocumentationofdeficienciesinaccordancewiththisprocedurewasreinforced.Permanentchangeswillbemadetoplantsurveillanceprocedurestodiscontinuethepracticeofpre-testlubricationofthevalvespriortosurveillancetesting.ThisactionwillbecompletedbyDecember1,1995.4.FullcompliancewasachievedonSeptember7,1995withthecompletionofitem2Aabove.  
Specification
St.LucieUnits1and2DocketNos.50-335and50-389ReplytoNoticeofViolationInsectionReort95-15VIOLATIONF:TechnicalSpecification6.8~1.arequiresthatwrittenproceduresbeestablished,implemented,andmaintainedcoveringtheactivitiesrecommendedinAppendixAofRegulatoryGuide1.33,Rev.2,February1978.AppendixA,paragraph1.dincludesadministrativeproceduresforproceduraladherence.ProcedureQI5-PR/PSL-1,Rev.62,"Preparation,Revision,Review/ApprovalofProcedures,"Section5.13.2,statesthatallproceduresshallbestrictlyadheredto.ADM-08.02,Rev7,"ConductofMaintenance,"Appendix5,step5,requiredthatproceduresbepresentduringworkandthatindividualstepsbeinitialedonceperformed.Contrarytotheabove,inspectionofworkinprogressrevealedthatindividualstepswerenotinitialedonceperformeduponcompletionforworkconductedinaccordancewithPlantChange/Modification11-195.RESPONSEF:1.REASONFORVIOLATIONTherootcauseofthisviolationwascognitivepersonnelerroronthepartofanElectricalDepartmentjourneymanwhofailedtoproperlydocumentthecompletionofstepswhileperformingworkactivitiesassociatedwiththetripsolenoidsonthe1BEmergencyDieselGenerator(EDG).Thestepswerenotinitialedastheywerebeingperformed,inaccordancewithapprovedplantprocedure.2.CORRECTIVESTEPSTAKENANDTHERESULTSACHIEVEDA.ThestepsofthemaintenanceprocedurebeingworkedweresignedoffbythejourneymanimmediatelyfollowingthecompletionoftheworkonAugust31,1995,andthecompletedprocedurewasreviewedbythechiefelectricianandElectricalsupervisor.B.TheEDGcircuitrywassubsequentlytestedfollowingcompletionoftheworkonAugust31,1995,andperformedsatisfactorily.12  
6.8.1.arequiresthatwrittenprocedures
beestablished,
implemented,
andmaintained
coveringtheactivities
recommended
inAppendixAofRegulatory
Guide1.33,Rev.2,February1978.AppendixA,paragraph
1.dincludesadministrative
procedures
forprocedural
adherence.
Procedure
QI5-PR/PSL-1,
Rev.62,"Preparation,
Revision,
Review/Approval
ofProcedures,"
Section5'3.2,statesthatallprocedures
shallbestrictlyadheredto.OP1-0410022,
Rev22,"Shutdown
Cooling,"
step8.3.7,requiredthatV3652,theBShutdownCooling(SDC)hotlegsuctionisolation
valve,belockedopenwhileplacingtheBSDCloopinservice.Contrarytotheabove,onAugust29,acontrolroomoperatorfailedtoplaceV3652inalockedopencondition
whileplacingtheBSDCloopinservice.Asaresult,the1BLowPressureSafetyInjection
Pumpwasoperatedwithitssuctionlineisolated.
RESPONSED:REASONFORVIOLATION
Therootcauseofthisviolation
wascognitive
personnel
erroronthepartofautilitylicensedoperatorwhofailedtoproperlyverifythealignment
oftheshutdowncooling(SDC)systemflowpathinaccordance
withtheapprovedplantprocedure,
priortostartingthe1BLowPressureSafetyInjection
(LPSI)Pump.Thisresultedinthefailuretoopenthe1BLPSIPumpsuctionisolation
valve.2.CORRECTIVE
STEPSTAKENANDTHERESULTSACHIEVEDA.TheControlRoomoperators
notedtheerrorinvalvealignment
andtheLPSIpumpwassecuredapproximately
5minutesafterbeingstarted.Asubsequent
inspection
determined
thatnodamagehadoccurredduringtheshortperiodofpumpoperation.
B.Thesystemwasrealigned
inaccordance
withtheapprovedprocedure
andtheLPSIpumpwasrestarted.
Subsequent
operation
oftheLPSIpumpwassatisfactory.
C.AnASMESectionXIcoderunwasperformed
satisfactorily
onthe1BLPSIPumpandasubsequent
Engineering
assessment
concluded
thatpumpoperability
hadnotbeenadversely
affected.  
St.LucieUnits.1and2DocketNos.50-335and50-389ReplytoNoticeofViolation
InsectionReort95-153.CORRECTIVE
STEPSTOAVOIDFURTHERVIOLATIONS
A.Thelicensedoperatorinvolvedinthiseventwasdisciplined
inaccordance
withplantpolicy.B.Operations
implemented
procedure
changeswhichrequiretheuseofadedicated
procedure
readertoassistintheimplementation
ofSDCrelatedevolutions.
C.AllOperations
NuclearPlantSupervisors
(NPS)heldmeetingswiththeircrewssubsequent
tothiseventtoreiterate
FPL'sgoalforerrorfreeperformance.
D.Theplanthasadoptedverbatimcompliance
astheonlyacceptable
meansofprocedure
compliance.
Thisrequirement
hasbeenincorporated
intoplantQualityInstruction
QI5-PR/PSL-1,
"Preparation,
Revision,
Review/Approval
ofProcedures."
E.Thiseventwillbeincludedintolicensedoperator,
requalification
training.
Thisactionwillbecompleted
byJanuary1,1996.4.Fullcompliance
wasachievedonAugust29,1995withthecompletion
ofitem2Aand2Babove.  
St.LucieUnits1and2DocketNos.50-335and50-389ReplytoNoticeofViolation
InsectionReort95-15VIOLATION
E:Technical
Specification
6.8.1.arequiresthatwrittenprocedures
beestablished,
implemented,
andmaintained
coveringtheactivities
recommended
inAppendixAofRegulatory
Guide1.33,Rev.2,February1978.AppendixA,paragraph
1.dincludesadministrative
procedures
forprocedural
adherence.
Procedure
QI5-PR/PSL-1,
Rev.62,"Preparation,
Revision,
Review/Approval
ofProcedures,"
Section5.13.2,statesthatallprocedures
shallbestrictlyadheredto.QI16-PR/PSL-2,
Rev.1,"St.LucieActionReport(STAR)Program,"
requiredthatSTARsbeinitiated
forQualityAssurance
auditfindingsandindependent
technical
reviewrecommendations'ontrary
totheabove,aSTARwasnotgenerated
whenaQualityAssurance
reviewofaninadvertent
Unit1containment
spraydown,
documented
ininteroffice
correspondence
JQQ-95-143,
identified
thepracticeofprelubricating
FCV-07-1A,
Containment
SprayheaderAflowcontrolvalve,whenperforming
valvestroketimetesting.RESPONSEE:1.REASONFORVIOLATION
Therootcauseofthisviolation
wascognitive
personnel
erroronthepartofutilityQualityAssurance
(QA)personnel.
QApersonnel
wereintheprocessofconducting
anindependent
reviewfocusingonthecontributing
factorsassociated
withaUnit1containment
spraydownevent.Thepracticeofpre-lubricating
Containment
SprayheaderflowcontrolvalveFCV-07-lApriortosurveillance
testingwasidentified
duringthis.review,butwasnotdetermined
tobeacontributing
factortothisevent.Recommendations
tocorrectthisdeficiency
weretherefore
notcontained
intheresulting
QAreport,norwasaSt.LucieActionRequest(STAR)generated
inatimelymanner.2.=CORRECTIVE
STEPSTAKENANDTHERESULTSACHIEVEDA.ASt.LucieActionRequest(STAR951048)wasgenerated
onSeptember
7,1995todocumentthedeficient
practiceofpre-lubricating
Unit1andUnit2containment
sprayflowcontrolvalvespriortosurveillance
stroketimetesting.B.Temporary
changeswereissuedtoplantsurveillance
procedures
onSeptember
2,1995toremovethepracticeof'pre-lubricating
valvespriortosurveillance
testing.10  
St.LucieUnits1and2DocketNos.50-335and50-389ReplytoNoticeofViolation
