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{{#Wiki_filter:__ _ _ _ _ _ _ _ _ _ _ - _             - - _ _ _ _ _ _ _ _ .                     - _ _ - _ _ __ ___ _ _ _ - ________-__ ____--______ - ______-____ -___ -_.
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                                                                          U.S. NUCLEAR REGULATORY COMMISSION
-___ -_.
                                                                                                                                                                    '
                                                                                                                              REGIONlil
                                                                Docket Nos:        50 010, 50 237, 50 249
                                                                License Nos:        DPR-02, DPR 19, DPR 25
                                                                Report Nos:        50-010/97024(DRP), 50-237/97024(DRP),
                                                                                    50 249/97024(DRP)
                                                                Licensee:          Commonwealth Edison
                                                                Facility:          Dresden Nuclear Station, Units 1,2 and 3
                                                                Location:          6500 N. Dresden Road
                                                                                    Morris, IL 60450
                                                                Dates:              October 16 November 22,1997
                                                                Inspectors:        K. Riemer, Senior Resident inspector
                                                                                    D. Roth, Resident inspector
                                                                                    J. Roman, Illinois Department of Nuclear Safety Resident
                                                                                                inspector
                                                                                    B. Dickson, Resident inspector in Training
                                                                                    J. Ellis, Operator Licensing Examiner, Region ill
                                                                Approved By;        M. Ring, Chief
'
'
                                                                                    Reactor Projects Branch 1
.
                                                                                                                                                                  i
U.S. NUCLEAR REGULATORY COMMISSION
                                                                                                                                                                I
'
                                9712   127 971219
REGIONlil
                                PDR A   K 05000010.
Docket Nos:
                                G                                   PDR - i
50 010, 50 237, 50 249
                                __
License Nos:
DPR-02, DPR 19, DPR 25
Report Nos:
50-010/97024(DRP), 50-237/97024(DRP),
50 249/97024(DRP)
Licensee:
Commonwealth Edison
Facility:
Dresden Nuclear Station, Units 1,2 and 3
Location:
6500 N. Dresden Road
Morris, IL 60450
Dates:
October 16 November 22,1997
Inspectors:
K. Riemer, Senior Resident inspector
D. Roth, Resident inspector
J. Roman, Illinois Department of Nuclear Safety Resident
inspector
B. Dickson, Resident inspector in Training
J. Ellis, Operator Licensing Examiner, Region ill
Approved By;
M. Ring, Chief
Reactor Projects Branch 1
'
i
I
9712
127 971219
PDR
A
K 05000010.
G
PDR - i
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- . _ _ - .
                                                                                                                                                            :
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EXECUTIVE SUMMARY
Dresden Generatin Nation, Units 1,2 and 3 -
i
i
                                                                                                    EXECUTIVE SUMMARY
NRC Inspection Reports No. 60-010/9702d t #iM; 50 237/97024(DRP); 50 24g/g7024(DRP)
                                                                                            Dresden Generatin Nation, Units 1,2 and 3 -                    i
{
                            NRC Inspection Reports No. 60-010/9702d t #iM; 50 237/97024(DRP); 50 24g/g7024(DRP)                                           {
This inspection included routine resident inspect 6on with augmentation from the lilinois
                    This inspection included routine resident inspect 6on with augmentation from the lilinois                                             ,
                    Department of Nuclear Safety and NRC Region Ill.                                                                                        .
                    Oserations
                    *                        The inspectors concluded that the licensee's operational plan for dealing with the                          _
                                                                                                                                                          l
                                            increased unidentified leakage in the drywell was good. The licensee commenced taking
                                            actions well ahead of TS limits. The planning and execution reflected a careful and                          ;
                                            conservetive operating environment (Section 01.2)                                                            !
                    *                        When faced with conflicting indications between the alarm and the local reading, licensee
                                            personnel relied on the less conservative of the two indications and did not declare the
                                            standby liquid control (SBLC) system inoperable. The licensee operated the piant for                          ;
                                                                                                                                                          -
                                            more than 34 hours without an operable SBLC system, well beyond the allowable
                                            8 hours. Lack of knowledge of the exact locations of the temperature sensor and switch
                                            contributed to this decision. A violation was issued for failing to comply with TSs
                                            (Section 02.1).
                    *                        The SBLC temperature annunciator procedure did not provide advance woming of                                  i
                                            exceeding a TS limit. The licensee was aware of this, but had chosen to delsy
                                            implementing a change to the procedure based on operations monitoring of the local
                                            temperature of the SBLC system (Section 02.1).                                                                4
,
,
                    +                        The licensee generally performed routine operations in a safe manner (Section 04.1).
Department of Nuclear Safety and NRC Region Ill.
                    *                        The inspectors concluded that overall performance during the shutdown and startup was
.
                                            good. However, the inspectors identified examples of some minor problems in                                   :
Oserations
                                            knowledge of system status, communication, and procedural use (Section 04.2).
The inspectors concluded that the licensee's operational plan for dealing with the
                    *                        The usual response of operators to annunciator alarms was to follow the appropriate                           ,
_
                                            annunciator procedure. However, in two instances, the inspectors observed that crews
l
                                            failed to follow the annunciator procedures completely when an alarm recurred
*
                                            (Section 04.3).
increased unidentified leakage in the drywell was good. The licensee commenced taking
                    *                        The Unit 2 single loop activities witnessed by the inspectors were performed well. The
actions well ahead of TS limits. The planning and execution reflected a careful and
                                            inspectors observed operators enforce three way communicationsi follow plant                                 !
;
                                            procedures, and coordinate activities well with other involved departments                                   ;
conservetive operating environment (Section 01.2)
                                            (Section 04.4).
!
  -           _
When faced with conflicting indications between the alarm and the local reading, licensee
                    +                        The operators responded well to material condition induced challenges and transients
*
                                            (Section 04.5),
personnel relied on the less conservative of the two indications and did not declare the
                    *                        The inspectors concluded that the operations department showed a lack of a questioning
standby liquid control (SBLC) system inoperable. The licensee operated the piant for
                                            attitude during the September 7 operability surveillance run to declare the Unit 3 high -
;
                                            pressure coolant injection (HPCI) system operable. The shift displayed a weak
more than 34 hours without an operable SBLC system, well beyond the allowable
                                                                                                                s
-
                                                                                                              2'
8 hours. Lack of knowledge of the exact locations of the temperature sensor and switch
                .   . _ _ . _ . - . , . _ . . _ _ _ _ _ _ . _ _ . _ _ _ . _ _ _ _ . - - _                                                   _ _ _ _ . __
contributed to this decision. A violation was issued for failing to comply with TSs
(Section 02.1).
The SBLC temperature annunciator procedure did not provide advance woming of
i
*
exceeding a TS limit. The licensee was aware of this, but had chosen to delsy
implementing a change to the procedure based on operations monitoring of the local
temperature of the SBLC system (Section 02.1).
4
,
The licensee generally performed routine operations in a safe manner (Section 04.1).
+
The inspectors concluded that overall performance during the shutdown and startup was
*
good. However, the inspectors identified examples of some minor problems in
:
knowledge of system status, communication, and procedural use (Section 04.2).
The usual response of operators to annunciator alarms was to follow the appropriate
*
,
annunciator procedure. However, in two instances, the inspectors observed that crews
failed to follow the annunciator procedures completely when an alarm recurred
(Section 04.3).
The Unit 2 single loop activities witnessed by the inspectors were performed well. The
*
inspectors observed operators enforce three way communicationsi follow plant
!
procedures, and coordinate activities well with other involved departments
;
(Section 04.4).
-
_
The operators responded well to material condition induced challenges and transients
+
(Section 04.5),
The inspectors concluded that the operations department showed a lack of a questioning
*
attitude during the September 7 operability surveillance run to declare the Unit 3 high -
pressure coolant injection (HPCI) system operable. The shift displayed a weak
s
2'
.
. _ _ . _ . - . , . _ . . _ _ _ _ _ _ . _ _ . _ _ _ . _ _ _ _ . - - _
.


                                                                                              .  ._
                                                                                                      l
.
.
                                                                                                      l
._
                                                                                                      !
l
                                                                                                      i
.
                                                                                                    -
knowledge of the operationalimplications of the HPCI turbine exhaust and vent system
        knowledge of the operationalimplications of the HPCI turbine exhaust and vent system
-
        and how it was affected by the status of the Unit 3 HPCI system (Section 08.1).
and how it was affected by the status of the Unit 3 HPCI system (Section 08.1).
  Maintenance
Maintenance
  +      The work perfcrmed on the Unit 2 feedwater control system was poorly planned. The
The work perfcrmed on the Unit 2 feedwater control system was poorly planned. The
        failure to provide adequate work instructions directly challenged the operators. The
+
        history of feedwater system work and resulting transients showed that feedwater work
failure to provide adequate work instructions directly challenged the operators. The
        needed more stringent reviews than those provided (Section M2.1).
history of feedwater system work and resulting transients showed that feedwater work
  +      The surveille. ice activities observed were satisfactorily completed and met the
needed more stringent reviews than those provided (Section M2.1).
        procedure's acceptance criteria (Section M2.2).
The surveille. ice activities observed were satisfactorily completed and met the
  *      Due to a lack of detail on a sketch provided by engineering and a lack of a questioning
+
        attitude by a maintenance worker, the licensee demonstrated poor performance and work
procedure's acceptance criteria (Section M2.2).
        practices regarding the installation of Temp Alt lll 1197 (Section M4.1).
Due to a lack of detail on a sketch provided by engineering and a lack of a questioning
  +      The inspectors noted several examples of maintenance rework following the forced
*
        outage activities (Section M4.2).
attitude by a maintenance worker, the licensee demonstrated poor performance and work
  +      For the most part, the self assessments were of sufficient scope and depth. The
practices regarding the installation of Temp Alt lll 1197 (Section M4.1).
        self assessments were hard hitting and critical of the malatenance process. The
The inspectors noted several examples of maintenance rework following the forced
        exception was the self assessment on unauthorized modifications. This self assessment
+
        did not have sufficient depth to leam the workers' knowledge of administrative processes
outage activities (Section M4.2).
        in place to control unauthorized modifications, as proved by an NRC violation issued
For the most part, the self assessments were of sufficient scope and depth. The
        shortly after the self assessment was performed (Section M7.1).
+
  *      The Q&SA organization was satisfactorily monitoring the activities in maintenance. The
self assessments were hard hitting and critical of the malatenance process. The
        audit reports and surveillance were complete, thorough, and critical. The field monitoring
exception was the self assessment on unauthorized modifications. This self assessment
        reports were an indication that Q&SA personnel performed sufficient field monitoring
did not have sufficient depth to leam the workers' knowledge of administrative processes
        activities (Section M7.2).
in place to control unauthorized modifications, as proved by an NRC violation issued
  Enoineerina
shortly after the self assessment was performed (Section M7.1).
  .      The licensee did not have all vendor information related to emergency diesel generator
The Q&SA organization was satisfactorily monitoring the activities in maintenance. The
        cylinder test valves. Applicable information sent to another Comed site had not been
*
        forwarded to the licensee. The actions taken in response to a pavious NRC-identified
audit reports and surveillance were complete, thorough, and critical. The field monitoring
        violation for failing to incorporate vendor information regarding cylinder test valves were
reports were an indication that Q&SA personnel performed sufficient field monitoring
        not sufficient because additionalinformation received by Comed 2 months before the
activities (Section M7.2).
        licensee's response to the Notice was not incorporated (Section E2.1).
Enoineerina
  Plant Support
The licensee did not have all vendor information related to emergency diesel generator
  *      The licensee improperly determined that a problem experienced at Braldwood Station
.
        was not present at Dresden Station. After discussions with the inspectors, the licensee
cylinder test valves. Applicable information sent to another Comed site had not been
        concluded the problem was applicable and the licensee formulated corrective actions.
forwarded to the licensee. The actions taken in response to a pavious NRC-identified
        This issue, combined with the licensee's failure to test lights adequately, caused the
violation for failing to incorporate vendor information regarding cylinder test valves were
        inspectors to consider the overall material condition of the lights to be marginal
not sufficient because additionalinformation received by Comed 2 months before the
        (Section F2.1).
licensee's response to the Notice was not incorporated (Section E2.1).
                                                    3
Plant Support
The licensee improperly determined that a problem experienced at Braldwood Station
*
was not present at Dresden Station. After discussions with the inspectors, the licensee
concluded the problem was applicable and the licensee formulated corrective actions.
This issue, combined with the licensee's failure to test lights adequately, caused the
inspectors to consider the overall material condition of the lights to be marginal
(Section F2.1).
3


            __                   .. _ - ___       _ = _ _ - _ _ _ _ _                           _ ___ _ _ .               _ ._. _ _ _ . _ ._- _ _ _ _ _
__
                                  .
.. _ - ___
                                                                                                          Report Details                                                   4
_ = _ _ - _ _ _ _ _
                                                                                                                                                                            l
_ ___ _ _ .
                                                                                                                                                                          i
_ ._. _ _ _ . _ ._- _ _ _ _ _
                                            Unit 2 was maintained at full power except for short uuration load drops to support routine
.
                                            surveillance tests throughout the first part of the inspection period. On November 16, the
Report Details
                                            licensee decreased power to 25 percent and tripped one recirculation pump motor generator
4
                                            (MG) to perform MG brush replacement and to enter the drywell to add oil to the 2A recirculation                             >
i
                                            pump motor. On November 18, the licensee performed maintenance on the feedwater system
Unit 2 was maintained at full power except for short uuration load drops to support routine
                                                                                                                                                                          ,
surveillance tests throughout the first part of the inspection period. On November 16, the
                                            and inadvertently caused a feedwater transient. The licensee held power at 650 MWe pending
licensee decreased power to 25 percent and tripped one recirculation pump motor generator
                                            investigation of the issue.
(MG) to perform MG brush replacement and to enter the drywell to add oil to the 2A recirculation
                                            Unit 3 was near full thermal power at the beginning of this inspection period. Full thermal power
>
                                            on Unit 3 was not achieved because the main turbine control valve positions were limited to an
pump motor. On November 18, the licensee performed maintenance on the feedwater system
                                            average of 85 percent open with no greater than 90 percent open on any one control valve, and
and inadvertently caused a feedwater transient. The licensee held power at 650 MWe pending
                                            feedwater flow was limited to g.735 Mlbm/h (instead of the approximately g.8 Mibm/h at full
,
                                            power) as a result of a review of the fuel cycle analysis performed by engineering personnel.                                 3
investigation of the issue.
                                            These limits remained in effect until the end of the inspection period, On November 1, Unit 3
Unit 3 was near full thermal power at the beginning of this inspection period. Full thermal power
                                            power was decreased to 300 MWe to facilitate drywell entry to investigate increased drywell                                   ;
on Unit 3 was not achieved because the main turbine control valve positions were limited to an
                                                                                                                                                                          '
average of 85 percent open with no greater than 90 percent open on any one control valve, and
                                            leakage. The licensee identified unisolable leakage from the 3B reactor recirculation loop
feedwater flow was limited to g.735 Mlbm/h (instead of the approximately g.8 Mibm/h at full
                                            discharge flow element and manually shut down Unit 3 for repairs. On November 6, the licensee
power) as a result of a review of the fuel cycle analysis performed by engineering personnel.
;                                           started up Unit 3.                                                                                                 ,
3
                                                                                                                                                                          i
These limits remained in effect until the end of the inspection period, On November 1, Unit 3
power was decreased to 300 MWe to facilitate drywell entry to investigate increased drywell
;
'
leakage. The licensee identified unisolable leakage from the 3B reactor recirculation loop
discharge flow element and manually shut down Unit 3 for repairs. On November 6, the licensee
;
started up Unit 3.
,
i
:
:
I
I
                                                                                                          1. Operations
1. Operations
                                            01       Conduct of Operations
01
                                            01.1     General Comments
Conduct of Operations
l                                                      Using inspec tion Procedure 71707, the inspectors conducted frequent reviews of ongoing
01.1
                                                      plant operations. Overall, the conduct of operations was safe and in accordance with
General Comments
                                                      procedures.
                                                      During the inspection period, one event occurred for which the licensee was required by
                                                      10 CFR 50.72 to notify the NRC, The event and the notification date are listed below;
                                                      November 1      (Unit 3) TS required shutdown because of pressure boundary leakage, A
                                                                        leak of 0.32 gpm from a weld on a tap-off of the B recirculation loop flow
                                                                        element was found during a drywell entry,
                                            01.2 (Unit 3) Response to Drvwell t.eakaoe
                                              a.      101pection Scope (71707)
                                                      The inspectors monitored the licensee's response to indications of a leak in the drywell.
                                                                                                                4
l
l
Using inspec tion Procedure 71707, the inspectors conducted frequent reviews of ongoing
plant operations. Overall, the conduct of operations was safe and in accordance with
procedures.
During the inspection period, one event occurred for which the licensee was required by
10 CFR 50.72 to notify the NRC, The event and the notification date are listed below;
November 1
(Unit 3) TS required shutdown because of pressure boundary leakage, A
leak of 0.32 gpm from a weld on a tap-off of the B recirculation loop flow
element was found during a drywell entry,
01.2 (Unit 3) Response to Drvwell t.eakaoe
a.
101pection Scope (71707)
The inspectors monitored the licensee's response to indications of a leak in the drywell.
4
l
l
l
l
  . . - . _ . - _. _ . _ _ . , ,-                                       .           ......_,_..,_,,r.m           . - _ . -     ,         . _ , , , , . _ . - -   , , _ .
l
. . - . _ . - _. _ . _ _ . , ,-
.
......_,_..,_,,r.m
. -
. -
,
. _ , , , , . _
. - -
, , _ .


                                                                                                      l
-
-
  .
.
                                                                                                      !
b.
                                                                                                      l
Observations and Findinat
    b.   Observations and Findinat
On October 17,1997, radiatinn protection personnel reported to operations that Unit 3
          On October 17,1997, radiatinn protection personnel reported to operations that Unit 3
drywell activity increased by a tactor of three. On October 18, operations determined that
          drywell activity increased by a tactor of three. On October 18, operations determined that
liquid going to the drywell floor drain sump increased from 0.50 to 0.67 gpm over
          liquid going to the drywell floor drain sump increased from 0.50 to 0.67 gpm over
24 hours. Dresden UFSAR Section 5.2.5.5 stated,"in the case of a steam leak,
          24 hours. Dresden UFSAR Section 5.2.5.5 stated,"in the case of a steam leak,
essentially all of the leak will be routed to the floor drain sump as condensate from the
          essentially all of the leak will be routed to the floor drain sump as condensate from the
drywell coolers." The leak rate quickly increased to 0.83 gpm by October 19.
          drywell coolers." The leak rate quickly increased to 0.83 gpm by October 19.
Operations established shutdown limits on total unidentified leakage and changes to
          Operations established shutdown limits on total unidentified leakage and changes to
unidentified leakage that were conservative compared with the requirements of TS 3.6.H.
          unidentified leakage that were conservative compared with the requirements of TS 3.6.H.
(less than or equal to 5 gpm of unidentified leakage; less than or equal to 2 gpm increase
          (less than or equal to 5 gpm of unidentified leakage; less than or equal to 2 gpm increase
in any 24 hour period).
          in any 24 hour period).
The licensee then developed and executed a " Unit 3 Drywell Leakage Plan." The plan
          The licensee then developed and executed a " Unit 3 Drywell Leakage Plan." The plan
included monitoring, reviews of industry avents, and sampling using the air sampling
          included monitoring, reviews of industry avents, and sampling using the air sampling
manifold system. The licensee also assigned senior reactor operators as owners of the
          manifold system. The licensee also assigned senior reactor operators as owners of the
plan.
          plan.
Air samplin0 and chemical analysis showed the leak to be primary coolant coming from
          Air samplin0 and chemical analysis showed the leak to be primary coolant coming from
the 3B recirculation pump area. Operations determined that a drywell entry was
          the 3B recirculation pump area. Operations determined that a drywell entry was
necessary to find the exact source of the leak.
          necessary to find the exact source of the leak.
Operations reduced power to 300 MWe on November 1, then entered the drywell and
          Operations reduced power to 300 MWe on November 1, then entered the drywell and
readily identified a non isolable leak on the 3B recir.:ulation flow sensing line. The leak
          readily identified a non isolable leak on the 3B recir.:ulation flow sensing line. The leak
was pressure boundary leakage, so operations immediately commenced a unit shutdown
          was pressure boundary leakage, so operations immediately commenced a unit shutdown
in accordance with TSs.
          in accordance with TSs.
c.
    c.   Conclusions
Conclusions
          The inspectors concluded that the licensee's plan for dealing with the increased
The inspectors concluded that the licensee's plan for dealing with the increased
          unidentified leaksge was good. The licensee commenced taking actions well ahead of
unidentified leaksge was good. The licensee commenced taking actions well ahead of
          TS limits. The planning and execution reflected a careful and conservative operating
TS limits. The planning and execution reflected a careful and conservative operating
          environment.
environment.
    02     Operational Status of Facilities and Equipment
02
    02.1 (Unit 3) Standby Li. quid Control System (SBLC)
Operational Status of Facilities and Equipment
    a.   Inspection Scope (71707)
02.1 (Unit 3) Standby Li. quid Control System (SBLC)
          At 0609 hours on October 27,1997, the SBLC low temperature alarm annunciated in the
a.
          control room. The licensee did not determine that the alarm was valid until 1530 hours on
Inspection Scope (71707)
          October 28,1997. The inspectors reviewed the licensee's investigation and
At 0609 hours on October 27,1997, the SBLC low temperature alarm annunciated in the
          troubleshooting.
control room. The licensee did not determine that the alarm was valid until 1530 hours on
                                                        5
October 28,1997. The inspectors reviewed the licensee's investigation and
troubleshooting.
5


- .
-
                                                                                                    l
.
                                                                                                      l
b.
                                                                                                    I
Observations and Findinos
    b. Observations and Findinos                                                                     ,
,
      identWication of the TS entry conditions
identWication of the TS entry conditions
      At 0609 hours on October 27,1997, the SBLC low temperature alarm annunciated in the
At 0609 hours on October 27,1997, the SBLC low temperature alarm annunciated in the
      control room. Per the annunciator procedure, the alarm was set for 78-83'F. By
control room. Per the annunciator procedure, the alarm was set for 78-83'F. By
      contrast, the TS required that the suction piping temperature be greater than or equal to
contrast, the TS required that the suction piping temperature be greater than or equal to
      83'F.
83'F.
      After the low SBLC suction piping temperature alam1 was received, the operators
After the low SBLC suction piping temperature alam1 was received, the operators
      checked local indication in accordance with the Dresden Annunciator Procedure (DAN);
checked local indication in accordance with the Dresden Annunciator Procedure (DAN);
      the local temperature indicator showed 90'F. The operators accepted the local Indication
the local temperature indicator showed 90'F. The operators accepted the local Indication
      as valid and assumed that a problem existed with the alarm or the alarm's temperature
as valid and assumed that a problem existed with the alarm or the alarm's temperature
      switch, so operations contacted maintenance to troubleshoot. In fact, the alarm was
switch, so operations contacted maintenance to troubleshoot. In fact, the alarm was
      valid, as will be further discussed below. Therefore, the operators chose not to believe
valid, as will be further discussed below. Therefore, the operators chose not to believe
      an annunciator without proving that the annunclator was invalid.
an annunciator without proving that the annunclator was invalid.
      Both operations and system engineering personnel were unaware at this time that the
Both operations and system engineering personnel were unaware at this time that the
      local indication came from a different location on the SBLC suction piping than the alarm
local indication came from a different location on the SBLC suction piping than the alarm
      sensor. The locallndication temperature sensor was closer to the SBLC tank and was
sensor. The locallndication temperature sensor was closer to the SBLC tank and was
      showing the correct temperature for its location. The temperature switch that provided
showing the correct temperature for its location. The temperature switch that provided
      the alarm signal was also correctly alarming because the SBLC suction temperature at
the alarm signal was also correctly alarming because the SBLC suction temperature at
      the switch's location was below the alarm setpoint.
the switch's location was below the alarm setpoint.
      During troubleshooting on October 28,1997, the licensen used a surface pyrometer and
During troubleshooting on October 28,1997, the licensen used a surface pyrometer and
      found that the SBLC suction piping temperature was only 80'F while the local indication
found that the SBLC suction piping temperature was only 80'F while the local indication
      showed 89'F. Operations then declared both SBLC subsystems to be inoperable. With
showed 89'F. Operations then declared both SBLC subsystems to be inoperable. With
      both SBLC subsystems inoperable, TS allow 8 hours to restore at least one subsystem or
both SBLC subsystems inoperable, TS allow 8 hours to restore at least one subsystem or
        12 hours after that to be in at least hot shutdown.
12 hours after that to be in at least hot shutdown.
      Immediate Corrective and Compensatory Actions
Immediate Corrective and Compensatory Actions
      Maintenance adjusted the controllers for the heat trace to raise temperature above the
Maintenance adjusted the controllers for the heat trace to raise temperature above the
      83'F TS requirement. The temperature was increased to above the TS requirement at
83'F TS requirement. The temperature was increased to above the TS requirement at
        16t5 on October 28,1997. Maintenance also observed that the heat trace controllers
16t5 on October 28,1997. Maintenance also observed that the heat trace controllers
      appeared to not be wired correctly.
appeared to not be wired correctly.
      The licensee ran an operability surveillance for the SBLC system, and the system passed.
The licensee ran an operability surveillance for the SBLC system, and the system passed.
      On October 28,1997, at 2033, operations began to monitor the suction piping
On October 28,1997, at 2033, operations began to monitor the suction piping
      temperatures with a surface pyrometer once a shift on both units.
temperatures with a surface pyrometer once a shift on both units.
      On October 31,1997, at 0930 during the shift rounds, a non-licensed operator found that
On October 31,1997, at 0930 during the shift rounds, a non-licensed operator found that
      the SBLC suction piping was 80'F. The non-licensed operator (NLO) did not recognize
the SBLC suction piping was 80'F. The non-licensed operator (NLO) did not recognize
      the significance of the extra readings, so the NLO failed to report the condition to the unii
the significance of the extra readings, so the NLO failed to report the condition to the unii
      superviser for more than i hour. The 1 hour delay was a significant portion of the
superviser for more than i hour. The 1 hour delay was a significant portion of the
      8-hour LCO. The licensee adjusted the heat trace controllers and increased the
8-hour LCO. The licensee adjusted the heat trace controllers and increased the
      temperatures to above the TS requirement at 1220 hours on October 31,1997. This was
temperatures to above the TS requirement at 1220 hours on October 31,1997. This was
      within the B-hour TS action statement.
within the B-hour TS action statement.
                                                  6
6


