Turbine bypass valve: Difference between revisions
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Revision as of 07:40, 14 March 2018
Site | Start date | Title | |
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05000000/LER-1986-038-02, :on 861209,reactor Scram Occurred Due to Low Condenser Vacuum.Caused by Personnel Error.Discussions W/Operating Personnel Involved Will Be Held.Procedure Qgp 1-1 to Be Revised | Quad Cities 05000000 | 23 December 1986 |
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05000155/LER-1988-002, :on 880205,plant Operators Manually Tripped Reactor in Response to Loss of Recirculation Flow.Caused by Personnel Error.Equipment Testing Performed to Insure That No Malfunctions Occurred or Damage Present | Big Rock Point | 7 March 1988 |
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05000155/LER-1988-008-01, :on 881028,load Rejection Occurred Due to Loss of Transmission Line.Caused by Lightning Rod Which Broke Off During High Winds.Control Rod Drive Motor Generator Set Repaired | Big Rock Point | 23 November 1988 |
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05000155/LER-1989-009-01, :on 891027 & 31,turbine Bypass Valve Would Not Open When Given Open Signal.Caused by Characteristics of Garlock Style 938 Which Hardens When Subj to Heat & Pressure.Valves Repacked Using Carbon Spacers | Big Rock Point | 9 January 1990 |
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05000155/LER-1996-010-01, :on 960916,automatic Reactor Scram Occurred During Startup Due to High Reactor Pressure.Fabrication Process Will Be Evaluated & Corrected | Big Rock Point | 15 October 1996 |
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05000155/LER-1998-001-01, :on 980714,during Facility Decommissioning, Found Liquid Poision Tank Discharge Pipe Severed.Caused by Corrosion.Staff Reviewed Current Decommissioning Surveillance Testing on safety-related SSCs | Big Rock Point | 6 August 1998 |
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05000219/LER-1981-021, Forwards LER 81-021/03L-0.Detailed Event Analysis Encl | Oyster Creek | 1 July 1981 | Forwards LER 81-021/03L-0.Detailed Event Analysis Encl |
05000219/LER-1985-015, :on 850708,scram Occurred on Low Condenser Vacuum.Caused by Cracked Drain Pump 1-1 Casing & Tube Leak in Steam Packing Exhauster.Drain Pump 1-1 Replaced & Drain Pump 1-2 & Tube Leak Repaired | Oyster Creek | 8 August 1985 |
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05000219/LER-1986-032, :on 861224,reactor Trip Occurred Due to High Neutron Flux Condition.Caused by Personnel Error & Configuration W/Respect to Feedwater Control Sys.Event Reviewed W/Each Oncoming Shift | Oyster Creek | 23 January 1987 |
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05000219/LER-1986-034, ,on 861229,manual Scram Due to Inability to Maintain Condenser Vacuum Occurred.Caused by Expansion Joint Failure in Vacuum.Procedure Limit of Saturation Temp Reduced to Prevent Recurrence | Oyster Creek | 30 January 1987 | ,on 861229,manual Scram Due to Inability to Maintain Condenser Vacuum Occurred.Caused by Expansion Joint Failure in Vacuum.Procedure Limit of Saturation Temp Reduced to Prevent Recurrence |
05000219/LER-1987-005, :on 870116,high Flux Reactor Scram Occurred Due to Increased Recirculation Flow.Caused by Starting of Pump W/Discharge Valve Partially Open.Second Scram Occurred Due to Calibr Error.Valves Readjusted | Oyster Creek | 27 February 1987 |
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05000219/LER-1987-011, :on 870214,anticipatory Reactor Scram Occurred Due to High Reactor Water Level Turbine Trip.Caused by Inadvertent Disconnection of Feedwater a Flow Signal Wire by Technician.Procedures Revised | Oyster Creek | 20 March 1987 |