InsectionReort95-153.CORRECTIVE
STEPSTOAVOIDFURTHERVIOLATIONS
A.B.C.AmeetingwasheldonSeptember
13,1995betweentheVicePresident
ofNuclearAssurance
andallSt.LucieQualityAssurance
andQualityControlpersonnel.
Duringthismeeting,clearexpectations
wereprovidedregarding
thethreshold
foridentification
anddocumentation
ofdeficiencies
byQualitypersonnel.
EOnOctober25,1995,asecondmeetingwasheldbetweenthesiteQualityManagerandSt.LucieQApersonnel.
Duringthismeeting,therequirements
oftheQualityInstruction
QI16-PR/PSL-2,
"St.LucieActionReport(STAR)Program"werereviewed.
Theresponsibility
ofQApersonnel
fortimelyidentification
anddocumentation
ofdeficiencies
inaccordance
withthisprocedure
wasreinforced.
Permanent
changeswillbemadetoplantsurveillance
procedures
todiscontinue
thepracticeofpre-testlubrication
ofthevalvespriortosurveillance
testing.Thisactionwillbecompleted
byDecember1,1995.4.Fullcompliance
wasachievedonSeptember
7,1995withthecompletion
ofitem2Aabove.  
St.LucieUnits1and2DocketNos.50-335and50-389ReplytoNoticeofViolation
InsectionReort95-15VIOLATION
F:Technical
Specification
6.8~1.arequiresthatwrittenprocedures
beestablished,
implemented,
andmaintained
coveringtheactivities
recommended
inAppendixAofRegulatory
Guide1.33,Rev.2,February1978.AppendixA,paragraph
1.dincludesadministrative
procedures
forprocedural
adherence.
Procedure
QI5-PR/PSL-1,
Rev.62,"Preparation,
Revision,
Review/Approval
ofProcedures,"
Section5.13.2,statesthatallprocedures
shallbestrictlyadheredto.ADM-08.02,
Rev7,"ConductofMaintenance,"
Appendix5,step5,requiredthatprocedures
bepresentduringworkandthatindividual
stepsbeinitialed
onceperformed.
Contrarytotheabove,inspection
ofworkinprogressrevealedthatindividual
stepswerenotinitialed
onceperformed
uponcompletion
forworkconducted
inaccordance
withPlantChange/Modification
11-195.RESPONSEF:1.REASONFORVIOLATION
Therootcauseofthisviolation
wascognitive
personnel
erroronthepartofanElectrical
Department
journeyman
whofailedtoproperlydocumentthecompletion
ofstepswhileperforming
workactivities
associated
withthetripsolenoids
onthe1BEmergency
DieselGenerator
(EDG).Thestepswerenotinitialed
astheywerebeingperformed,
inaccordance
withapprovedplantprocedure.
2.CORRECTIVE
STEPSTAKENANDTHERESULTSACHIEVEDA.Thestepsofthemaintenance
procedure
beingworkedweresignedoffbythejourneyman
immediately
following
thecompletion
oftheworkonAugust31,1995,andthecompleted
procedure
wasreviewedbythechiefelectrician
andElectrical
supervisor.
B.TheEDGcircuitry
wassubsequently
testedfollowing
completion
oftheworkonAugust31,1995,andperformed
satisfactorily.
12  
0  
0  
St.LucieUnits1and2DocketNos.50-335and50-389ReplytoNoticeofViolationInsectionReort95-153.CORRECTIVESTEPSTOAVOIDFURTHERVIOLATIONSA.MeetingswereheldfollowingthiseventwithElectricalMaintenanceemployeestoreviewthisincidentandemphasizemanagementexpectationsregardingthedocumentationofw'orkactivities.B.SupervisorsfromeachMaintenancedisciplinehaveconductedmeetingswiththeiremployeestoreinforcetheneedforstrictadherencetotheadministrativerequirementsrelatedtoprocedureuse.C.Theplanthasadoptedverbatimcomplianceastheonlyacceptablemeansofprocedurecompliance.ThisrequirementhasbeenincorporatedintoplantQualityInstructionQI5-PR/PSL-1,"Preparation,Revision,Review/ApprovalofProcedures."4.FullcompliancewasachievedonAugust31,1995withthecompletionofitem2Aand2Babove.13  
St.LucieUnits1and2DocketNos.50-335and50-389ReplytoNoticeofViolation
St.LucieUnits1and2DocketNos.50-335and50-389ReplytoNoticeofViolationInsectionReort95-15VIOLATIONG:10CFR50AppendixB,CriterionV,"Instructions,Procedures,andDrawings,"requires,inpart,thatactivitiesaffectingqualityshallbeprescribedbydocumentedproceduresofatypeappropriatetothecircumstances.Contrarytotheabove,onAugust18,1995,ventingoftheLowPressureSafetyInjection(LPSI)Systemwasconductedinaccordancewithaprocedurewhichwasinappropriatetothecircumstances.Specifically,OP1-0420060,Rev.0,"VentingoftheEmergencyCoreCoolingandContainmentSpraySystems,"didnotrequireaverificationthattheportionsofthesystembeingventedwerehydraulicallyisolatedfromadjacentsystemsandflowpaths.Asaresultofthisfailuretoestablishproperinitialconditions,waterdrivenbythe1ALPSIpumpwasinadvertentlydirectedtotheATrainContainmentSprayheader,resultinginaspraydownoftheUnit1ReactorContainmentBuilding.RESPONSEG:REASONFORVIOLATIONTherootcauseofthisviolationwasproceduraldeficiencyinthattheECCSventingprocedure,OP1-0420060,didnotstatetheplantconditionsrequiredtosuccessfullyventtheECCSbutreliedupontheRCSheatupproceduretosetplantconditions.Specifically,theventingproceduredidnotrequireoperatorstoverifythatthepropercontainmentsprayheaderisolationvalveswereclosedpriortorecirculatingthewaterintheSDCsystem.AcontributingfactortothiseventwasthattheoperationspersonnelperformingtheECCSventingproceduredidnotrecognizethattheexistingplantconditionswouldresultinflowtothe'A'ontainmentsprayheaderwhenflowwasalignedthroughtheShutdownCoolingHeatExchanger.AsecondcontributingfactorofthiseventwasthatFCV-07-1AwasplacedintheopenpositionbecausethisvalvehadfaileditsASMEstroketimetest.Plantmanagementmadethedecisiontodeferthevalverepairandpositionthisnormallyclosedvalvetoitsengineeredsafeguardsopenpositioninlieuofrepairingthevalvepriortostartup.14  
InsectionReort95-153.CORRECTIVE
St.LucieUnits1and2DocketNos.50-335and50-389ReplytoNoticeofViolationInsectionReort95-152.CORRECTIVESTEPSTAKENANDTHERESULTSACHIEVEDA.Operatorssecuredthe1ALPSIPumpandisolated,theflowpathtothecontainmentsprayheaderfromtheLPSIPump.TheReactorCavitysumpwasdrainedtotheWasteManagementSystem.B~Followingtheevent,allnonessentialworkatthesitewasplacedonhold,andUnit1wasmaintainedstableinMode3whileseniorplantmanagementconductedmeetingswithallavailablesitepersonneltostresstheneedforworkervigilanceandattentiontodetail.Theneedtoreduceequipmentdeficienciesthatimpactoperationswasalsodiscussed.C.Unit1wascooleddownanddepressurizedtoMode,5andaninspectionanddecontaminationofcontainmentwasthenconducted.TheeventwasevaluatedunderanEngineeringevaluation,whichresultedinacomprehensiveinspectionofcomponentsinsidecontainmenttoensurefuturecomponentreliability.D.Operatingprocedure,OP1-0420060,"VentingoftheEmergencyCoreCoolingan'dContainmentSpraySystem",wasrevisedSeptember1,1995toincludetheplantconditionsrequiredtobepresentduringventing.3.CORRECTIVESTEPSTOAVOIDFURTHERVIOLATIONSA.Plantpolicy105,"PlantOperationBeyondtheEnvelopeofApprovedPlantOperatingProcedures",wasrevisedtorequireatechnicalreviewofprocedureswhicharebeingimplementedforthefirsttimeorforwhichplantconditionsaredifferentfromthosedescribedintheprocedure.B.TheMaintenanceDepartmentestablishedateamcomposedofplantstaffandengineeringpersonnel,todeterminetherootcausefortheContainmentSprayheaderisolationvalverepeatfailuresanddeterminecorrectiveactionstoeliminatethisoperatorworkaround.FCV-07-1AwasrepairedpriortoreturningUnit1toservice.15  