  _ .. _. _ . ... _ _ _ _ . _ _ _ _ _ _                                           . __ ._ ._ _ . _ . . _ . . _ _ _ _ _ _ _ _ _ _ _ _ _ . .
_ .. _. _ . ... _ _ _ _ . _ _ _ _ _ _
      -
. __ ._ ._ _ . _ . . _ . . _ _ _ _ _ _ _ _ _ _ _ _ _ . .
                        .
-
                                                                                                                                                      1
.
                                          Cause of Temperature Problems                                                                               i
1
                                                                                                                                                      1
Cause of Temperature Problems
                                          The onset of cooler outside temperatures caused the ambient temperature of the SBLC                         I
i
                                          system area in the reactor building to decrease. This allowed the suction piping to cool.                 j
1
                                                                                                                                                      l
The onset of cooler outside temperatures caused the ambient temperature of the SBLC
;                                          Maintenance personnel concluded that two of the three heat trace circuits had their                       i
system area in the reactor building to decrease. This allowed the suction piping to cool.
                                                                                                                                                      '
j
;                                         controllers crossed such that the thermostat was sensing temperature on one section of
Maintenance personnel concluded that two of the three heat trace circuits had their
                                          piping, but controlling the heat. trace on another section of piping. The section of the pipe
i
;
'
;
controllers crossed such that the thermostat was sensing temperature on one section of
piping, but controlling the heat. trace on another section of piping. The section of the pipe
that had experienced the low temperature was affected by the wiring problem. The
i
4
4
                                          that had experienced the low temperature was affected by the wiring problem. The                        i
licensee corrected the error by the aftemoon of October 31.
                                          licensee corrected the error by the aftemoon of October 31.                                             i
i
,                                                                                                                                                 e
e
i                                         cause of Procedure Problems                                                                             ,
,
                                                                                                                                                    :
i
                                                                                                                                                    '
cause of Procedure Problems
                                          The alarm setpoints in the annunciator procedure DAN 902(3) 5 G-6 were below the
,
'
'
                                          TS setpoints. The alarm came in at 78'F, whereas TS required 83'F minimum
The alarm setpoints in the annunciator procedure DAN 902(3) 5 G-6 were below the
TS setpoints. The alarm came in at 78'F, whereas TS required 83'F minimum
'
'
                                          temperature. The low SBLC suction piping temperature was changed as part of the
temperature. The low SBLC suction piping temperature was changed as part of the
'
TS upgrade program from 80 to 83'F in June 1996. A decision was made then to defer
i
-
-
                                          TS upgrade program from 80 to 83'F in June 1996. A decision was made then to defer                      i
                                                                                                                                                    '
                                          the setpoint change until mid December of 1997. However, even without the TS upgrade                    '
                                          program, the old alarm would still have been below the old TS requirements. The
                                          deferral was made because the licer$see believed that routine operator rounds'                          ;
                                          temperature monitoring (which monitored local Indication, not the true suction                          ;
                                                                                                                                                    '
'
'
                                          temperature) was sufficient.
the setpoint change until mid December of 1997. However, even without the TS upgrade
                                                                                                                                                  \
'
'
                                          Licenses Event Report
program, the old alarm would still have been below the old TS requirements. The
                                                                                                                                                  '
deferral was made because the licer$see believed that routine operator rounds'
                                          On October 31,1997, the licensee identified that unit 3 was outside TS compliance when
;
                                          SBLC suction temperature was below 83'F (PlF# D1997 07873). The licensee                                 .
temperature monitoring (which monitored local Indication, not the true suction
                                          subsequently published Licensee Event Report No. 50 249/97-01100, "SBLC was                             :
;
                                          Inoperable from suction Line Low Temperature due to a Wiring discrepancy in the Heat
temperature) was sufficient.
'
'
\\
'
Licenses Event Report
On October 31,1997, the licensee identified that unit 3 was outside TS compliance when
'
SBLC suction temperature was below 83'F (PlF# D1997 07873). The licensee
.
subsequently published Licensee Event Report No. 50 249/97-01100, "SBLC was
:
Inoperable from suction Line Low Temperature due to a Wiring discrepancy in the Heat
'
'
i
i
                                          trace Controller Circuit."
trace Controller Circuit."
-;
The licensee event report (LER) discussed the correcting actions and the event causes.
4                                          The licensee event report (LER) discussed the correcting actions and the event causes.
- ;
                                          The LER did not discuss the operators' failure to believe the valid annunciator,
4
                                          in the LER, the licensee stated that personnel reviewed various SBLC work performed
The LER did not discuss the operators' failure to believe the valid annunciator,
                                          from 1988 to present and were unable to identify when the miswiring took place.                         :
in the LER, the licensee stated that personnel reviewed various SBLC work performed
                                          Event Significance
from 1988 to present and were unable to identify when the miswiring took place.
                                          The UFSAR Section 9.3.5 and the TS bases stated that the SBLC system temperature
:
                                          was required to be maintained at least 10'F above the saturation temperature of 62'F to
Event Significance
                                          guard against boron precipitation, Since the lowest observed temperatures were above
The UFSAR Section 9.3.5 and the TS bases stated that the SBLC system temperature
                                          the 62'F precipitation temperature, as were reactor building ambient temperatures,
was required to be maintained at least 10'F above the saturation temperature of 62'F to
                                          precipitation did not take place. The inspectors therefore concluded that the safety
guard against boron precipitation, Since the lowest observed temperatures were above
,                                        ' significance was small.
the 62'F precipitation temperature, as were reactor building ambient temperatures,
                                                                                                                                                  ,
precipitation did not take place. The inspectors therefore concluded that the safety
"                                        ! However, the event was significant for operations. . It demonstrated a willingness to
' significance was small.
                                          assume that a valid alarm was invalid without any supporting data. Additionally, even
,
,
! However, the event was significant for operations. . It demonstrated a willingness to
"
assume that a valid alarm was invalid without any supporting data. Additionally, even
n
n
                                                                                                                                                  '
7
'
>
>
                                                                                                                        7
4
4                                                                                                                                                L
L
              *-~re - s                     -     - =.se r;= w ew w-u-eme.-,er---                                                         e - -
:sz-x-
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                                                                                                  I
after operations started shiftily checks, operations did not assure that the personnel doing
    after operations started shiftily checks, operations did not assure that the personnel doing l
the checks understood the significance, as demonstrated by a failure of an NLO to report
                                                                                                  '
'
    the checks understood the significance, as demonstrated by a failure of an NLO to report
exceeding the TS minimums immediately upon discovery.
    exceeding the TS minimums immediately upon discovery.
Dresder. TS 3.4.A.1.b stated that with both standby liquid control subsystems inoperable,
    Dresder. TS 3.4.A.1.b stated that with both standby liquid control subsystems inoperable,
at least one must be restored to operable status within 8 hours or be in at least hot
    at least one must be restored to operable status within 8 hours or be in at least hot
shutdown within the next 12 hours.
    shutdown within the next 12 hours.
Contrary to the above, between October 27,1997,0609 hours and October 28,1997,
    Contrary to the above, between October 27,1997,0609 hours and October 28,1997,
1615 hours, both standby liquid control subsystems were inoperable for greater than
    1615 hours, both standby liquid control subsystems were inoperable for greater than
8 hours and the plant was not brought to at least a hot shutdown condition. This was a
    8 hours and the plant was not brought to at least a hot shutdown condition. This was a
violation (VIO 50-010; 237; 249/97024-01).
    violation (VIO 50-010; 237; 249/97024-01).
c.
c. Conclusions
Conclusions
    An error in wiring led to the SBLC suction piping heat trace not keeping the appropriate
An error in wiring led to the SBLC suction piping heat trace not keeping the appropriate
    sections of piping above TS minimum temperatures. An installed temperature switch in
sections of piping above TS minimum temperatures. An installed temperature switch in
    the SBLC system correctly sounded an alarm in the control room. Upon investigation,
the SBLC system correctly sounded an alarm in the control room. Upon investigation,
    operations found the local indication to be beyond the TS limits.
operations found the local indication to be beyond the TS limits.
    When faced with conflicting indications between the starm and the local reading, licensee
When faced with conflicting indications between the starm and the local reading, licensee
    personnel relied on the non-conservative of the two ir:dications and o.J not declare the
personnel relied on the non-conservative of the two ir:dications and o.J not declare the
    SBLC system inoperable. The licensee operated the plant for more than 34 hours without
SBLC system inoperable. The licensee operated the plant for more than 34 hours without
    an operable SBLC system, but the LCO for SBLC was only 8 hours. Lack of knowledge
an operable SBLC system, but the LCO for SBLC was only 8 hours. Lack of knowledge
    of the exact locations of the temperature sensor and switch contributed to this decision.
of the exact locations of the temperature sensor and switch contributed to this decision.
    A violation was issued for falling to comply with TSs.
A violation was issued for falling to comply with TSs.
    The SBLC temperature annunciator procedure did not provide advance waming of
The SBLC temperature annunciator procedure did not provide advance waming of
    exceeding a TS limit The licensee was aware of this, but had chosen to delay
exceeding a TS limit The licensee was aware of this, but had chosen to delay
    implementing a change to the procedure based on operations monitoring of the local
implementing a change to the procedure based on operations monitoring of the local
    temperature of the SBLC system.
temperature of the SBLC system.
04   Operator Knowledge and Performance
04
04.1 (Units 2. 3) Routine Operations
Operator Knowledge and Performance
a. Inspection Scqpe (71707. 83822)
04.1
    The inspectors conducted frequent reviews of ongoing plant operations in the control
(Units 2. 3) Routine Operations
    room and in the plant. The inspectors also discussed plant status and
a.
    pendingevolutionswith shift personnel in the control room.
Inspection Scqpe (71707. 83822)
b. pbservations and Findings
The inspectors conducted frequent reviews of ongoing plant operations in the control
    During routine operations the licensee met procedures and TSs (except for the SBLC
room and in the plant. The inspectors also discussed plant status and
    issue discussed in Section 02.1 of this report). Control room manning was adequate and
pendingevolutionswith shift personnel in the control room.
    the operators were not overburdened. No problems were found with indications or valve
b.
    lineups. Usually, shift personr'el were aware of plant conditions and operational
pbservations and Findings
    requirements were listed. The inspectors observed that the licensee continued to
During routine operations the licensee met procedures and TSs (except for the SBLC
    practice good communications.
issue discussed in Section 02.1 of this report). Control room manning was adequate and
                                                8
the operators were not overburdened. No problems were found with indications or valve
lineups. Usually, shift personr'el were aware of plant conditions and operational
requirements were listed. The inspectors observed that the licensee continued to
practice good communications.
8


                                    _
_
-
-
  .
.
    c.   Conclusions
c.
          The licensee generally performed routine operations in a safe manner.
Conclusions
    04.2 (Unit 3) Forced Outaae (D3F24) gnd Startuo for Pressure Boundary Leak
The licensee generally performed routine operations in a safe manner.
                                            .                                       t at
04.2 (Unit 3) Forced Outaae (D3F24) gnd Startuo for Pressure Boundary Leak at
    a.   Inspection Scope (71707_)
.
          The inspectors monitored the performance of operations during activities associated with
t
          the shutdown for and startup from the forced outage (D3F24) to repair pressure boundary
a.
          leakage.
Inspection Scope (71707_)
    b.   Observations and Findinos
The inspectors monitored the performance of operations during activities associated with
          Overall, the performance of operations during the Unit 3 startup was good. The
the shutdown for and startup from the forced outage (D3F24) to repair pressure boundary
          operators' actions were generally characterized by careful panel monitoring, good
leakage.
          communications, and good command and control of the plant. The operators were
b.
          challenged by equipment problems during the startup and responded generally correctly.
Observations and Findinos
          However, the inspectors noted that the operators' responses to some frequently alarming
Overall, the performance of operations during the Unit 3 startup was good. The
          annunciators degraded (see Section 04.3 for additional discussion).
operators' actions were generally characterized by careful panel monitoring, good
          Control Room Performance
communications, and good command and control of the plant. The operators were
          Overall, the control room performance was good. The inspectors observed that the
challenged by equipment problems during the startup and responded generally correctly.
          lice .Ne was carefully following procedures, maintaining good awareness of the plant,
However, the inspectors noted that the operators' responses to some frequently alarming
          k..d 8. eping the control room atmosphere quiet and professional.
annunciators degraded (see Section 04.3 for additional discussion).
          The unit supervisors (US) and shift managers (SM) held crew briefs at regular intervals to
Control Room Performance
          assure that the crews were fully aware of plant status and plans. The briefs conducted
Overall, the control room performance was good. The inspectors observed that the
          were thorough. The crews maintained three-way communicetions during the startup.
lice .Ne was carefully following procedures, maintaining good awareness of the plant,
          The performance by the nuclear station operators (NSOs) was generally good. The
k..d 8. eping the control room atmosphere quiet and professional.
          NSOs performed the procedures as written. The NSOs were generally very attentive to
The unit supervisors (US) and shift managers (SM) held crew briefs at regular intervals to
          the plant indications during the startup. The NSOs preformed frequent and detailed front
assure that the crews were fully aware of plant status and plans. The briefs conducted
          panel walkdowns.
were thorough. The crews maintained three-way communicetions during the startup.
          On November 1, during the Unit 3 shutdown, the inspectors questioned the US about the
The performance by the nuclear station operators (NSOs) was generally good. The
          status of the shutdown cooling system. The US was unaware that 3B shutdown cooling
NSOs performed the procedures as written. The NSOs were generally very attentive to
          pump was unavailable (the pump was in a testing status). Pumps A and C were available
the plant indications during the startup. The NSOs preformed frequent and detailed front
          and the licensee was meeting the TS. This showed an example of inattention to detail
panel walkdowns.
          during tumover.
On November 1, during the Unit 3 shutdown, the inspectors questioned the US about the
          During the startup on November 5, the inspectors reviewed a copy of the startup
status of the shutdown cooling system. The US was unaware that 3B shutdown cooling
          procedure and noted that one step sent the user to a wrong step during startup. The SM
pump was unavailable (the pump was in a testing status). Pumps A and C were available
          reviewed the procedure and concluded that the error was a typographical error. The US
and the licensee was meeting the TS. This showed an example of inattention to detail
          informed the shift manager that the typo in the autherized copy of the startup procedura
during tumover.
          hao already been noted and corrected. The inspectors considered the typo to be minor
During the startup on November 5, the inspectors reviewed a copy of the startup
          inattention to detail during procedure revision.
procedure and noted that one step sent the user to a wrong step during startup. The SM
                                                      9
reviewed the procedure and concluded that the error was a typographical error. The US
informed the shift manager that the typo in the autherized copy of the startup procedura
hao already been noted and corrected. The inspectors considered the typo to be minor
inattention to detail during procedure revision.
9


                          .
.
.
  .
.
                                                                                                      l
.
                                                                                                      !
l
                                                                                                      !
Also, during the startup on November 5, the inspectors identified an instance of failing to
          Also, during the startup on November 5, the inspectors identified an instance of failing to ,
,
          complete an annunciator procedure. This issue is discussed in Section 04.3.                 ;
complete an annunciator procedure. This issue is discussed in Section 04.3.
          Field Performance
Field Performance
          The inspectors observed part of the performance of a procedure for starting the steam
The inspectors observed part of the performance of a procedure for starting the steam
          jet air ejector.
jet air ejector.
          The non licensed operators (NLos) performing the procedure followed all the required
The non licensed operators (NLos) performing the procedure followed all the required
          procedure steps and administrative requirements, including radiation protection
procedure steps and administrative requirements, including radiation protection
          requirements.
requirements.
          The procedure was not frequently performed. The licensee took advantage of the startup
The procedure was not frequently performed. The licensee took advantage of the startup
          to train additional NLOs on the required actions. The inspectors consWered this to be
to train additional NLOs on the required actions. The inspectors consWered this to be
          prudent. The NLO doing the task provided careful and knowledgeable instruction
prudent. The NLO doing the task provided careful and knowledgeable instruction
          The evolution was not successful due to material condition. The Unit 3 hydrogen
The evolution was not successful due to material condition. The Unit 3 hydrogen
          analyzer system could not be placed in service because one train was blocked and the
analyzer system could not be placed in service because one train was blocked and the
          other train apparently had a slug of water introduced during the shutdown. The NLO
other train apparently had a slug of water introduced during the shutdown. The NLO
          attempting to place the system in service identified the water intrusion problem and
attempting to place the system in service identified the water intrusion problem and
          correctly reported the condition to the system engineer (who was pre ent) and to the Unit
correctly reported the condition to the system engineer (who was pre ent) and to the Unit
          Supervisor.
Supervisor.
          The licensee could not restore either system, so chose to startup the plant directly into
The licensee could not restore either system, so chose to startup the plant directly into
          the TS LCO for inoperable hydrogen analyzers.
the TS LCO for inoperable hydrogen analyzers.
          The inspectors concluded that the NLOs performed the evolution in a careful and
The inspectors concluded that the NLOs performed the evolution in a careful and
          controlled manner. The NLos showed a good ability to recognize abnorrnalindications
controlled manner. The NLos showed a good ability to recognize abnorrnalindications
          for system operating parameters that are entry level conditions for TSs.
for system operating parameters that are entry level conditions for TSs.
          On a different shift, the inspectors noted one instance of an unexpected alarm caused by
On a different shift, the inspectors noted one instance of an unexpected alarm caused by
            NLOs energizing plant equipment. The NLOs did not inform the control room immediately
NLOs energizing plant equipment. The NLOs did not inform the control room immediately
            before energi:ing the equipment, but instead radioed the control room immediately after
before energi:ing the equipment, but instead radioed the control room immediately after
            causing an alarm. After the inspectors asked if the NLOs had informed the control room
causing an alarm. After the inspectors asked if the NLOs had informed the control room
          to expect ar? alarm, the unit supervisors remir'ded all NLOs to provide advance notice
to expect ar? alarm, the unit supervisors remir'ded all NLOs to provide advance notice
            immediately before energizing equipment.
immediately before energizing equipment.
    c.     Conclusions
c.
          The inspectors concluded that the overall performance during the shutdown and startup
Conclusions
          was good. However, the inspectols identified examples of some minor problems in
The inspectors concluded that the overall performance during the shutdown and startup
            knowledge of system status, communication, and procedural use.
was good. However, the inspectols identified examples of some minor problems in
    04.3 (Units 2. 3) Response to Annuncictgn
knowledge of system status, communication, and procedural use.
    a.     Inspection Scope (71707)
04.3 (Units 2. 3) Response to Annuncictgn
            The inspectors monitored the operators' use of Dresden Annunciator Procedures, in
a.
            particular, the inspectors checked for compliance with annunciators that were repetitive.
Inspection Scope (71707)
                                                    10
The inspectors monitored the operators' use of Dresden Annunciator Procedures, in
particular, the inspectors checked for compliance with annunciators that were repetitive.
10
.


                                                                                                  . _ _ _
. _ _ _
                                                                                                          I
.
                                                                                                          .
.
.
  ,
,
    b. Observations and Findinas
b.
      The normal response of an operator to an annunciator alarm was to complete the actions
Observations and Findinas
      listed in the Dresden annunciator response procedure (DAN). The inspectors observed
The normal response of an operator to an annunciator alarm was to complete the actions
      many instances of operators correctly reviewing and executing the appropriate DAN.
listed in the Dresden annunciator response procedure (DAN). The inspectors observed
      On October 20, the inspectors observed an oncoming NSO receive an alarm on the gland
many instances of operators correctly reviewing and executing the appropriate DAN.
      seal condenser, then clear and reset the alarm without referencing any procedure. The
On October 20, the inspectors observed an oncoming NSO receive an alarm on the gland
      off going NGO had told the oncoming NSO that the alarm had been repeatedly coming in
seal condenser, then clear and reset the alarm without referencing any procedure. The
      due to a material condition problem.
off going NGO had told the oncoming NSO that the alarm had been repeatedly coming in
      The inspectors informed senior licensee management about the failure to use the
due to a material condition problem.
      annunciator procedure. The licensee Quality and Skfety Assessment (Q&SA) department
The inspectors informed senior licensee management about the failure to use the
      had written problem identification form (PIF) # D1997 07317 on September 28 for a
annunciator procedure. The licensee Quality and Skfety Assessment (Q&SA) department
      similar issue. The licensee determined that the significance level of the PIF was
had written problem identification form (PIF) # D1997 07317 on September 28 for a
      " Condition Not Adverse to Quality" and had closed the issue.
similar issue. The licensee determined that the significance level of the PIF was
      On November 5, during the startup, the inspectors observed the following: the operators
" Condition Not Adverse to Quality" and had closed the issue.
      were at a point in the startup that required frequent changes to the range setting for the
On November 5, during the startup, the inspectors observed the following: the operators
      intermediate range monitors (IRMs). The material condition of the IRMs was challenging
were at a point in the startup that required frequent changes to the range setting for the
      the operators because the changing of the range switch for IRM 14 was causing IRM
intermediate range monitors (IRMs). The material condition of the IRMs was challenging
      downscale alarms to occur. Shortly after the first spurious downscale alarms, the
the operators because the changing of the range switch for IRM 14 was causing IRM
      inspectors reviewed the backpanel indications and observed one IRM with a "Hi" alarm lit,
downscale alarms to occur. Shortly after the first spurious downscale alarms, the
      and another with alamis for both "Hi" and "Hi-Hi" lit, but the readings for all IRMs were
inspectors reviewed the backpanel indications and observed one IRM with a "Hi" alarm lit,
      below alarm setpoints. No IRM associated annunciators were in alarm on the control
and another with alamis for both "Hi" and "Hi-Hi" lit, but the readings for all IRMs were
      room front panels. The inspectors reviewed the annunciatormsponse procedure
below alarm setpoints. No IRM associated annunciators were in alarm on the control
      (DAN 902(3) 5 C-5, "lRM Downscale," Rev. 06) and noted that it required review of
room front panels. The inspectors reviewed the annunciatormsponse procedure
      back panelindications as a subsequent action for the alarm.
(DAN 902(3) 5 C-5, "lRM Downscale," Rev. 06) and noted that it required review of
      When the operators next changed the range of IRM 14, the IRM downscale alarm again
back panelindications as a subsequent action for the alarm.
      came in. The operators briefly discussed the alarm, noted it was the same IRM, and
When the operators next changed the range of IRM 14, the IRM downscale alarm again
      concluded that the range switch contacts might be the source and that a work request to
came in. The operators briefly discussed the alarm, noted it was the same IRM, and
      investigate must be written. Although the operators reviewed the annunciator response
concluded that the range switch contacts might be the source and that a work request to
      procedure, no operator was sent to recheck the backpanelindication. Because the
investigate must be written. Although the operators reviewed the annunciator response
      operators did not check the backpanel, they were unaware that the backpanel indications
procedure, no operator was sent to recheck the backpanelindication. Because the
      showed signs of spiking high.
operators did not check the backpanel, they were unaware that the backpanel indications
      When the NSO next ranged IRM 14. a half scram due to "Hi-Hi" level occurred. The
showed signs of spiking high.
      operators then reviewed the back panels and saw and cleared the IRM channel alarms.
When the NSO next ranged IRM 14. a half scram due to "Hi-Hi" level occurred. The
      In addition, the operators bypassed the noisy IRM and called maintenance and
operators then reviewed the back panels and saw and cleared the IRM channel alarms.
      engineering for assistance.
In addition, the operators bypassed the noisy IRM and called maintenance and
      After the half scram, the inspectors asked the unit supervisor if the alarm response
engineering for assistance.
      procedure for the previous IRM downscale had been completed. The US said,"No," and
After the half scram, the inspectors asked the unit supervisor if the alarm response
      acknowledged that it should have. The inspectors asked the NSO who was responsible
procedure for the previous IRM downscale had been completed. The US said,"No," and
      for ranging the IRMs if anyone had reported completion of the alarm response procedure
acknowledged that it should have. The inspectors asked the NSO who was responsible
      to him, and he said *No." The inspectors discussed the concem of completing the
for ranging the IRMs if anyone had reported completion of the alarm response procedure
      annunciator response procedure with the shift manager, and the shift manager
to him, and he said *No." The inspectors discussed the concem of completing the
      reemphasized to the operators that DANs need to be followed completely, even for
annunciator response procedure with the shift manager, and the shift manager
      expected or nuisance alarms caused by equipment problems, The shift manager also
reemphasized to the operators that DANs need to be followed completely, even for
                                                  11
expected or nuisance alarms caused by equipment problems, The shift manager also
11


