ENS 51720: Difference between revisions

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| event date = 02/09/2016 14:15 EST
| event date = 02/09/2016 14:15 EST
| last update date = 02/09/2016
| last update date = 02/09/2016
| title = Eccs Discharge To Rcs Via Charging System
| title = Eccs Discharge to Rcs Via Charging System
| event text = At 1415 EST on 02/09/2016, Sequoyah Unit 1 was at 0 percent power (mode 3, 526F, 2235 psig) when a low steam line pressure Safety Injection actuated from Loop 2 Steam Generator.  Prior to this event, the Loop 2 Main Steam Isolation Valve bypass was opened at 1413 EST for main steam line warm up in preparation for unit startup.  Loop 2 Main Steam Isolation Valve bypass closed automatically following low steam line pressure Safety Injection.
| event text = At 1415 EST on 02/09/2016, Sequoyah Unit 1 was at 0 percent power (mode 3, 526F, 2235 psig) when a low steam line pressure Safety Injection actuated from Loop 2 Steam Generator.  Prior to this event, the Loop 2 Main Steam Isolation Valve bypass was opened at 1413 EST for main steam line warm up in preparation for unit startup.  Loop 2 Main Steam Isolation Valve bypass closed automatically following low steam line pressure Safety Injection.
Following the Safety Injection, all safety-related equipment operated as designed.
Following the Safety Injection, all safety-related equipment operated as designed.

Latest revision as of 21:45, 1 March 2018

ENS 51720 +/-
Where
Sequoyah Tennessee Valley Authority icon.png
Tennessee (NRC Region 2)
Reporting
10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge

10 CFR 50.72(b)(3)(iv)(A), System Actuation
Time - Person (Reporting Time:+-1.83 h-0.0763 days <br />-0.0109 weeks <br />-0.00251 months <br />)
Opened: Bruce Buch
17:25 Feb 9, 2016
NRC Officer: Jeff Rotton
Last Updated: Feb 9, 2016
51720 - NRC Website
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