STEPSTOAVOIDFURTHERVIOLATIONS
St.LucieUnits1and2DocketNos.50-335and50-389ReplytoNoticeofViolationInsectionReort95-15C.Existingplantdeficiencieswerereviewedbyseniorplantmanagement.AdditionaldeficiencieswhichcouldimpactoperationswereaddedtotheworkscopeoftheUnit1shutdown.Thesedeficiencieswerecorrectedpriortoreturningtheunittoservice.D.Administrativeprocedure,AP-0010147,"AssessmentofAbnormalPlantConfigurationsorSignificantMaterialDeficient'ConditionsonPlantOperation",wasdevelopedtoenhanceoutagescopereviewandensurethatequipmentdeficienciesarerestoredinatimelymanner.E.St.Luciemanagementinstitutedaweeklyreviewofappropriateperformanceindicatorsandworkbacklogstatus,includingtheageofopenitemsandoperatorworkarounds.F.AllOperationsNuclearPlantSupervisors(NPS)heldmeetingswiththeircrewssubsequenttothiseventtoreiterateFPL'sgoalforerro'rfreeperformance.G.Thiseventwillbeincorporatedintolicensedoperatorrequalificationtraining.ThisactionwillbecompletebyJanuary1,1996.4.FullcompliancewasachievedonAugust18,1995withthecompletionofitems2A,2Cand2Dabove.16
A.Meetingswereheldfollowing
thiseventwithElectrical
Maintenance
employees
toreviewthisincidentandemphasize
management
expectations
regarding
thedocumentation
ofw'orkactivities.
B.Supervisors
fromeachMaintenance
discipline
haveconducted
meetingswiththeiremployees
toreinforce
theneedforstrictadherence
totheadministrative
requirements
relatedtoprocedure
use.C.Theplanthasadoptedverbatimcompliance
astheonlyacceptable
meansofprocedure
compliance.
Thisrequirement
hasbeenincorporated
intoplantQualityInstruction
QI5-PR/PSL-1,
"Preparation,
Revision,
Review/Approval
ofProcedures."
4.Fullcompliance
wasachievedonAugust31,1995withthecompletion
ofitem2Aand2Babove.13  
St.LucieUnits1and2DocketNos.50-335and50-389ReplytoNoticeofViolation
InsectionReort95-15VIOLATION
G:10CFR50AppendixB,Criterion
V,"Instructions,
Procedures,
andDrawings,"
requires,
inpart,thatactivities
affecting
qualityshallbeprescribed
bydocumented
procedures
ofatypeappropriate
tothecircumstances.
Contrarytotheabove,onAugust18,1995,ventingoftheLowPressureSafetyInjection
(LPSI)Systemwasconducted
inaccordance
withaprocedure
whichwasinappropriate
tothecircumstances.
Specifically,
OP1-0420060,
Rev.0,"VentingoftheEmergency
CoreCoolingandContainment
SpraySystems,"
didnotrequireaverification
thattheportionsofthesystembeingventedwerehydraulically
isolatedfromadjacentsystemsandflowpaths.
Asaresultofthisfailuretoestablish
properinitialconditions,
waterdrivenbythe1ALPSIpumpwasinadvertently
directedtotheATrainContainment
Sprayheader,resulting
inaspraydown
oftheUnit1ReactorContainment
Building.
RESPONSEG:REASONFORVIOLATION
Therootcauseofthisviolation
wasprocedural
deficiency
inthattheECCSventingprocedure,
OP1-0420060,
didnotstatetheplantconditions
requiredtosuccessfully
venttheECCSbutreliedupontheRCSheatupprocedure
tosetplantconditions.
Specifically,
theventingprocedure
didnotrequireoperators
toverifythatthepropercontainment
sprayheaderisolation
valveswereclosedpriortorecirculating
thewaterintheSDCsystem.Acontributing
factortothiseventwasthattheoperations
personnel
performing
theECCSventingprocedure
didnotrecognize
thattheexistingplantconditions
wouldresultinflowtothe'A'ontainment
sprayheaderwhenflowwasalignedthroughtheShutdownCoolingHeatExchanger.
Asecondcontributing
factorofthiseventwasthatFCV-07-1A
wasplacedintheopenpositionbecausethisvalvehadfaileditsASMEstroketimetest.Plantmanagement
madethedecisiontodeferthevalverepairandpositionthisnormallyclosedvalvetoitsengineered
safeguards
openpositioninlieuofrepairing
thevalvepriortostartup.14  
St.LucieUnits1and2DocketNos.50-335and50-389ReplytoNoticeofViolation
InsectionReort95-152.CORRECTIVE
STEPSTAKENANDTHERESULTSACHIEVEDA.Operators
securedthe1ALPSIPumpandisolated,
theflowpathtothecontainment
sprayheaderfromtheLPSIPump.TheReactorCavitysumpwasdrainedtotheWasteManagement
System.B~Following
theevent,allnonessential
workatthesitewasplacedonhold,andUnit1wasmaintained
stableinMode3whileseniorplantmanagement
conducted
meetingswithallavailable
sitepersonnel
tostresstheneedforworkervigilance
andattention
todetail.Theneedtoreduceequipment
deficiencies
thatimpactoperations
wasalsodiscussed.
C.Unit1wascooleddownanddepressurized
toMode,5andaninspection
anddecontamination
ofcontainment
wasthenconducted.
Theeventwasevaluated
underanEngineering
evaluation,
whichresultedinacomprehensive
inspection
ofcomponents
insidecontainment
toensurefuturecomponent
reliability.
D.Operating
procedure,
OP1-0420060,
"VentingoftheEmergency
CoreCoolingan'dContainment
SpraySystem",wasrevisedSeptember
1,1995toincludetheplantconditions
requiredtobepresentduringventing.3.CORRECTIVE
STEPSTOAVOIDFURTHERVIOLATIONS
A.Plantpolicy105,"PlantOperation
BeyondtheEnvelopeofApprovedPlantOperating
Procedures",
wasrevisedtorequireatechnical
reviewofprocedures
whicharebeingimplemented
forthefirsttimeorforwhichplantconditions
aredifferent
fromthosedescribed
intheprocedure.
B.TheMaintenance
Department
established
ateamcomposedofplantstaffandengineering
personnel,
todetermine
therootcausefortheContainment
Sprayheaderisolation
valverepeatfailuresanddetermine
corrective
actionstoeliminate
thisoperatorworkaround.
FCV-07-1A
wasrepairedpriortoreturning
Unit1toservice.15  
St.LucieUnits1and2DocketNos.50-335and50-389ReplytoNoticeofViolation
InsectionReort95-15C.Existingplantdeficiencies
werereviewedbyseniorplantmanagement.
Additional
deficiencies
whichcouldimpactoperations
wereaddedtotheworkscopeoftheUnit1shutdown.
Thesedeficiencies
werecorrected
priortoreturning
theunittoservice.D.Administrative
procedure,
AP-0010147,
"Assessment
ofAbnormalPlantConfigurations
orSignificant
MaterialDeficient
'Conditions
onPlantOperation",
wasdeveloped
toenhanceoutagescopereviewandensurethatequipment
deficiencies
arerestoredinatimelymanner.E.St.Luciemanagement
instituted
aweeklyreviewofappropriate
performance
indicators
andworkbacklogstatus,including
theageofopenitemsandoperatorworkarounds.
F.AllOperations
NuclearPlantSupervisors
(NPS)heldmeetingswiththeircrewssubsequent
tothiseventtoreiterate
FPL'sgoalforerro'rfreeperformance.
G.Thiseventwillbeincorporated
intolicensedoperatorrequalification
training.
ThisactionwillbecompletebyJanuary1,1996.4.Fullcompliance
wasachievedonAugust18,1995withthecompletion
ofitems2A,2Cand2Dabove.16
}}
}}

