ENS 51720: Difference between revisions
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StriderTol (talk | contribs) (Created page by program invented by Mark Hawes) |
StriderTol (talk | contribs) (Created page by program invented by StriderTol) |
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| event date = 02/09/2016 14:15 EST | | event date = 02/09/2016 14:15 EST | ||
| last update date = 02/09/2016 | | last update date = 02/09/2016 | ||
| title = Eccs Discharge | | title = Eccs Discharge to Rcs Via Charging System | ||
| event text = At 1415 EST on 02/09/2016, Sequoyah Unit 1 was at 0 percent power (mode 3, 526F, 2235 psig) when a low steam line pressure Safety Injection actuated from Loop 2 Steam Generator. Prior to this event, the Loop 2 Main Steam Isolation Valve bypass was opened at 1413 EST for main steam line warm up in preparation for unit startup. Loop 2 Main Steam Isolation Valve bypass closed automatically following low steam line pressure Safety Injection. | | event text = At 1415 EST on 02/09/2016, Sequoyah Unit 1 was at 0 percent power (mode 3, 526F, 2235 psig) when a low steam line pressure Safety Injection actuated from Loop 2 Steam Generator. Prior to this event, the Loop 2 Main Steam Isolation Valve bypass was opened at 1413 EST for main steam line warm up in preparation for unit startup. Loop 2 Main Steam Isolation Valve bypass closed automatically following low steam line pressure Safety Injection. | ||
Following the Safety Injection, all safety-related equipment operated as designed. | Following the Safety Injection, all safety-related equipment operated as designed. |
Latest revision as of 21:45, 1 March 2018
Where | |
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Sequoyah Tennessee (NRC Region 2) | |
Reporting | |
10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
Time - Person (Reporting Time:+-1.83 h-0.0763 days <br />-0.0109 weeks <br />-0.00251 months <br />) | |
Opened: | Bruce Buch 17:25 Feb 9, 2016 |
NRC Officer: | Jeff Rotton |
Last Updated: | Feb 9, 2016 |
51720 - NRC Website
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