                                      - - .         _       _           _     __         _.               . _
- - .
_
_
_
__
_.
.
_
*
*
                                                                                                                            l
.
          .
,
                                                                                                                            ,
!
                                                                                                                          !
l
                                                                                                                          l
directed that backpanel tours be done on 15 minute intervals rather than on the usual
                  directed that backpanel tours be done on 15 minute intervals rather than on the usual
1 hour interval to detect any other IRM spikes,
                  1 hour interval to detect any other IRM spikes,
.
                                                                                                                          .
Procedure DAP 07 50," Conduct of Safe Operations," Rev. O Step 6.3.2 stated," . . .
                  Procedure DAP 07 50," Conduct of Safe Operations," Rev. O Step 6.3.2 stated," . . .
after receiving unexpected alarms, reference appropriate procedures." Step 6.3.3 stated,
                  after receiving unexpected alarms, reference appropriate procedures." Step 6.3.3 stated,
" . . when responding to annunciators . . . follow the annunciator procedure as written."
                  " . . when responding to annunciators . . . follow the annunciator procedure as written."
.
                    .
Step 7.2.3 stated to announce an alarm and * Pull out the annunciator procedures (DAN)
                  Step 7.2.3 stated to announce an alarm and * Pull out the annunciator procedures (DAN)
l
                                                                                                                          l
and take the appropriate actions at directed by the procedures."
                  and take the appropriate actions at directed by the procedures."
The operators' actions on October 26 and November 5 did not meet DAP 07 50. In both
                  The operators' actions on October 26 and November 5 did not meet DAP 07 50. In both
instances, the repetitive alarms caused by material condition problems caused the
                                                                                                                          :
:
                  instances, the repetitive alarms caused by material condition problems caused the
operators to become complacent about following the annunciator procedure. Although
                  operators to become complacent about following the annunciator procedure. Although
the actions were contrary to procedures, no violation was issued because this issue
                  the actions were contrary to procedures, no violation was issued because this issue
would be expected to be encompassed by licensee corrective actions to a recently issued
                  would be expected to be encompassed by licensee corrective actions to a recently issued
violation for operators not following procedures (50 237; 249/97019-02)
                  violation for operators not following procedures (50 237; 249/97019-02)
c.
              c.   Conclusions
Conclusions
                  The usud response of operators to annunciator alarms was to foll0w the approprihte                     '
The usud response of operators to annunciator alarms was to foll0w the approprihte
                                                                                                                          .
.'
                  annuriciator procedure.
annuriciator procedure.
                  However, in two instances, the inspectors observed the crews failed to follow the
However, in two instances, the inspectors observed the crews failed to follow the
                  annunciator procedures completely when an alarm recurred. in one instance the
annunciator procedures completely when an alarm recurred. in one instance the
                  consequence of not following the procedure was the operators being unaware that an
consequence of not following the procedure was the operators being unaware that an
                  IRM was spiking "Hi" And "Hi-Hi" as well as downscale.
IRM was spiking "Hi" And "Hi-Hi" as well as downscale.
            04.4 Unit 2 Sinole Looo Operations
04.4 Unit 2 Sinole Looo Operations
              e,   inspection Scope (71707)
e,
                  The inspectors monitored the response by the licensee to the discovery of uneven
inspection Scope (71707)
                  wearing of *e brushes on the 2B reactor recirculation motor generator (MG) set. The                   ,
The inspectors monitored the response by the licensee to the discovery of uneven
                  replacement of the brushes required the licensee to secure the MG set, and thus to enter
wearing of *e brushes on the 2B reactor recirculation motor generator (MG) set. The
                  single loop operations on November 16.
,
                  The inspectors observed and reviewed licensee plane for the evolution, the plant
replacement of the brushes required the licensee to secure the MG set, and thus to enter
                  operations review committee (PORC), control room activities, and maintenance work in
single loop operations on November 16.
                  the field.
The inspectors observed and reviewed licensee plane for the evolution, the plant
              b.   Observations and Findinos
operations review committee (PORC), control room activities, and maintenance work in
                  UnN 2 Single Loop Activities
the field.
                  Licensee personnelidentifiod that several brushes on the 2B MG set were wom much
b.
                  more than the others. The licensee developed plans tu replace the bmshes and inspect
Observations and Findinos
                  the rings on the MG set. The MG set had to be secured to perform the task. The
UnN 2 Single Loop Activities
                  licensee elected to do the task on-line by tripping one recirculation pump and operating
Licensee personnelidentifiod that several brushes on the 2B MG set were wom much
                  the plant in single-loop.
more than the others. The licensee developed plans tu replace the bmshes and inspect
                                                            12
the rings on the MG set. The MG set had to be secured to perform the task. The
_ _ _ . ._                              ,_         _                     _              _              _    - _ _ _
licensee elected to do the task on-line by tripping one recirculation pump and operating
the plant in single-loop.
12
. .
,_
_
- _ _ _


    _       _ _ -             . _ _ . _ _ _ - _ _ _ _ _ _ _ _ . - _ _ . _ _                                         _ _ . _ _ _ _ _ _ . _ _
_
      *           .
_ _ -
  ,                                                                           i
. _ _ . _ _ _ - _ _ _ _ _ _ _ _ . - _ _ . _ _
                                      Historica.ly, tripping a pump on-line and restarting was a significant event for Dresden.
_ _ . _ _ _ _ _ _ . _ _
*
.
i
,
Historica.ly, tripping a pump on-line and restarting was a significant event for Dresden.
As documen6ed in inspection Report No. 50 237/95004(DRP); 50 249/95004(DRP), in
i
<
<
                                      As documen6ed in inspection Report No. 50 237/95004(DRP); 50 249/95004(DRP), in                                                      i
1995, the 25 teactor recirculation pump tripped because of a technician inadvertently
                                        1995, the 25 teactor recirculation pump tripped because of a technician inadvertently                                                 j
j
                                      closing the contreeler for the 28 recirculation pump motor generator set temperature -                                                 ;
closing the contreeler for the 28 recirculation pump motor generator set temperature -
                                      control valve (TCV) while attempting to repair the 2A TCV Operations reviewed the                                                     .
;
                                      requirements for a restart of the pump and found that the bottom head drain temperature                                               !
control valve (TCV) while attempting to repair the 2A TCV Operations reviewed the
.
requirements for a restart of the pump and found that the bottom head drain temperature
!
was needed. However, the bottom head drain had been clogged for mar *y years. The
j
,
,
                                      was needed. However, the bottom head drain had been clogged for mar *y years. The                                                    j
operating crew concluded that sitomate temperature indications could be used to meet
                                      operating crew concluded that sitomate temperature indications could be used to meet                                                 ,
,
.
.
                                      the TS and procedural intent. This determination was made without discussion with
the TS and procedural intent. This determination was made without discussion with
j                                       senior operations management, station management, or engineering personnel, and
j
4                                      against the advios of an independent site engineering group (ISEG) engineer. This
senior operations management, station management, or engineering personnel, and
                                      resulted in escalated enforcement action. Since 1995, the licensee improved the material
against the advios of an independent site engineering group (ISEG) engineer. This
                                      condition by cleaning out the bottom head drain, and improved the overall conduct of                                                 !
4
                                        operations. However, the licensee had not performed single loop operations since the                                                 ;
resulted in escalated enforcement action. Since 1995, the licensee improved the material
                                        1995 event.                                                                                                                         j
condition by cleaning out the bottom head drain, and improved the overall conduct of
                                                                                                                                                                            ;
!
operations. However, the licensee had not performed single loop operations since the
;
1995 event.
j
The planning for the brush replacement was thorough. The licensee used a wide range
;
of resources, including the vendor.
{
,
,
                                      The planning for the brush replacement was thorough. The licensee used a wide range
i
i
                                        of resources, including the vendor.                                                                                                  {
.
.
The review of the plan was also thorough. Thc PORC thoroughly discussed the planned
!
3
3
                                      The review of the plan was also thorough. Thc PORC thoroughly discussed the planned                                                  !
maintenance work, possible contingencies, and operational requirements for a single loop
i-                                      maintenance work, possible contingencies, and operational requirements for a single loop                                             l
l
;                                       condition,                                                                                                                           j
i-
;
condition,
j
.
On November 16,1997, the licensee removed the 28 recirculation loop from service to
;
perform the brush replacement activities. The inspectors verified that the operators
!
:
complied with the T8 requirements and closely follow the approved plan. The inspectors
!
,
vonfied that plant parameters were within T8 requirements for recovery of the idle loop
.
.
                                        On November 16,1997, the licensee removed the 28 recirculation loop from service to                                                  ;
and that the operators propert*, retumed the loop to service. The inspectors also noted
:                                      perform the brush replacement activities. The inspectors verified that the operators                                                !
>
,                                      complied with the T8 requirements and closely follow the approved plan. The inspectors                                              !
;
                                        vonfied that plant parameters were within T8 requirements for recovery of the idle loop                                              .
close coordination and communications between operations department personnel,
                                                                                                                                                                            >
;
                                        and that the operators propert*, retumed the loop to service. The inspectors also noted
maintenance and engineering personnel, and the designated project manager for the
;                                       close coordination and communications between operations department personnel,                                                       ;
i
                                        maintenance and engineering personnel, and the designated project manager for the                                                   i
evolution.
                                        evolution.
,
                                                                                                                                                                            ,
c.
                            c.         G9DQlusion
G9DQlusion
                                                                                                                                                                            1
1
                                      The Unit 2 single loop activities witnessed by the inspectors were performed well. The                                               l
The Unit 2 single loop activities witnessed by the inspectors were performed well. The
                                                                                                                                                                            '
l
                                        inspectors observed operators enforce three way communications, follow plant
inspectors observed operators enforce three way communications, follow plant
                                        procedures, and coordinate activities well with other involved depa 1ments.
'
[
[
                          04.5 Qperators Response to Material Condition Induced Transients
procedures, and coordinate activities well with other involved depa 1ments.
                                                                                                                                                                            E
04.5 Qperators Response to Material Condition Induced Transients
                            a.         Inspection Ecoce (71707)                                                                                                             ?
E
                                                                                                                                                                            *
a.
                                      - The material condition of the plant caused challenges and transients during the
Inspection Ecoce (71707)
                                        Inspection period. The inspectors observed and reviewed operator performance in
?
                                        response to these events.           t
- The material condition of the plant caused challenges and transients during the
c                                                                                                                                                                           3
*
                                                                                                                                                                            ,
Inspection period. The inspectors observed and reviewed operator performance in
                                                                                                                                                                            5
t
                                                                                  13                                                                                         l
response to these events.
                                                                                                                                                                            t
c
                                                                                                                                                                            !
3
                                                                                                                                                                            t
,
  .w_...___.,~.-_2..________.._________                                                 _ _ . _ _ , , , _ , , . . .                         , . _ _ _ . _ _ _ , _ . . . .
5
l
13
t
!
t
.w_...___.,~.-_2..________.._________
_ _ . _ _ , , , _ , , . . .
, . _ _ _ . _ _ _ , _ . . . .


-
-
  .
.
    b. Qp.ittyggng.and Findinog
b.
      Reactor Feed Pump Ventilation
Qp.ittyggng.and Findinog
      On November 17,1997, Unit 2 operators noticed an increase in the 2C reactor feed partp
Reactor Feed Pump Ventilation
      (RFP) stator temperature. The temperature of the 2C stator temperature was
On November 17,1997, Unit 2 operators noticed an increase in the 2C reactor feed partp
      apprnximately 80'C (crocedurallimit of 85'C) and slowly rising, while the stator
(RFP) stator temperature. The temperature of the 2C stator temperature was
      temperature of the otner runninD RFP (2B RFP) was approximately 46'C. Operators fp
apprnximately 80'C (crocedurallimit of 85'C) and slowly rising, while the stator
      the field identified that the ventilation damper for the 20 RFP had failed to open.
temperature of the otner runninD RFP (2B RFP) was approximately 46'C. Operators fp
      Operators started the 2A RFP and secured the 2C RFP. The operators placed the 2C
the field identified that the ventilation damper for the 20 RFP had failed to open.
      RFP in a Standby lineup and caution carded it for emergency use only. During
Operators started the 2A RFP and secured the 2C RFP. The operators placed the 2C
      subsequent troubleshooting, the damper operated as expected and operators retumed
RFP in a Standby lineup and caution carded it for emergency use only. During
      the RFPs to their original configurations.
subsequent troubleshooting, the damper operated as expected and operators retumed
      On November 18,1997, the operators noticed that the stator temperatures of the 2B and
the RFPs to their original configurations.
      2C RFPs were trending upwards. An oper2 tor dispatched to the field identified that the
On November 18,1997, the operators noticed that the stator temperatures of the 2B and
      ventilation dampers were not in their expected positions. The individual pump vent
2C RFPs were trending upwards. An oper2 tor dispatched to the field identified that the
      dampers were in the correct positions, however, the recirculation damper was full open.
ventilation dampers were not in their expected positions. The individual pump vent
      The operators wired the recirculation damper closed and the exhaust damper open in an
dampers were in the correct positions, however, the recirculation damper was full open.
      emergency attempt to lower stator temperatures (this was procedurally allowed to protect
The operators wired the recirculation damper closed and the exhaust damper open in an
      equipment). The stator temperatures trended downwards and stabilized around GO'C for
emergency attempt to lower stator temperatures (this was procedurally allowed to protect
      both of the pumps. The licensee documented the occurrence via problem identif: cation
equipment). The stator temperatures trended downwards and stabilized around GO'C for
      forms (PlF) D199708145 and D1997 08101.
both of the pumps. The licensee documented the occurrence via problem identif: cation
      The inspectors concluded that the operators performed well by identifying the unexpected
forms (PlF) D199708145 and D1997 08101.
      temperature increase and restoring the RFPs and RFP ventilation system to a stable
The inspectors concluded that the operators performed well by identifying the unexpected
      condition.
temperature increase and restoring the RFPs and RFP ventilation system to a stable
      The inspectors noted similaritPs between the problems encountered on August 12,
condition.
      August 13, and the November 18 ventilation problems, in all cases, the operators were
The inspectors noted similaritPs between the problems encountered on August 12,
      required to perform emergency downpower maneuvers when reactor feedpump
August 13, and the November 18 ventilation problems, in all cases, the operators were
      ventilation problems occurred.
required to perform emergency downpower maneuvers when reactor feedpump
      2A2 Flash Tank Level Control Problems
ventilation problems occurred.
      On November 17,1997, control room operators noticed level swings in the 2A2 Flash
2A2 Flash Tank Level Control Problems
      Tank. Since the level swings were increasing to the point of automatic opening of the
On November 17,1997, control room operators noticed level swings in the 2A2 Flash
      bypass valve, the operators were concemed with the potential tripping of the heater string
Tank. Since the level swings were increasing to the point of automatic opening of the
      and subsequent impact on feedwater temperature. Licensee personnel performed a
bypass valve, the operators were concemed with the potential tripping of the heater string
      heater bay entry rnd identified that the positioner arm oa 'he level control valve was
and subsequent impact on feedwater temperature. Licensee personnel performed a
      broken. Maintenance personnel repaired she level conWI valve and the heater string was
heater bay entry rnd identified that the positioner arm oa 'he level control valve was
      retumed to a normal status. Licensee personnel documented the occurrence via
broken. Maintenance personnel repaired she level conWI valve and the heater string was
      PIF D1997-08160.
retumed to a normal status. Licensee personnel documented the occurrence via
      The inspectors concluded that the operators performed well by identifying the unexpected
PIF D1997-08160.
      level swingt early enough to allow for corrective action before automatic tripping of the
The inspectors concluded that the operators performed well by identifying the unexpected
      heater string.
level swingt early enough to allow for corrective action before automatic tripping of the
      The inspectors noted that this issue was similar to problems operators encountered with
heater string.
      heatet level controls previously documented in inspection reports 97012 and 97013.
The inspectors noted that this issue was similar to problems operators encountered with
                                                  14
heatet level controls previously documented in inspection reports 97012 and 97013.
14


      - - . -                           . -.     -         - - _ - .                     -    -_
- - . -
  -
. -.
    .
-
                                                                                                                l
- - _ - .
                                                                                                                i
-
                                                                                                                '
-_
                  2A Feedwater Regulating Valve
-
                  On November 18,1997, licensee maintenance personnel were doing work on the 2A
.
                  feedwater regulating valve (FRV) when operators notice >d that the 28 FRV had switched        ,
                                                                                                                '
                  from submetic control to manual centrol. The operators entered trcnsient level control,
                  but experienced some d fficulty in matching steam flow and feed flow to stabilize level
                  since the low flow FRV was still in automatic and was attempting to control level.
                  Operators were subsequently able to place the low flow FRV in manual control and
                  restore reactor level to its proper level. During the transient, reactor level went as high as
                  32 inches (normallevelis 30 inches) and as low as 22 inches. The operators had
                  direction to insert a manual reactor trip (scram) if level dropped as low as 20 inches. An
'
                  inadequate work package and deficient work instructions caused the reactor water level
                  transient (reference Section M2.1 of this report for additional discussion of this issue).
                  The operators responded well to an unexpected reactor water level transient caused by
                  improper maintenance work in the field. The operator's successful recovery of water
                  level, and restoration to the proper level band, demonstrated effective corrective actions
                  started after operators mishandled a levt,l transient in July 1997 (see inspection
                  Report No. 50 237/97016(DRS) for more information).
              c. .Qgnqlgig
                  The operators reonded well to material condition induced challenges and transients.
l                However, the challenges themselves were similar in nature to previous occurrences and
                  Indicated ineffe:tive licensee efforts to correct known plant deficiencies. The inspectors
                  were concemed about the equipment problems discussed above since material condition
                  issues continued to challenge operators. The items above were repeat items and were
                  similar in nature to items previously documented in NRC intpection reports. The
                  inspectors concluded that licensee effort to address known material condition deficiencies    ,
                  were not completely effeJive.
            08  Miscellaneous Operations issues
!            08.1 (Unit 3) Hioh Pressure Coolant inlection (HFCl) System
1-             a. inspection Scope (71707)
                  On September 5, the licensee declared the Unit 3 high pressure coolant injection (HPCI)
l                system inoperable due to a malfunctioning level control! alarm switch in the HPCI gland
                  seal condenser hotwell. The licensee issued LER 50 249/97-009 to document the event.
l                The inspectors discussed the LER with the licensee, and reviewed and observed
!                subsequent operability surveillances performed on September 7 and September 8 to
l                declare HPCI operable.
l
l
l              b. Ob6ervations and Findinas
i
                  On September 6, the licerisee isolated the HPCI system steam line in preps,ation for
2A Feedwater Regulating Valve
                  completing repairs on the HPCI system gland seal condenser hotwell. On September 7,
'
                  after replacing the level control / alarm switch in the HPCI gland seal condenser hotwell,
On November 18,1997, licensee maintenance personnel were doing work on the 2A
                                                                        15
feedwater regulating valve (FRV) when operators notice >d that the 28 FRV had switched
,
'
from submetic control to manual centrol. The operators entered trcnsient level control,
but experienced some d fficulty in matching steam flow and feed flow to stabilize level
since the low flow FRV was still in automatic and was attempting to control level.
Operators were subsequently able to place the low flow FRV in manual control and
restore reactor level to its proper level. During the transient, reactor level went as high as
32 inches (normallevelis 30 inches) and as low as 22 inches. The operators had
direction to insert a manual reactor trip (scram) if level dropped as low as 20 inches. An
inadequate work package and deficient work instructions caused the reactor water level
'
transient (reference Section M2.1 of this report for additional discussion of this issue).
The operators responded well to an unexpected reactor water level transient caused by
improper maintenance work in the field. The operator's successful recovery of water
level, and restoration to the proper level band, demonstrated effective corrective actions
started after operators mishandled a levt,l transient in July 1997 (see inspection
Report No. 50 237/97016(DRS) for more information).
c.
.Qgnqlgig
The operators reonded well to material condition induced challenges and transients.
l
l
                                                          - - .           .
However, the challenges themselves were similar in nature to previous occurrences and
Indicated ineffe:tive licensee efforts to correct known plant deficiencies. The inspectors
were concemed about the equipment problems discussed above since material condition
issues continued to challenge operators. The items above were repeat items and were
similar in nature to items previously documented in NRC intpection reports. The
inspectors concluded that licensee effort to address known material condition deficiencies
,
were not completely effeJive.
08
Miscellaneous Operations issues
!
08.1
(Unit 3) Hioh Pressure Coolant inlection (HFCl) System
1-
a.
inspection Scope (71707)
On September 5, the licensee declared the Unit 3 high pressure coolant injection (HPCI)
l
system inoperable due to a malfunctioning level control! alarm switch in the HPCI gland
seal condenser hotwell. The licensee issued LER 50 249/97-009 to document the event.
l
The inspectors discussed the LER with the licensee, and reviewed and observed
!
subsequent operability surveillances performed on September 7 and September 8 to
l
declare HPCI operable.
l
l
b.
Ob6ervations and Findinas
On September 6, the licerisee isolated the HPCI system steam line in preps,ation for
completing repairs on the HPCI system gland seal condenser hotwell. On September 7,
after replacing the level control / alarm switch in the HPCI gland seal condenser hotwell,
15
l
- - .
.


  -
-
    .
.
      the licensee placed the Unit 3 HPCI system back in service and attempted to complete
the licensee placed the Unit 3 HPCI system back in service and attempted to complete
      DOS 2300-03, "High Pressure Coolant injection System Operability Verification."
DOS 2300-03, "High Pressure Coolant injection System Operability Verification."
      Immediately after opening the steam supply shutoff valve (3 23013) many exhaust drain
Immediately after opening the steam supply shutoff valve (3 23013) many exhaust drain
      pot high level alarms were received in the control room causing the NSO to trip the HPCI
pot high level alarms were received in the control room causing the NSO to trip the HPCI
      system turt>lne.
system turt>lne.
      Step I.1 of DOS 2300-33 required the licensee to drain the HPCI exhaust drain pot. The
Step I.1 of DOS 2300-33 required the licensee to drain the HPCI exhaust drain pot. The
      inspectors reviewed the completed surveillance procedure and noted that unit supervisor
inspectors reviewed the completed surveillance procedure and noted that unit supervisor
      administering this surveillance had initialed the procedural steps as ' conditions met"
administering this surveillance had initialed the procedural steps as ' conditions met"
      (C/M). However, if the condition was met, then the HPCI system would not have tripped.
(C/M). However, if the condition was met, then the HPCI system would not have tripped.
      The inspectors found no entry in the NSO logs nor the US logs that documented the drain
The inspectors found no entry in the NSO logs nor the US logs that documented the drain
      pot being drained. During subsequent interviews, the licensee stated that the US
pot being drained. During subsequent interviews, the licensee stated that the US
      believed that the condition was met based on information from the previous shift's US.
believed that the condition was met based on information from the previous shift's US.
      Specifically, the previous US said that the exhaust drain pot had been drained on two
Specifically, the previous US said that the exhaust drain pot had been drained on two
      prior shifts. The inspectors Mquested a copy of the completed procedure in which this
prior shifts. The inspectors Mquested a copy of the completed procedure in which this
      activity was performed to verify this information, but the licensee could not find the
activity was performed to verify this information, but the licensee could not find the
      completed procedures. The licensee was unable to produce any documentation to
completed procedures. The licensee was unable to produce any documentation to
support of the use of" conditions met"instead of draining the drain pot.
'
'
      support of the use of" conditions met"instead of draining the drain pot.
According to the system engineer, the drain pot had partially filled with condensed steam
      According to the system engineer, the drain pot had partially filled with condensed steam
(from the OOS HPCI steam line) which slowly leaked past the steam supply shutoff valve
      (from the OOS HPCI steam line) which slowly leaked past the steam supply shutoff valve
(3 2301 3). With the drain pot partially filled, there was not enough volume to receive the
      (3 2301 3). With the drain pot partially filled, there was not enough volume to receive the
condensate normally experienced during HPCI operation, so equalization problems
      condensate normally experienced during HPCI operation, so equalization problems
occurred. The exhaust drain pot was quickly filled, ultimately causing the turbine casing
      occurred. The exhaust drain pot was quickly filled, ultimately causing the turbine casing
to fill via the casing drain lines. The cystem engineer added that an addition 61 contributor
      to fill via the casing drain lines. The cystem engineer added that an addition 61 contributor
may have been the short time (one hour) between clearing the OOS (opening utoam
      may have been the short time (one hour) between clearing the OOS (opening utoam
valves 2301-4 and 23015) and restarting the surveillance (opening valves 23013 and
      valves 2301-4 and 23015) and restarting the surveillance (opening valves 23013 and
the turbine stop valve). After proper drainage of the HPCI system exhaust drain pot, the
      the turbine stop valve). After proper drainage of the HPCI system exhaust drain pot, the
operability surveillance was completed successfully.
      operability surveillance was completed successfully.
Step F.8. of DAP 09-13 *Procedura! Adherence" stated that " Condition Met (C/M) should
      Step F.8. of DAP 09-13 *Procedura! Adherence" stated that " Condition Met (C/M) should
be entered IP an Individual finds that the requirements of a procedure step are already
      be entered IP an Individual finds that the requirements of a procedure step are already
satisfied, e.g., the step calls for starting a pump; however, the pump is already running."
      satisfied, e.g., the step calls for starting a pump; however, the pump is already running."
Based on interviews with the licensee and the review of licensee documentation, there
      Based on interviews with the licensee and the review of licensee documentation, there
was no clear evidence that the procedural step was already satisfied. The licensee is
      was no clear evidence that the procedural step was already satisfied. The licensee is
required by TS 6.8.A to implement applicable procedures recommended in Appendix A of
      required by TS 6.8.A to implement applicable procedures recommended in Appendix A of
Regulatory GV.de (RG) 1.33, Rev. 2, Feb.1978. Administrative procedures goveming
      Regulatory GV.de (RG) 1.33, Rev. 2, Feb.1978. Administrative procedures goveming
procedure adherence are recommended in RG 1.33. Contrary to this, the licensee failed
      procedure adherence are recommended in RG 1.33. Contrary to this, the licensee failed
to follow DAP 09-13 guidance for determining if a condition had been met, and
      to follow DAP 09-13 guidance for determining if a condition had been met, and
consequently had to trip the HPCI system during a surveillance test manually. Although
      consequently had to trip the HPCI system during a surveillance test manually. Although
the actions were contrary to procedures, no violation was issued because the violation
      the actions were contrary to procedures, no violation was issued because the violation
would be expected to be encompassed by licensee corrective actions to a recently issued
      would be expected to be encompassed by licensee corrective actions to a recently issued
violation for operators not following procedures (50-237; 249/97019-2)
      violation for operators not following procedures (50-237; 249/97019-2)
16
                                                  16
..
                                                                                                    ..