Revision as of 15:54, 29 June 2018

Forwards Response to NRC Ltr Re Violations Noted in Insp Repts 50-335/95-15 & 50-389/95-15.Corrective Actions:Msis Was Blocked & Reset Immediately Following Event on 950802
ML17228B327
Person / Time
Site: Saint Lucie  NextEra Energy icon.png
Issue date: 11/15/1995
From: GOLDBERG J H
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
L-95-306, NUDOCS 9511210113
Download: ML17228B327 (23)


See also: IR 05000335/1995015

Text

RIGRITY1ACCELERATED

RIDSPROCESSING),

REGULATORY

INFORMATION

DISTRIBUTION

SYSTEM(RIDS)r'ESSIONNBR9511210113

DOC~DATE'5/11/15

NOTARIZED

NOFACIL:50-335

St.LuciePlant,Unit1,FloridaPower&LightCo.50-389St.LuciePlant,Unit2,FloridaPower&LightCo.AUTH.NAMEAUTHORAFFILIATION

GOLDBERG,J.H.

FloridaPower&'ightCo.RECIP.NAME

RECIPIENT

AFFILIATION

DocumentControlBranch(Document

ControlDesk)SUBJECT:ForwardsresponsetoNRCltrreviolations

notedininsprepts50-335/95-15

&50-389/95-15.Corrective

actions:MSIS

wasblocked&resetimmediately

following

eventon950802.IDISTRIBUTION

CODE:IE01DCOPIESRECEIVED:LTR

ENCLSIZE:TITLE:General(50Dkt)-Insp

Rept/Notice

ofViolation

ResponseNOTESDOCKETN0500033505000389INTERNAL:

RECIPIENT

IDCODE/NAME

PD2-1PDACRSAEOD/SPD/RAB

DEDRONRR/DISP/PIPB

NRR/DRPM/PECB

OEDIRRGN2FILE01COPIESRECIPIENT

LTTRENCLIDCODE/NAME

11NORRIS,J2AEOD/DEIB

1A'E.1FILECENTER1/'DRC8/HFB1NUDOCS-ABSTRACT

1'GC/HDS31COPIESLTTRENCL11111111111111EXTERNAL:

LITCOBRYCE,JHNRCPDR1111NOAC11iNOTETOALLRIDS"RECIPIEYTS:

PLEASEHELPUSTOREDUCE4VASTE!CONTACTTHEDOCL'!iIEYT

CO."iTROL

DESK,ROOiiIPl-37(EXT.504-2083)TOELIiIINATEYOURNA!iIEFROiIDISTRIBUTIOY.

LISTSFORDOCL'IiIEi'I'S

5'OUDOi"I'L'LD!TOTALNUMBEROFCOPIESREQUIRED:

LTTR19ENCL19

40'

0FloridaPowerLLightCompany,P.O.Box14000,JunoBeach,FL334080420NOV15$995L-95-30610CFR2.201U.S.NuclearRegulatory

Commission

Attn:DocumentControlDeskWashington,

D.C.20555Re:St.LucieUnits1and2DocketNos.50-335and50-389ReplytoNoticeofViolation

InsectionReort95-15FloridaPowerandLightCompany(FPL)hasreviewedthesubjectinspection

reportandpursuantto10CFR2.201theresponsetothenoticeofviolation

isattached.