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05000219/LER-1987-011, :on 870214,reactor Scram Occurred as Result of High Reactor Water Level Turbine Trip.Caused by Faulty Wire Installation During Plant Const or Maint.Terminations in Control Room Inspected & Tightened | Oyster Creek | 4 May 1987 |
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05000219/LER-1990-010, :on 900718,electromatic Relief Valve High Pressure Relief Setpoints Discovered to Exceed Tech Spec Limit.Caused by Setpoint Repeatability & Instrument Drift. Pressure Switches Adjusted to Be within Limit | Oyster Creek | 20 August 1990 |
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05000219/LER-1992-006, :on 920510,EMRV Pressure Sensor Surveillance, as Found Trip Setpoint for High Pressure Relief Function Above TS Limit.Caused by Instrument Setpoint Repeatability. Pressure Switch Immediately Adjusted | Oyster Creek | 3 June 1992 |
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05000219/LER-1994-007, :on 940531,reactor Scram Occurred Due to Modification Work in Switchyard.Placing Modification on Hold Pending Engineering Review & Strengthening Procedural Controls Over Switchyard Work | Oyster Creek | 30 June 1994 |
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05000219/LER-1994-008, :on 940419,setpoints for High Pressure Relief Function on Two EMRVs Were Above That Specified in Tss. Caused by Setpoint Repeatability & Instrument Drift.Pressure Switches Were Adjusted within TS Limits | Oyster Creek | 19 July 1994 |
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05000219/LER-1995-005, :on 950825,identified non-conservative Instrument Setpoint for Anticipatory Scram Bypass Pressure Switches Due to Original Plant Design.Revised Plant Operation Procedures | Oyster Creek | 21 September 1995 |
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05000219/LER-1995-008, :on 951218,reactor Scram Occurred on High RPV Pressure Due to Main Generator Runback.Repaired Faulty Temp Control Valve | Oyster Creek | 18 January 1996 |
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05000219/LER-1996-005, :on 960430,reactor Scram Occurred on Low Water Level Due to Personnel Error.Discussion of Event Issued to Operators & Interim Guidance Issued to Operators on Reactor Water Level Control | Oyster Creek | 11 June 1996 |
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05000219/LER-2013-004 | Oyster Creek | 14 December 2013 | Manual SCRAM due to rise in Reactor Pressure during Turbine Valve Testing |
05000219/LER-2014-006 | Oyster Creek | Reactor SCRAM due to Decreasing Reactor Water Level | |
05000219/LER-2016-004 | Oyster Creek | Technical Specification Violation Due to Main Steam Safety Valve Setpoint Discovered Out of Tolerance | |
05000219/LER-2017-003 | Oyster Creek | 3 July 2017 31 August 2017 | Automatic Scram while Suberitical due to Low Reactor Level LER 17-003-00 for Oyster Creek Regarding Automatic Scram while Subcritical due to Low Reactor Level |
05000220/LER-1985-022, :on 851107,turbine Bypass Valve 12-H Inadvertently Closed,Causing Decrease in Reactor Water Level & Subsequent Scram & Initiation of HPCI Mode of Feedwater. Valve to Be Inspected | Nine Mile Point | 6 December 1985 |
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05000220/LER-1985-023, :on 851108,during Preparations for Main Turbine Startup,High Temp in Main Turbine Exhaust Hood Caused Turbine Trip & Actuation of HPCI Mode of Feedwater Flow | Nine Mile Point | 6 December 1985 |
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05000220/LER-1999-004-01, :on 990723,reactor Scram Was Noted.Caused by Mechanical Pressure Regulator Suppressor Valve Failure. Cleaned Pressure Suppressor Valve & Provided Guidance for Valve Disassembly & Insp.With | Nine Mile Point | 23 August 1999 |