      -
-
        c.   Qanslution
c.
              The inspectors concluded that the operations departmerW showed a lack of a questioning
Qanslution
              attitude during the September 7 operability surveillance run to declare the HPCI system .
The inspectors concluded that the operations departmerW showed a lack of a questioning
              operable. The inspectors also concluded that the shift i;'c,d a weak knowledge of
attitude during the September 7 operability surveillance run to declare the HPCI system .
              the operational implications of the HPCI turbine exhaust and vont system and how it was
operable. The inspectors also concluded that the shift i;'c,d a weak knowledge of
              effooted by the status of the Unit 3 HPCI system,
the operational implications of the HPCI turbine exhaust and vont system and how it was
                                                  11. Mainlanance
effooted by the status of the Unit 3 HPCI system,
        M2-   Maintonenee and Material Condition of Faellities and Equipment
11. Mainlanance
        M2.1 (Units 2 & Si trW of Feedwater Raoulatina Valve (FWRV) Maintenance
M2-
        a.   Inanection Boone (62707. 93702)
Maintonenee and Material Condition of Faellities and Equipment
              The inspectors reviewed the licensee's response to a level transient that occurred on
M2.1 (Units 2 & Si trW of Feedwater Raoulatina Valve (FWRV) Maintenance
              Unit 2 on November 18,1997. The review included assessing the licensee's response
a.
              and preliminary root causs.
Inanection Boone (62707. 93702)
        b.   Observations and Findinos
The inspectors reviewed the licensee's response to a level transient that occurred on
              On November 18,1997, with Unit 2 at approximately 80 percent power, maintenance and
Unit 2 on November 18,1997. The review included assessing the licensee's response
              engineering were allowed to do maintenance on the 2A FWRV. The work was to address
and preliminary root causs.
              soms instability exhibited by the 2A FWRV in positions between 30 - 80 percent open by
b.
:              replacing the linear variable differential transformer (LVDT). The licensee repleoed a
Observations and Findinos
On November 18,1997, with Unit 2 at approximately 80 percent power, maintenance and
engineering were allowed to do maintenance on the 2A FWRV. The work was to address
soms instability exhibited by the 2A FWRV in positions between 30 - 80 percent open by
replacing the linear variable differential transformer (LVDT). The licensee repleoed a
:
solenoid on the valve's operator during the single-loop operations of November 18, but
#
#
              solenoid on the valve's operator during the single-loop operations of November 18, but
the valve continued to exhibit erratic operation, so the licensee was next trying the LVDT.
              the valve continued to exhibit erratic operation, so the licensee was next trying the LVDT.
,
,
              The licensee used WR 97012985 01, "2A FW REG VLV; Valve Exhibits instability -
The licensee used WR 97012985 01, "2A FW REG VLV; Valve Exhibits instability -
,              between 20 and 52 percent replacement.' When a lead was lifted from the LVDT, the 28
between 20 and 52 percent replacement.' When a lead was lifted from the LVDT, the 28
:             FWRV swapped from automatic control to manual control. The swap caused a loss of
,
              automatic reaclor pressure vessel (RPV) level control, and cycling of the low-flow
:
              feedwater regulating valve. The operators were challenged, but recovered RPV level
FWRV swapped from automatic control to manual control. The swap caused a loss of
              -(see Section 04.4).
automatic reaclor pressure vessel (RPV) level control, and cycling of the low-flow
feedwater regulating valve. The operators were challenged, but recovered RPV level
-(see Section 04.4).
The preliminary investigation by the licensee, and presented to the Plant Operations
'
'
              The preliminary investigation by the licensee, and presented to the Plant Operations
Review Committee (PORC) on November 20,1997, determined that the response of the
              Review Committee (PORC) on November 20,1997, determined that the response of the
feedwater control system was correct. The system was designed to place the FWRVs in
              feedwater control system was correct. The system was designed to place the FWRVs in
manual mode if the LVDT current loop opens. The automatic modo swap was designed
              manual mode if the LVDT current loop opens. The automatic modo swap was designed
to fall the valve "as-is"in the nont of a problem with the quality of the signal. This -
              to fall the valve "as-is"in the nont of a problem with the quality of the signal. This -
feature had not been identified in the work package. The work request was reviewed by
              feature had not been identified in the work package. The work request was reviewed by
a senior reactor operator before execution, but the SRO also did not realize that the work
              a senior reactor operator before execution, but the SRO also did not realize that the work
on the 2A LVDT would affect the control of the 28 FWRV.
              on the 2A LVDT would affect the control of the 28 FWRV.
The licensee's investigation team informed :he PORC that the type and number of
              The licensee's investigation team informed :he PORC that the type and number of
reviews done for the WR were correct per DAP 15-06, but the reviews were inadequate,
                reviews done for the WR were correct per DAP 15-06, but the reviews were inadequate,
one of the proposed corrective actions was to have feedwater level control system
                one of the proposed corrective actions was to have feedwater level control system
corrective type work have a technical review. -
                corrective type work have a technical review. -
17
                                                          17
.
                                                                                    .
..l
  ..l                                                                                               --
--
                                                                                                          ,
,


          - _ _ _ . . __ .______                                                                                     _._               -__-____
- _ _ _ . . __ .______
  l                                                                                                                                                                                                                                 h
_._
    a             ,
-__-____
                                                                                                                                                                                                                                    r
l
                                                                                                                                                                                                                                    i
h
i                                                                                                                                                                                                                                  !
a
                                                                                                                                                                                                                                    r
r
                                        The inspectors noted that some precursor events suggested the need for greater                                                                                                            ;
                                        attention to foodwater level control system procedures, in inspection Repori No. 97012                                                                                                    ;
                                        Section M1.1, the inspectors documented the June is unexpected opening of the
  ;                                      SA FWRV due to a procedure revision error. The inspectors also noted that
i                                      PlF# Digg7-07698, "3A FWRV Found in Test Mode," Novenhor 2,1997, desenbod the                                                                                                            -i
                                        operators' discovery that the Unit 3 A FWRV had unexpectedy gone into ' Test" mode                                                                                                        :
                                                                                                                                                                                                                                    i
                                        following the shutdown of Unit 3. The system engineer informed operations that, "the tog
                                        valves will automaticalh go into twt mode on a loss of LVDT signal," and theortrod that -                                                                                                  i
                                        the rapid response of the FWRV following the scram may have caused a momentary loss                                                                                                        !
  ;                                      of LVDT signal to the controller. This had not occurred before, so the iloonsee replaced                                                                                                  !
i                                      the LVDT oscillator card to reduce the likelihood of a re:urrence. The inspectors                                                                                                          !
                                        recognized that there are a ome differences between the Unit 2 and Valt 3 FWCS,                                                                                                            !
                                        (according to the system engineer, placing Unit 3 FWC8 into test before lifting the lead                                                                                                  ;
                                                                                                                                                                                                                                    ;
                                        would have been sufficient; the Unit 3 LVDTs would not have to be separately placed in
                                        test). However, the inspectors concluded that the incident documented in the PlF                                                                                                          ,
                                        demonstrated that LVDT c9n impact the valve configuratinn,                                                                                                                                f,
                                      _
                                        The history of feedwater level control system problems at Dresden showed that feedwater                                                                                                    ;
-                                        maintenance needed thorough reviews. On May 31, igg 6, during testing of the                                                                                                              ;
                                        feedwater level control system, Unit 2 experienced a level transient of sufficient                                                                                                        !
                                                                                                                                                                                                                                    '
                                        - magnitude to cause the operators to shut down the plant. The event was described in
                                        Inspection report g6006 Section 02.1 and LER 237/g6-00g-00, " Manual Reactor Scram                                                                                                        !
4                                        due to Lowering Reactor Water Level due to Automatic Foodwater Level Control System
j                                        Design Deficiency." The LER stated:
2
                                                  "The decisions made during the FWC8 [feedwater control system) testing                                                                                                  /        t
!                                                  should have been more conservative . . . The review and assessment of                                                                                                          l
                                                  the risks and consequences associated with change could have been                                                                                                                ;
i.                                                mote thorough. Indicatior.s of the need to strengthen the conservative
i                                                  safety culture are as follows:
,
,
                                                  b.         It was riot recognized by the testing team that the on line
i
                                                              configuration function of the Bailey Network N was a potentially
i
j                                                            untested function and that it should have been tested prior to                                                                                                       ;
!
                                                                                                                                                                                                                                    '
r
                                                              relying on it for the logic configuration change."
The inspectors noted that some precursor events suggested the need for greater
                                                  d.        A review with independent personnel outside the test team was not                                                                                                     [
;
                                                                                                                                                                                                                                  '
attention to foodwater level control system procedures, in inspection Repori No. 97012
                                                              performed and may have identified the importance of placing the -
;
                                                              Master Station into manual prior to performing the evolution. "
Section M1.1, the inspectors documented the June is unexpected opening of the
SA FWRV due to a procedure revision error. The inspectors also noted that
;
PlF# Digg7-07698, "3A FWRV Found in Test Mode," Novenhor 2,1997, desenbod the
- i
i
operators' discovery that the Unit 3 A FWRV had unexpectedy gone into ' Test" mode
:
i
following the shutdown of Unit 3. The system engineer informed operations that, "the tog
valves will automaticalh go into twt mode on a loss of LVDT signal," and theortrod that -
i
the rapid response of the FWRV following the scram may have caused a momentary loss
!
;
of LVDT signal to the controller. This had not occurred before, so the iloonsee replaced
!
i
the LVDT oscillator card to reduce the likelihood of a re:urrence. The inspectors
!
recognized that there are a ome differences between the Unit 2 and Valt 3 FWCS,
!
(according to the system engineer, placing Unit 3 FWC8 into test before lifting the lead
;
would have been sufficient; the Unit 3 LVDTs would not have to be separately placed in
;
test). However, the inspectors concluded that the incident documented in the PlF
,
demonstrated that LVDT c9n impact the valve configuratinn,
f
,
The history of feedwater level control system problems at Dresden showed that feedwater
;
maintenance needed thorough reviews. On May 31, igg 6, during testing of the
_
;
-
feedwater level control system, Unit 2 experienced a level transient of sufficient
!
'
'
                                        Many of the statements in the LER could be directly applied to the November 18
- magnitude to cause the operators to shut down the plant. The event was described in
                                        transient. In the November 18 transient, the licensee did not recognize that changing the
Inspection report g6006 Section 02.1 and LER 237/g6-00g-00, " Manual Reactor Scram
                                        configuration of the LVDT (by lifting lead) affected the FWCS, and no independent review                                                                                                 *
!
                                        of the WR was performed that could have identified the importance of placing the control                                                                                                   ;
due to Lowering Reactor Water Level due to Automatic Foodwater Level Control System
                                        - stations h manual,
4
                                        Dresden Station TS 6.8.a required that written procedures be established, implemented,                                                                                                   i
j
                                        'and maintained covering the applicable procedures recommended in Appendix A of                                                                                                             .
Design Deficiency." The LER stated:
                                        RG 1.33, Revision 2 February 978. Appendix A of RG 1.33, Revision 2 February 1978,
"The decisions made during the FWC8 [feedwater control system) testing
/
t
2
!
should have been more conservative . . . The review and assessment of
l
the risks and consequences associated with change could have been
;
i .
mote thorough. Indicatior.s of the need to strengthen the conservative
i
safety culture are as follows:
b.
It was riot recognized by the testing team that the on line
,
configuration function of the Bailey Network N was a potentially
j
untested function and that it should have been tested prior to
;
'
relying on it for the logic configuration change."
d.
A review with independent personnel outside the test team was not
[
performed and may have identified the importance of placing the -
'
Master Station into manual prior to performing the evolution. "
Many of the statements in the LER could be directly applied to the November 18
'
transient. In the November 18 transient, the licensee did not recognize that changing the
configuration of the LVDT (by lifting lead) affected the FWCS, and no independent review
*
of the WR was performed that could have identified the importance of placing the control
;
- stations h manual,
Dresden Station TS 6.8.a required that written procedures be established, implemented,
i
'and maintained covering the applicable procedures recommended in Appendix A of
.
RG 1.33, Revision 2 February 978. Appendix A of RG 1.33, Revision 2 February 1978,
referenced procedures for the repair or replacement of equipment. The
-
-
                                        referenced procedures for the repair or replacement of equipment. The
.
                                                                                                                                                                                                                                    .
18
                                                                                                      18
:
                                                                                                                                                                                                                                    :
i
                                                                                                                                                                                                                                  i
e
e
  w sue.==   e-   w-wr=+-*--   w--'e     em   -e --M-- e-vo--,,,r---Nte -vv-, - vv - - - . - + = - = . - s.$--e,www-.n-y-ww.w + - - - * + v-4+ www we r= r-- e e==u-- w n -e m er v e ee v=%.e +w rece--ee,ce, w-w irr   wev*
w
sue.==
e-
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em
-e
--M--
e-vo--,,,r---Nte
-vv-,
-
vv - - - . - + = - = . -
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w n -e m er v e ee v=%.e +w rece--ee,ce, w-w irr
wev*


4
4
        work request 97012985-01 was inadequate to perform the repairs of the feedwater         :
work request 97012985-01 was inadequate to perform the repairs of the feedwater
        control system. Consequently, an unexpected reactor pressure vessellevel transient       l
control system. Consequently, an unexpected reactor pressure vessellevel transient
        occurred, and the operators had to take manual control of the feedwater level control   l
occurred, and the operators had to take manual control of the feedwater level control
        system.
system.
        Although the preparation of the procedure was inadequate, no violation was issued       ,
Although the preparation of the procedure was inadequate, no violation was issued
        because the licensee had not yet responded to a recently issued violation for inadequate
,
        procedure and corTective actions for tha previous violation would be expected to
because the licensee had not yet responded to a recently issued violation for inadequate
        encompass this issue (50-237; 249/97019-01).
procedure and corTective actions for tha previous violation would be expected to
  c.   Conclusions
encompass this issue (50-237; 249/97019-01).
        The work performed on the Unit 2 feedwater control system was poorly planned. The
c.
        failure to provided adequate work instructions directly challenged the operators. The
Conclusions
        history of feedwater system work and resulting transients showed that feedwater work
The work performed on the Unit 2 feedwater control system was poorly planned. The
        needed more stringent reviews than those provided.
failure to provided adequate work instructions directly challenged the operators. The
  M2.2 Surveillance Performance
history of feedwater system work and resulting transients showed that feedwater work
  a.   Inspection Scope (61726)
needed more stringent reviews than those provided.
        The inspectors witnessed and performed a documentation review for surveillance
M2.2 Surveillance Performance
        DIS-263-05, Rev. 8, " Unit 2 Anticipated Transient W.9out Scram (ATWS) Recirculation
a.
        Pump Trip and Attemate Rod Injection (RPT/ARI) and Emergency Core Cooling System
Inspection Scope (61726)
        (ECCS) Level Master Trip Unit (MTU) and Slave Trip Unit (STU) Channel Functional
The inspectors witnessed and performed a documentation review for surveillance
        Test."
DIS-263-05, Rev. 8, " Unit 2 Anticipated Transient W.9out Scram (ATWS) Recirculation
  b.   Observations and Findinal
Pump Trip and Attemate Rod Injection (RPT/ARI) and Emergency Core Cooling System
        During the performance of the surveillance, communication was established between the
(ECCS) Level Master Trip Unit (MTU) and Slave Trip Unit (STU) Channel Functional
        control room and the auxiliary electric equipment room. Three way communications were
Test."
        used in the performance of the surveillance. The inspectors researched the Updated
b.
        Final Safety Analysis Report (UFSAR) and TE s. The puriodicity of the surveillance was
Observations and Findinal
        compared with the TS requirements. The survoillance acceptance criteria listed in the
During the performance of the surveillance, communication was established between the
        procedure met the TS requirements. The surveillance was completed in a professional
control room and the auxiliary electric equipment room. Three way communications were
        manner.
used in the performance of the surveillance. The inspectors researched the Updated
  c.   Conclusion
Final Safety Analysis Report (UFSAR) and TE s. The puriodicity of the surveillance was
        The surveillance was satisfactorily completed and met the procedurn's acceptance
compared with the TS requirements. The survoillance acceptance criteria listed in the
        criteria. The surveillance was completed in a timely manner and met regulatory
procedure met the TS requirements. The surveillance was completed in a professional
        requirements,
manner.
  M4   Malntenance Staff Knowledge and Performance
c.
  M4.1 Condensate and Feedwater System
Conclusion
  a.   inspigtion Scope
The surveillance was satisfactorily completed and met the procedurn's acceptance
        The inspectors reviewed the worn instructions and interviewed licensee personnel
criteria. The surveillance was completed in a timely manner and met regulatory
        regarding the completion of Temp Alt Ill 1197 (Reference WR#970082873), and
requirements,
                                                  19
M4
Malntenance Staff Knowledge and Performance
M4.1 Condensate and Feedwater System
a.
inspigtion Scope
The inspectors reviewed the worn instructions and interviewed licensee personnel
regarding the completion of Temp Alt Ill 1197 (Reference WR#970082873), and
19


                      -- _ _           -.           .-     .-.             -         _ --         . - - - -           - .
-- _ _
  .
-.
                  reviewed the information about URI 50-010; 237; 249/97013-04 provided by the licensee                 i
.-
                  in Hs reply to a Notice (ref. JSPLTR: 97 0195).
.-.
      b.         QhattYah9fundf0f091                                                                                   ;
-
                                                                                                                          :
_ --
                  On August 3, in an attempt to alleviate repeated draining and flashing of the
. - - - -
                  3D2 HP heater high level switch (3 3541 558) reference leg, the licensee attempted a                   l
- .
                                                                                                                          '
.
                  temporary alteration (Reference Temp Att lll 1197 and WR#970082873). Maintenance
reviewed the information about URI 50-010; 237; 249/97013-04 provided by the licensee
                  personnel connected the reference jeg to the high-pressure side of the heater rather than
i
                  the low pressure side as diagramed in the work instructions. The temporary ahoration                   '
in Hs reply to a Notice (ref. JSPLTR: 97 0195).
                  work failed its acceptance criteria during performance of functional testing. The licensee
b.
                  discovered that the reference leg had been connected to the wrong pipe.
QhattYah9fundf0f091
                  Results of investigation and inspector interviews of maintenance and engineering
;
                  personnel suggest workers became confused due to labeling problems during installation
:
                  and a poor sketch from engineering included in the work instruction.
On August 3, in an attempt to alleviate repeated draining and flashing of the
                                                                                                                          I
3D2 HP heater high level switch (3 3541 558) reference leg, the licensee attempted a
                  The workers' action to continue of with work despite this confusion demonstrated poor
l
                                                                                                                          i
temporary alteration (Reference Temp Att lll 1197 and WR#970082873). Maintenance
                  work prtctices, since DAP 05 08 " Control of Temporary System AHerstions" stated that,
'
                  "Whi!e performing a temporary aHeration, if field conditions are different from shown in
personnel connected the reference jeg to the high-pressure side of the heater rather than
                  wort, psckage then stop and contact the preparer." The inspectors verified that this had
the low pressure side as diagramed in the work instructions. The temporary ahoration
                                                                                                                          +
'
'
                  not occurred.
work failed its acceptance criteria during performance of functional testing. The licensee
                  The licensee reported that the maintenance workers who performed the work were
discovered that the reference leg had been connected to the wrong pipe.
                  coached by the department supervisor and the engineer who mad < the poor , ketch
Results of investigation and inspector interviews of maintenance and engineering
                  agreed that the sketch should have provided clearer guidance. Tin licensee initiated a
personnel suggest workers became confused due to labeling problems during installation
                  Nuclear Tracking System (NTS) ltem (NTS 237100-97-01304A) to coach the engineer
and a poor sketch from engineering included in the work instruction.
                  regarding engineering standards. The involved workers were contract employees and
I
                  were no longer working at the site.
The workers' action to continue of with work despite this confusion demonstrated poor
                  The licensee was required by TS 6.8.A to implement applicable procedures
work prtctices, since DAP 05 08 " Control of Temporary System AHerstions" stated that,
                  recommended in Appendix A of RG 1.33, Rev. 2, Feb.1978. Adherones to administrative
i
                  procedure goveming temporary alteration is recommended in RG 1.33.
"Whi!e performing a temporary aHeration, if field conditions are different from shown in
                  Since this self revealing and corrected violation occurred while working on
wort, psckage then stop and contact the preparer." The inspectors verified that this had
                  nonsafety-related equipment, and did not adversely affect the safe operation of the
+
                  reactor, the violation is being treated as a Non Cited Violation, consistent with
not occurred.
                  Section Vll.B.1 of the NRC Enforcement Policy (NCV 50 237/97024-02(DRP)).
'
      c.         Conclusion
The licensee reported that the maintenance workers who performed the work were
                  Due to a lack of detail on a sketch provided by engineering and a lack of a questioning
coached by the department supervisor and the engineer who mad < the poor , ketch
                  attitude by a maintenance worker, the licensee demonstrated poor performance and work
agreed that the sketch should have provided clearer guidance. Tin licensee initiated a
                  practices regarding the installation of Temp Alt lll 1197.                                             <
Nuclear Tracking System (NTS) ltem (NTS 237100-97-01304A) to coach the engineer
      M4.2 Rework (62707)
regarding engineering standards. The involved workers were contract employees and
                  The inspectors noted several examples of maintenance rework following the forced
were no longer working at the site.
                  outage activities.
The licensee was required by TS 6.8.A to implement applicable procedures
                                                              20
recommended in Appendix A of RG 1.33, Rev. 2, Feb.1978. Adherones to administrative
    - . . - . . .                 -         .         -   -     . . . - . . - . .- . . . . . -             , - --.
procedure goveming temporary alteration is recommended in RG 1.33.
Since this self revealing and corrected violation occurred while working on
nonsafety-related equipment, and did not adversely affect the safe operation of the
reactor, the violation is being treated as a Non Cited Violation, consistent with
Section Vll.B.1 of the NRC Enforcement Policy (NCV 50 237/97024-02(DRP)).
c.
Conclusion
Due to a lack of detail on a sketch provided by engineering and a lack of a questioning
attitude by a maintenance worker, the licensee demonstrated poor performance and work
practices regarding the installation of Temp Alt lll 1197.
<
M4.2 Rework (62707)
The inspectors noted several examples of maintenance rework following the forced
outage activities.
20
-
. . - . . .
-
.
-
-
. . . - . . - . .- . . . . . -
, - --.


.                                                                                                   :
.
  .
.
        *     The licensee identified that the correct post maintenance testing (PMT) was not
*
                performed following the weld repairs on the recirculation piping. As a
The licensee identified that the correct post maintenance testing (PMT) was not
                consequence, the licensee had to redo the weld repair; almost 300 additional and
performed following the weld repairs on the recirculation piping. As a
                unnecessary millirem were received by station personnel as a result.
consequence, the licensee had to redo the weld repair; almost 300 additional and
        *      Prior to the shutdown, the number 3 bypass valve showed conflicting position
unnecessary millirem were received by station personnel as a result.
                indication. Position indication repair was included in the forced outage schedule.
Prior to the shutdown, the number 3 bypass valve showed conflicting position
                After the outage, however, the valve still showed conflicting posit.on indication,
*
        o      Prior to the forced outage, intermediate range monitor (IRM) 16 experienced
indication. Position indication repair was included in the forced outage schedule.
                erratic indication. The licensee's repair efforts were unsuccessful; following the
After the outage, however, the valve still showed conflicting posit.on indication,
                outage maintenance work, the IRM still displayed erratic indication. The licensee
Prior to the forced outage, intermediate range monitor (IRM) 16 experienced
                subsequently c'etermined that moisture was present in the IRM cable and the IRM
o
                would require further repairs during the next refueling outage.
erratic indication. The licensee's repair efforts were unsuccessful; following the
        The consequences of the maintenance rework issues were not severe; husever, they
outage maintenance work, the IRM still displayed erratic indication. The licensee
        were indicative of weak maintenance performance. In the case of the IRM, the scope of
subsequently c'etermined that moisture was present in the IRM cable and the IRM
        the work was not correctly diagnosed; a situation similar to previous concems about
would require further repairs during the next refueling outage.
        correct problem diagnosis documented in prior NRC inspection reports.
The consequences of the maintenance rework issues were not severe; husever, they
    M7   Quality Assurance in Maintenance Activities
were indicative of weak maintenance performance. In the case of the IRM, the scope of
    M7.1 Licensee Self Atitssments Activities (40500)
the work was not correctly diagnosed; a situation similar to previous concems about
    a. Inspection Scope (71707. 83822)
correct problem diagnosis documented in prior NRC inspection reports.
        The inspectors reviewed three licensee self-assessments in the maintenance area. The
M7
        self assessment's scope, depth, and conclusions were reviewed.
Quality Assurance in Maintenance Activities
    b. Observations and Findinat
M7.1
        The following licensee self assessments were reviewed:
Licensee Self Atitssments Activities (40500)
        1.     NIf assessment of the maintenance process for the potential of unauthorized
a.
                modifications. The assessment dates were January 7,1997, to January 29,1997.
Inspection Scope (71707. 83822)
                The objective of the assessment was to review a sample of completed corrective
The inspectors reviewed three licensee self-assessments in the maintenance area. The
                maintenance work requests from the past four years for unauthorized
self assessment's scope, depth, and conclusions were reviewed.
                modifications.
b.
                A ssmple of 315 work requests was reviewed. The sample size was determined
Observations and Findinat
                using American National Standard Sampling Procedures and Tables for
The following licensee self assessments were reviewed:
                Inspection (ANSI /ASQC Z1.4-1993). One unauthorizea modification was
1.
                identified in which a cover was bolte1 over a temperature switch. The
NIf assessment of the maintenance process for the potential of unauthorized
                assessment also found one instanca where a vendor manual was not properly
modifications. The assessment dates were January 7,1997, to January 29,1997.
                updated. Using a table in ANSI /ASQC Z1.4-1993, it was determined with a
The objective of the assessment was to review a sample of completed corrective
                99.85 percent confidence level that corrective maintenance work requests
maintenance work requests from the past four years for unauthorized
                completed during the period did not result in unauthorized modifications. Based
modifications.
                on the confidence level it was concluded that no further actions were roquired.
A ssmple of 315 work requests was reviewed. The sample size was determined
                                                  21
using American National Standard Sampling Procedures and Tables for
Inspection (ANSI /ASQC Z1.4-1993). One unauthorizea modification was
identified in which a cover was bolte1 over a temperature switch. The
assessment also found one instanca where a vendor manual was not properly
updated. Using a table in ANSI /ASQC Z1.4-1993, it was determined with a
99.85 percent confidence level that corrective maintenance work requests
completed during the period did not result in unauthorized modifications. Based
on the confidence level it was concluded that no further actions were roquired.
21