Verytrulyyours,J.H.GoldbergPresident

-NuclearDivisionJHG/DAS/EJB

Attachment

cc:StewartD.Ebneter,RegionalAdministrator,

USNRCRegionIISeniorResidentInspector,

USNRC,St.LuciePlant95ii210i13

'it5iii5PDRADOCK050003359PDRanFPLGroupcompany

FPLRESPONSETOINSPECTION

REPORT95-15SUMMARYNRCInspection

Report50-335/389/95-15

considered

St.LuciePlantperformance

duringthesix(6)weekperiodfromJuly30,1995throughSeptember

16,1995.Theviolations

belowoccurredduringarelatively

shortperiodoftime,asdescribed

intheinspection

report,andseveralofthecorrective

actionswereinstituted

following

ananalysisoftheevents,collectively.

Thecorrective

stepstoavoidfurtherviolations

wereinsomecasesdetermined

tobegenericfollowing

thisanalysis,

andaretherefore

repeatedinanumberoftheresponses.

TheInspection

Reportidentified

seven(7)violations

whicharelistedbelow.Violation

A:FailuretoFollowProcedures

andBlockMSISActuation

Violation

B:FailuretoFollowProcedures

DuringRCPSealRestaging

Violation

C:FailuretoFollowProcedure

andDocumentAbnormalValvePositionintheValve,SwitchDeviation

logViolation

D:FailuretoFollowProcedures

duringAlignment

ofShutdownCoolingSystemViolation

E:FailuretoFollowProcedure

andDocumentaDeficiency

onContainment

SprayValveSurveillance

TestProcedure

Violation

F:FailuretoInitialMaintenance

Procedure

StepsasWorkwasCompleted

Violation

G:FailuretoFollowProcedures

DuringVentingofECCSSystemResultedinContainment

Spraydown

Additionally,

bothFloridaPowerandLight(FPL)andtheNRCevaluated

planteventstoidentifycommonunderlying

themes.FPLpresented

asummaryofeventstotheNRConAugust29,1995.Weaknesses

identified

inthissummaryincludedprocedure

contentanduse,aswellasmanagement

oversight

ofeguipment

performance.

FPL'sPlantoImprovetheOperational

Performance

atSt.Luciewasdeveloped

asaresultoftheAugust29,1995,meetingandsubmitted

totheNRConSeptember

15,1995.Todate,FPLhascompleted

theactivities

according

totheimprovement

planschedule.

S=.LucieUnits1and2DocketNos.50-335and50-389ReplytoNoticeofViolation

InsectionReort95-15VIOLATION

A:Technical

Specification

6.8.1.arequiresthatwrittenprocedures

beestablished,

implemented,

andmaintained

coveringtheactivities

recommended

inAppendixAofRegulatory

Guide1.33,Rev.2,February1978.AppendixA,paragraph

1.dincludesadministrative

procedures

forprocedural

adherence.

Procedure

QI5-PR/PSL-1,

Rev.62,"Preparation,

Revision,

Review/Approval

ofProcedures,"

Section5.13.2,statesthatallprocedures

shallbestrictlyadheredto.OP1-0030127,

Rev68,"ReactorPlantCooldown-HotStandbytoColdShutdown,"

required,

inpart,thatoperators

blockMainSteamIsolation

System(MSIS)actuation

whenblockpermissive

annunciations

werereceived.

ONOP1-0030131,

Rev60,"PlantAnnunciator

Summary,"

requiredthat,uponvalidreceiptofannunciators

Q-18andQ-20,operators

immediately

blockchannelsAandB,respectively.

Contrarytotheabove,onAugust2,1995,duringacooldownofSt.LucieUnit1,validblock.permissive

annunciators

werereceived,

however,operators

failedtoestablish

therequiredMSISblocks,resulting

inAandBchannelMSISactuations.

RESPONSEA:REASONFORVIOLATION

Therootcauseofthisviolation

wascognitive

personnel

erroronthepartofautilitylicensedoperatorwhofailedtoblocktheactuation

ofthemainsteamisolation

signal(MSIS)inaccordance

withtherequirements

oftheapprovedplantoperating

procedure.

2.CORRECTIVE

STEPSTAKENANDTHERESULTSACHIEVEDA.Themainsteamisolation

signal(MSIS)wasblockedandresetimmediately

following

theeventonAugust2,1995.

St.LucieUnits1and2DocketNos.50-335and50-389ReplytoNoticeofViolation

InsectionReort95-153.CORRECTXVE

STEPSTOAVOXDFURTHERVXOLATXONS

A.Thelicensedoperatorwhowasinvolvedintheeventwascounseled

ontheneedtofollowprocedures

andreceiveddiscipline

inaccordance

withplant'policy.

B.AllOperations

NuclearPlantSupervisors

(NPS)heldmeetingswiththeircrewssubsequent

tothiseventtoreiterate

FPL'sgoalforerrorfreeperformance.

C.Thiseventwillbeincorporated

intolicensedoperatorrequalification

trainingtoemphasize

procedural

compliance,

propercommunication

amongtheControlRoom'team,andtheimportance

ofsupervision

-inthecontrolroommaintaining

anoverallawareness,

ofactivities.

ThisactionwillbecompletebyJanuary1,1996.D.St.LuciePlantadoptedverbatimcompliance

astheonlyacceptable

meansofprocedure

compliance.

Thisrequirement

hasbeenincorporated

intoplantQualityInstruction

QI5-PR/PSL-1,

"Preparation,

Revision,

Review/Approval

ofProcedures'~

"4.Fullcompliance

wasachievedonAugust2,1995withthecompletion

ofitem2above.

St.LucieUnits1and2DocketNos.50-335and50-389ReplytoNoticeofViolation

InsectionReort95-15VIOLATION

B:Technical

Specification

6.8.1.arequiresthatwrittenprocedures

beestablished,

implemented,

andmaintained

coveringtheactivities

recommended

inAppendixAofRegulatory

Guide1.33,Rev.2,February1978.AppendixA,paragraph

1..dincludesadministrative

procedures

forprocedural

adherence.

Procedure

QI5-PR/PSL-1,

Rev.62,"Preparation,

Revision,

Review/Approval

ofProcedures,"

Section5.13.2,statesthatallprocedures

shallbestrictlyadheredto.Contrarytotheabove,procedures

werenotadheredtostrictlyinthefollowing

examples:

OP1-0120020,

Rev.72,"FillingandVentingtheRCS,"precaution

4.2,requiredthatReactorCoolantSystem(RCS)venting,described

intheprocedure,

notbeattempted

ifRCStemperature

wasabove200'F.OnAugust2,1995,ReactorCoolantPump(RCP)sealventing,performed

inanattempttocorrectsealpackageleakageinthe1A2RCPinaccordance

withAppendixEofthesubjectprocedure,

wasperformed

whileRCStemperature

wasapproximately

370'F.Asaresult,designtemperatures

ofRCPsealcomponents

wereapproached

orexceeded.

2.OP1-0120020,

Rev.72,"FillingandVentingtheRCS,"AppendixE,"Restaging

ReactorCoolantPumpSeals,"requiredtheuseofRCPsealinjection

whilerestaging

wasattempted.

OnAugust2,1995,restaging

ofthe1A2RCPsealpackagewasattempted

withoutsealinjection

alignedtothesealpackage.Asaresult,designtemperatures

ofRCPsealcomponents

wereapproached

orexceeded.