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05000220/LER-2003-002 | |||
05000220/LER-2004-004 | 30 August 2004 | ||
05000220/LER-2005-001 | 7 March 2005 | Automatic Reactor Scram due to a Failure in the Circuitry for a Moisture Separator Tank Level Switch | |
05000220/LER-2005-003 | 18 August 2005 | Automatic Reactor Scram during Surveillance Testing due to Inadvertently De-energizing 4160 VAC Power Board 11 | |
05000220/LER-2008-002 | Docket Number | 23 October 2008 | Manual Reactor Scram Due to Loss of Reactor Pressure Control |
05000220/LER-2009-002 | Docket Number | High Pressure Coolant Injection System Initiation Following a Manual Turbine Trip Due to High Turbine Bearing Vibrations | |
05000220/LER-2009-003 | Docket Number | 5 October 2009 | Manual Scram and High Pressure Coolant Injection Following a Loss of Feedwater Level Control Due to Firmware Deficiency |
05000220/LER-2011-001 | Nine Mile Point | 2 May 2011 | Turbine Trip Due to Oil Pressure Fluctuations to the Turbine Master Trip Solenoid |
05000220/LER-2012-001 | Nine Mile Point | Automatic Reactor Scram due to Electronic Pressure Regulator Failure | |
05000220/LER-2012-002 | Nine Mile Point | Automatic Reactor Scram due to Automatic Generator Protective Trip | |
05000220/LER-2012-004 | Nine Mile Point | Automatic Reactor Scram Due to a Generator Load Reject | |
05000220/LER-2012-005 | Nine Mile Point | Feedwater Level Control Failure, HPCI initiation and Reactor Scram | |
05000220/LER-2012-006 | Nine Mile Point | Technical Specification Required Shutdown Due to Containment Leakage | |
05000220/LER-2015-004 | Nine Mile Point | 4 September 2015 | Automatic Reactor Scram Due to Main Steam Isolation Valve Closure |
05000220/LER-2017-002 | Nine Mile Point | 18 May 2017 | Manual Reactor Scram Due to Pressure Oscillations LER 17-002-00 for Nine Mile Point Nuclear Station, Unit 1 Regarding Manual Reactor Scram Due to Pressure Oscillations |
05000220/LER-2017-003 | Nine Mile Point | 6 September 2017 2 November 2017 | Automatic Reactor Scram due to Reactor Vessel Low Water Level LER 17-003-00 for Nine Mile Point, Unit 1, Regarding Automatic Reactor Scram due to Reactor Vessel Low Water Level |
05000237/LER-2004-002 | Docket Number | 24 April 2004 | Dresden Nuclear Power Station Unit 2 05000237 1 of 5 |
05000237/LER-2005-002 | Dresden | 24 March 2005 | Unit 2 Group 1 Isolation and Resulting Scram |
05000245/LER-1981-038, Forwards LER 81-038/03L-1.Detailed Event Analysis Encl | Millstone | 13 January 1982 | Forwards LER 81-038/03L-1.Detailed Event Analysis Encl |
05000245/LER-1990-018-01, :on 901212,discovered That Condenser Vacuum Switches Out of Tolerance Due to Instrument Drift.Barksdale Condenser Low Vacuum Scram Pressure Switches Replaced W/ Static O-Ring Pressure Switches | Millstone | 15 September 1994 |
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05000245/LER-1993-010-01, :on 930917,determined Unit 1 Has No Automatic Reactor Recirculation Pump Runback Circuitry in Place.Caused by Incorrect Analysis Assumption in Original Plant Accident analysis.Re-analysis Performed | Millstone | 18 October 1993 |
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05000245/LER-1997-007-01, :on 970131,flow-biased High Flux Reactor Scram Credited in Establishing Not Single Failure Proof.Cause of Event Still Under Investigation.Rept Will Be Supplemented by 970331,w/cause of Event | Millstone | 3 March 1997 |
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05000245/LER-1997-034-01, :on 970812,Unit 1 Switchgear Failed During Unit 2 High Energy Line Break.Caused by Incorrect Assumption by HELB Analysis Performed by A&E.No Immediate Corrective Actions Required | Millstone | 11 September 1997 |
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