      __       . _ . . . _ . _ . _ _                     . . _ . . _ . _ . _ . _         __.             _ . _ . _ _ _ _ _ _
__
    -
. _ . . . _ . _ . _ _
              .
. . _ . . _ . _ . _ . _
                                              The self assessment did not identify that maintenance personnel t'eoded
__.
                                              additional training in modifications. Shortly after the self assessment, the NRC
_ . _ . _ _ _ _ _ _
                                            - Issued a violation for an unauthortrod modification (an installed and unattended
-
                                              digital voltmeter on a safety-related battery).. The response to the violation stated     ,
.
                                              the unauthorized modification occurred due to the individual n0t being fully aware       j
The self assessment did not identify that maintenance personnel t'eoded
                                              of the requirements for temporary modifications. The response to the violation           !
additional training in modifications. Shortly after the self assessment, the NRC
                                              stated maintenance p%f onnel would be trained on the temporary modificat6on               !
- Issued a violation for an unauthortrod modification (an installed and unattended
                                                procedure. The inspeaors therefore concluded that the self-assessment failed to         !
digital voltmeter on a safety-related battery).. The response to the violation stated
                                              :dentify the training weakness.                                                           !
,
                                                                                                                                        ,
the unauthorized modification occurred due to the individual n0t being fully aware
;                                     2.       Self assessment of the conduct of maintenance. The assessment dates were                 i
j
of the requirements for temporary modifications. The response to the violation
!
stated maintenance p%f onnel would be trained on the temporary modificat6on
!
procedure. The inspeaors therefore concluded that the self-assessment failed to
!
:dentify the training weakness.
!
,
;
2.
Self assessment of the conduct of maintenance. The assessment dates were
i
'
'
                                              February 1,1997, through February 28,1997. The objective of the assessment               l
February 1,1997, through February 28,1997. The objective of the assessment
                                              was to determite if work practices used during the conduct of maintenance were           [
l
                                              in keeping with t,.e highest industry standards,                                         j
was to determite if work practices used during the conduct of maintenance were
                                              Procedures, policies, the problem identification form (PIF) data base, .               I '
[
                                              main'enance monthly performance reports, and other documents were reviewed
in keeping with t,.e highest industry standards,
                                              by the self assessment team. In addition, interviews and in the-fleid obtervations
j
                                              were performed.                                                                           :
Procedures, policies, the problem identification form (PIF) data base, .
                                              There were 28 findings listed in the self assessment. They could be summartzed
I
                                              as findings of work start delays and procedural nonoompliance events durit's
main'enance monthly performance reports, and other documents were reviewed
                                              planning, scheduling, work performance, and work documentation. There were no             ,
'
                                              strengths documented in the self assessmem. The report stated that all areas
by the self assessment team. In addition, interviews and in the-fleid obtervations
                                                                                                                                        i
were performed.
                                              evaluated during the self estessment were found to need improvement. The _
:
                                              report further stated, "The overall performance trend found in most cases was
There were 28 findings listed in the self assessment. They could be summartzed
                                              either stagnated, cyclic, or had a declining performance trend."
as findings of work start delays and procedural nonoompliance events durit's
                                                                                                                                        ,
planning, scheduling, work performance, and work documentation. There were no
                                      3.       Self assessment of maintenance cerformance indicators. The assessment dates
,
                                              were September 15 through September 26,1997. The objective of the self
strengths documented in the self assessmem. The report stated that all areas
                                              assessment was to perform an effectiveness determination of the maintenance
i
                                              performance indicators.
evaluated during the self estessment were found to need improvement. The _
                                              Interviews with maintenance management were conducted to get their impression           ;
report further stated, "The overall performance trend found in most cases was
                                              of maintenance performance indicators.                                                   l
either stagnated, cyclic, or had a declining performance trend."
                                              The findings of the self assessment were that the maintenance department has
3.
                                              failed to: 1) take ownership and communicate the expectations and requirements
Self assessment of maintenance cerformance indicators. The assessment dates
                                              for the measurement of performance indicators, and 2) provide for the adequate
,
                                              resources for properiy maintaining and evaluating the performance indicators.           '
were September 15 through September 26,1997. The objective of the self
                                              There were no strengths documented in the self assessment.
assessment was to perform an effectiveness determination of the maintenance
                          c.         Conclusion
performance indicators.
                                      For the most part the self assessments were of sufficient scope and depth. The
Interviews with maintenance management were conducted to get their impression
                                      self assessments were hard hitting and critical of the maintenance process. The
;
                                      exception was the self assessment on unauthorized inodifications because it did not             3
of maintenance performance indicators.
                                                                                                                                        '
l
                                      identify that some workers' knowledge of modification requirements was deficient.-
The findings of the self assessment were that the maintenance department has
                                                                                                                                        '
failed to: 1) take ownership and communicate the expectations and requirements
                                                                                    22
for the measurement of performance indicators, and 2) provide for the adequate
                                                                                                                                        i
resources for properiy maintaining and evaluating the performance indicators.
  :     =.- .- .                         :     = - - .. -                       _-         .. - -.- - - -.:-.- -.                 =
'
There were no strengths documented in the self assessment.
c.
Conclusion
For the most part the self assessments were of sufficient scope and depth. The
self assessments were hard hitting and critical of the maintenance process. The
exception was the self assessment on unauthorized inodifications because it did not
3
identify that some workers' knowledge of modification requirements was deficient.-
'
'
22
i
:
=.- .- .
:
= - - .. -
-
.. - -.- - - -.:-.- -.
=


--                                                     .
--
                                                                                                          _
.
                                      .
.
  .
_
    M7.2 Lleenste Quality and_ Safety Assessment Activities f40500)
.
      a.   Inspection Sco,pe f71707. 84822)
M7.2 Lleenste Quality and_ Safety Assessment Activities f40500)
            The inspectors reviewed licensee Quality and Safety Assessment (Q&SA) activities in tne
a.
            maintenante area. Documents reviowed included audit reports, completed surveillance
Inspection Sco,pe f71707. 84822)
            reports, and field monitoring reports.
The inspectors reviewed licensee Quality and Safety Assessment (Q&SA) activities in tne
      b.   Observations and Findinot
maintenante area. Documents reviowed included audit reports, completed surveillance
            Q&SA audit reports are documentation of in depth reviews of se'ected areas. The audits
reports, and field monitoring reports.
            are usually conducted by a team of Individuals. In the maintenance area the inspectors
b.
            reviewed the fo! lowing audit reports:
Observations and Findinot
                      QAA 12 96-09,         Unit i decommissioning
Q&SA audit reports are documentation of in depth reviews of se'ected areas. The audits
                      QAA 12 9610,           ASME code / maintenance / contractor activities
are usually conducted by a team of Individuals. In the maintenance area the inspectors
                      QAA 12 97 02,         Staffing and training
reviewed the fo! lowing audit reports:
                      QAA 12 07 0/,         Corrective actions
QAA 12 96-09,
                      QAA 12 9710,           Outage activl'..a
Unit i decommissioning
                      QAA 12 9715,           Station blatkout system
QAA 12 9610,
            The audit reports contained many negative findings including corrective action records
ASME code / maintenance / contractor activities
              (CARS), PlFs, and recommendations. The audit reports also included some positive
QAA 12 97 02,
              comments. The reports did not back away from criticizing licensee practices and did not
Staffing and training
              focus on unimportant details.
QAA 12 07 0/,
              The Q&SA surveillance reports are of much less depth than aun,ts. They are usually
Corrective actions
              performed by a few people and focused on a specific atea or topic. The following
QAA 12 9710,
              surveillance reports were reviewed:
Outage activl'..a
                      QAS 12 96 01,         Vendor technical information program
QAA 12 9715,
                      QAS 12 96-04,           instrument out of tolerance trend
Station blatkout system
                      QAS 12 96-06,           Material condition on unit 2 east low pressure coolant
The audit reports contained many negative findings including corrective action records
                                              injection comer room
(CARS), PlFs, and recommendations. The audit reports also included some positive
                      QAS 12 96-17,         GE HGA relay investigation
comments. The reports did not back away from criticizing licensee practices and did not
                      QAS 12 96-26,         Electrical bus 331 maintenance
focus on unimportant details.
                      QAS 12 96-33           Reactor building ventilation
The Q&SA surveillance reports are of much less depth than aun,ts. They are usually
                      QAS 12 96-30           Rework / repeat work
performed by a few people and focused on a specific atea or topic. The following
                      QAS 12 96-43,           in-place repair of 3B reactor recirculation pump motor
surveillance reports were reviewed:
                      QAS 12 97-16,           Commitments for Meriin Gerirt circuit breakers
QAS 12 96 01,
                      QAS 12-9719,           Scheduled adherence during Ihe refueling outage
Vendor technical information program
                      QAS 12 97 25,           NRC Generic Letter 96-01," Testing of Safety Related Logic
QAS 12 96-04,
                                              Circuits"
instrument out of tolerance trend
                      QAS 12 97 26,           Corrective actions to improve electronic work control
QAS 12 96-06,
              The surveillance reports, while of less depth than the audit reports, still contained many
Material condition on unit 2 east low pressure coolant
              good recommendations and findings. The reports were critical and well balanced.
injection comer room
              The Q&SA field monitoring reports (FMRs) documented the observations the made while
QAS 12 96-17,
              touring the station. They were short and stated what the Q&SA individual observed and
GE HGA relay investigation
                                                          23
QAS 12 96-26,
                                                                    _ _ - _ - _ _ - _ _ - - - - -
Electrical bus 331 maintenance
QAS 12 96-33
Reactor building ventilation
QAS 12 96-30
Rework / repeat work
QAS 12 96-43,
in-place repair of 3B reactor recirculation pump motor
QAS 12 97-16,
Commitments for Meriin Gerirt circuit breakers
QAS 12-9719,
Scheduled adherence during Ihe refueling outage
QAS 12 97 25,
NRC Generic Letter 96-01," Testing of Safety Related Logic
Circuits"
QAS 12 97 26,
Corrective actions to improve electronic work control
The surveillance reports, while of less depth than the audit reports, still contained many
good recommendations and findings. The reports were critical and well balanced.
The Q&SA field monitoring reports (FMRs) documented the observations the made while
touring the station. They were short and stated what the Q&SA individual observed and
23
_ _ - _ - _ _ - _ _ - - - - -


  .
.
concluded. The inspectors reviewed 112 FMRs made from June through October 1997.
'
'
          concluded. The inspectors reviewed 112 FMRs made from June through October 1997.
The inspectors considered the number of reports to show an active Q&SA organization.
          The inspectors considered the number of reports to show an active Q&SA organization.
c.
    c.   Qonclusion
Qonclusion
          The Q&SA organ!zation was satisfactorily monitoring the cctivities in maintenance. The
The Q&SA organ!zation was satisfactorily monitoring the cctivities in maintenance. The
          audit reports and surveillance were complet6, thorough, and critical. The field monitoring
audit reports and surveillance were complet6, thorough, and critical. The field monitoring
          reports were an indication that Q&SA personnel performed sufficient field monitoring
reports were an indication that Q&SA personnel performed sufficient field monitoring
          activities.
activities.
    M8     Miscellaneous Maintenance issues
M8
    M81.1 (Closed) LER 50-249/97-09-00: HPCI System Declared Inoperable Following Gland Seal
Miscellaneous Maintenance issues
          Leakoff Condenser Hotwell High Level During to Drain Pump Stop Switch Failure. This
M81.1 (Closed) LER 50-249/97-09-00: HPCI System Declared Inoperable Following Gland Seal
          LER documented the self-revealing failure of the Unit 3 HPCI system during routine
Leakoff Condenser Hotwell High Level During to Drain Pump Stop Switch Failure. This
          surveillance testing. The failure occurred on September 5,1997, and the HPCI system
LER documented the self-revealing failure of the Unit 3 HPCI system during routine
          was restored following repairs on September 8. This issue was discussed in
surveillance testing. The failure occurred on September 5,1997, and the HPCI system
          Report 97019 and in Section 08.1 of this report. This issue is closed.                                 i
was restored following repairs on September 8. This issue was discussed in
    M8.2 (Closed) URI 50-010: 237: 249/97013-04f DRP): Failure of Temporary Alteration 111-11-97
Report 97019 and in Section 08.1 of this report. This issue is closed.
          to Mset Acceptance Criteria Requirements During Performance of Functional Testing Due
i
          to Maintenance Error. This item was discussed in Section M4.1 of this report. This item
M8.2 (Closed) URI 50-010: 237: 249/97013-04f DRP): Failure of Temporary Alteration 111-11-97
          is closed.
to Mset Acceptance Criteria Requirements During Performance of Functional Testing Due
                                              Ill. Enaineerina
to Maintenance Error. This item was discussed in Section M4.1 of this report. This item
    E2     Engineering Suppott of Facilities and Equipment
is closed.
    E2.1   Enaineerina Support of Emeraency Diesel Generators
Ill. Enaineerina
      a.   Insoection Scope (37551)
E2
            The inspectors reviewed the licensee's awareness of and compliance with the
Engineering Suppott of Facilities and Equipment
            recommendations for torquing cylinder test valves on the emergency diesel generators.
E2.1
            The inspectors also reviewed the licensee's corrective actions for an event that took
Enaineerina Support of Emeraency Diesel Generators
            place last year when a cylinder test valve was ejected during a Unit 3 EDG surveClance
a.
            test.
Insoection Scope (37551)
      b.   Observations and Findinas
The inspectors reviewed the licensee's awareness of and compliance with the
            On November 24,1996, a cylinder test valve was ejected from the Unit 3 EDG during a
recommendations for torquing cylinder test valves on the emergency diesel generators.
            surveillance test. Sections 02.2 and E4.1 of Inspection Report No. 96014 documented
The inspectors also reviewed the licensee's corrective actions for an event that took
            the inspectors' review of the issue, and the discovery by the inspectors that the current
place last year when a cylinder test valve was ejected during a Unit 3 EDG surveClance
            vendor information regarding the cylinder test valves was not entered into the licensee's
test.
            Vendor Equipment Technical Information Program (VETIP). The NRC documented the
b.
            failure in violation VIO 50-237; 249/96014-02.
Observations and Findinas
            On November 12,1997, personnel at the LaSalle station found a loose cylinder test
On November 24,1996, a cylinder test valve was ejected from the Unit 3 EDG during a
            valve. During review of the LaSalle event, the inspectors at LaSalle found vendor
surveillance test. Sections 02.2 and E4.1 of Inspection Report No. 96014 documented
                                                        24
the inspectors' review of the issue, and the discovery by the inspectors that the current
                                                                                          -__________-____ _ _ _ -
vendor information regarding the cylinder test valves was not entered into the licensee's
                                                                                            .
Vendor Equipment Technical Information Program (VETIP). The NRC documented the
failure in violation VIO 50-237; 249/96014-02.
On November 12,1997, personnel at the LaSalle station found a loose cylinder test
valve. During review of the LaSalle event, the inspectors at LaSalle found vendor
24
-__________-____ _ _ _ -
.


--               .   ..     .     -.                     - _ - - - _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _
--
  <
.
    .
..
.
-.
- _ - - - _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _
<
.
I
I
      information that was not incorporated into LaSalle procedures, although it was in the
information that was not incorporated into LaSalle procedures, although it was in the
      LaSalle vendor manuals. The information was a letter dated January 2,1997, from Klene
LaSalle vendor manuals. The information was a letter dated January 2,1997, from Klene
      Diesel Accessorie s, Inc., to the diesel system engineer at Quad Cites Station. The
Diesel Accessorie s, Inc., to the diesel system engineer at Quad Cites Station. The
      letters subject was, "V-24A/AX-8SA, Indicator Valve / Adapter Assemt:ty Installation in
letters subject was, "V-24A/AX-8SA, Indicator Valve / Adapter Assemt:ty Installation in
      Electromotive Engines," and the letter transmitted the recommended installation
Electromotive Engines," and the letter transmitted the recommended installation
      instructions of the cylinder Indicator (or test) valve and adapter.
instructions of the cylinder Indicator (or test) valve and adapter.
        The inspector discussed the contents of the letter with the system engineers at Dresden,
The inspector discussed the contents of the letter with the system engineers at Dresden,
        and the system engineers said that they had not received the letter. However, they
and the system engineers said that they had not received the letter. However, they
        believed that the routine work request to verify the torque on the cylinder test valves
believed that the routine work request to verify the torque on the cylinder test valves
        developed in response to the November 24,1996, event was sufficient.
developed in response to the November 24,1996, event was sufficient.
        The inspectors reviewed WR # 970087465-01, "[ Unit 2) Engine Standby Diesel
The inspectors reviewed WR # 970087465-01, "[ Unit 2) Engine Standby Diesel
        Generator, Verify Torque on Cylinder Test Velves", last completed October 1,1997. The
Generator, Verify Torque on Cylinder Test Velves", last completed October 1,1997. The
        task required " Torque packing nut to 65 ft/lbs, plus or minus 1 ft/lb. Torque values
task required " Torque packing nut to 65 ft/lbs, plus or minus 1 ft/lb. Torque values
        acquired from V TIP D1164." V-TIP D1164 war not related to cylinder test valves, but
acquired from V TIP D1164." V-TIP D1164 war not related to cylinder test valves, but
        V-TIP D1163, pages 215, stated that for the original cylinder test valves,"If a cylinder
V-TIP D1163, pages 215, stated that for the original cylinder test valves,"If a cylinder
        test valve is leaking, check that packing nut . . . has been torqued to 81-88 Nm (60-65 ft-
test valve is leaking, check that packing nut . . . has been torqued to 81-88 Nm (60-65 ft-
        Ibs), if nut has been overtightened, change seat, , , . , and correctly torque packing nut."
Ibs), if nut has been overtightened, change seat, , , . , and correctly torque packing nut."
        The January 2,1997, letter from the cylinder test valve vendor stated that "ths adapter
The January 2,1997, letter from the cylinder test valve vendor stated that "ths adapter
        should be installed into the engine and tightened with 45 to 50 ft-lbs of torque, and then
should be installed into the engine and tightened with 45 to 50 ft-lbs of torque, and then
        the packing gland nut should be tightened against the packing gland enough to hold it in
the packing gland nut should be tightened against the packing gland enough to hold it in
        place. The V-24A Valve is then installed . . . and tightened to 75 ft-lbs of torque."
place. The V-24A Valve is then installed . . . and tightened to 75 ft-lbs of torque."
        The licensee was unable to find any documentation that showed that the cylinder test
The licensee was unable to find any documentation that showed that the cylinder test
        valves were installed in accordance with the January 2,1997, letter. The licensee wrote
valves were installed in accordance with the January 2,1997, letter. The licensee wrote
        action requests to verify the torques, and the verifications had not been completed at the
action requests to verify the torques, and the verifications had not been completed at the
          end of the inspection period.
end of the inspection period.
          Inspection Report No. 50-237/96014(DRP) issued Violation 50 237/96014-02 for failing to
Inspection Report No. 50-237/96014(DRP) issued Violation 50 237/96014-02 for failing to
          incorporate vendor information regarding the cylinder test valves into the VETIP manuals.
incorporate vendor information regarding the cylinder test valves into the VETIP manuals.
          The licensee's response (JSPLTR: 97-0045, dated March 6,1997) stated that the failure
The licensee's response (JSPLTR: 97-0045, dated March 6,1997) stated that the failure
          was attributed to a system engineefs failure to take action to update the technical manual
was attributed to a system engineefs failure to take action to update the technical manual
          when a new component we= installed in the dieselin January of 1996. Also, as of
when a new component we= installed in the dieselin January of 1996. Also, as of
          February of 1997, the venovr stated that no technical manual change will be issued
February of 1997, the venovr stated that no technical manual change will be issued
          addressing the replacement valve as new diesels will be delivered with the old style
addressing the replacement valve as new diesels will be delivered with the old style
          cylinder test valve installed. The response did not state if the vendor of the new-style
cylinder test valve installed. The response did not state if the vendor of the new-style
          valves .nlanned to issue any vendor information. The response also discussed Dresden-
valves .nlanned to issue any vendor information. The response also discussed Dresden-
          site specific actions taken to assure all vendor information received at Dresderi was
site specific actions taken to assure all vendor information received at Dresderi was
          incorporated.
incorporated.
          The system engineer gave the inspectors a copy of E-mail from Comed corporate
The system engineer gave the inspectors a copy of E-mail from Comed corporate
          engineering regarding the LaSalle cylinder test valves that concluded that "the deviation
engineering regarding the LaSalle cylinder test valves that concluded that "the deviation
          from the vendors procedure in this case would not affect the operability of the diesels."
from the vendors procedure in this case would not affect the operability of the diesels."
          The inspectors noted that the licensee's diesels had all passed their surveillances (except
The inspectors noted that the licensee's diesels had all passed their surveillances (except
            for operations-based problems documented in report 97019), and that no visual evidence
for operations-based problems documented in report 97019), and that no visual evidence
            of loose cylinder test valves was found during routine walkdowns, and corcluded that the
of loose cylinder test valves was found during routine walkdowns, and corcluded that the
            lack of incorporation of vendor information did not result in an immediate operability
lack of incorporation of vendor information did not result in an immediate operability
            concem.
concem.
                                                      25
25
                                                                                                                                                        _ _ _ _ __ -
_ _ _ _ __
-


              - - - - _ _ _                   _
- - - - _ _ _
                                                    -_ - _ _ _ _ _ _ _ _ . _ _ . .   ._
_
  *         .
-_ - _ _ _ _ _
_ _ _ .
_ _ . .
._
*
.
I
I
                            The bspectors determined that the response to the Notice was insufficient because
The bspectors determined that the response to the Notice was insufficient because
i                            vendor information regarding the cylinder test valves was still not captured into the
vendor information regarding the cylinder test valves was still not captured into the
                            VETIP The unincorporated information was dated January 2,1997, and was sent to a
i
                            Comed site more than two months before the licensee issued the response to the Notice.
VETIP The unincorporated information was dated January 2,1997, and was sent to a
                            Therefore, the licensee should have identified the vendors information before issuing the
Comed site more than two months before the licensee issued the response to the Notice.
                            response. Acccrdingly, the status of violation VIO 50-237/96014 02 will remain OPEN
Therefore, the licensee should have identified the vendors information before issuing the
                            pending review of how the vendors information was sent to one Comed licensee, but not
response. Acccrdingly, the status of violation VIO 50-237/96014 02 will remain OPEN
                            another.
pending review of how the vendors information was sent to one Comed licensee, but not
              c.             Conclusion
another.
                            The licensee did not have all vendor information related to emergency diesel generator
c.
                              cylinder test valves. Applicable information sent to another Comed site had not been
Conclusion
                              forwarded to the licensee. The actions taken in response to a previous NRC-identified
The licensee did not have all vendor information related to emergency diesel generator
                              violation for failing to incorporate vendor information regarding cylinder test valves were
cylinder test valves. Applicable information sent to another Comed site had not been
                              not sufficient because additionalinformation received by Comed 2 months before the
forwarded to the licensee. The actions taken in response to a previous NRC-identified
                              licensee's response to the Notice was not incorporated.
violation for failing to incorporate vendor information regarding cylinder test valves were
                                                                    IV Plant SuDDort
not sufficient because additionalinformation received by Comed 2 months before the
              F2               Status of Fire Protection Facilities and Equipment
licensee's response to the Notice was not incorporated.
              F2,1             Safe Shutdown Emeroency Liohtino Material Condition
IV Plant SuDDort
              a.             Inspection Scope (62707)
F2
                              The inspectors reviewed Inspection Followup item (IFI) 50-237; 249/97019-03. The
Status of Fire Protection Facilities and Equipment
                              inspectors also reviewed emerging problems with all Unit 2 safe shutdown (SSD)
F2,1
                              emergency lights being declared inoperable due to a missed surveillance test.
Safe Shutdown Emeroency Liohtino Material Condition
                b,             Observations and Findinos
a.
                                The inspectors reviewed problems with the installation of batteries within many
Inspection Scope (62707)
                                  emergency lights, The lights were missing either the battery tray and/or the pressure bar.
The inspectors reviewed Inspection Followup item (IFI) 50-237; 249/97019-03. The
                                  Within the emergency light assembly, the battery rests on the battery tray and is pressed
inspectors also reviewed emerging problems with all Unit 2 safe shutdown (SSD)
                                  against the front of the unit by the pressure bar Without either of these items the battery
emergency lights being declared inoperable due to a missed surveillance test.
                                  is free to move around inside the emergency light assembly This could affect the
b,
                                  seismic qualification of the emergency lights. After being notified of the problems with the
Observations and Findinos
                                  emergency light, licensee personnelinitiated a PlF (# D1997-07316) and notified site and
The inspectors reviewed problems with the installation of batteries within many
                                  design engineering for assistance with the seismic concems,
emergency lights, The lights were missing either the battery tray and/or the pressure bar.
                                  While interviewing electrical maintenance and engineering personnel, the inspectors
Within the emergency light assembly, the battery rests on the battery tray and is pressed
                                  asked if they were aware of a similar problem in the past at Braidwood station
against the front of the unit by the pressure bar Without either of these items the battery
                                  (ref. Braidwood PlF# 456-201-97-0601 dated March 6,1997). The licensee first M vm
is free to move around inside the emergency light assembly This could affect the
                                  that the problem at Braidwood was a different problem for which Dresden had been
seismic qualification of the emergency lights. After being notified of the problems with the
                                  evaluated. The licensee personnel mistakeniy believed the problem from Braidwood was
emergency light, licensee personnelinitiated a PlF (# D1997-07316) and notified site and
                                  with the "J" hook that secures the SSD emergency light to the mounting shelf. Arter the
design engineering for assistance with the seismic concems,
                                  inspectors described the Braidwood problem clearly to Dresden personnel, the licensee
While interviewing electrical maintenance and engineering personnel, the inspectors
                                  concurred that the problem was applicable to Dresden.
asked if they were aware of a similar problem in the past at Braidwood station
                                                                                    26
(ref. Braidwood PlF# 456-201-97-0601 dated March 6,1997). The licensee first M vm
                              ..      .
that the problem at Braidwood was a different problem for which Dresden had been
    _ _ - _
evaluated. The licensee personnel mistakeniy believed the problem from Braidwood was
with the "J" hook that secures the SSD emergency light to the mounting shelf. Arter the
inspectors described the Braidwood problem clearly to Dresden personnel, the licensee
concurred that the problem was applicable to Dresden.
26
_ _ - _
..
.