RESPONSEB:REASONFORVIOLATION

Therootcauseofthisviolation

wascognitive

personnel

erroronthepartofautilitylicensedoperatorwhofailedtofollowanapprovedplantprocedure

whileperforming

arestaging

evolution

onaReactorCoolant'Pump(RCP)sealpackage.Theoperatordidnotstrictlyadheretotheconditions

contained

intheprocedure

whichrequiredthatRCStemperature

benogreaterthan200'F,andthatsealinjection

beinservice.

0

St.LucieUnits1and2DocketNos.50-335and50-389Reply'oNoticeofViolation

InsectionReort95-152.CORRECTXVE

STEPSTAKENANDTHERESULTSACHIEVEDA.TheRCP'estaging

evolution

wasdiscontinued,

andOperations

cooledanddepressurized

theReactorCoolantSystem(RCS)inaccordance

withapprovedplantprocedure

tolowerRCPsealtemperatures

towithintheacceptable

range.The1A2RCPwassecured.B.Thedamaged1A2RCPsealpackagewasreplacedpriortoreturning

Unit1tooperation.

3.CORRECTIVE

STEPSTOAVOIDFURTHERVXOLATXONS

A.Thelicensedoperatorinvolvedinthiseventwasdisciplined

inaccordance

withplantpolicy.B.Theprocedure

appendixwhichwasusedforperforming

therestaging

oftheRCPswasdeletedandisnolongeravailable

foruse.C.Plantmanagement

performed

anassessment

ofthedecisionmakingprocessthatledtotherestaging

oftheRCPsealundertheexistingplantconditions.

Basedonthisassessment,

Plantpolicy105,"PlantOperation

BeyondtheEnvelopeofApprovedPlantOperating

Procedures",

wasrevisedtorequireatechnical

reviewofprocedures

whicharebeingimplemented

forthefirsttimeorforwhichplantconditions

aredifferent

fromthosedescribed

intheprocedures

D.AllOperations

NuclearPlantSupervisors

(NPS)heldmeetingswiththeircrewssubsequent

tothiseventtoreiterate

FPL'sgoalforerrorfreeperformance.

E.St.LuciePlantadoptedverbatimcompliance

astheonlyacceptable

meansofprocedure

compliance.

Thisrequirement

hasbeenincorporated

intoplantQualityInstruction

QI5-PR/PSL-1,

"Preparation,

Revision,

Review/Approval

ofProcedures."

4.Fullcompliance

wasachievedonAugust2,1995withthecompletion

ofitem2A,above.

St.LucieUnits1and2DocketNos.50-335and50-389ReplytoNoticeofViolation

InsectionReort95-15VIOLATION

C:Technical

Specification

6.8.1.arequiresthatwrittenprocedures

beestablished,

implemented,

andmaintained

coveringtheactivities

recommended

inAppendixAofRegulatory

Guide1.33,Rev.2,February1978.AppendixA,paragraph

1.dincludesadministrative

procedures

forprocedural

adherence.

Procedure

QI5-PR/PSL-1,

Rev.62,"Preparation,

Revision,

Review/Approval

ofProcedures,"

Section5.13',statesthatallprocedures

shallbestrictlyadheredto.AP1-0010123,

Rev99,"Administrative

ControlsofValves,Locks,andSwitches,"

step8.1.6,required,

inpart,thatallvalvepositiondeviations

bedocumented

intheValveSwitchDeviation

Log.Contrarytotheabove,onoraboutAugust1,1995,HCV-25-1through7wererepositioned

andleftintheclosedpositionwithouttherequiredentriesbeingmadeintheValveSwitchDeviation

Log.TheValves'ositions

complicated

alossofRCSinventory.

RESPONSEC:REASONFORVIOLATION

Therootcauseofthisviolation

wascognitive

personnel

erroronthepartofutilitylicensedoperators

whodidnotproperlydocumenttheclosedstatusofthesubjectvalvesintheValveSwitchDeviation

Log,asrequiredbytheapprovedplantprocedure.

2.CORRECTIVE

STEPSTAKENANDTHERESULTSACHIEVEDTheSafeguards

PumpRoomSumpIsolation

valves,HCV25-1throughHCV25-7,wererealigned

totheopenpositionimmediately

following

thelossofRCSinventory

eventonAugust10,1995,whenControlRoomoperators

discovered

theclosedstatusofthevalves.

St.LucieUnits1and2DocketNos.50-335and50-389ReplytoNoticeofViolation

InsectionReort95-153.CORRECTXVE

STEPSTOAVOXDFURTHERVXOLATXONS

A.AllOperations

NuclearPlantSupervisors

(NPS)heldmeetingswiththeircrewssubsequent

tothiseventtoreiterate

FPL'sgoalforerrorfreeperformance.

B.C.D.Theplanthasadoptedverbatimcompliance

astheonlyacceptable

meansofprocedure

compliance.

Thisrequirement

hasbeenincorporated

intoplantQualityInstruction

QI5-PR/PSL-1,

"Preparation,

Revision,

Review/Approval

ofProcedures."

Management

isconducting

adailyreviewofControlRoomchronological

logstoreinforce

theexpectation

fordetailandcompleteness.

IPlantadministrative

procedures

havebeenrevisedtoprovideforincreased

reviewsbyplantstaffofthelogscontrolling

valverepositioning.

Fullcompliance

wasachievedonAugust10,1995,withthecompletion

ofitem2above.

St.LucieUnits1and2DocketNos.50-335and50-389ReplytoNoticeofViolation

InsectionReort95-15VIOLATION

D:Technical

Specification

6.8.1.arequiresthatwrittenprocedures

beestablished,

implemented,

andmaintained

coveringtheactivities

recommended

inAppendixAofRegulatory

Guide1.33,Rev.2,February1978.AppendixA,paragraph

1.dincludesadministrative

procedures

forprocedural

adherence.

Procedure

QI5-PR/PSL-1,

Rev.62,"Preparation,

Revision,

Review/Approval

ofProcedures,"

Section5'3.2,statesthatallprocedures

shallbestrictlyadheredto.OP1-0410022,

Rev22,"Shutdown

Cooling,"

step8.3.7,requiredthatV3652,theBShutdownCooling(SDC)hotlegsuctionisolation

valve,belockedopenwhileplacingtheBSDCloopinservice.Contrarytotheabove,onAugust29,acontrolroomoperatorfailedtoplaceV3652inalockedopencondition

whileplacingtheBSDCloopinservice.Asaresult,the1BLowPressureSafetyInjection

Pumpwasoperatedwithitssuctionlineisolated.

RESPONSED:REASONFORVIOLATION

Therootcauseofthisviolation

wascognitive

personnel

erroronthepartofautilitylicensedoperatorwhofailedtoproperlyverifythealignment

oftheshutdowncooling(SDC)systemflowpathinaccordance

withtheapprovedplantprocedure,

priortostartingthe1BLowPressureSafetyInjection

(LPSI)Pump.Thisresultedinthefailuretoopenthe1BLPSIPumpsuctionisolation

valve.2.CORRECTIVE

STEPSTAKENANDTHERESULTSACHIEVEDA.TheControlRoomoperators

notedtheerrorinvalvealignment

andtheLPSIpumpwassecuredapproximately

5minutesafterbeingstarted.Asubsequent

inspection

determined

thatnodamagehadoccurredduringtheshortperiodofpumpoperation.

