ENS 43132: Difference between revisions

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| event date = 01/29/2007 23:10 EST
| event date = 01/29/2007 23:10 EST
| last update date = 02/01/2007
| last update date = 02/01/2007
| title = Automatic Reactor Scram On Low Reactor Pressure Vessel (Rpv) Water Level
| title = Automatic Reactor Scram on Low Reactor Pressure Vessel (Rpv) Water Level
| event text = On 1/29/07 with Hope Creek reactor startup in progress, in mode 1 at 22% Reactor power, Secondary Condensate Pump Minimum Flow Control Valves began to cycle. Reactor water level reached 39" (RPV level 7) and then lowered to 30" (RPV level 4). Manual control of the Reactor Feed pumps was taken, however, RPV water level continued to lower to 15" (Reactor scram on RPV water level is 12.5") at which time the reactor mode switch was locked in shutdown. There were no ECCS injections and all ECCS systems are operable. Initial review of the event indicates that all systems operated as expected with the exception of the Secondary Condensate pump minimum flow valves and the 'A' IRM failed to insert. Current plant conditions as of 1/30/07 at 0010 are: Hope Creek is in mode 3 at 565 psig. The Main Steam Line Isolation valves are open. 'B' and 'C' Primary Condensate Pumps, 'B' and 'C' Secondary Condensate Pumps, and 'A' Rx Feed Pump are feeding the vessel. All control rods have fully inserted on the scram and Main Turbine Bypass valves are removing decay heat.
| event text = On 1/29/07 with Hope Creek reactor startup in progress, in mode 1 at 22% Reactor power, Secondary Condensate Pump Minimum Flow Control Valves began to cycle. Reactor water level reached 39" (RPV level 7) and then lowered to 30" (RPV level 4). Manual control of the Reactor Feed pumps was taken, however, RPV water level continued to lower to 15" (Reactor scram on RPV water level is 12.5") at which time the reactor mode switch was locked in shutdown. There were no ECCS injections and all ECCS systems are operable. Initial review of the event indicates that all systems operated as expected with the exception of the Secondary Condensate pump minimum flow valves and the 'A' IRM failed to insert. Current plant conditions as of 1/30/07 at 0010 are: Hope Creek is in mode 3 at 565 psig. The Main Steam Line Isolation valves are open. 'B' and 'C' Primary Condensate Pumps, 'B' and 'C' Secondary Condensate Pumps, and 'A' Rx Feed Pump are feeding the vessel. All control rods have fully inserted on the scram and Main Turbine Bypass valves are removing decay heat.
The licensee will inform the LAC (Lower Alloways Creek Township) and has informed the NRC Resident Inspector.
The licensee will inform the LAC (Lower Alloways Creek Township) and has informed the NRC Resident Inspector.

Latest revision as of 22:17, 1 March 2018

ENS 43132 +/-
Where
Hope Creek PSEG icon.png
New Jersey (NRC Region 1)
Reporting
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation
Time - Person (Reporting Time:+-3.35 h-0.14 days <br />-0.0199 weeks <br />-0.00459 months <br />)
Opened: Bernie Litkett
00:49 Jan 30, 2007
NRC Officer: Steve Sandin
Last Updated: Feb 1, 2007
43132 - NRC Website
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