    .         _-.. .-. - ...- -.-                                           -- ~ ._- - - - . -           . _ - - - .       .- - - .
.
                                                                                                                                          :
_-.. .-. - ...- -.-
  ~e.       . .                                                                                                                          f
-- ~ ._- - - - . -
                                                                                                                                      .
. _ - - - .
b                                                                                                                                         i
.- -
                                                                                                                                          l
- .
                                                                                                                                          r
:
                                                                                                                            L
. .
                                    The inspectors reviewed a memo (Doc ids 0005537204), written by Comed Design
f
                                      Engineering, which states the SSD emergency lights do not have to be seismically                     ,
~e.
.
b
i
l
r
L
The inspectors reviewed a memo (Doc ids 0005537204), written by Comed Design
Engineering, which states the SSD emergency lights do not have to be seismically
,
qualified but only have to address seitmic interaction concoms. T he memo states the
''
''
                                    qualified but only have to address seitmic interaction concoms. T he memo states the
missing battery tray or the pressure bar would not aNoct the seismic interaction of the
                                      missing battery tray or the pressure bar would not aNoct the seismic interaction of the
SSD emergency lights.- From discussions with the Design Engineering Structural Lead
-                                    SSD emergency lights.- From discussions with the Design Engineering Structural Lead
-
                                  ' who approved the memo, engineering judgement was used to decide that the battery
' who approved the memo, engineering judgement was used to decide that the battery
-                                    would not be thrown from the SSD emergency light assembly during an earthquake.-
would not be thrown from the SSD emergency light assembly during an earthquake.-
                                      Electrical maintenance personnel stated that, based on there being no seismic cencom,
-
                                    . they plan to determine the requirements for property installing the batteries in the SSD -
Electrical maintenance personnel stated that, based on there being no seismic cencom,
. they plan to determine the requirements for property installing the batteries in the SSD -
. emergency lights, during the performance of the next quarterty SSD emergency light
,
,
                                    . emergency lights, during the performance of the next quarterty SSD emergency light
surveillance. They then plan to correct the battery installation during the following
                                      surveillance. They then plan to correct the battery installation during the following               i
i
j-                                   quartetty surveillance,
j-
                                    - During a Q&SA audit it was oetermined that the battery discharge surveillance on all the
quartetty surveillance,
- During a Q&SA audit it was oetermined that the battery discharge surveillance on all the
unit 2 SSD emergency lights was over due. With the surveillance past its due date, the
,
,
                                      unit 2 SSD emergency lights was over due. With the surveillance past its due date, the
licensee declared all SSD emergency lights on unit 2 inoperable. Dresden Administrative
I                                    licensee declared all SSD emergency lights on unit 2 inoperable. Dresden Administrative
I
L                                     Technical Requirement (DATR) 3.2.3.1 was entered. The DATR stated that inoperable
L
                                      SSD emergency lights must be retumed to operable within 7 days or to establish backup
Technical Requirement (DATR) 3.2.3.1 was entered. The DATR stated that inoperable
                                      lighting, if this could not be done, then the equipment illuminated by the SSD emergency
SSD emergency lights must be retumed to operable within 7 days or to establish backup
!                                     lights must be treated as inoperable. The station decided to replace the batteries in all
lighting, if this could not be done, then the equipment illuminated by the SSD emergency
l;                                 - the unit 2 SSD emergency lights with new batteries rather than do the discharge test.
!
                                  - The batteries were successfully replaced within the 7-day DATR. During the battery
lights must be treated as inoperable. The station decided to replace the batteries in all
                                      replacement, the parts requirement document to correct the battery installation was
l;
                                      generated.
- the unit 2 SSD emergency lights with new batteries rather than do the discharge test.
                                      Also, during the Q&SA audit it was identified that certain areas in the plant, where manual
- The batteries were successfully replaced within the 7-day DATR. During the battery
                                      actions are required in SSD procedures, did not contain SSD emergency lights. These
replacement, the parts requirement document to correct the battery installation was
                                      areas are required to have SSD emergency lights. The licensee began fire watches in
generated.
;                                     the effected areas until temporary SSD emergency 1:ghts could be put in place. Work is -
Also, during the Q&SA audit it was identified that certain areas in the plant, where manual
l                                     in process to put permanent SSD emergency lights in place in these areas.
actions are required in SSD procedures, did not contain SSD emergency lights. These
i-                       c.         ConclusioD1
areas are required to have SSD emergency lights. The licensee began fire watches in
;
the effected areas until temporary SSD emergency 1:ghts could be put in place. Work is -
l
in process to put permanent SSD emergency lights in place in these areas.
i-
c.
ConclusioD1
i
i
r                                     The licensee improperly determined that the problem experienced at Braidwood Station -
r
!                                   was not present at Dresden Station. The licensee determined through engineering
The licensee improperly determined that the problem experienced at Braidwood Station -
j~                                   judgement that the battery being improperly restrained inside the SSD emergency lights -
!
                                      did not aNect the seismic interaction of the equipment. The licensee planned to install the
was not present at Dresden Station. The licensee determined through engineering
                                      batteries in the SSD emergency lights correctly. The licensee dealt with SSD emergency
j~
                                      light issues from a Q&SA audit quickly. However, due to all the problems with SSD
judgement that the battery being improperly restrained inside the SSD emergency lights -
                                  . emergency lights, the overall material condition of the lights was considered marginal.
did not aNect the seismic interaction of the equipment. The licensee planned to install the
batteries in the SSD emergency lights correctly. The licensee dealt with SSD emergency
light issues from a Q&SA audit quickly. However, due to all the problems with SSD
. emergency lights, the overall material condition of the lights was considered marginal.
:
:
:
:
                                                                              '
'
                                                                                                                                        ,
                                                                                                27-
,
,
      =,-,e                                 ..r.     ----w   ..- __u- . _
27-
,
=,-,e
..r.
----w
..-
u- .
.
.
.
.
m
m
.
.
. .
.
m
.
_ . , _ _
. . .


      _     __        _ _             _..               _. . . _ . -                         - . _ .
_
  . .
_ _
  !
_ _
                                          V, Mananoment Meetinas
_..
        - X1 Exit Meeting Summary
_.
        The inspectors presented the inspection restits to members of licensee management at
. . _ .
        the conclusion of the inspection on November 22,1997. The licensee acknowledged the -
-
        findings presented. The inspectors asked the licensee whether any materials examined
-
        during the inspection should be considered proprietary. No proprietary information was
. _ .
        identified.                                                                                   ,
.
.
!
V, Mananoment Meetinas
- X1 Exit Meeting Summary
The inspectors presented the inspection restits to members of licensee management at
the conclusion of the inspection on November 22,1997. The licensee acknowledged the -
findings presented. The inspectors asked the licensee whether any materials examined
during the inspection should be considered proprietary. No proprietary information was
identified.
,
:
:
i
i
.
.
                                                      28
28
              .   -     ._. .- . .-       . _ _ _ _
.
-
._.
.- . .-
.
-
-
-
-
- -
-
-
-


        _ _ . -                     . __.  -
_ _ . -
                                                .    ._.    _  -.  . . ~ . -_ .,
. __.
    -
      m.
.
.
                                    PARTIAL LIST OF PERSONS CONTACTED
._.
          Licensee
_
          *G. Abrell >           NRC Coordinator-
-.
          *L. Weir               Design Engineering Superintendent-
.
a        *D. Ambler             Acting Regulatory Supervisor
. ~ . -_
          *J. Tenz               System Engineering Safety Group Lead
.,
          *R. Peaks             Programs Engineering Supervisor
-
          *S. Perry.             Site Vice President
-
          *B. Holbrook           Training Manager
m.
          *S. Kuczynski         Shift Operatoins Supervisor
.
                                                        '                            '
PARTIAL LIST OF PERSONS CONTACTED
          *R. Whalen             Plant Engineering
Licensee
          *D. Willis             Electrical Superintendent
*G. Abrell >
:         *W. Lipscomb           SVP Staff '
NRC Coordinator-
*L. Weir
Design Engineering Superintendent-
*D. Ambler
Acting Regulatory Supervisor
a
*J. Tenz
System Engineering Safety Group Lead
*R. Peaks
Programs Engineering Supervisor
*S. Perry.
Site Vice President
*B. Holbrook
Training Manager
*S. Kuczynski
Shift Operatoins Supervisor
*R. Whalen
Plant Engineering
'
'
*D. Willis
Electrical Superintendent
:
*W. Lipscomb
SVP Staff '
*C, Richards
Audit Supervisor
,
,
          *C, Richards          Audit Supervisor
.
  .
~ *M. Friedmann
        ~ *M. Friedmann         Lead Health Physicist
Lead Health Physicist
          * Present at exit meeting of November 21.
* Present at exit meeting of November 21.
!
!
i
i
i
i
5
5
                                                          29
29
                                                                                    ,
,
.-,
%
.-
. ~ - - - - - - - - , , .
- - - _ . - -
-
--
.


                              . -.                 _   -- .       .       -           .             . . .~
. -.
  *
_
                                                                                                              .
-- .
                                      INSPECTION PROCEDURES USED
.
                                    ~
-
    - Inspection Module: 71707f Operational Safety Verification
.
      Inspection Module: 83822       Radiation Protection -
.
      Inspection Module: 62707       Maintenance
. .~
      inspection Module: 61726       Surveillance Observations
*
      inspection Module: 40500       Effectiveness of Licensee Controls in Identifying, Resolving, and
.
                                      Preventing Problems
INSPECTION PROCEDURES USED
                                ITEMS OPEN, CLOSED, AND DISCUSSED
~
      Opened
- Inspection Module: 71707f Operational Safety Verification
      50-249/97024-01     VIO       SBLC inoperable in excess of TS times.
Inspection Module: 83822
      50-237/97024-02     NCV Failure to install temp att correctly,
Radiation Protection -
      Closed
Inspection Module: 62707
      50-249/97-09-00     LER       HPCI System Declared inoperable Following Gland Seal Leakoff
Maintenance
                                      Condenser Hotwell High Level During to Drain Pump Stop Switch
inspection Module: 61726
                                      Failure.
Surveillance Observations
      50-010;237;249/
inspection Module: 40500
        97013-04           URI       Failure of Temporary Alteration 111-11-97 to Meet Acceptance
Effectiveness of Licensee Controls in Identifying, Resolving, and
                                      Criteria Requirements During Performance of Functional Testing
Preventing Problems
                                      Due to Maintenance Error.
ITEMS OPEN, CLOSED, AND DISCUSSED
      50-237/97024-02     NCV Failure to install temp alt correctly.
Opened
      DitMSMd
50-249/97024-01
      50-237;249/
VIO
        97019-03           IFl       Review of the seismic requirements '- tr,e emergency lights.
SBLC inoperable in excess of TS times.
50-237/97024-02
NCV Failure to install temp att correctly,
Closed
50-249/97-09-00
LER
HPCI System Declared inoperable Following Gland Seal Leakoff
Condenser Hotwell High Level During to Drain Pump Stop Switch
Failure.
50-010;237;249/
97013-04
URI
Failure of Temporary Alteration 111-11-97 to Meet Acceptance
Criteria Requirements During Performance of Functional Testing
Due to Maintenance Error.
50-237/97024-02
NCV Failure to install temp alt correctly.
DitMSMd
50-237;249/
97019-03
IFl
Review of the seismic requirements '- tr,e emergency lights.
50-249/97-011-00
LER
SBLC was Inoperable from Suction Line Low Temperature due to a
,
,
      50-249/97-011-00    LER        SBLC was Inoperable from Suction Line Low Temperature due to a
Wiring discrepancy in the Heat trace Controller Circuit
                                      Wiring discrepancy in the Heat trace Controller Circuit
237/96-009-00
      237/96-009-00       LER       Manual Reactor Scram due to Lowering Reactor Water Level due
LER
                                      to Automatic Feedwater Level Control System Design Defic:ency
Manual Reactor Scram due to Lowering Reactor Water Level due
"
to Automatic Feedwater Level Control System Design Defic:ency
      50-237;249/
"
        96014-02           VIO       Failure to enter EDG test valve tech info into VETIP
50-237;249/
                                                        30
96014-02
VIO
Failure to enter EDG test valve tech info into VETIP
30
-
. .
.
.
.
.
.


      .   ... _.   -       -     . .         . - . . - - . .     . . . . - . . -
.
                                                                                  ,
... _.
    -
-
                                                                                  1
-
                                          LIST OF ACRONYMS USED
. .
          DAN-       Dresden Annunciator Procedure
. - . . - - . .
          DAP       Dresden Administrative Procedure                             ,
.
          DATR       Dresden Administrative Technical Requirement
. .
          DEOP       Dresden Emergency Operating Procedure
.
          DGA       Dresden General Abnormal Procedure                           .
- . . -
          DOA'.     Dresden System Operating Abnormal Procedure
,
          DOP       Dresden System Operating Procedure
1
        HPCI       High Pressure Coolant Injection                             ;
-
        IFl         Inspection Followup item
LIST OF ACRONYMS USED
        IPE         Individual Plant Evaluation
DAN-
        IR     .
Dresden Annunciator Procedure
                    Inspection Report .
DAP
        ISEG       Independent Site Engineering Group
Dresden Administrative Procedure
        ISI         inservice inspection
,
        LCO         Limiting Condition for Operation
DATR
        LER         Licensee Event Report
Dresden Administrative Technical Requirement
        LPCI       Low Pressure Coolant injection
DEOP
        NCV         Non-Cited Violation
Dresden Emergency Operating Procedure
        NLO         Non-licensed Operator
DGA
Dresden General Abnormal Procedure
.
DOA'.
Dresden System Operating Abnormal Procedure
DOP
Dresden System Operating Procedure
HPCI
High Pressure Coolant Injection
;
IFl
Inspection Followup item
IPE
Individual Plant Evaluation
IR
.
Inspection Report .
ISEG
Independent Site Engineering Group
ISI
inservice inspection
LCO
Limiting Condition for Operation
LER
Licensee Event Report
LPCI
Low Pressure Coolant injection
NCV
Non-Cited Violation
NLO
Non-licensed Operator
- NOV
Notice of Violation
'
'
        - NOV        Notice of Violation
NRC.
        NRC.       Nuclear Regulatory Commission
Nuclear Regulatory Commission
<
NRR
        NRR        Office of Nuclear Reactor Regulation                         .
Office of Nuclear Reactor Regulation
L       NSO .       Nuclear Station Operator
.
<
L
NSO .
Nuclear Station Operator
NSWP
Nuclear Station Work Procedure -
'
'
        NSWP        Nuclear Station Work Procedure -
OE '
        OE '       Office of Enforcement
Office of Enforcement
        Ol         Office of Investigations -
Ol
        OOS         Out-of Service
Office of Investigations -
        PIF         Problem identification Form
OOS
        PORC       Plant Operations Review Committee
Out-of Service
        RUFSAR     Revised Updated Final Safety Analysis Report
PIF
F       Q&SA       Quality and Safety Assessment
Problem identification Form
        QC         Quality Control
PORC
        TS         Technical Specification
Plant Operations Review Committee
RUFSAR
Revised Updated Final Safety Analysis Report
F
Q&SA
Quality and Safety Assessment
QC
Quality Control
TS
Technical Specification
'
'
        VIO         Violation
VIO
        WEC         Work Execution Center
Violation
        WR         Work Request
WEC
Work Execution Center
WR
Work Request
.
.
1~
1 ~
                                                              31
31
i
i
.
.
.
}}
}}

Latest revision as of 05:59, 24 May 2025

Insp Repts 50-010/97-24,50-237/97-24 & 50-249/97-24 on 971016-1122.Violations Noted.Major Areas Inspected: Operations,Maint,Engineering & Plant Support
ML20197F054
Person / Time
Site: Dresden  
Issue date: 12/19/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20197E973 List:
References
50-010-97-24, 50-10-97-24, 50-237-97-24, 50-249-97-24, NUDOCS 9712300127
Download: ML20197F054 (31)


See also: IR 05000010/1997024

Text

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U.S. NUCLEAR REGULATORY COMMISSION

'

REGIONlil

Docket Nos:

50 010, 50 237, 50 249

License Nos:

DPR-02, DPR 19, DPR 25

Report Nos:

50-010/97024(DRP), 50-237/97024(DRP),

50 249/97024(DRP)

Licensee:

Commonwealth Edison

Facility:

Dresden Nuclear Station, Units 1,2 and 3

Location:

6500 N. Dresden Road

Morris, IL 60450

Dates:

October 16 November 22,1997

Inspectors:

K. Riemer, Senior Resident inspector

D. Roth, Resident inspector

J. Roman, Illinois Department of Nuclear Safety Resident

inspector

B. Dickson, Resident inspector in Training

J. Ellis, Operator Licensing Examiner, Region ill

Approved By;

M. Ring, Chief

Reactor Projects Branch 1

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9712

127 971219

PDR

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K 05000010.

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PDR - i

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EXECUTIVE SUMMARY

Dresden Generatin Nation, Units 1,2 and 3 -

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NRC Inspection Reports No. 60-010/9702d t #iM; 50 237/97024(DRP); 50 24g/g7024(DRP)

{

This inspection included routine resident inspect 6on with augmentation from the lilinois

,

Department of Nuclear Safety and NRC Region Ill.

.

Oserations

The inspectors concluded that the licensee's operational plan for dealing with the

_

l

increased unidentified leakage in the drywell was good. The licensee commenced taking

actions well ahead of TS limits. The planning and execution reflected a careful and

conservetive operating environment (Section 01.2)

!

When faced with conflicting indications between the alarm and the local reading, licensee

personnel relied on the less conservative of the two indications and did not declare the

standby liquid control (SBLC) system inoperable. The licensee operated the piant for

more than 34 hours3.935185e-4 days <br />0.00944 hours <br />5.621693e-5 weeks <br />1.2937e-5 months <br /> without an operable SBLC system, well beyond the allowable

-

8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />. Lack of knowledge of the exact locations of the temperature sensor and switch

contributed to this decision. A violation was issued for failing to comply with TSs

(Section 02.1).

The SBLC temperature annunciator procedure did not provide advance woming of

i

exceeding a TS limit. The licensee was aware of this, but had chosen to delsy

implementing a change to the procedure based on operations monitoring of the local

temperature of the SBLC system (Section 02.1).

4

,

The licensee generally performed routine operations in a safe manner (Section 04.1).

+

The inspectors concluded that overall performance during the shutdown and startup was

good. However, the inspectors identified examples of some minor problems in

knowledge of system status, communication, and procedural use (Section 04.2).

The usual response of operators to annunciator alarms was to follow the appropriate

,

annunciator procedure. However, in two instances, the inspectors observed that crews

failed to follow the annunciator procedures completely when an alarm recurred

(Section 04.3).

The Unit 2 single loop activities witnessed by the inspectors were performed well. The

inspectors observed operators enforce three way communicationsi follow plant

!

procedures, and coordinate activities well with other involved departments

(Section 04.4).

-

_

The operators responded well to material condition induced challenges and transients

+

(Section 04.5),

The inspectors concluded that the operations department showed a lack of a questioning

attitude during the September 7 operability surveillance run to declare the Unit 3 high -

pressure coolant injection (HPCI) system operable. The shift displayed a weak

s

2'

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. _ _ . _ . - . , . _ . . _ _ _ _ _ _ . _ _ . _ _ _ . _ _ _ _ . - - _

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knowledge of the operationalimplications of the HPCI turbine exhaust and vent system

-

and how it was affected by the status of the Unit 3 HPCI system (Section 08.1).

Maintenance

The work perfcrmed on the Unit 2 feedwater control system was poorly planned. The

+

failure to provide adequate work instructions directly challenged the operators. The

history of feedwater system work and resulting transients showed that feedwater work

needed more stringent reviews than those provided (Section M2.1).

The surveille. ice activities observed were satisfactorily completed and met the

+

procedure's acceptance criteria (Section M2.2).

Due to a lack of detail on a sketch provided by engineering and a lack of a questioning

attitude by a maintenance worker, the licensee demonstrated poor performance and work

practices regarding the installation of Temp Alt lll 1197 (Section M4.1).

The inspectors noted several examples of maintenance rework following the forced

+

outage activities (Section M4.2).

For the most part, the self assessments were of sufficient scope and depth. The

+

self assessments were hard hitting and critical of the malatenance process. The

exception was the self assessment on unauthorized modifications. This self assessment

did not have sufficient depth to leam the workers' knowledge of administrative processes

in place to control unauthorized modifications, as proved by an NRC violation issued

shortly after the self assessment was performed (Section M7.1).

The Q&SA organization was satisfactorily monitoring the activities in maintenance. The

audit reports and surveillance were complete, thorough, and critical. The field monitoring

reports were an indication that Q&SA personnel performed sufficient field monitoring

activities (Section M7.2).

Enoineerina

The licensee did not have all vendor information related to emergency diesel generator

.

cylinder test valves. Applicable information sent to another Comed site had not been

forwarded to the licensee. The actions taken in response to a pavious NRC-identified

violation for failing to incorporate vendor information regarding cylinder test valves were

not sufficient because additionalinformation received by Comed 2 months before the

licensee's response to the Notice was not incorporated (Section E2.1).

Plant Support

The licensee improperly determined that a problem experienced at Braldwood Station

was not present at Dresden Station. After discussions with the inspectors, the licensee

concluded the problem was applicable and the licensee formulated corrective actions.

This issue, combined with the licensee's failure to test lights adequately, caused the

inspectors to consider the overall material condition of the lights to be marginal

(Section F2.1).

3

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_ ___ _ _ .

_ ._. _ _ _ . _ ._- _ _ _ _ _

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Report Details

4

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Unit 2 was maintained at full power except for short uuration load drops to support routine

surveillance tests throughout the first part of the inspection period. On November 16, the

licensee decreased power to 25 percent and tripped one recirculation pump motor generator

(MG) to perform MG brush replacement and to enter the drywell to add oil to the 2A recirculation

>

pump motor. On November 18, the licensee performed maintenance on the feedwater system

and inadvertently caused a feedwater transient. The licensee held power at 650 MWe pending

,

investigation of the issue.

Unit 3 was near full thermal power at the beginning of this inspection period. Full thermal power

on Unit 3 was not achieved because the main turbine control valve positions were limited to an

average of 85 percent open with no greater than 90 percent open on any one control valve, and

feedwater flow was limited to g.735 Mlbm/h (instead of the approximately g.8 Mibm/h at full

power) as a result of a review of the fuel cycle analysis performed by engineering personnel.

3

These limits remained in effect until the end of the inspection period, On November 1, Unit 3

power was decreased to 300 MWe to facilitate drywell entry to investigate increased drywell

'

leakage. The licensee identified unisolable leakage from the 3B reactor recirculation loop

discharge flow element and manually shut down Unit 3 for repairs. On November 6, the licensee

started up Unit 3.

,

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1. Operations

01

Conduct of Operations

01.1

General Comments

l

Using inspec tion Procedure 71707, the inspectors conducted frequent reviews of ongoing

plant operations. Overall, the conduct of operations was safe and in accordance with

procedures.

During the inspection period, one event occurred for which the licensee was required by

10 CFR 50.72 to notify the NRC, The event and the notification date are listed below;

November 1

(Unit 3) TS required shutdown because of pressure boundary leakage, A

leak of 0.32 gpm from a weld on a tap-off of the B recirculation loop flow

element was found during a drywell entry,

01.2 (Unit 3) Response to Drvwell t.eakaoe

a.

101pection Scope (71707)

The inspectors monitored the licensee's response to indications of a leak in the drywell.

4

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. . - . _ . - _. _ . _ _ . , ,-

.

......_,_..,_,,r.m

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,

. _ , , , , . _

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, , _ .

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.

b.

Observations and Findinat

On October 17,1997, radiatinn protection personnel reported to operations that Unit 3

drywell activity increased by a tactor of three. On October 18, operations determined that

liquid going to the drywell floor drain sump increased from 0.50 to 0.67 gpm over

24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. Dresden UFSAR Section 5.2.5.5 stated,"in the case of a steam leak,

essentially all of the leak will be routed to the floor drain sump as condensate from the

drywell coolers." The leak rate quickly increased to 0.83 gpm by October 19.

Operations established shutdown limits on total unidentified leakage and changes to

unidentified leakage that were conservative compared with the requirements of TS 3.6.H.

(less than or equal to 5 gpm of unidentified leakage; less than or equal to 2 gpm increase

in any 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> period).

The licensee then developed and executed a " Unit 3 Drywell Leakage Plan." The plan

included monitoring, reviews of industry avents, and sampling using the air sampling

manifold system. The licensee also assigned senior reactor operators as owners of the

plan.

Air samplin0 and chemical analysis showed the leak to be primary coolant coming from

the 3B recirculation pump area. Operations determined that a drywell entry was

necessary to find the exact source of the leak.

Operations reduced power to 300 MWe on November 1, then entered the drywell and

readily identified a non isolable leak on the 3B recir.:ulation flow sensing line. The leak

was pressure boundary leakage, so operations immediately commenced a unit shutdown

in accordance with TSs.

c.

Conclusions

The inspectors concluded that the licensee's plan for dealing with the increased

unidentified leaksge was good. The licensee commenced taking actions well ahead of

TS limits. The planning and execution reflected a careful and conservative operating

environment.

02

Operational Status of Facilities and Equipment

02.1 (Unit 3) Standby Li. quid Control System (SBLC)

a.

Inspection Scope (71707)

At 0609 hours0.00705 days <br />0.169 hours <br />0.00101 weeks <br />2.317245e-4 months <br /> on October 27,1997, the SBLC low temperature alarm annunciated in the

control room. The licensee did not determine that the alarm was valid until 1530 hours0.0177 days <br />0.425 hours <br />0.00253 weeks <br />5.82165e-4 months <br /> on

October 28,1997. The inspectors reviewed the licensee's investigation and

troubleshooting.

5

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b.

Observations and Findinos

,

identWication of the TS entry conditions

At 0609 hours0.00705 days <br />0.169 hours <br />0.00101 weeks <br />2.317245e-4 months <br /> on October 27,1997, the SBLC low temperature alarm annunciated in the

control room. Per the annunciator procedure, the alarm was set for 78-83'F. By

contrast, the TS required that the suction piping temperature be greater than or equal to

83'F.

After the low SBLC suction piping temperature alam1 was received, the operators

checked local indication in accordance with the Dresden Annunciator Procedure (DAN);

the local temperature indicator showed 90'F. The operators accepted the local Indication

as valid and assumed that a problem existed with the alarm or the alarm's temperature

switch, so operations contacted maintenance to troubleshoot. In fact, the alarm was

valid, as will be further discussed below. Therefore, the operators chose not to believe

an annunciator without proving that the annunclator was invalid.

Both operations and system engineering personnel were unaware at this time that the

local indication came from a different location on the SBLC suction piping than the alarm

sensor. The locallndication temperature sensor was closer to the SBLC tank and was

showing the correct temperature for its location. The temperature switch that provided

the alarm signal was also correctly alarming because the SBLC suction temperature at

the switch's location was below the alarm setpoint.

During troubleshooting on October 28,1997, the licensen used a surface pyrometer and

found that the SBLC suction piping temperature was only 80'F while the local indication

showed 89'F. Operations then declared both SBLC subsystems to be inoperable. With

both SBLC subsystems inoperable, TS allow 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> to restore at least one subsystem or

12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> after that to be in at least hot shutdown.

Immediate Corrective and Compensatory Actions

Maintenance adjusted the controllers for the heat trace to raise temperature above the

83'F TS requirement. The temperature was increased to above the TS requirement at

16t5 on October 28,1997. Maintenance also observed that the heat trace controllers

appeared to not be wired correctly.

The licensee ran an operability surveillance for the SBLC system, and the system passed.

On October 28,1997, at 2033, operations began to monitor the suction piping

temperatures with a surface pyrometer once a shift on both units.

On October 31,1997, at 0930 during the shift rounds, a non-licensed operator found that

the SBLC suction piping was 80'F. The non-licensed operator (NLO) did not recognize

the significance of the extra readings, so the NLO failed to report the condition to the unii

superviser for more than i hour. The 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> delay was a significant portion of the

8-hour LCO. The licensee adjusted the heat trace controllers and increased the

temperatures to above the TS requirement at 1220 hours0.0141 days <br />0.339 hours <br />0.00202 weeks <br />4.6421e-4 months <br /> on October 31,1997. This was

within the B-hour TS action statement.

6

_ .. _. _ . ... _ _ _ _ . _ _ _ _ _ _

. __ ._ ._ _ . _ . . _ . . _ _ _ _ _ _ _ _ _ _ _ _ _ . .