B.Thesystemwasrealigned

inaccordance

withtheapprovedprocedure

andtheLPSIpumpwasrestarted.

Subsequent

operation

oftheLPSIpumpwassatisfactory.

C.AnASMESectionXIcoderunwasperformed

satisfactorily

onthe1BLPSIPumpandasubsequent

Engineering

assessment

concluded

thatpumpoperability

hadnotbeenadversely

affected.

St.LucieUnits.1and2DocketNos.50-335and50-389ReplytoNoticeofViolation

InsectionReort95-153.CORRECTIVE

STEPSTOAVOIDFURTHERVIOLATIONS

A.Thelicensedoperatorinvolvedinthiseventwasdisciplined

inaccordance

withplantpolicy.B.Operations

implemented

procedure

changeswhichrequiretheuseofadedicated

procedure

readertoassistintheimplementation

ofSDCrelatedevolutions.

C.AllOperations

NuclearPlantSupervisors

(NPS)heldmeetingswiththeircrewssubsequent

tothiseventtoreiterate

FPL'sgoalforerrorfreeperformance.

D.Theplanthasadoptedverbatimcompliance

astheonlyacceptable

meansofprocedure

compliance.

Thisrequirement

hasbeenincorporated

intoplantQualityInstruction

QI5-PR/PSL-1,

"Preparation,

Revision,

Review/Approval

ofProcedures."

E.Thiseventwillbeincludedintolicensedoperator,

requalification

training.

Thisactionwillbecompleted

byJanuary1,1996.4.Fullcompliance

wasachievedonAugust29,1995withthecompletion

ofitem2Aand2Babove.

St.LucieUnits1and2DocketNos.50-335and50-389ReplytoNoticeofViolation

InsectionReort95-15VIOLATION

E:Technical

Specification

6.8.1.arequiresthatwrittenprocedures

beestablished,

implemented,

andmaintained

coveringtheactivities

recommended

inAppendixAofRegulatory

Guide1.33,Rev.2,February1978.AppendixA,paragraph

1.dincludesadministrative

procedures

forprocedural

adherence.

Procedure

QI5-PR/PSL-1,

Rev.62,"Preparation,

Revision,

Review/Approval

ofProcedures,"

Section5.13.2,statesthatallprocedures

shallbestrictlyadheredto.QI16-PR/PSL-2,

Rev.1,"St.LucieActionReport(STAR)Program,"

requiredthatSTARsbeinitiated

forQualityAssurance

auditfindingsandindependent

technical

reviewrecommendations'ontrary

totheabove,aSTARwasnotgenerated

whenaQualityAssurance

reviewofaninadvertent

Unit1containment

spraydown,

documented

ininteroffice

correspondence

JQQ-95-143,

identified

thepracticeofprelubricating

FCV-07-1A,

Containment

SprayheaderAflowcontrolvalve,whenperforming

valvestroketimetesting.RESPONSEE:1.REASONFORVIOLATION

Therootcauseofthisviolation

wascognitive

personnel

erroronthepartofutilityQualityAssurance

(QA)personnel.

QApersonnel

wereintheprocessofconducting

anindependent

reviewfocusingonthecontributing

factorsassociated

withaUnit1containment

spraydownevent.Thepracticeofpre-lubricating

Containment

SprayheaderflowcontrolvalveFCV-07-lApriortosurveillance

testingwasidentified

duringthis.review,butwasnotdetermined

tobeacontributing

factortothisevent.Recommendations

tocorrectthisdeficiency

weretherefore

notcontained

intheresulting

QAreport,norwasaSt.LucieActionRequest(STAR)generated

inatimelymanner.2.=CORRECTIVE

STEPSTAKENANDTHERESULTSACHIEVEDA.ASt.LucieActionRequest(STAR951048)wasgenerated

onSeptember

7,1995todocumentthedeficient

practiceofpre-lubricating

Unit1andUnit2containment

sprayflowcontrolvalvespriortosurveillance

stroketimetesting.B.Temporary

changeswereissuedtoplantsurveillance

procedures

onSeptember

2,1995toremovethepracticeof'pre-lubricating

valvespriortosurveillance

testing.10

St.LucieUnits1and2DocketNos.50-335and50-389ReplytoNoticeofViolation

InsectionReort95-153.CORRECTIVE

STEPSTOAVOIDFURTHERVIOLATIONS

A.B.C.AmeetingwasheldonSeptember

13,1995betweentheVicePresident

ofNuclearAssurance

andallSt.LucieQualityAssurance

andQualityControlpersonnel.

Duringthismeeting,clearexpectations

wereprovidedregarding

thethreshold

foridentification

anddocumentation

ofdeficiencies

byQualitypersonnel.

EOnOctober25,1995,asecondmeetingwasheldbetweenthesiteQualityManagerandSt.LucieQApersonnel.

Duringthismeeting,therequirements

oftheQualityInstruction

QI16-PR/PSL-2,

"St.LucieActionReport(STAR)Program"werereviewed.

Theresponsibility

ofQApersonnel

fortimelyidentification

anddocumentation

ofdeficiencies

inaccordance

withthisprocedure

wasreinforced.

Permanent

changeswillbemadetoplantsurveillance

procedures

todiscontinue

thepracticeofpre-testlubrication

ofthevalvespriortosurveillance

testing.Thisactionwillbecompleted

byDecember1,1995.4.Fullcompliance

wasachievedonSeptember

7,1995withthecompletion

ofitem2Aabove.

St.LucieUnits1and2DocketNos.50-335and50-389ReplytoNoticeofViolation

InsectionReort95-15VIOLATION

F:Technical

Specification

6.8~1.arequiresthatwrittenprocedures

beestablished,

implemented,

andmaintained

coveringtheactivities

recommended

inAppendixAofRegulatory

Guide1.33,Rev.2,February1978.AppendixA,paragraph

1.dincludesadministrative

procedures

forprocedural

adherence.

Procedure

QI5-PR/PSL-1,

Rev.62,"Preparation,

Revision,

Review/Approval

ofProcedures,"

Section5.13.2,statesthatallprocedures

shallbestrictlyadheredto.ADM-08.02,

Rev7,"ConductofMaintenance,"

Appendix5,step5,requiredthatprocedures

bepresentduringworkandthatindividual

stepsbeinitialed

onceperformed.

Contrarytotheabove,inspection

ofworkinprogressrevealedthatindividual

stepswerenotinitialed

onceperformed

uponcompletion

forworkconducted

inaccordance

withPlantChange/Modification

11-195.RESPONSEF:1.REASONFORVIOLATION

Therootcauseofthisviolation

wascognitive

personnel

erroronthepartofanElectrical

Department

journeyman

whofailedtoproperlydocumentthecompletion

ofstepswhileperforming

workactivities

associated

withthetripsolenoids

onthe1BEmergency

DieselGenerator

(EDG).Thestepswerenotinitialed

astheywerebeingperformed,

inaccordance

withapprovedplantprocedure.