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1

Cause of Temperature Problems

i

1

The onset of cooler outside temperatures caused the ambient temperature of the SBLC

system area in the reactor building to decrease. This allowed the suction piping to cool.

j

Maintenance personnel concluded that two of the three heat trace circuits had their

i

'

controllers crossed such that the thermostat was sensing temperature on one section of

piping, but controlling the heat. trace on another section of piping. The section of the pipe

that had experienced the low temperature was affected by the wiring problem. The

i

4

licensee corrected the error by the aftemoon of October 31.

i

e

,

i

cause of Procedure Problems

,

'

The alarm setpoints in the annunciator procedure DAN 902(3) 5 G-6 were below the

TS setpoints. The alarm came in at 78'F, whereas TS required 83'F minimum

'

temperature. The low SBLC suction piping temperature was changed as part of the

'

TS upgrade program from 80 to 83'F in June 1996. A decision was made then to defer

i

-

'

the setpoint change until mid December of 1997. However, even without the TS upgrade

'

program, the old alarm would still have been below the old TS requirements. The

deferral was made because the licer$see believed that routine operator rounds'

temperature monitoring (which monitored local Indication, not the true suction

temperature) was sufficient.

'

'

\\

'

Licenses Event Report

On October 31,1997, the licensee identified that unit 3 was outside TS compliance when

'

SBLC suction temperature was below 83'F (PlF# D1997 07873). The licensee

.

subsequently published Licensee Event Report No. 50 249/97-01100, "SBLC was

Inoperable from suction Line Low Temperature due to a Wiring discrepancy in the Heat

'

i

trace Controller Circuit."

The licensee event report (LER) discussed the correcting actions and the event causes.

- ;

4

The LER did not discuss the operators' failure to believe the valid annunciator,

in the LER, the licensee stated that personnel reviewed various SBLC work performed

from 1988 to present and were unable to identify when the miswiring took place.

Event Significance

The UFSAR Section 9.3.5 and the TS bases stated that the SBLC system temperature

was required to be maintained at least 10'F above the saturation temperature of 62'F to

guard against boron precipitation, Since the lowest observed temperatures were above

the 62'F precipitation temperature, as were reactor building ambient temperatures,

precipitation did not take place. The inspectors therefore concluded that the safety

' significance was small.

,

,

! However, the event was significant for operations. . It demonstrated a willingness to

"

assume that a valid alarm was invalid without any supporting data. Additionally, even

n

7

'

>

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after operations started shiftily checks, operations did not assure that the personnel doing

the checks understood the significance, as demonstrated by a failure of an NLO to report

'

exceeding the TS minimums immediately upon discovery.

Dresder. TS 3.4.A.1.b stated that with both standby liquid control subsystems inoperable,

at least one must be restored to operable status within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> or be in at least hot

shutdown within the next 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.

Contrary to the above, between October 27,1997,0609 hours0.00705 days <br />0.169 hours <br />0.00101 weeks <br />2.317245e-4 months <br /> and October 28,1997,

1615 hours0.0187 days <br />0.449 hours <br />0.00267 weeks <br />6.145075e-4 months <br />, both standby liquid control subsystems were inoperable for greater than

8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> and the plant was not brought to at least a hot shutdown condition. This was a

violation (VIO 50-010; 237; 249/97024-01).

c.

Conclusions

An error in wiring led to the SBLC suction piping heat trace not keeping the appropriate

sections of piping above TS minimum temperatures. An installed temperature switch in

the SBLC system correctly sounded an alarm in the control room. Upon investigation,

operations found the local indication to be beyond the TS limits.

When faced with conflicting indications between the starm and the local reading, licensee

personnel relied on the non-conservative of the two ir:dications and o.J not declare the

SBLC system inoperable. The licensee operated the plant for more than 34 hours3.935185e-4 days <br />0.00944 hours <br />5.621693e-5 weeks <br />1.2937e-5 months <br /> without

an operable SBLC system, but the LCO for SBLC was only 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />. Lack of knowledge

of the exact locations of the temperature sensor and switch contributed to this decision.

A violation was issued for falling to comply with TSs.

The SBLC temperature annunciator procedure did not provide advance waming of

exceeding a TS limit The licensee was aware of this, but had chosen to delay

implementing a change to the procedure based on operations monitoring of the local

temperature of the SBLC system.

04

Operator Knowledge and Performance

04.1

(Units 2. 3) Routine Operations

a.

Inspection Scqpe (71707. 83822)

The inspectors conducted frequent reviews of ongoing plant operations in the control

room and in the plant. The inspectors also discussed plant status and

pendingevolutionswith shift personnel in the control room.

b.

pbservations and Findings

During routine operations the licensee met procedures and TSs (except for the SBLC

issue discussed in Section 02.1 of this report). Control room manning was adequate and

the operators were not overburdened. No problems were found with indications or valve

lineups. Usually, shift personr'el were aware of plant conditions and operational

requirements were listed. The inspectors observed that the licensee continued to

practice good communications.

8

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c.

Conclusions

The licensee generally performed routine operations in a safe manner.

04.2 (Unit 3) Forced Outaae (D3F24) gnd Startuo for Pressure Boundary Leak at

.

t

a.

Inspection Scope (71707_)

The inspectors monitored the performance of operations during activities associated with

the shutdown for and startup from the forced outage (D3F24) to repair pressure boundary

leakage.

b.

Observations and Findinos

Overall, the performance of operations during the Unit 3 startup was good. The

operators' actions were generally characterized by careful panel monitoring, good

communications, and good command and control of the plant. The operators were

challenged by equipment problems during the startup and responded generally correctly.

However, the inspectors noted that the operators' responses to some frequently alarming

annunciators degraded (see Section 04.3 for additional discussion).

Control Room Performance

Overall, the control room performance was good. The inspectors observed that the

lice .Ne was carefully following procedures, maintaining good awareness of the plant,

k..d 8. eping the control room atmosphere quiet and professional.

The unit supervisors (US) and shift managers (SM) held crew briefs at regular intervals to

assure that the crews were fully aware of plant status and plans. The briefs conducted

were thorough. The crews maintained three-way communicetions during the startup.

The performance by the nuclear station operators (NSOs) was generally good. The

NSOs performed the procedures as written. The NSOs were generally very attentive to

the plant indications during the startup. The NSOs preformed frequent and detailed front

panel walkdowns.

On November 1, during the Unit 3 shutdown, the inspectors questioned the US about the

status of the shutdown cooling system. The US was unaware that 3B shutdown cooling

pump was unavailable (the pump was in a testing status). Pumps A and C were available

and the licensee was meeting the TS. This showed an example of inattention to detail

during tumover.

During the startup on November 5, the inspectors reviewed a copy of the startup

procedure and noted that one step sent the user to a wrong step during startup. The SM

reviewed the procedure and concluded that the error was a typographical error. The US

informed the shift manager that the typo in the autherized copy of the startup procedura

hao already been noted and corrected. The inspectors considered the typo to be minor

inattention to detail during procedure revision.

9

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Also, during the startup on November 5, the inspectors identified an instance of failing to

,

complete an annunciator procedure. This issue is discussed in Section 04.3.

Field Performance

The inspectors observed part of the performance of a procedure for starting the steam

jet air ejector.

The non licensed operators (NLos) performing the procedure followed all the required

procedure steps and administrative requirements, including radiation protection

requirements.

The procedure was not frequently performed. The licensee took advantage of the startup

to train additional NLOs on the required actions. The inspectors consWered this to be

prudent. The NLO doing the task provided careful and knowledgeable instruction

The evolution was not successful due to material condition. The Unit 3 hydrogen

analyzer system could not be placed in service because one train was blocked and the

other train apparently had a slug of water introduced during the shutdown. The NLO

attempting to place the system in service identified the water intrusion problem and

correctly reported the condition to the system engineer (who was pre ent) and to the Unit

Supervisor.

The licensee could not restore either system, so chose to startup the plant directly into

the TS LCO for inoperable hydrogen analyzers.

The inspectors concluded that the NLOs performed the evolution in a careful and

controlled manner. The NLos showed a good ability to recognize abnorrnalindications

for system operating parameters that are entry level conditions for TSs.

On a different shift, the inspectors noted one instance of an unexpected alarm caused by

NLOs energizing plant equipment. The NLOs did not inform the control room immediately

before energi:ing the equipment, but instead radioed the control room immediately after

causing an alarm. After the inspectors asked if the NLOs had informed the control room

to expect ar? alarm, the unit supervisors remir'ded all NLOs to provide advance notice

immediately before energizing equipment.

c.

Conclusions

The inspectors concluded that the overall performance during the shutdown and startup

was good. However, the inspectols identified examples of some minor problems in

knowledge of system status, communication, and procedural use.

04.3 (Units 2. 3) Response to Annuncictgn

a.

Inspection Scope (71707)

The inspectors monitored the operators' use of Dresden Annunciator Procedures, in

particular, the inspectors checked for compliance with annunciators that were repetitive.

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b.

Observations and Findinas

The normal response of an operator to an annunciator alarm was to complete the actions

listed in the Dresden annunciator response procedure (DAN). The inspectors observed

many instances of operators correctly reviewing and executing the appropriate DAN.

On October 20, the inspectors observed an oncoming NSO receive an alarm on the gland

seal condenser, then clear and reset the alarm without referencing any procedure. The

off going NGO had told the oncoming NSO that the alarm had been repeatedly coming in

due to a material condition problem.

The inspectors informed senior licensee management about the failure to use the

annunciator procedure. The licensee Quality and Skfety Assessment (Q&SA) department

had written problem identification form (PIF) # D1997 07317 on September 28 for a

similar issue. The licensee determined that the significance level of the PIF was

" Condition Not Adverse to Quality" and had closed the issue.

On November 5, during the startup, the inspectors observed the following: the operators

were at a point in the startup that required frequent changes to the range setting for the

intermediate range monitors (IRMs). The material condition of the IRMs was challenging

the operators because the changing of the range switch for IRM 14 was causing IRM

downscale alarms to occur. Shortly after the first spurious downscale alarms, the

inspectors reviewed the backpanel indications and observed one IRM with a "Hi" alarm lit,

and another with alamis for both "Hi" and "Hi-Hi" lit, but the readings for all IRMs were

below alarm setpoints. No IRM associated annunciators were in alarm on the control

room front panels. The inspectors reviewed the annunciatormsponse procedure

(DAN 902(3) 5 C-5, "lRM Downscale," Rev. 06) and noted that it required review of

back panelindications as a subsequent action for the alarm.

When the operators next changed the range of IRM 14, the IRM downscale alarm again

came in. The operators briefly discussed the alarm, noted it was the same IRM, and

concluded that the range switch contacts might be the source and that a work request to

investigate must be written. Although the operators reviewed the annunciator response

procedure, no operator was sent to recheck the backpanelindication. Because the

operators did not check the backpanel, they were unaware that the backpanel indications

showed signs of spiking high.

When the NSO next ranged IRM 14. a half scram due to "Hi-Hi" level occurred. The

operators then reviewed the back panels and saw and cleared the IRM channel alarms.

In addition, the operators bypassed the noisy IRM and called maintenance and

engineering for assistance.

After the half scram, the inspectors asked the unit supervisor if the alarm response

procedure for the previous IRM downscale had been completed. The US said,"No," and

acknowledged that it should have. The inspectors asked the NSO who was responsible

for ranging the IRMs if anyone had reported completion of the alarm response procedure

to him, and he said *No." The inspectors discussed the concem of completing the

annunciator response procedure with the shift manager, and the shift manager

reemphasized to the operators that DANs need to be followed completely, even for

expected or nuisance alarms caused by equipment problems, The shift manager also

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directed that backpanel tours be done on 15 minute intervals rather than on the usual

1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> interval to detect any other IRM spikes,

.

Procedure DAP 07 50," Conduct of Safe Operations," Rev. O Step 6.3.2 stated," . . .

after receiving unexpected alarms, reference appropriate procedures." Step 6.3.3 stated,

" . . when responding to annunciators . . . follow the annunciator procedure as written."

.

Step 7.2.3 stated to announce an alarm and * Pull out the annunciator procedures (DAN)

l

and take the appropriate actions at directed by the procedures."

The operators' actions on October 26 and November 5 did not meet DAP 07 50. In both

instances, the repetitive alarms caused by material condition problems caused the

operators to become complacent about following the annunciator procedure. Although

the actions were contrary to procedures, no violation was issued because this issue

would be expected to be encompassed by licensee corrective actions to a recently issued

violation for operators not following procedures (50 237; 249/97019-02)

c.

Conclusions

The usud response of operators to annunciator alarms was to foll0w the approprihte

.'

annuriciator procedure.

However, in two instances, the inspectors observed the crews failed to follow the

annunciator procedures completely when an alarm recurred. in one instance the

consequence of not following the procedure was the operators being unaware that an

IRM was spiking "Hi" And "Hi-Hi" as well as downscale.

04.4 Unit 2 Sinole Looo Operations

e,

inspection Scope (71707)

The inspectors monitored the response by the licensee to the discovery of uneven

wearing of *e brushes on the 2B reactor recirculation motor generator (MG) set. The

,

replacement of the brushes required the licensee to secure the MG set, and thus to enter

single loop operations on November 16.

The inspectors observed and reviewed licensee plane for the evolution, the plant

operations review committee (PORC), control room activities, and maintenance work in

the field.

b.

Observations and Findinos

UnN 2 Single Loop Activities

Licensee personnelidentifiod that several brushes on the 2B MG set were wom much

more than the others. The licensee developed plans tu replace the bmshes and inspect

the rings on the MG set. The MG set had to be secured to perform the task. The

licensee elected to do the task on-line by tripping one recirculation pump and operating

the plant in single-loop.

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Historica.ly, tripping a pump on-line and restarting was a significant event for Dresden.

As documen6ed in inspection Report No. 50 237/95004(DRP); 50 249/95004(DRP), in

i

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1995, the 25 teactor recirculation pump tripped because of a technician inadvertently

j

closing the contreeler for the 28 recirculation pump motor generator set temperature -

control valve (TCV) while attempting to repair the 2A TCV Operations reviewed the

.

requirements for a restart of the pump and found that the bottom head drain temperature

!

was needed. However, the bottom head drain had been clogged for mar *y years. The

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operating crew concluded that sitomate temperature indications could be used to meet

,

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the TS and procedural intent. This determination was made without discussion with

j

senior operations management, station management, or engineering personnel, and

against the advios of an independent site engineering group (ISEG) engineer. This

4

resulted in escalated enforcement action. Since 1995, the licensee improved the material

condition by cleaning out the bottom head drain, and improved the overall conduct of

!

operations. However, the licensee had not performed single loop operations since the

1995 event.

j

The planning for the brush replacement was thorough. The licensee used a wide range

of resources, including the vendor.

{

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The review of the plan was also thorough. Thc PORC thoroughly discussed the planned

!

3

maintenance work, possible contingencies, and operational requirements for a single loop

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condition,

j

.

On November 16,1997, the licensee removed the 28 recirculation loop from service to

perform the brush replacement activities. The inspectors verified that the operators

!

complied with the T8 requirements and closely follow the approved plan. The inspectors

!

,

vonfied that plant parameters were within T8 requirements for recovery of the idle loop

.

and that the operators propert*, retumed the loop to service. The inspectors also noted

>

close coordination and communications between operations department personnel,

maintenance and engineering personnel, and the designated project manager for the

i

evolution.

,

c.

G9DQlusion

1

The Unit 2 single loop activities witnessed by the inspectors were performed well. The

l

inspectors observed operators enforce three way communications, follow plant

'

[

procedures, and coordinate activities well with other involved depa 1ments.

04.5 Qperators Response to Material Condition Induced Transients

E

a.

Inspection Ecoce (71707)

?

- The material condition of the plant caused challenges and transients during the

Inspection period. The inspectors observed and reviewed operator performance in

t

response to these events.

c

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5

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.w_...___.,~.-_2..________.._________

_ _ . _ _ , , , _ , , . . .

, . _ _ _ . _ _ _ , _ . . . .

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b.

Qp.ittyggng.and Findinog

Reactor Feed Pump Ventilation

On November 17,1997, Unit 2 operators noticed an increase in the 2C reactor feed partp

(RFP) stator temperature. The temperature of the 2C stator temperature was

apprnximately 80'C (crocedurallimit of 85'C) and slowly rising, while the stator

temperature of the otner runninD RFP (2B RFP) was approximately 46'C. Operators fp

the field identified that the ventilation damper for the 20 RFP had failed to open.

Operators started the 2A RFP and secured the 2C RFP. The operators placed the 2C

RFP in a Standby lineup and caution carded it for emergency use only. During

subsequent troubleshooting, the damper operated as expected and operators retumed

the RFPs to their original configurations.

On November 18,1997, the operators noticed that the stator temperatures of the 2B and

2C RFPs were trending upwards. An oper2 tor dispatched to the field identified that the

ventilation dampers were not in their expected positions. The individual pump vent

dampers were in the correct positions, however, the recirculation damper was full open.

The operators wired the recirculation damper closed and the exhaust damper open in an

emergency attempt to lower stator temperatures (this was procedurally allowed to protect

equipment). The stator temperatures trended downwards and stabilized around GO'C for

both of the pumps. The licensee documented the occurrence via problem identif: cation

forms (PlF) D199708145 and D1997 08101.

The inspectors concluded that the operators performed well by identifying the unexpected

temperature increase and restoring the RFPs and RFP ventilation system to a stable

condition.

The inspectors noted similaritPs between the problems encountered on August 12,

August 13, and the November 18 ventilation problems, in all cases, the operators were

required to perform emergency downpower maneuvers when reactor feedpump

ventilation problems occurred.

2A2 Flash Tank Level Control Problems

On November 17,1997, control room operators noticed level swings in the 2A2 Flash

Tank. Since the level swings were increasing to the point of automatic opening of the

bypass valve, the operators were concemed with the potential tripping of the heater string

and subsequent impact on feedwater temperature. Licensee personnel performed a

heater bay entry rnd identified that the positioner arm oa 'he level control valve was

broken. Maintenance personnel repaired she level conWI valve and the heater string was

retumed to a normal status. Licensee personnel documented the occurrence via

PIF D1997-08160.

The inspectors concluded that the operators performed well by identifying the unexpected

level swingt early enough to allow for corrective action before automatic tripping of the

heater string.

The inspectors noted that this issue was similar to problems operators encountered with

heatet level controls previously documented in inspection reports 97012 and 97013.

14

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2A Feedwater Regulating Valve

'

On November 18,1997, licensee maintenance personnel were doing work on the 2A

feedwater regulating valve (FRV) when operators notice >d that the 28 FRV had switched

,

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from submetic control to manual centrol. The operators entered trcnsient level control,

but experienced some d fficulty in matching steam flow and feed flow to stabilize level

since the low flow FRV was still in automatic and was attempting to control level.

Operators were subsequently able to place the low flow FRV in manual control and

restore reactor level to its proper level. During the transient, reactor level went as high as

32 inches (normallevelis 30 inches) and as low as 22 inches. The operators had

direction to insert a manual reactor trip (scram) if level dropped as low as 20 inches. An

inadequate work package and deficient work instructions caused the reactor water level

'

transient (reference Section M2.1 of this report for additional discussion of this issue).

The operators responded well to an unexpected reactor water level transient caused by

improper maintenance work in the field. The operator's successful recovery of water

level, and restoration to the proper level band, demonstrated effective corrective actions

started after operators mishandled a levt,l transient in July 1997 (see inspection

Report No. 50 237/97016(DRS) for more information).

c.

.Qgnqlgig

The operators reonded well to material condition induced challenges and transients.

l

However, the challenges themselves were similar in nature to previous occurrences and

Indicated ineffe:tive licensee efforts to correct known plant deficiencies. The inspectors

were concemed about the equipment problems discussed above since material condition

issues continued to challenge operators. The items above were repeat items and were

similar in nature to items previously documented in NRC intpection reports. The

inspectors concluded that licensee effort to address known material condition deficiencies

,

were not completely effeJive.

08

Miscellaneous Operations issues

!

08.1

(Unit 3) Hioh Pressure Coolant inlection (HFCl) System

1-

a.

inspection Scope (71707)

On September 5, the licensee declared the Unit 3 high pressure coolant injection (HPCI)

l

system inoperable due to a malfunctioning level control! alarm switch in the HPCI gland

seal condenser hotwell. The licensee issued LER 50 249/97-009 to document the event.

l

The inspectors discussed the LER with the licensee, and reviewed and observed

!

subsequent operability surveillances performed on September 7 and September 8 to

l

declare HPCI operable.

l

l

b.

Ob6ervations and Findinas

On September 6, the licerisee isolated the HPCI system steam line in preps,ation for

completing repairs on the HPCI system gland seal condenser hotwell. On September 7,

after replacing the level control / alarm switch in the HPCI gland seal condenser hotwell,

15

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the licensee placed the Unit 3 HPCI system back in service and attempted to complete

DOS 2300-03, "High Pressure Coolant injection System Operability Verification."

Immediately after opening the steam supply shutoff valve (3 23013) many exhaust drain

pot high level alarms were received in the control room causing the NSO to trip the HPCI

system turt>lne.

Step I.1 of DOS 2300-33 required the licensee to drain the HPCI exhaust drain pot. The

inspectors reviewed the completed surveillance procedure and noted that unit supervisor

administering this surveillance had initialed the procedural steps as ' conditions met"

(C/M). However, if the condition was met, then the HPCI system would not have tripped.

The inspectors found no entry in the NSO logs nor the US logs that documented the drain

pot being drained. During subsequent interviews, the licensee stated that the US

believed that the condition was met based on information from the previous shift's US.

Specifically, the previous US said that the exhaust drain pot had been drained on two

prior shifts. The inspectors Mquested a copy of the completed procedure in which this

activity was performed to verify this information, but the licensee could not find the

completed procedures. The licensee was unable to produce any documentation to

support of the use of" conditions met"instead of draining the drain pot.

'

According to the system engineer, the drain pot had partially filled with condensed steam

(from the OOS HPCI steam line) which slowly leaked past the steam supply shutoff valve

(3 2301 3). With the drain pot partially filled, there was not enough volume to receive the

condensate normally experienced during HPCI operation, so equalization problems

occurred. The exhaust drain pot was quickly filled, ultimately causing the turbine casing

to fill via the casing drain lines. The cystem engineer added that an addition 61 contributor

may have been the short time (one hour) between clearing the OOS (opening utoam

valves 2301-4 and 23015) and restarting the surveillance (opening valves 23013 and

the turbine stop valve). After proper drainage of the HPCI system exhaust drain pot, the

operability surveillance was completed successfully.

Step F.8. of DAP 09-13 *Procedura! Adherence" stated that " Condition Met (C/M) should

be entered IP an Individual finds that the requirements of a procedure step are already

satisfied, e.g., the step calls for starting a pump; however, the pump is already running."

Based on interviews with the licensee and the review of licensee documentation, there

was no clear evidence that the procedural step was already satisfied. The licensee is

required by TS 6.8.A to implement applicable procedures recommended in Appendix A of

Regulatory GV.de (RG) 1.33, Rev. 2, Feb.1978. Administrative procedures goveming

procedure adherence are recommended in RG 1.33. Contrary to this, the licensee failed

to follow DAP 09-13 guidance for determining if a condition had been met, and

consequently had to trip the HPCI system during a surveillance test manually. Although

the actions were contrary to procedures, no violation was issued because the violation

would be expected to be encompassed by licensee corrective actions to a recently issued

violation for operators not following procedures (50-237; 249/97019-2)

16

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c.

Qanslution

The inspectors concluded that the operations departmerW showed a lack of a questioning

attitude during the September 7 operability surveillance run to declare the HPCI system .

operable. The inspectors also concluded that the shift i;'c,d a weak knowledge of

the operational implications of the HPCI turbine exhaust and vont system and how it was

effooted by the status of the Unit 3 HPCI system,

11. Mainlanance

M2-

Maintonenee and Material Condition of Faellities and Equipment

M2.1 (Units 2 & Si trW of Feedwater Raoulatina Valve (FWRV) Maintenance

a.

Inanection Boone (62707. 93702)

The inspectors reviewed the licensee's response to a level transient that occurred on

Unit 2 on November 18,1997. The review included assessing the licensee's response

and preliminary root causs.

b.

Observations and Findinos

On November 18,1997, with Unit 2 at approximately 80 percent power, maintenance and

engineering were allowed to do maintenance on the 2A FWRV. The work was to address

soms instability exhibited by the 2A FWRV in positions between 30 - 80 percent open by

replacing the linear variable differential transformer (LVDT). The licensee repleoed a

solenoid on the valve's operator during the single-loop operations of November 18, but

the valve continued to exhibit erratic operation, so the licensee was next trying the LVDT.

,

The licensee used WR 97012985 01, "2A FW REG VLV; Valve Exhibits instability -

between 20 and 52 percent replacement.' When a lead was lifted from the LVDT, the 28

,

FWRV swapped from automatic control to manual control. The swap caused a loss of

automatic reaclor pressure vessel (RPV) level control, and cycling of the low-flow

feedwater regulating valve. The operators were challenged, but recovered RPV level

-(see Section 04.4).

The preliminary investigation by the licensee, and presented to the Plant Operations

'

Review Committee (PORC) on November 20,1997, determined that the response of the

feedwater control system was correct. The system was designed to place the FWRVs in

manual mode if the LVDT current loop opens. The automatic modo swap was designed

to fall the valve "as-is"in the nont of a problem with the quality of the signal. This -

feature had not been identified in the work package. The work request was reviewed by

a senior reactor operator before execution, but the SRO also did not realize that the work

on the 2A LVDT would affect the control of the 28 FWRV.

The licensee's investigation team informed :he PORC that the type and number of

reviews done for the WR were correct per DAP 15-06, but the reviews were inadequate,

one of the proposed corrective actions was to have feedwater level control system

corrective type work have a technical review. -

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The inspectors noted that some precursor events suggested the need for greater

attention to foodwater level control system procedures, in inspection Repori No. 97012

Section M1.1, the inspectors documented the June is unexpected opening of the

SA FWRV due to a procedure revision error. The inspectors also noted that

PlF# Digg7-07698, "3A FWRV Found in Test Mode," Novenhor 2,1997, desenbod the

- i

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operators' discovery that the Unit 3 A FWRV had unexpectedy gone into ' Test" mode

i

following the shutdown of Unit 3. The system engineer informed operations that, "the tog

valves will automaticalh go into twt mode on a loss of LVDT signal," and theortrod that -

i

the rapid response of the FWRV following the scram may have caused a momentary loss

!

of LVDT signal to the controller. This had not occurred before, so the iloonsee replaced

!

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the LVDT oscillator card to reduce the likelihood of a re:urrence. The inspectors

!

recognized that there are a ome differences between the Unit 2 and Valt 3 FWCS,

!

(according to the system engineer, placing Unit 3 FWC8 into test before lifting the lead

would have been sufficient; the Unit 3 LVDTs would not have to be separately placed in

test). However, the inspectors concluded that the incident documented in the PlF

,

demonstrated that LVDT c9n impact the valve configuratinn,

f

,

The history of feedwater level control system problems at Dresden showed that feedwater

maintenance needed thorough reviews. On May 31, igg 6, during testing of the

_

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feedwater level control system, Unit 2 experienced a level transient of sufficient

!

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- magnitude to cause the operators to shut down the plant. The event was described in

Inspection report g6006 Section 02.1 and LER 237/g6-00g-00, " Manual Reactor Scram

!

due to Lowering Reactor Water Level due to Automatic Foodwater Level Control System

4

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Design Deficiency." The LER stated:

"The decisions made during the FWC8 [feedwater control system) testing

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should have been more conservative . . . The review and assessment of

l

the risks and consequences associated with change could have been

i .

mote thorough. Indicatior.s of the need to strengthen the conservative

i

safety culture are as follows:

b.

It was riot recognized by the testing team that the on line

,

configuration function of the Bailey Network N was a potentially

j

untested function and that it should have been tested prior to

'

relying on it for the logic configuration change."

d.

A review with independent personnel outside the test team was not

[

performed and may have identified the importance of placing the -

'

Master Station into manual prior to performing the evolution. "

Many of the statements in the LER could be directly applied to the November 18

'

transient. In the November 18 transient, the licensee did not recognize that changing the

configuration of the LVDT (by lifting lead) affected the FWCS, and no independent review

of the WR was performed that could have identified the importance of placing the control

- stations h manual,

Dresden Station TS 6.8.a required that written procedures be established, implemented,

i

'and maintained covering the applicable procedures recommended in Appendix A of

.

RG 1.33, Revision 2 February 978. Appendix A of RG 1.33, Revision 2 February 1978,

referenced procedures for the repair or replacement of equipment. The

-

.

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work request 97012985-01 was inadequate to perform the repairs of the feedwater

control system. Consequently, an unexpected reactor pressure vessellevel transient

occurred, and the operators had to take manual control of the feedwater level control

system.

Although the preparation of the procedure was inadequate, no violation was issued

,

because the licensee had not yet responded to a recently issued violation for inadequate

procedure and corTective actions for tha previous violation would be expected to

encompass this issue (50-237; 249/97019-01).

c.

Conclusions

The work performed on the Unit 2 feedwater control system was poorly planned. The

failure to provided adequate work instructions directly challenged the operators. The

history of feedwater system work and resulting transients showed that feedwater work

needed more stringent reviews than those provided.

M2.2 Surveillance Performance

a.

Inspection Scope (61726)

The inspectors witnessed and performed a documentation review for surveillance

DIS-263-05, Rev. 8, " Unit 2 Anticipated Transient W.9out Scram (ATWS) Recirculation

Pump Trip and Attemate Rod Injection (RPT/ARI) and Emergency Core Cooling System

(ECCS) Level Master Trip Unit (MTU) and Slave Trip Unit (STU) Channel Functional

Test."

b.

Observations and Findinal

During the performance of the surveillance, communication was established between the

control room and the auxiliary electric equipment room. Three way communications were

used in the performance of the surveillance. The inspectors researched the Updated

Final Safety Analysis Report (UFSAR) and TE s. The puriodicity of the surveillance was

compared with the TS requirements. The survoillance acceptance criteria listed in the

procedure met the TS requirements. The surveillance was completed in a professional

manner.

c.

Conclusion

The surveillance was satisfactorily completed and met the procedurn's acceptance

criteria. The surveillance was completed in a timely manner and met regulatory

requirements,

M4

Malntenance Staff Knowledge and Performance

M4.1 Condensate and Feedwater System

a.

inspigtion Scope

The inspectors reviewed the worn instructions and interviewed licensee personnel

regarding the completion of Temp Alt Ill 1197 (Reference WR#970082873), and

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reviewed the information about URI 50-010; 237; 249/97013-04 provided by the licensee

i

in Hs reply to a Notice (ref. JSPLTR: 97 0195).

b.

QhattYah9fundf0f091

On August 3, in an attempt to alleviate repeated draining and flashing of the

3D2 HP heater high level switch (3 3541 558) reference leg, the licensee attempted a

l

temporary alteration (Reference Temp Att lll 1197 and WR#970082873). Maintenance

'

personnel connected the reference jeg to the high-pressure side of the heater rather than

the low pressure side as diagramed in the work instructions. The temporary ahoration

'

work failed its acceptance criteria during performance of functional testing. The licensee

discovered that the reference leg had been connected to the wrong pipe.

Results of investigation and inspector interviews of maintenance and engineering

personnel suggest workers became confused due to labeling problems during installation

and a poor sketch from engineering included in the work instruction.

I

The workers' action to continue of with work despite this confusion demonstrated poor

work prtctices, since DAP 05 08 " Control of Temporary System AHerstions" stated that,

i

"Whi!e performing a temporary aHeration, if field conditions are different from shown in

wort, psckage then stop and contact the preparer." The inspectors verified that this had

+

not occurred.

'

The licensee reported that the maintenance workers who performed the work were

coached by the department supervisor and the engineer who mad < the poor , ketch

agreed that the sketch should have provided clearer guidance. Tin licensee initiated a

Nuclear Tracking System (NTS) ltem (NTS 237100-97-01304A) to coach the engineer

regarding engineering standards. The involved workers were contract employees and

were no longer working at the site.

The licensee was required by TS 6.8.A to implement applicable procedures

recommended in Appendix A of RG 1.33, Rev. 2, Feb.1978. Adherones to administrative

procedure goveming temporary alteration is recommended in RG 1.33.

Since this self revealing and corrected violation occurred while working on

nonsafety-related equipment, and did not adversely affect the safe operation of the

reactor, the violation is being treated as a Non Cited Violation, consistent with

Section Vll.B.1 of the NRC Enforcement Policy (NCV 50 237/97024-02(DRP)).

c.

Conclusion

Due to a lack of detail on a sketch provided by engineering and a lack of a questioning

attitude by a maintenance worker, the licensee demonstrated poor performance and work

practices regarding the installation of Temp Alt lll 1197.

<

M4.2 Rework (62707)

The inspectors noted several examples of maintenance rework following the forced

outage activities.

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The licensee identified that the correct post maintenance testing (PMT) was not

performed following the weld repairs on the recirculation piping. As a

consequence, the licensee had to redo the weld repair; almost 300 additional and

unnecessary millirem were received by station personnel as a result.

Prior to the shutdown, the number 3 bypass valve showed conflicting position

indication. Position indication repair was included in the forced outage schedule.

After the outage, however, the valve still showed conflicting posit.on indication,

Prior to the forced outage, intermediate range monitor (IRM) 16 experienced

o

erratic indication. The licensee's repair efforts were unsuccessful; following the

outage maintenance work, the IRM still displayed erratic indication. The licensee

subsequently c'etermined that moisture was present in the IRM cable and the IRM

would require further repairs during the next refueling outage.

The consequences of the maintenance rework issues were not severe; husever, they

were indicative of weak maintenance performance. In the case of the IRM, the scope of

the work was not correctly diagnosed; a situation similar to previous concems about

correct problem diagnosis documented in prior NRC inspection reports.

M7

Quality Assurance in Maintenance Activities

M7.1

Licensee Self Atitssments Activities (40500)

a.

Inspection Scope (71707. 83822)

The inspectors reviewed three licensee self-assessments in the maintenance area. The

self assessment's scope, depth, and conclusions were reviewed.

b.

Observations and Findinat

The following licensee self assessments were reviewed:

1.

NIf assessment of the maintenance process for the potential of unauthorized

modifications. The assessment dates were January 7,1997, to January 29,1997.

The objective of the assessment was to review a sample of completed corrective

maintenance work requests from the past four years for unauthorized

modifications.

A ssmple of 315 work requests was reviewed. The sample size was determined

using American National Standard Sampling Procedures and Tables for

Inspection (ANSI /ASQC Z1.4-1993). One unauthorizea modification was

identified in which a cover was bolte1 over a temperature switch. The

assessment also found one instanca where a vendor manual was not properly

updated. Using a table in ANSI /ASQC Z1.4-1993, it was determined with a

99.85 percent confidence level that corrective maintenance work requests

completed during the period did not result in unauthorized modifications. Based

on the confidence level it was concluded that no further actions were roquired.

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The self assessment did not identify that maintenance personnel t'eoded

additional training in modifications. Shortly after the self assessment, the NRC

- Issued a violation for an unauthortrod modification (an installed and unattended

digital voltmeter on a safety-related battery).. The response to the violation stated

,

the unauthorized modification occurred due to the individual n0t being fully aware

j

of the requirements for temporary modifications. The response to the violation

!

stated maintenance p%f onnel would be trained on the temporary modificat6on

!

procedure. The inspeaors therefore concluded that the self-assessment failed to

!

dentify the training weakness.

!

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2.

Self assessment of the conduct of maintenance. The assessment dates were

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February 1,1997, through February 28,1997. The objective of the assessment

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was to determite if work practices used during the conduct of maintenance were

[

in keeping with t,.e highest industry standards,

j

Procedures, policies, the problem identification form (PIF) data base, .

I

main'enance monthly performance reports, and other documents were reviewed

'

by the self assessment team. In addition, interviews and in the-fleid obtervations

were performed.

There were 28 findings listed in the self assessment. They could be summartzed

as findings of work start delays and procedural nonoompliance events durit's

planning, scheduling, work performance, and work documentation. There were no

,

strengths documented in the self assessmem. The report stated that all areas

i

evaluated during the self estessment were found to need improvement. The _

report further stated, "The overall performance trend found in most cases was

either stagnated, cyclic, or had a declining performance trend."

3.

Self assessment of maintenance cerformance indicators. The assessment dates

,

were September 15 through September 26,1997. The objective of the self

assessment was to perform an effectiveness determination of the maintenance

performance indicators.

Interviews with maintenance management were conducted to get their impression

of maintenance performance indicators.

l

The findings of the self assessment were that the maintenance department has

failed to: 1) take ownership and communicate the expectations and requirements

for the measurement of performance indicators, and 2) provide for the adequate

resources for properiy maintaining and evaluating the performance indicators.

'

There were no strengths documented in the self assessment.

c.

Conclusion

For the most part the self assessments were of sufficient scope and depth. The

self assessments were hard hitting and critical of the maintenance process. The

exception was the self assessment on unauthorized inodifications because it did not

3

identify that some workers' knowledge of modification requirements was deficient.-

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M7.2 Lleenste Quality and_ Safety Assessment Activities f40500)

a.

Inspection Sco,pe f71707. 84822)

The inspectors reviewed licensee Quality and Safety Assessment (Q&SA) activities in tne

maintenante area. Documents reviowed included audit reports, completed surveillance

reports, and field monitoring reports.

b.

Observations and Findinot

Q&SA audit reports are documentation of in depth reviews of se'ected areas. The audits

are usually conducted by a team of Individuals. In the maintenance area the inspectors

reviewed the fo! lowing audit reports:

QAA 12 96-09,

Unit i decommissioning

QAA 12 9610,

ASME code / maintenance / contractor activities

QAA 12 97 02,

Staffing and training

QAA 12 07 0/,

Corrective actions

QAA 12 9710,

Outage activl'..a

QAA 12 9715,

Station blatkout system

The audit reports contained many negative findings including corrective action records

(CARS), PlFs, and recommendations. The audit reports also included some positive

comments. The reports did not back away from criticizing licensee practices and did not

focus on unimportant details.

The Q&SA surveillance reports are of much less depth than aun,ts. They are usually

performed by a few people and focused on a specific atea or topic. The following

surveillance reports were reviewed:

QAS 12 96 01,

Vendor technical information program

QAS 12 96-04,

instrument out of tolerance trend

QAS 12 96-06,

Material condition on unit 2 east low pressure coolant

injection comer room

QAS 12 96-17,

GE HGA relay investigation

QAS 12 96-26,

Electrical bus 331 maintenance

QAS 12 96-33

Reactor building ventilation

QAS 12 96-30

Rework / repeat work

QAS 12 96-43,

in-place repair of 3B reactor recirculation pump motor

QAS 12 97-16,

Commitments for Meriin Gerirt circuit breakers

QAS 12-9719,

Scheduled adherence during Ihe refueling outage

QAS 12 97 25,

NRC Generic Letter 96-01," Testing of Safety Related Logic

Circuits"

QAS 12 97 26,

Corrective actions to improve electronic work control

The surveillance reports, while of less depth than the audit reports, still contained many

good recommendations and findings. The reports were critical and well balanced.

The Q&SA field monitoring reports (FMRs) documented the observations the made while

touring the station. They were short and stated what the Q&SA individual observed and

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concluded. The inspectors reviewed 112 FMRs made from June through October 1997.

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The inspectors considered the number of reports to show an active Q&SA organization.

c.

Qonclusion

The Q&SA organ!zation was satisfactorily monitoring the cctivities in maintenance. The

audit reports and surveillance were complet6, thorough, and critical. The field monitoring

reports were an indication that Q&SA personnel performed sufficient field monitoring

activities.

M8

Miscellaneous Maintenance issues

M81.1 (Closed) LER 50-249/97-09-00: HPCI System Declared Inoperable Following Gland Seal

Leakoff Condenser Hotwell High Level During to Drain Pump Stop Switch Failure. This

LER documented the self-revealing failure of the Unit 3 HPCI system during routine

surveillance testing. The failure occurred on September 5,1997, and the HPCI system

was restored following repairs on September 8. This issue was discussed in

Report 97019 and in Section 08.1 of this report. This issue is closed.

i

M8.2 (Closed) URI 50-010: 237: 249/97013-04f DRP): Failure of Temporary Alteration 111-11-97

to Mset Acceptance Criteria Requirements During Performance of Functional Testing Due

to Maintenance Error. This item was discussed in Section M4.1 of this report. This item

is closed.

Ill. Enaineerina

E2

Engineering Suppott of Facilities and Equipment

E2.1

Enaineerina Support of Emeraency Diesel Generators

a.

Insoection Scope (37551)

The inspectors reviewed the licensee's awareness of and compliance with the

recommendations for torquing cylinder test valves on the emergency diesel generators.

The inspectors also reviewed the licensee's corrective actions for an event that took

place last year when a cylinder test valve was ejected during a Unit 3 EDG surveClance

test.

b.

Observations and Findinas

On November 24,1996, a cylinder test valve was ejected from the Unit 3 EDG during a

surveillance test. Sections 02.2 and E4.1 of Inspection Report No. 96014 documented

the inspectors' review of the issue, and the discovery by the inspectors that the current

vendor information regarding the cylinder test valves was not entered into the licensee's

Vendor Equipment Technical Information Program (VETIP). The NRC documented the

failure in violation VIO 50-237; 249/96014-02.

On November 12,1997, personnel at the LaSalle station found a loose cylinder test

valve. During review of the LaSalle event, the inspectors at LaSalle found vendor

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information that was not incorporated into LaSalle procedures, although it was in the

LaSalle vendor manuals. The information was a letter dated January 2,1997, from Klene

Diesel Accessorie s, Inc., to the diesel system engineer at Quad Cites Station. The

letters subject was, "V-24A/AX-8SA, Indicator Valve / Adapter Assemt:ty Installation in

Electromotive Engines," and the letter transmitted the recommended installation

instructions of the cylinder Indicator (or test) valve and adapter.

The inspector discussed the contents of the letter with the system engineers at Dresden,

and the system engineers said that they had not received the letter. However, they

believed that the routine work request to verify the torque on the cylinder test valves

developed in response to the November 24,1996, event was sufficient.

The inspectors reviewed WR # 970087465-01, "[ Unit 2) Engine Standby Diesel

Generator, Verify Torque on Cylinder Test Velves", last completed October 1,1997. The

task required " Torque packing nut to 65 ft/lbs, plus or minus 1 ft/lb. Torque values

acquired from V TIP D1164." V-TIP D1164 war not related to cylinder test valves, but

V-TIP D1163, pages 215, stated that for the original cylinder test valves,"If a cylinder

test valve is leaking, check that packing nut . . . has been torqued to 81-88 Nm (60-65 ft-

Ibs), if nut has been overtightened, change seat, , , . , and correctly torque packing nut."

The January 2,1997, letter from the cylinder test valve vendor stated that "ths adapter

should be installed into the engine and tightened with 45 to 50 ft-lbs of torque, and then

the packing gland nut should be tightened against the packing gland enough to hold it in

place. The V-24A Valve is then installed . . . and tightened to 75 ft-lbs of torque."

The licensee was unable to find any documentation that showed that the cylinder test

valves were installed in accordance with the January 2,1997, letter. The licensee wrote

action requests to verify the torques, and the verifications had not been completed at the

end of the inspection period.

Inspection Report No. 50-237/96014(DRP) issued Violation 50 237/96014-02 for failing to

incorporate vendor information regarding the cylinder test valves into the VETIP manuals.

The licensee's response (JSPLTR: 97-0045, dated March 6,1997) stated that the failure

was attributed to a system engineefs failure to take action to update the technical manual

when a new component we= installed in the dieselin January of 1996. Also, as of

February of 1997, the venovr stated that no technical manual change will be issued

addressing the replacement valve as new diesels will be delivered with the old style

cylinder test valve installed. The response did not state if the vendor of the new-style

valves .nlanned to issue any vendor information. The response also discussed Dresden-

site specific actions taken to assure all vendor information received at Dresderi was

incorporated.

The system engineer gave the inspectors a copy of E-mail from Comed corporate

engineering regarding the LaSalle cylinder test valves that concluded that "the deviation

from the vendors procedure in this case would not affect the operability of the diesels."

The inspectors noted that the licensee's diesels had all passed their surveillances (except

for operations-based problems documented in report 97019), and that no visual evidence

of loose cylinder test valves was found during routine walkdowns, and corcluded that the

lack of incorporation of vendor information did not result in an immediate operability

concem.

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The bspectors determined that the response to the Notice was insufficient because

vendor information regarding the cylinder test valves was still not captured into the

i

VETIP The unincorporated information was dated January 2,1997, and was sent to a

Comed site more than two months before the licensee issued the response to the Notice.

Therefore, the licensee should have identified the vendors information before issuing the

response. Acccrdingly, the status of violation VIO 50-237/96014 02 will remain OPEN

pending review of how the vendors information was sent to one Comed licensee, but not

another.

c.

Conclusion

The licensee did not have all vendor information related to emergency diesel generator

cylinder test valves. Applicable information sent to another Comed site had not been

forwarded to the licensee. The actions taken in response to a previous NRC-identified

violation for failing to incorporate vendor information regarding cylinder test valves were

not sufficient because additionalinformation received by Comed 2 months before the

licensee's response to the Notice was not incorporated.

IV Plant SuDDort

F2

Status of Fire Protection Facilities and Equipment

F2,1

Safe Shutdown Emeroency Liohtino Material Condition

a.

Inspection Scope (62707)

The inspectors reviewed Inspection Followup item (IFI) 50-237; 249/97019-03. The

inspectors also reviewed emerging problems with all Unit 2 safe shutdown (SSD)

emergency lights being declared inoperable due to a missed surveillance test.

b,

Observations and Findinos

The inspectors reviewed problems with the installation of batteries within many

emergency lights, The lights were missing either the battery tray and/or the pressure bar.

Within the emergency light assembly, the battery rests on the battery tray and is pressed

against the front of the unit by the pressure bar Without either of these items the battery

is free to move around inside the emergency light assembly This could affect the

seismic qualification of the emergency lights. After being notified of the problems with the

emergency light, licensee personnelinitiated a PlF (# D1997-07316) and notified site and

design engineering for assistance with the seismic concems,

While interviewing electrical maintenance and engineering personnel, the inspectors

asked if they were aware of a similar problem in the past at Braidwood station

(ref. Braidwood PlF# 456-201-97-0601 dated March 6,1997). The licensee first M vm

that the problem at Braidwood was a different problem for which Dresden had been

evaluated. The licensee personnel mistakeniy believed the problem from Braidwood was

with the "J" hook that secures the SSD emergency light to the mounting shelf. Arter the

inspectors described the Braidwood problem clearly to Dresden personnel, the licensee

concurred that the problem was applicable to Dresden.

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The inspectors reviewed a memo (Doc ids 0005537204), written by Comed Design

Engineering, which states the SSD emergency lights do not have to be seismically

,

qualified but only have to address seitmic interaction concoms. T he memo states the

missing battery tray or the pressure bar would not aNoct the seismic interaction of the

SSD emergency lights.- From discussions with the Design Engineering Structural Lead

-

' who approved the memo, engineering judgement was used to decide that the battery

would not be thrown from the SSD emergency light assembly during an earthquake.-

-

Electrical maintenance personnel stated that, based on there being no seismic cencom,

. they plan to determine the requirements for property installing the batteries in the SSD -

. emergency lights, during the performance of the next quarterty SSD emergency light

,

surveillance. They then plan to correct the battery installation during the following

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quartetty surveillance,

- During a Q&SA audit it was oetermined that the battery discharge surveillance on all the

unit 2 SSD emergency lights was over due. With the surveillance past its due date, the

,

licensee declared all SSD emergency lights on unit 2 inoperable. Dresden Administrative

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Technical Requirement (DATR) 3.2.3.1 was entered. The DATR stated that inoperable

SSD emergency lights must be retumed to operable within 7 days or to establish backup

lighting, if this could not be done, then the equipment illuminated by the SSD emergency

!

lights must be treated as inoperable. The station decided to replace the batteries in all

l;

- the unit 2 SSD emergency lights with new batteries rather than do the discharge test.

- The batteries were successfully replaced within the 7-day DATR. During the battery

replacement, the parts requirement document to correct the battery installation was

generated.

Also, during the Q&SA audit it was identified that certain areas in the plant, where manual

actions are required in SSD procedures, did not contain SSD emergency lights. These

areas are required to have SSD emergency lights. The licensee began fire watches in

the effected areas until temporary SSD emergency 1:ghts could be put in place. Work is -

l

in process to put permanent SSD emergency lights in place in these areas.

i-

c.

ConclusioD1

i

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The licensee improperly determined that the problem experienced at Braidwood Station -

!

was not present at Dresden Station. The licensee determined through engineering

j~

judgement that the battery being improperly restrained inside the SSD emergency lights -

did not aNect the seismic interaction of the equipment. The licensee planned to install the

batteries in the SSD emergency lights correctly. The licensee dealt with SSD emergency

light issues from a Q&SA audit quickly. However, due to all the problems with SSD

. emergency lights, the overall material condition of the lights was considered marginal.

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V, Mananoment Meetinas

- X1 Exit Meeting Summary

The inspectors presented the inspection restits to members of licensee management at

the conclusion of the inspection on November 22,1997. The licensee acknowledged the -

findings presented. The inspectors asked the licensee whether any materials examined

during the inspection should be considered proprietary. No proprietary information was

identified.

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PARTIAL LIST OF PERSONS CONTACTED

Licensee

  • G. Abrell >

NRC Coordinator-

  • L. Weir

Design Engineering Superintendent-

  • D. Ambler

Acting Regulatory Supervisor

a

  • J. Tenz

System Engineering Safety Group Lead

  • R. Peaks

Programs Engineering Supervisor

  • S. Perry.

Site Vice President

  • B. Holbrook

Training Manager

  • S. Kuczynski

Shift Operatoins Supervisor

  • R. Whalen

Plant Engineering

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  • D. Willis

Electrical Superintendent

  • W. Lipscomb

SVP Staff '

  • C, Richards

Audit Supervisor

,

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~ *M. Friedmann

Lead Health Physicist

  • Present at exit meeting of November 21.

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INSPECTION PROCEDURES USED

~

- Inspection Module: 71707f Operational Safety Verification

Inspection Module: 83822

Radiation Protection -

Inspection Module: 62707

Maintenance

inspection Module: 61726

Surveillance Observations

inspection Module: 40500

Effectiveness of Licensee Controls in Identifying, Resolving, and

Preventing Problems

ITEMS OPEN, CLOSED, AND DISCUSSED

Opened

50-249/97024-01

VIO

SBLC inoperable in excess of TS times.

50-237/97024-02

NCV Failure to install temp att correctly,

Closed

50-249/97-09-00

LER

HPCI System Declared inoperable Following Gland Seal Leakoff

Condenser Hotwell High Level During to Drain Pump Stop Switch

Failure.50-010;237;249/

97013-04

URI

Failure of Temporary Alteration 111-11-97 to Meet Acceptance

Criteria Requirements During Performance of Functional Testing

Due to Maintenance Error.

50-237/97024-02

NCV Failure to install temp alt correctly.

DitMSMd

50-237;249/

97019-03

IFl

Review of the seismic requirements '- tr,e emergency lights.

50-249/97-011-00

LER

SBLC was Inoperable from Suction Line Low Temperature due to a

,

Wiring discrepancy in the Heat trace Controller Circuit

237/96-009-00

LER

Manual Reactor Scram due to Lowering Reactor Water Level due

to Automatic Feedwater Level Control System Design Defic:ency

"

50-237;249/

96014-02

VIO

Failure to enter EDG test valve tech info into VETIP

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LIST OF ACRONYMS USED

DAN-

Dresden Annunciator Procedure

DAP

Dresden Administrative Procedure

,

DATR

Dresden Administrative Technical Requirement

DEOP

Dresden Emergency Operating Procedure

DGA

Dresden General Abnormal Procedure

.

DOA'.

Dresden System Operating Abnormal Procedure

DOP

Dresden System Operating Procedure

HPCI

High Pressure Coolant Injection

IFl

Inspection Followup item

IPE

Individual Plant Evaluation

IR

.

Inspection Report .

ISEG

Independent Site Engineering Group

ISI

inservice inspection

LCO

Limiting Condition for Operation

LER

Licensee Event Report

LPCI

Low Pressure Coolant injection

NCV

Non-Cited Violation

NLO

Non-licensed Operator

- NOV

Notice of Violation

'

NRC.

Nuclear Regulatory Commission

NRR

Office of Nuclear Reactor Regulation

.

<

L

NSO .

Nuclear Station Operator

NSWP

Nuclear Station Work Procedure -

'

OE '

Office of Enforcement

Ol

Office of Investigations -

OOS

Out-of Service

PIF

Problem identification Form

PORC

Plant Operations Review Committee

RUFSAR

Revised Updated Final Safety Analysis Report

F

Q&SA

Quality and Safety Assessment

QC

Quality Control

TS

Technical Specification

'

VIO

Violation

WEC

Work Execution Center

WR

Work Request

.

1 ~

31

i

.

.

.