2.CORRECTIVE

STEPSTAKENANDTHERESULTSACHIEVEDA.Thestepsofthemaintenance

procedure

beingworkedweresignedoffbythejourneyman

immediately

following

thecompletion

oftheworkonAugust31,1995,andthecompleted

procedure

wasreviewedbythechiefelectrician

andElectrical

supervisor.

B.TheEDGcircuitry

wassubsequently

testedfollowing

completion

oftheworkonAugust31,1995,andperformed

satisfactorily.

12

0

St.LucieUnits1and2DocketNos.50-335and50-389ReplytoNoticeofViolation

InsectionReort95-153.CORRECTIVE

STEPSTOAVOIDFURTHERVIOLATIONS

A.Meetingswereheldfollowing

thiseventwithElectrical

Maintenance

employees

toreviewthisincidentandemphasize

management

expectations

regarding

thedocumentation

ofw'orkactivities.

B.Supervisors

fromeachMaintenance

discipline

haveconducted

meetingswiththeiremployees

toreinforce

theneedforstrictadherence

totheadministrative

requirements

relatedtoprocedure

use.C.Theplanthasadoptedverbatimcompliance

astheonlyacceptable

meansofprocedure

compliance.

Thisrequirement

hasbeenincorporated

intoplantQualityInstruction

QI5-PR/PSL-1,

"Preparation,

Revision,

Review/Approval

ofProcedures."

4.Fullcompliance

wasachievedonAugust31,1995withthecompletion

ofitem2Aand2Babove.13

St.LucieUnits1and2DocketNos.50-335and50-389ReplytoNoticeofViolation

InsectionReort95-15VIOLATION

G:10CFR50AppendixB,Criterion

V,"Instructions,

Procedures,

andDrawings,"

requires,

inpart,thatactivities

affecting

qualityshallbeprescribed

bydocumented

procedures

ofatypeappropriate

tothecircumstances.

Contrarytotheabove,onAugust18,1995,ventingoftheLowPressureSafetyInjection

(LPSI)Systemwasconducted

inaccordance

withaprocedure

whichwasinappropriate

tothecircumstances.

Specifically,

OP1-0420060,

Rev.0,"VentingoftheEmergency

CoreCoolingandContainment

SpraySystems,"

didnotrequireaverification

thattheportionsofthesystembeingventedwerehydraulically

isolatedfromadjacentsystemsandflowpaths.

Asaresultofthisfailuretoestablish

properinitialconditions,

waterdrivenbythe1ALPSIpumpwasinadvertently

directedtotheATrainContainment

Sprayheader,resulting

inaspraydown

oftheUnit1ReactorContainment

Building.

RESPONSEG:REASONFORVIOLATION

Therootcauseofthisviolation

wasprocedural

deficiency

inthattheECCSventingprocedure,

OP1-0420060,

didnotstatetheplantconditions

requiredtosuccessfully

venttheECCSbutreliedupontheRCSheatupprocedure

tosetplantconditions.

Specifically,

theventingprocedure

didnotrequireoperators

toverifythatthepropercontainment

sprayheaderisolation

valveswereclosedpriortorecirculating

thewaterintheSDCsystem.Acontributing

factortothiseventwasthattheoperations

personnel

performing

theECCSventingprocedure

didnotrecognize

thattheexistingplantconditions

wouldresultinflowtothe'A'ontainment

sprayheaderwhenflowwasalignedthroughtheShutdownCoolingHeatExchanger.

Asecondcontributing

factorofthiseventwasthatFCV-07-1A

wasplacedintheopenpositionbecausethisvalvehadfaileditsASMEstroketimetest.Plantmanagement

madethedecisiontodeferthevalverepairandpositionthisnormallyclosedvalvetoitsengineered

safeguards

openpositioninlieuofrepairing

thevalvepriortostartup.14

St.LucieUnits1and2DocketNos.50-335and50-389ReplytoNoticeofViolation

InsectionReort95-152.CORRECTIVE

STEPSTAKENANDTHERESULTSACHIEVEDA.Operators

securedthe1ALPSIPumpandisolated,

theflowpathtothecontainment

sprayheaderfromtheLPSIPump.TheReactorCavitysumpwasdrainedtotheWasteManagement

System.B~Following

theevent,allnonessential

workatthesitewasplacedonhold,andUnit1wasmaintained

stableinMode3whileseniorplantmanagement

conducted

meetingswithallavailable

sitepersonnel

tostresstheneedforworkervigilance

andattention

todetail.Theneedtoreduceequipment

deficiencies

thatimpactoperations

wasalsodiscussed.

C.Unit1wascooleddownanddepressurized

toMode,5andaninspection

anddecontamination

ofcontainment

wasthenconducted.

Theeventwasevaluated

underanEngineering

evaluation,

whichresultedinacomprehensive

inspection

ofcomponents

insidecontainment

toensurefuturecomponent

reliability.

D.Operating

procedure,

OP1-0420060,

"VentingoftheEmergency

CoreCoolingan'dContainment

SpraySystem",wasrevisedSeptember

1,1995toincludetheplantconditions

requiredtobepresentduringventing.3.CORRECTIVE

STEPSTOAVOIDFURTHERVIOLATIONS

A.Plantpolicy105,"PlantOperation

BeyondtheEnvelopeofApprovedPlantOperating

Procedures",

wasrevisedtorequireatechnical

reviewofprocedures

whicharebeingimplemented

forthefirsttimeorforwhichplantconditions

aredifferent

fromthosedescribed

intheprocedure.

B.TheMaintenance

Department

established

ateamcomposedofplantstaffandengineering

personnel,

todetermine

therootcausefortheContainment

Sprayheaderisolation

valverepeatfailuresanddetermine

corrective

actionstoeliminate

thisoperatorworkaround.

FCV-07-1A

wasrepairedpriortoreturning

Unit1toservice.15

St.LucieUnits1and2DocketNos.50-335and50-389ReplytoNoticeofViolation

InsectionReort95-15C.Existingplantdeficiencies

werereviewedbyseniorplantmanagement.

Additional

deficiencies

whichcouldimpactoperations

wereaddedtotheworkscopeoftheUnit1shutdown.

Thesedeficiencies

werecorrected

priortoreturning

theunittoservice.D.Administrative

procedure,

AP-0010147,

"Assessment

ofAbnormalPlantConfigurations

orSignificant

MaterialDeficient

'Conditions

onPlantOperation",

wasdeveloped

toenhanceoutagescopereviewandensurethatequipment

deficiencies

arerestoredinatimelymanner.E.St.Luciemanagement

instituted

aweeklyreviewofappropriate

performance

indicators

andworkbacklogstatus,including

theageofopenitemsandoperatorworkarounds.

F.AllOperations

NuclearPlantSupervisors

(NPS)heldmeetingswiththeircrewssubsequent

tothiseventtoreiterate

FPL'sgoalforerro'rfreeperformance.

G.Thiseventwillbeincorporated

intolicensedoperatorrequalification

training.

ThisactionwillbecompletebyJanuary1,1996.4.Fullcompliance

wasachievedonAugust18,1995withthecompletion

ofitems2A,2Cand2Dabove.16